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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000354/LER-1990-0091990-07-0505 July 1990 LER 90-009-00:on 900607,HPCI Sys Oil Samples Indicated High Water Content & Traces of Sediment Contamination.Caused by Design Deficiency in HPCI Turbine Lube Oil Reservoir. Reservoir Cleaned,Flushed & Wiped down.W/900705 Ltr 05000354/LER-1990-0081990-07-0505 July 1990 LER 90-008-00:on 900604,reactor Bldg Exhaust Radiation Monitor Trip Setpoint Found Nonconservatively High.Caused by Personnel Error.Technicians Disciplined,Rept Reviewed W/All Personnel & Setpoint Included in procedure.W/900705 Ltr 1990-07-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F1501999-10-12012 October 1999 Special Rept:On 990929,south Plant Vent (SPV) Range Ng Monitor Was Inoperable.Monitor Was Inoperable for More than 72 H.Caused by Electronic Noise Generated from Noise Suppression Circuit.Replaced Circuit ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20217M0211999-09-20020 September 1999 Part 21 Rept Re Possible Deviation of NLI Dc Power Supply Over Voltage Protection Circuit Actuation.Caused by Electrical Circuit Conditions Unique to Remote Engine Panel. Travelled to Hope Creek to Witness Startup Sequence of DG ML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20211B3781999-08-13013 August 1999 Special Rept 99-002:on 990730,NPV Radiation Monitoring Sys Was Declared Inoperable.Caused by Voltage Induced in Detector Output by Power Cable to Low Range Sample Pump. Separated Cables & Secured in Place to Prevent Recurrence ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20216D8721999-07-26026 July 1999 Review of Submittal in Response to USNRC GL 88-20,Suppl 4: 'Ipeees,' Fire Submittal Screening Review Technical Evaluation Rept:Hope Creek Rev 1:980518 ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8901999-06-30030 June 1999 IPEEEs Technical Evaluation Rept High Winds,Floods & Other External Events ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8451999-04-30030 April 1999 Rev 1, Submittal-Only Screening Review of Hope Creek Unit 1 IPEEE (Seismic Portion). Finalized April 1999 ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) LR-N990157, Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced1999-04-12012 April 1999 Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20202F6861999-01-26026 January 1999 Engine Sys,Inc Part 21 (10CFR21-0078) Rept Re Degradation of Synchrostat Model ESSB-4AT Speed Switches Resulting in Heat Related Damage to Power Supply Card Components.Caused by Incorrect Sized Resistor.Notification Sent to Customers ML18107A1871998-12-31031 December 1998 PSEG Annual Rept for 1998. ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With ML18107A1881998-12-31031 December 1998 PECO 1998 Annual Rept. LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With ML20198N4161998-11-12012 November 1998 MSIV Alternate Leakage Treatment Pathway Seismic Evaluation LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with ML20155J9861998-10-31031 October 1998 Non-proprietary TR NEDO-32511, Safety Review for HCGS SRVs Tolerance Analyses LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 ML20236E9491998-06-30030 June 1998 Rev 0 to non-proprietary Rept 24A5392AB, Lattice Dependent MAPLHGR Rept for Hope Creek Generating Station Reload 7 Cycle 8 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 ML20248C7381998-05-22022 May 1998 Rev 0 to Safety Evaluation 98-015, Extension of Allowed Out of Service Time for B Emergency Diesel Generator LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML18106A5851998-03-0303 March 1998 Emergency Response Graded Exercise,S98-03. Nuclear Business Unit Salem,Hope Creek Emergency Preparedness, 980303 1999-09-08
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& ff j . Public Service Electnc and Gas Company P.O. Box 236 Hancockt, Bndge, New Jers ey 08038 Hopo Creek Generating Station ,
Y July 5, 1990 U. 8. Nuclear Regulatory Commission Document Control Denk Washington, DC 20555 ..
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1 Dear Sir HOPE CREEK-GENERATING STATION DOCKET No. 50-354 UNIT NO. 1 LICENSEE EVENT REPORTt 90-009-00 This Licensee Event Report is being submitted pursuant to
.;i the requirements of 10CFR50.73 (a) (2) (v) . ll Sincerely,
/
J.J. agan General Manager - Ui Hope Creek Operations RBC/
. Attachment SORC Mtg.90-062 C Distribution s
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9007100154 900705 Nh PDR ADOCK 05000354 R PDC / g
' The Energy People n am ssu> nu 1 l_-- ,
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NAME 1111NNE NtMGR Richard Owleo, Senior Stati thgirner - hdinical 609 3 3 9 1 4 3 1 (IMITIE (NE IJNE RR FA01 GMKNINT IAlllRE N0iTV IN 1HIS RDmt (13)
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All!?IRACT (16)
On 6/7/90 at 1016, the System Engineer responsible for the liigh Pressure Coolant Injection (llPCI ) systern reported to the Senior Nuclear Shift Supervisor (SNSS, SRO licensed) that !!PCI oil samples indicated high watar content and traces of sedicent contamination. The SNSS declared the IIPCI system inoperable, and a e-rk request was initiated to clean the llPCI turbine lube oil reservoir and change out the llPCI turbine lube oil. The primary cause of the oil contamination is a design deficiency in the HPCI turbine lube oil reservoir that does not allow for complete draining of reservoir during oil changes. The reservoir is not equipped with a drain line at the low point. As such, it is possible for water and sludge to collect at the low point over time due to condensation in the reservoir as llPCI room temperatures change. Corrective actions included cleaning, flushing, and wipe down of the llPCI turbine lube oil reservoir, rosampling the lube oil, and reviewing the llPCI lube oil trending program.
