Similar Documents at Salem |
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LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl |
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PSEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station March 8, 1983 Mr.
R. C. Haynes Regional Administrator USNRC Region 1 631 Park Avenue Kirig of Prussia, Pennsylvania 19406
Dear Mr. Haynes:
IICENSE NO. DPR-70 DUCKET YO. 50-272 Rff?ORTALLE OCCURRENCE 83- 010/03L Pursuant to the requirements of Salem Generating Station Unit No, 1, Technical Specificaticns, Section 6.9.1.9.b, we are sQmitting Li.censee Event F.eport for Reportable Occuirence 83-010/03L.
This report is required within thirty (?0) days of the occurrence.
Sincerely yours, lle \\}<blwJ H. J.
Midura General Manager -
Salem Operations RF:ks CC:
Distribution T
Q 8303180361 830308 PDR ADOCK 05000272 S
PDR The Energy People
% vmaw: n m a
R0 port Nunbsr:
83-010/03L Report Date:
03-07-83 Occurrence Date:
02-05-83 Facility:
Salem Generating Station Unit 1 Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Containment Systems - Containment Type B and C Leak Rate -
Out-of-Specification.
This report was initiated by Incident Report 82-118.
.CMQ1TIONS PRI.01 TO GCIUl!EElqE:
Mode 5 - RX Power 0 $ - Unit Load 0 MNe.
DESC_RIETION OF GCCURRENCS:
From October 16, 1982 to February 5. 1983, during a scheduled refueling, routine surveillance of Containment Type B and C ccmponents revealed three containrent isolztion valves with leakage rates greater than the maximum range of the leak rate test equipment (20,000 secm).
Tne components involved were Containmerit isolation Valves 1CC215, 14GB4 and 1VC8.
Since actual leakage due to each vcive could nct be ascertained, it was not possible to demonstrate that the total Type E and C leakage was less than 0.60 La as required by Technical Specifications Limiting Condition for Operation 3.6.1.2b (applicable only in Modes'l through 4).
The integrity of redundant containment boundaries had been maintained during previous operation; total leakage past redundant containment isolation valves did not constitute an abnormal portion of the total allowable leakage.
The valves involved were repaired and satisfactorily tested; combined Type B and C leakage was determined to be within specification prior to returning to Mode 4 operation.
APPARENT CAUSE OF OCCURRENCE:
Investigation revealed that the stroke of Valves 1CC215 and 1VC8 was out of adjustment.
Disassembly of Steam Generator Blowdown Valve 14GB4 revealed that the valve seating surfaces were damaged by wire cutting.
Both Valves 1CC215 and 14GB4 had failed the previous leak
. rate testing in 1980-81, and had been reworked at that time.
The range of the test equipment in use at the time, however, was insufficient to allow quantification of lesser leakage (maximum range 2,000secm).
ANALYSIS OF OCCURRENCE:
The limitations on containment leakage rates ensure that the total containment leakage volume will not exceed the value assumed in the accident analyses at the peak accident pressure of 47 psig.
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LER'83-010/03L
' ANALYSIS OF OCCURRENCE: (cont'd) i Action. Statement 3.6.1.2Erequires:
With eitherfthe measured overall integrated containment-leakage rate exceeding 0.75.La, or with the. measured combined leakage 4
rate-for_all penetrations and valves subject to Type B and C tests exceeding 0.60 La, rest' ore the leakage rate (s) to within i
'the_ limit (s) prior to increasing the Reactor Coolant System (RCS)
- - temperature-above 200 F.
[
Leakage? rate limits 'during performance of-periodic tests incorporate conservatism to account for possible. degradation of the leakage
. barriers between testing.
The combined leakage rate had previously been demonstrated within specification during leak rate cesting. n i
1980-81.. As roted, the valves were~ repaired and total leakage was
- - demonstrated to;be within, specification during the recent testing.
Finally. redundant barriers and therefore containment integrity were maintained.
The occurrence thue. did not involve any riek to the health and safety of the public.
