Similar Documents at Salem |
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LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl |
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PS~G Public Service Electric and Gas Companv P.O. Box E Hancocks Bridge. New Jersev qf.Q.38 Salem Generating Station'-.
February 2 2, 19 8 3 Mr. R. C. Haynes Regional Administrator USN RC Region 1 631 Park Avenue King of Prussia, Pennsylvania
Dear Mr. Haynes:
LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 83~005/03L 19406 Pursuant to the requirements of Salem.Generating Station Unit No.. 2, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for_~eportable Occ,urrence 83-005/03L.
This* report is. required within.
thirty (30) days of the ocriurrence.
CC:
Pistribution
- sincerely yours, H. J. Midura General !1anager Salem Operations
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Repor:t Number:
Report Date:
83'-005/03L 02-17-83 Occurren~e Date:
01-22-8~
Facility:
Salem Generating *station Unit 2 Publiq S~rvice Electric & Gaa Company Hancock's Bridge, New Jerse¥ 08038 IDENTIFICATION OF QCCURR~:
Reactor Coolant System -
Pressuriz~r Overpressure Protection System -
Inoperable.
This report was initiated by Incident Report 83-b20.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 4 -
RX Power 0 % - Unit Load 0 MWe.
DESCRIPTION QF QC-CURRENCE:
January a1, 1983, during the planned shutdown for refu~ling Df-Salem Unit 2, a cooldown *or the Reactor CooLant System (RCS) was initiated.
Due to leakage problems with the power operated relief valves (PORVs),
Block Valves 2PR6 and 2FR7 had been closed since prior to unit startup in October, 19~1 (See LER 81-59/03X-1);
- Isol-atf-oh of *the relief 'line-s*
had rendered Pressurizer Ovetpressurization Protection System (POPS)
Val v es 2 PR 4 7 and 2 PR 4 8 in operable.
- In accordance with established ~roceduie, the POPS would first b~ -
demonst~ated operable then would.be placed in operation when RCS tempera t_ure reached 312°F.:. A. bubqle would be* mai ntai ne*d, and*..
- foll~wing degasifi-cation and fUrt~er cooldown*to i8o°F, -~ cleanup ot
.the RGS would be conductetj utilizing Reactor Coolant Pumps and
- .hyd.rogen peroxide addition.. *"After co'mpletion of the cleanup',* "the pressuriz*er would be cooled down, the RCS taken sblid and a vent establisped.
Attempts to demonstrate the operability ~f_the POPS valves failed due to excessive leakage in the pressurizer relief lines.
In view of the recurrent problems with the relief valves, and the resultant questionable status of the POPS, the cooldown was continued to place the plant in a vented, safe condition.
At 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />, January 22, 1983, when the RCS ~emperature reached 3 1 2 o F, Ac ti on St a t em en t f. 4. 1 0
The pr e-s s u r i z e r relief line valves were cycled and reseated in at'temp.t.s to reduce 1 ea k a g e and re store at 1 ea s t one. P 0 P s*- ch an n e 1 to an <JP er ab 1 e status.
The attempts failed, however, and at 1930 hour0.0223 days <br />0.536 hours <br />0.00319 weeks <br />7.34365e-4 months <br />s~ Ja~uary 22, 1983, Action Statement 3.0.3 came into effect~
_,,. /
The cooldown was continued in orderly fasfif0n,~uritil 0423 hours0.0049 days <br />0.118 hours <br />6.994048e-4 weeks <br />1.609515e-4 months <br />, January 23, when the leakage on Valve 2PR47 was reduced to an acceptable level.
The valve was declared operable, and with only one
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LER 83-005/03L.-*-
DESCRIPTION OF OCCURRENCE: (cont I q)
POPS channel.fnop:erabl.e, Action_Statem...e.p,t 3.4.10.3a awied.
_Tpe cool down was subsequently completed, and'-at. 1242 hours0.0144 days <br />0.345 hours <br />0.00205 weeks <br />4.72581e-4 months <br />;--January-24, 1983, an RCS vent was established.
A bubbi~~in the pressurizer was maintained until one POPS valve was operable,'~nd no RC~ pressure transients were involv~d.
The integrity of multiple fission product barriers was ma._:Ln-t-rlffe{:r_ th_roughout the occurrence.
