05000285/FIN-2013018-01
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Finding | |
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Title | Failure to Correctly Translate Design Requirements into Installed Plant Configuration |
Description | The team identified a violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, associated with the licensees failure to assure that applicable regulatory requirements and the design bases, as defined in 10 CFR 50.2 and as specified in the license application, for those structure, systems and components to which this appendix applies, were correctly translated into specifications, drawings, procedures, and instructions. Specifically, from initial construction through October 2013, the licensee failed to fully incorporate applicable design requirements for components needed to ensure the capability to shut down the reactor and maintain it in a safe shutdown condition following a high energy line break. The licensee addressed this deficiency by reconstituting the design analysis associated with the high energy line break and environmental qualification programs, receiving a change to the facilities licensing basis, and implementing plant modifications. This issue was entered into the licensees corrective action program as Condition Report CR 2013-2857. The failure to ensure that design requirements were correctly translated into installed plant equipment was a performance deficiency. This performance deficiency was more than minor, and therefore a finding, because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensees failure to translate the design requirements into installed plant equipment resulted in a condition where structures, systems, and components necessary to mitigate the effects of a high energy line break may not have functioned as required. The team evaluated the finding using Inspection Manual Chapter (IMC) 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, and determined that this finding required a detailed risk evaluation because it was a deficiency affecting the design and qualification of a mitigating structure, system, or component that resulted in a loss of operability or functionality and represented a loss of system and/or function.
NOV- 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part, that, measures shall be established to assure that applicable regulatory requirements and the design bases, as defined in 10 CFR 50.2 and as specified in the license application, for those structure, systems and components to which this appendix applies, are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, from initial construction through October 2013, the licensee failed to assure that applicable regulatory requirements and the design bases, as defined in 10 CFR 50.2 and as specified in the license application, for those structure, systems and components to which this appendix applies, were correctly translated into specifications, drawings, procedures, and instructions. Specifically, the licensee failed to fully incorporate applicable design requirements to ensure that components subjected to a harsh environment maintained the capability to shut down the reactor and maintain it in a safe shutdown condition following a postulated high energy line break. This deficiency adversely affected a number of systems and components required for safe shutdown including auxiliary feedwater, charging, containment isolation, containment cooling, and shutdown cooling. This violation is associated with a White Significance Determination Process Finding. |
Site: | Fort Calhoun |
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Report | IR 05000285/2013018 Section 1R21 |
Date counted | Dec 31, 2014 (2014Q4) |
Type: | Violation: White |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.21 |
Inspectors (proximate) | A Vegel C Smith J Josey J Wingebach N Patel T Lighty |
Violation of: | 10 CFR 50 Appendix B Criterion III, Design Control |
INPO aspect | |
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Finding - Fort Calhoun - IR 05000285/2013018 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Fort Calhoun) @ 2014Q4
Self-Identified List (Fort Calhoun)
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