Due to the loss of redundancy in containment barriers, the,cVent constituted operation in a degraded mode permitted by a liniting' condition for operation.
The occurence is reportable in accordance with Technical Specification 6.9.1.9b.
CORRECTIVE ACTION
Valves 1CC215 and 1VC8 were restroked and satisfactorily tested.
. Valve 14GB4 internals were reworked, the gasket and packing were replaced, and the valve was also satisfactorily tested.
With the valves repaired, and no further problems ~ encountered, on: February 5, 1983, the' final results of Type B'and C leak rate testing demonstrated
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combined leakage was within. specification.
Due to the recurrence'of excessive leakage by two'of the valves, particularly Valve 14GB4, the Nuclear Engineering Department was notified of the cccurrence.
Appropriate corrective action will be implemented pending investigation of the problems.
FAILURE DATA:
- Masoneilan International, Inc.
3 inch Control Valve t
Model-38-20721 i
" Prepared By R.
Frahm dendral Manager -
3 l
Salem Operations l
.SORC Meeting No.89-028 4
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b
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| 05000272/LER-1983-001-03, /03L-0:on 830104,vital Bus 1B Tripped,Rendering RHR Loop Inoperable.Caused by Differential Relay Protection. Redundant RHR Loop Immediately Placed in Operation | /03L-0:on 830104,vital Bus 1B Tripped,Rendering RHR Loop Inoperable.Caused by Differential Relay Protection. Redundant RHR Loop Immediately Placed in Operation | | | 05000311/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-001-03, /03L-0:on 830106,reactor Trip Breaker a Failed to Open Following Reactor Trip.Caused by Malfunctioning Breaker Undervoltage Relay Due to Binding of Relay Mechanism by Dirt or Corrosion.Breaker Replaced.Periodic Insp Initiate | /03L-0:on 830106,reactor Trip Breaker a Failed to Open Following Reactor Trip.Caused by Malfunctioning Breaker Undervoltage Relay Due to Binding of Relay Mechanism by Dirt or Corrosion.Breaker Replaced.Periodic Insp Initiated | | | 05000311/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-002-03, /03L-0:on 830314,discovered Pressurizer Code Safety Valves 2PR3,2PR4 & 2PR5,tested by Wyle Labs During 830224-25,lifted Below 2,485 Psig Plus/Minus 1% Pressure Range & Displayed Heavy Audible & Visual Seat Leakage | /03L-0:on 830314,discovered Pressurizer Code Safety Valves 2PR3,2PR4 & 2PR5,tested by Wyle Labs During 830224-25,lifted Below 2,485 Psig Plus/Minus 1% Pressure Range & Displayed Heavy Audible & Visual Seat Leakage | | | 05000272/LER-1983-002-01, /01T-0:on 830106,station Power Transformer 12 de-energized for Planned Maint.Loss of Power to Automatic Starting Feature on Both Diesel Fire Pumps Resulted.Caused by Oversight Due to Human Error.Personnel Counseled | /01T-0:on 830106,station Power Transformer 12 de-energized for Planned Maint.Loss of Power to Automatic Starting Feature on Both Diesel Fire Pumps Resulted.Caused by Oversight Due to Human Error.Personnel Counseled | | | 05000272/LER-1983-003, Forwards LER 83-003/04L-0.Detailed Event Analysis Encl | Forwards LER 83-003/04L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-003-04, /04L-0:on 830121,during Commencement of Refueling Shutdown for Unit 2,Unit 1 Restart Delayed Approx 7 Wks. Caused by Problems W/Steam Generator Nozzle Dams & Degradation of Welds in Svc Water Piping | /04L-0:on 830121,during Commencement of Refueling Shutdown for Unit 2,Unit 1 Restart Delayed Approx 7 Wks. Caused by Problems W/Steam Generator Nozzle Dams & Degradation of Welds in Svc Water Piping | | | 05000311/LER-1983-003-03, /03L-0:on 830111,rod Position