05000293/LER-1981-015, Updated LER 81-015/03X-1:on 810417,during Surveillance Testing,Nozzle on 23-ft Level Cardox Sys Hose Reel Failed to Deliver Adequate Stream.Caused by Operator Error.Fire Brigade Training revised.W/840319 Ltr

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Updated LER 81-015/03X-1:on 810417,during Surveillance Testing,Nozzle on 23-ft Level Cardox Sys Hose Reel Failed to Deliver Adequate Stream.Caused by Operator Error.Fire Brigade Training revised.W/840319 Ltr
ML20087N262
Person / Time
Site: Pilgrim
Issue date: 03/19/1984
From: Hamilton P, Harrington W
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
BECO-#84-043, BECO-#84-43, LER-81-015-03X, LER-81-15-3X, NUDOCS 8404030276
Download: ML20087N262 (3)


LER-2081-015, Updated LER 81-015/03X-1:on 810417,during Surveillance Testing,Nozzle on 23-ft Level Cardox Sys Hose Reel Failed to Deliver Adequate Stream.Caused by Operator Error.Fire Brigade Training revised.W/840319 Ltr
Event date:
Report date:
2932081015R00 - NRC Website

text

UPDATE REPORT PREVIOUS REPORT ISSUED 5/19/81 u.c. tun.;4a r.ncutarmy camuison n aremvn ov w e r;nM see siso. con y#Td se LICENSEE EVENT REPORT ke (PLEASE PRINT OR TYPE ALL REQutRED INFORMATION)

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EVENT OESCRIPTION ANO PROBABLE CoNSE0uENCES o2 lOn4/17/81,at1130 hours, routine @surveillancetestingwasbeingconductedonl lTl q l the Cardox System hose reels and nozzles. After successfully testing the 51 ft.l

,p ;g level hose station, a test was conducted on the 23 ft. level hose reel and noz- l lol3ll zie. The nozzle failed to deliver an adequate stream. A fire watch was im- l l

lo ls l l mediately established as required by Technical Specifications. Approximately lo l7 ll two hours later, the system was satisf actorily retested and returned to service.]

l o l 8 l l (Ref er to attachment.) This event caused no threat to the public health and saf y.

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l1li ll has determined that the nozzles will not permit C07 discharge unless the trigger l Fire Brigade training l liTill on the hose station actuation valve is fully depressed.

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P. J. Hamilton pgang (617) 746-7900 NAME oF PREPARER

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PILGRIM NUCLEAR POWER STATION DOCKET NO. 50-293 Attachment t 31 -015-03X-1 Description On April 17, 1981, the once a cycle surveillance (8.B.5) was being con-ducted on the Cardox Fire Protection System. This system consists of a storage at a low ur.'t.having temperaturea.(-l'F) capacity of four and low tons which pressure (300 maintains psig). liquid COThesystemks used for fire protection of the cable spreading room, as a supply source for three CO, fire hose stations (23' switchgear, 37' switchgcar and 51' generator area) and for generator purge.

When a CO h ze n zzle is removed from its brackets the mastor selector

/alve for the 2 hose system opens allowing CO2 reach all three nozzles.

C0 can then be discharged by operating the squeeze trigger on the noz-zl  :

The C0 7 hose reel on the 51' elevation was the first tested and was satis-factor?. The 23' elevation was then tested and failed. The 37' elevation was then satisf actorily tested. The testing at the 51' elevation permitted liquid and vaporous CO2 t reach all three hose reels. Heavy frost coating was observed on the pipes during this testing. The 23' elevation was re-tested within minutes and again failed. This CO3 station was declared in-operable, a maintenance request issued and a fire watch established. Two hours later this hose station was satisf actorily tested and declared operable.

Cause and Corrective Action A review of the event by engineering revealed that the cause of the event was due to operator error and not a frozen hose station as described in the previous report. As a result of this followup investigation to the incident, it has been determined that the nozzles will not permit C0 7 dis-charge if the trigger or the handle is not f ully depressed. To elimTnate a recurrence of this incident, the Training Department has revised the Fire Brigade training curriculum and members of the Fire Brigade have been in-structed on the correct method of activating the Cardox System.

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WORTON EDISON COMPANY b 500 GovLaTON STRrrY l BOSTON. MAESACHUSETTs 02199 WILLIAM O. NARRINsTON g.

March 19,1984 BEco. #84- 043 Regional Administrator, Region I U.S. Nuclear Regulatory Connission 631 Park Avenue King of Prussia, PA 19406 Docket Number 50-293 License DPR-35 Gentlemen: l The attached. updated License Event Report 81-015/03X-1 "C02 System Hose Inoperable", is hereby submitted in accordance with the requirements of Pilgrim Nuclear Power Station Technical Specification 6.9.B.2.b.

.If there are any questions on this subject, please do not hesitate to contact the. undersigned.

Very truly yours, 1))

William D. Harrington WDH/mg L

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Enclosures:

LER 81-015/03X-1 cc: Document Control Desk Office of Management Information and Program Control U.S. Nuclear Regulatory Comission Washington, D.C. 20555 Standard BECo. LER distribution Y

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