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LER-1982-121, Forwards LER 82-121/03L-0.Detailed Event Analysis Encl |
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'O PSEG
'~
Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station October 27, 1982 Mr.
R.
C. Haynes Regional Administrator USNRC Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
Dear Mr. Haynes:
LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 82-121/03L Pursuant to the requirements of Salem Generating Station Unit No.
2, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 82-121/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours, e
i H.
J. Midura General Manager -
Salem Operations RF:ks CC:
Distribution ok k
0 S
The Energy People AM 95 21R) (201/) 1181
Report Number:
82-121/03L Report Date:
10-27-82 Occurrence Date:
10-04-82 Facility:
Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
No. 23 Auxiliary Feedwater Pump - Inoperable.
This report was initiated by Incident Reports82-333 and 82-334.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 - Rx Power 82% - Unit Load 900 MWe.
DESCRIPTION OF OCCURRENCE:
At 1703 hours0.0197 days <br />0.473 hours <br />0.00282 weeks <br />6.479915e-4 months <br />, October 4, 1982, during radiographic surveillance of the internals of Check Valve 23MS46, it was discovered that the valve disc had separated from the hanger arm.
The stud on the disc had broken and the portion with the nut and cotter pin were missing.
The valve is a check valve in one of two steam supplies to No. 23 Auxiliary Feedwater Pump (AFP); the pump was declared inoperable and Action Statement 3.7.1.2.a was entered, retroactive to the time of discovery of the problem.
The steam supplies were isolated and tagged in preparation for disassembly of the valve.
At 0345 hours0.00399 days <br />0.0958 hours <br />5.704365e-4 weeks <br />1.312725e-4 months <br />, October 5, 1982, while walking through the unit Inner Penetration Area, the Shift Technical Advisor noticed an excessive amount of steam issuing from the pump vents.
Investi-gation revealed that Valve 23MS45, Steam Isolation to No. 23 AFP was still locked open; Valve 23AF23, Auxiliary Feedwater to No. 23 Steam Generator, had been erroneously closed and tagged.
The valves were immediately placed in the proper positions in accordance with the tagout.
All other valves on the tagout were found in the correct position, with their tags in place.
No. 21 and 22 AFP's and flow paths to the other three steam generators were operable throughout the occurrence.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
A number of problems with this type of valve have occurred, including distortion of the hanger arm and sheared studs on the disc.
An engineering evaluation is being performed to determine the mechanism of the failure.
}
LER 82-121/03L s O
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:The improper tagout resulted from personnel inadvertently operating the incorrect valve.
The locks on the valves involved utilized the same key, allowing the wrong valve to be operated.
Verification of the tagout had been performed, but failed to detect the error.
The same error had occurred on August 18, 1982; due to this and other tagging problems, an investigation into possible underlying causes is underway.
ANALYSIS OF OCCURRENCE:
The operability of the Auxiliary Feedwater System ensures that the Reactor Coolant System can be cooled down to less than 350 F from normal operating conditions in the event of a total loss of offsite power.
The Auxiliary Feedwater System is equipped with two parallel pumping systems for redundancy.
It is designed such that should either pumping system become inoperable the redundant system is fully capable of cooling down the unit.
Only 1 out of the 4 steam generators are necessary to perform this function.
As noted, the redundant system and 3 steam generators were operable throughout the occurrence.
The event, therefore, involved no risk to the health and safety of the general public.
Inoperability of No. 23 Auxiliary Feedwater Pump and the supply to No. 23 Steam Generator constituted operation in a degraded mode permitted by a limiting condition for operation, and is reportable in accordance with Technical Specification 6.9.1.9.b.
Action Statement 3.7.1.2.a requires:
With one Auxiliary Feedwater Pump inoperable, restore the required auxiliary feedwater pumps to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, or be in at least hot stand-by within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and in hot shutdown within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
1 The tagging incident constituted an inadequacy in the implementation of administrative and procedural controls which threatened to reduce the redundancy in engineered safety feature systems.
It is therefore reportable in accordance with Technical Specification 6.9.1.9.c.
CORRECTIVE ACTION
The missing parts of Valve 23MS46 were located and retrieved.
The failed disc and hanger were replaced, and No. 23 AFP was satis-factorily tested.
The pump was declared operable, and at 0247 hours0.00286 days <br />0.0686 hours <br />4.083995e-4 weeks <br />9.39835e-5 months <br />, October 6, 1982, Action Statement 3.7.1.2.a was terminated.
Radio-graphy of the Type MS46 Valves is currently being conducted weekly to provide early, warning of valve failures.
Personnel involved in the tagging deficiency were counseled concerning the incident.
A Supplemental Report will be submitted when both the valve and tagging problems are finally resolved.
,,LER 82-121/03L,
FAILURE DATA:
Velan Valve Corporation 6" Swing Check Valve Type B142114B2TS
- - Prepared By R.
Frahm h
i General Manager -
l Salem Operations l
SORC Meeting No.
82-96 e
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| 05000311/LER-1982-001, Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | | | 05000272/LER-1982-001-03, Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | | | 05000311/LER-1982-001-03, /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | | | 05000272/LER-1982-001, Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-002-01, /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | | | 05000311/LER-1982-002-03, /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | | | 05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | | | 05000311/LER-1982-002, Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Vo | Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Voltage | | | 05000311/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-003-03, /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | | | 05000311/LER-1982-003-03, /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | | | 05000272/LER-1982-004-03, /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | | | 05000272/LER-1982-004, Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | | | 05000311/LER-1982-004, Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-005-01, /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. All C Assemblies Scheduled for Reuse in Core | /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. 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Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | | | 05000272/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006-03, /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | | | 05000272/LER-1982-007-01, /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | | | 05000272/LER-1982-007, Forwards LER 82-007/01X-2 | Forwards LER 82-007/01X-2 | | | 05000272/LER-1982-008, Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | | | 05000272/LER-1982-008-03, /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | | | 05000311/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-008-03, /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | | | 05000311/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-009, Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | | | 05000272/LER-1982-009-03, /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | | | 05000311/LER-1982-009-03, /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | | | 05000311/LER-1982-010-03, /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | | | 05000272/LER-1982-010-03, /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | | | 05000311/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-010, Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-011-03, /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | | | 05000272/LER-1982-011, Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-012, Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-012-03, /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | | | 05000272/LER-1982-012-03, /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | | | 05000272/LER-1982-013-03, /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | | | 05000311/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-013-03, L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | | | 05000272/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-014-03, /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | | | 05000272/LER-1982-014-03, /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | | | 05000311/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | |
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