Indicator Channel 1SA2 Indicated Approx Half Scale,Contrary to Flux Map Indication That No Change in Rod Position Occurred.Caused by Failed Signal Conditioner.Module Replaced | /03L-0:on 830111,rod Position Indicator Channel 1SA2 Indicated Approx Half Scale,Contrary to Flux Map Indication That No Change in Rod Position Occurred.Caused by Failed Signal Conditioner.Module Replaced | | | 05000311/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-004-04, /04L-0:on 830317,during Gaseous Effluent Testing, Iodine/Particulate Collection Device Sample Pump Deenergized.Caused by Not Including Pump on Electrical Distribution List.Tagging Sys Will Be Revised | /04L-0:on 830317,during Gaseous Effluent Testing, Iodine/Particulate Collection Device Sample Pump Deenergized.Caused by Not Including Pump on Electrical Distribution List.Tagging Sys Will Be Revised | | | 05000311/LER-1983-004, Forwards LER 83-004/04L-0.Detailed Event Analysis Encl | Forwards LER 83-004/04L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-004, Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-004-03, /03L-0:on 830124,equipment Operator Discovered Leak on Diesel Generator 1B Jacket Water Sys.Caused by Cracked Piping Nipple Due to Personnel Standing on Jacket Water Sys Piping.Cracked Nipple Replaced | /03L-0:on 830124,equipment Operator Discovered Leak on Diesel Generator 1B Jacket Water Sys.Caused by Cracked Piping Nipple Due to Personnel Standing on Jacket Water Sys Piping.Cracked Nipple Replaced | | | 05000311/LER-1983-005-03, /03X-1:on 830122,both Channels of Pressurizer Overpressurization Protection Sys Declared Inoperable Due to Leakage in Pressurizer Relief Lines.Porv Plugs Replaced & PORV Circuitry Modified | /03X-1:on 830122,both Channels of Pressurizer Overpressurization Protection Sys Declared Inoperable Due to Leakage in Pressurizer Relief Lines.Porv Plugs Replaced & PORV Circuitry Modified | | | 05000311/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-005-03, /03L-0:on 830121,RHR Sys Automatic Isolation Function Not Tested Prior to Placing RHR Sys in Operation. Caused by Procedure Problems & Personnel Inexperience. Procedures Revised | /03L-0:on 830121,RHR Sys Automatic Isolation Function Not Tested Prior to Placing RHR Sys in Operation. Caused by Procedure Problems & Personnel Inexperience. Procedures Revised | | | 05000311/LER-1983-006-04, /04L-0:on 830408,decreased Sensitivity of Channel 2R41C Plant Vent Noble Gas Monitor Rendered Waste Gas Discharge Line Automatic Isolation Feature Inoperable.Caused by Leakage on Monitor Sample Lines & Internal Connections | /04L-0:on 830408,decreased Sensitivity of Channel 2R41C Plant Vent Noble Gas Monitor Rendered Waste Gas Discharge Line Automatic Isolation Feature Inoperable.Caused by Leakage on Monitor Sample Lines & Internal Connections | | | 05000311/LER-1983-006, Forwards LER 83-006/04L-0.Detailed Event Analysis Encl | Forwards LER 83-006/04L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-006-03, /03L-0:on 830126 & 28 Nonseismically Qualified Components & Power Boxes Discovered Installed in Dc Control Power Feeds to Emergency Diesel Generators.Caused by Personnel Oversight.Power Box Components Replaced | /03L-0:on 830126 & 28 Nonseismically Qualified Components & Power Boxes Discovered Installed in Dc Control Power Feeds to Emergency Diesel Generators.Caused by Personnel Oversight.Power Box Components Replaced | | | 05000272/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-007, Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days | Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days | | | 05000272/LER-1983-007-03, /03L-0:on 830129,control Room Operator Discovered Low Flow Through Number 14 Reactor