Additionally, prior to this occurrence, Systems Engineering had initiated a design change to install a drain line at the low point in the reservoir to facilitate periodic draining of accumulated water and sludge.
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ll(DISEE BINT RIERT (!R) int (INTINJATICE ;
GCIIJ1Y NAPE 'l) D00It NLMifR (2) l a NU3 D __(6) PME (3)
YrAR 'a NtMfR " RIN IDE CRIH (IMRATING STATICW 0500054 1 0 0 9 -
0 0 02 7 0 3 ;
PhANT AND SYSTEM IDENTIFICATION l
General Electric - Boiling Water Reactor (BWR/4) i High Pressure Coolant Injection System (EIIS Designation: BJ) ,
j IDENTIFICATION OF OCCURRENCE High Pressure Coolant Injection System Declared Inoperable '
Based on Results of 011 Sample Analysis - Design Deficiency in 4
Drain Arrangment of Lube Oil Reservoir Event Date: 6/7/90 Event Time: 1016 This'LER was initiated by Incident Report No.90-062 CONDITIONS PRIOR TO OCCURRENCE Plant in OPERATIONAL CONDITION 1 (Power Operation), Reactor J Power 100%, Unit Load 1100MWo.
DESCRIPTION OF OCCURRENC.E
' Chi 6/7/90 at 1016, the System Engineer responsible for the High Pressure Coolant Injection (HPCI) system reported to the Senior Nuclear Shift Supervisor (SNSS, SRO licensed) that quarterly HPCI oil sample analysis indicated unacceptable levels of moisture content and traces of sediment contamination. The ,
SNSS declared HPCI inoperable at this time. A work order was-initiated to clean the HPCI turbine lube oil reservoir, change the oil, and resample the oil. Additionally, the SNSS ;
initiated a four hour non-omergency report IAW 10CFR50.72 due to declaring HPCI (a single train safety system) inoperable. ,
Following completion of a system oil changeout and cleaning of .
the HPCI turbine lube oil reservoir, the HPCI eystem was i declared operable on 6/7/90 at 1811. !
APPARENT CAUSE OF OCCURRENCE i The proximate cause of this incident was moisture and entrained 1 sediment in the quarterly HPCI oil sample. The root cause of the unacceptable oil quality is a design deficiency in the HPCI turbine lube oil reservoir that does not allow for complete draining of the= reservoir during oil changes. The reservoir is ;
not equipped with a drain at the low point. As such, it is possible for water and sludge to collect at the' low point over-time due- to condensation in the reservoir as HPCI room temperatures change.
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LIONSEE DThT 16:KRT (IIR) HXT ENTINUATIW FACILITV KNE (1) DOILT HlMER (2) ' ilR NLMD (6) _ PAGE (3) iTAR \\ NLMR \\ RD' itXE OGIK GMRATING ITIATIW 0 % 00354 d
M -
0 0 9 -
0 0 0 3 T O 3 PREVIOUS OCCURP.ENCES ;
This is the first occurrence, at Hope Creek, of HPCI being declared inoperable due to unacceptable oil cample results.
4 EhEETY BIGNIFICANCE During the time that HPCI was inoperable, all other Emergency I Core Cooling Systems (Core Spray, Low Pressure' Coolant ,
Injection mode of the Residual Heat Removal System, Automatic' '
Depressurization System), as well as the Reactor Core Isolation Cooling system,' wore operable. Technical Specifications allow continued operation of the reactor for up to 14 days with HPCI inoperable. For this reason, the safety significance of 'tlis incident was minimal, and the safe operation of the plant was not compromised.
CORRECTIVE' ACTIONS .
- 1. The. HPCI turbine lube oil reservoir was cleaned, inspected, and the oil replaced. l t
- 2. Samples were drawn of the new lube oil, both from the barrels prior to transfer and after retest run of HPCI.
c? Analysis indicates satisfactory lube oil quality.
- 3. Prior to this occurrence, Systems Engineering had .
initiated a design change to install a drain line at the low point in the reservoir to facilitate periodic draining of accumulated water and sludge. ,
- 4. Systems Engineering will conduct a review of the HPCI lube oil analysis trending program to determine if enhancements are needed to, identify adverse oil quality trends prior to oil quality exceeding acceptable limits.
Sinc rely, J lagan Gene al Manager -
Hope Creek Operations SORC Mtg.90-062 ;
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05000354/LER-1990-008 | LER 90-008-00:on 900604,reactor Bldg Exhaust Radiation Monitor Trip Setpoint Found Nonconservatively High.Caused by Personnel Error.Technicians Disciplined,Rept Reviewed W/All Personnel & Setpoint Included in procedure.W/900705 Ltr | | 05000354/LER-1990-009 | LER 90-009-00:on 900607,HPCI Sys Oil Samples Indicated High Water Content & Traces of Sediment Contamination.Caused by Design Deficiency in HPCI Turbine Lube Oil Reservoir. Reservoir Cleaned,Flushed & Wiped down.W/900705 Ltr | |
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