LER-1978-054, /03L-0 on 781115:during Test of Reactor Water Level,Level Switches L1S-263-57A&B Observed to Trip at Values Greater than Specified in Tech Specs.Caused by Minor Setpoint Drift |
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| 2931978054R03 - NRC Website |
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V-] p ] l T)uring perforn.ance of routine surveil. ance test, Reactor Water Level (RpS/pCIS), 1cvel g j switches LIS.263-57A&ll were Observed 'to trip at values greater than those specified in 3 ]3 ) ; Table 3.2.A of t.he T.S.
These switches provide high water isolatfo. of the main steam yg lines when not 'in the run mode and reac tor pressure is greater than 880 pSIG.
Re-y ; dundant switches with proper setpoints were operable, therefore, public health and l
q safety were not affected.
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The switches were calibrated and tested ;
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The existing surveillance program is considered adequate to detect gl problems of this type, therefore, no further corrective action is contemplated.
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