Coolant Loop Resistance Thermometer Detector Bypass.Caused by Obstruction in Hot Leg Flowpath.Hot Leg Cycled & Bypass Flow Restored to Norm | /03L-0:on 830129,control Room Operator Discovered Low Flow Through Number 14 Reactor Coolant Loop Resistance Thermometer Detector Bypass.Caused by Obstruction in Hot Leg Flowpath.Hot Leg Cycled & Bypass Flow Restored to Normal | | | 05000272/LER-1983-007, Forwards LER 83-007/03L-0.Detailed Event Analysis Encl | Forwards LER 83-007/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-007-01, /01T-0:on 830210 & 11,during Routine Surveillance Testing,Two Steam Generator Snubbers Failed to Meet Acceleration & Bleed Test Requirements.Caused by Aging of Snubber Piston Seal Rubber Matl.Seals Will Be Rebuilt | /01T-0:on 830210 & 11,during Routine Surveillance Testing,Two Steam Generator Snubbers Failed to Meet Acceleration & Bleed Test Requirements.Caused by Aging of Snubber Piston Seal Rubber Matl.Seals Will Be Rebuilt | | | 05000272/LER-1983-008, Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating Conditions | Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating Conditions | | | 05000272/LER-1983-008-03, /03L-0:on 830311,discovered Pressurizer Code Safety Valves Tested for Lift Set Pressure & Seat Leakage by Wyle Labs During 821102-13 Lifted in Excess of Tech Specs & Exhibited Heavy Seat Leakage.Cause Undetermined | /03L-0:on 830311,discovered Pressurizer Code Safety Valves Tested for Lift Set Pressure & Seat Leakage by Wyle Labs During 821102-13 Lifted in Excess of Tech Specs & Exhibited Heavy Seat Leakage.Cause Undetermined | | | 05000311/LER-1983-008-99, /99X-0:on 830218,diesel Generator Area Low Pressure Carbon Monoxide Sys Automatic Initiation Feature Disabled & Tagged Out for Planned Maint.Continuous Fire Watch Established.On 830131,event Became Reportable | /99X-0:on 830218,diesel Generator Area Low Pressure Carbon Monoxide Sys Automatic Initiation Feature Disabled & Tagged Out for Planned Maint.Continuous Fire Watch Established.On 830131,event Became Reportable | | | 05000311/LER-1983-008, Forwards LER 83-008/99X-0.Detailed Event Anaysis Encl | Forwards LER 83-008/99X-0.Detailed Event Anaysis Encl | | | 05000272/LER-1983-009-99, /99X-0:on 830130,during Routine Plant Cooldown, Inadvertent Safety Injection Occurred Due to Low Pressurizer Pressure.Caused by Operator Overlooking Decreasing Pressure. All safety-related Equipment Functioned as Designed | /99X-0:on 830130,during Routine Plant Cooldown, Inadvertent Safety Injection Occurred Due to Low Pressurizer Pressure.Caused by Operator Overlooking Decreasing Pressure. All safety-related Equipment Functioned as Designed | | | 05000272/LER-1983-009, Forwards LER 83-009/99X-0.Detailed Event Analysis Encl | Forwards LER 83-009/99X-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-009, Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-009-03, /03L-0:on 830203,during Shutdown Operation,Sample Analysis of RCS Boron Concentration Revealed Concentration Less than Tech Spec Limit.Caused by Hydrolazing Steam Generators.Rcs Boration Performed to Maintain Concentration | /03L-0:on 830203,during Shutdown Operation,Sample Analysis of RCS Boron Concentration Revealed Concentration Less than Tech Spec Limit.Caused by Hydrolazing Steam Generators.Rcs Boration Performed to Maintain Concentration | | | 05000272/LER-1983-010-03, /03L-0:from 821016-830205,during Testing of Type B & C Components,Three Containment Isolation Valves Exhibited Leakage Rates in Excess of Test Equipment Range. Valves 1CC215 & 1VC8 Restroked.Valve 14GB4 Reworked | /03L-0:from 821016-830205,during Testing of Type B & C Components,Three Containment Isolation Valves Exhibited Leakage Rates in Excess of Test Equipment Range. Valves 1CC215 & 1VC8 Restroked.Valve 14GB4 Reworked | | | 05000311/LER-1983-010-03, /03L-0:on 830126,during Shutdown Operations, Control Air Header 21 Isolated & Tagged for Leak Rate Testing.Porv 2PR1 Closed Resulting in Loss of RCS Vent Path. Caused by Surge in Header 22 Due to Failed Valve | /03L-0:on 830126,during Shutdown Operations, Control Air Header 21 Isolated & Tagged for Leak Rate Testing.Porv 2PR1 Closed Resulting in Loss of RCS Vent Path. Caused by Surge in Header 22 Due to Failed Valve | | | 05000311/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-011, Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-011-03, /03L-0:on 830401,discovered That Monthly Testing of Control Room Emergency Air Conditioning Sys Was Overlooked.Caused by Insp Order Sys Card Requiring Testing Being Erroneously Stated.Card Revised | /03L-0:on 830401,discovered That Monthly Testing of Control Room Emergency Air Conditioning Sys Was Overlooked.Caused by Insp Order Sys Card Requiring Testing Being Erroneously Stated.Card Revised | | | 05000311/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-012-01, /01T-0:on 830222,during Startup,Reactor Manually Tripped.Caused by Rapidly Decreasing Steam Generator Levels. Manual Trip Obscured Failure of Trip Breakers to Open Automatically.Plant Cooldown Commenced | /01T-0:on 830222,during Startup,Reactor Manually Tripped.Caused by Rapidly Decreasing Steam Generator Levels. Manual Trip Obscured Failure of Trip Breakers to Open Automatically.Plant Cooldown Commenced | | | 05000311/LER-1983-012-03, /03L-0:on 830406,10-ton Cardox Sys Pilot Valve Found in Closed Position & All Low Pressure Sys Declared Inoperable.Caused by Inadequacies in Sys Recharging Operation on 830304.Procedures Revised | /03L-0:on 830406,10-ton Cardox Sys Pilot Valve Found in Closed Position & All Low Pressure Sys Declared Inoperable.Caused by Inadequacies in Sys Recharging Operation on 830304.Procedures Revised | | | 05000311/LER-1983-012, Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-013, Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-013-99, /99T-0:on 830215,calculated Moderator Temp Coefficient (Mtc) Value for All Control Rods Withdrawn Found More Positive than Tech Spec Allowance But within Expected Deviation.Limitation on Withdrawal Will Be Maintained | /99T-0:on 830215,calculated Moderator Temp Coefficient (Mtc) Value for All Control Rods Withdrawn Found More Positive than Tech Spec Allowance But within Expected Deviation.Limitation on Withdrawal Will Be Maintained | | | 05000311/LER-1983-013-03, /03L-0:on 830409,during Routine Shutdown,Lube Oil Temp Increases Observed on Charging Pump 22.Caused by Restricted Svc Water Flow to Pump Due to Oyster Shells & Miscellaneous Mollusks.Shells Removed | /03L-0:on 830409,during Routine Shutdown,Lube Oil Temp Increases Observed on Charging Pump 22.Caused by Restricted Svc Water Flow to Pump Due to Oyster Shells & Miscellaneous Mollusks.Shells Removed | | | 05000272/LER-1983-013, Forwards LER 83-013/99T-0.Detailed Event Analysis Encl | Forwards LER 83-013/99T-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-014-03, /03L-1:on 830413 & 18,operating Loads on 2A 4kV & 460-volt Vital Buses Observed to Trip.Caused by Spurious Operation of Safeguards Equipment Control Sys Due to Design Deficiencies.Equipment Restarted | /03L-1:on 830413 & 18,operating Loads on 2A 4kV & 460-volt Vital Buses Observed to Trip.Caused by Spurious Operation of Safeguards Equipment Control Sys Due to Design Deficiencies.Equipment Restarted | | | 05000272/LER-1983-014, Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | |
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