APPARENT CAUSE OF OCCURRENCE:
POPS Valves 2PR47 and 2PR48 had been reworked.due to excessive leakage during initial fueling of the unit in 1980 (See LER 80-05/03L).
Valve 2PR47 had exhibited similar problems during shuydown operatiori in 1981 (See LER 81-43/03L).
As noted, in October 1981 1
during the plant startup, the pressurizer relief lines had been isolated to stop leakage from the PORVs; Unit 2 was then operat~d at power until the current shutdown for refueling, when the problems with the POPS valves were re-encountered.
Further investigation of the problems is pending disassembly of the valves, which is scheduled for the current refueling.
ANALYSIS OF OCCURRENCE:
The operability of two POPS valves or _9n RCS vent opening of greater than 3.14 square inches ensures that the RCS will be protected from pressure transients which could exceed the limits of 10 CFR 50 Appendix G when one or more RGS cold.legs are l"Ef*ss* than.or equal to 312°F.
- Either P6PS has adequate relieving capability to p~otect the RCS from overpressurization resulting from e.vents~--postulated. to occur including.starting. an idle reactor. coolant pump or a. safety injection pump with a solid RCS.
- *Action S~atem~nt. 3.4.l0.3b requ~res~
With both POPs in6perable, depressuriie and vent the. RCS thfoug~.
- a*3.1.4-squ*are(-in-ch*_.vent(s) w*ithin; 8 hour*s.
As noted, due to plant conditions, the RCS vent could not be established within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> as required, and Action ~tatement 3.0.3 applied.
Th*e action statement requires:
When a.limiting condition ~or operation is not met except as provided in the associated action statements, within one hour action shall be initiated to place the unit in a mode in which the specification does not apply, by placing it; as applicable, in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, hot sh~tdown within the following* 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, -and cord shutctown wtthin-the subsequent 2 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
Where corrective m-ea s ~t._es _ia:re completed that permit operation under the ~etion retjuirem~nts, the action may be taken in accordance with th~ speciri ed... time limits as measured from the time of the fai~ure to mee~ the limiting.
condition for operation.
As mentioned, a plant cooldown was already in progress, and thus action was being taken to e~tablish the required RCS vent within 24
LER 83-005/03L hours, in compliance with the limiting condftion for*- opera ti on-~
With the restoratlon of one POPS channel to an* ~perable status, Action Statement 3.4.10~3a came into effect requiring:
With one POPS inoperable, restore the inoperable POPS to operable status within 7 days or depressurize and.. vent the ~CS through a 3.14 square inch vent(s) within the next B hours.
The POPS is designed t"o.. protect the integrity of the RCS Pressure Boundary, one of the multiple fission product* boundaries required by 10 CFR 50 (others includ~ the containment and cladding).
As noted, the integrity of all fission product boundaries was maintained.
For this reason, and since one operable channel was obtained and the vent was established within the intervals specified, nc risk to the health and safety of the public ~as involved.
The event constituted operation in a degraded mode permitted by a limiting. condition for operation, and is reportable in accordance with Technical Specification 6.9.1.9b.
CORRECTIVE ACTION
FAILURE DATA; Marotta Scientific Controls Relief Valve Model. MV-225-c Prepared By R. Frahm SORC~-Meeting No.83-019'*
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Gene anager -
Salem Operations
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| 05000272/LER-1983-001-03, /03L-0:on 830104,vital Bus 1B Tripped,Rendering RHR Loop Inoperable.Caused by Differential Relay Protection. Redundant RHR Loop Immediately Placed in Operation | /03L-0:on 830104,vital Bus 1B Tripped,Rendering RHR Loop Inoperable.Caused by Differential Relay Protection. Redundant RHR Loop Immediately Placed in Operation | | | 05000311/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-001-03, /03L-0:on 830106,reactor Trip Breaker a Failed to Open Following Reactor Trip.Caused by Malfunctioning Breaker Undervoltage Relay Due to Binding of Relay Mechanism by Dirt or Corrosion.Breaker Replaced.Periodic Insp Initiate | /03L-0:on 830106,reactor Trip Breaker a Failed to Open Following Reactor Trip.Caused by Malfunctioning Breaker Undervoltage Relay Due to Binding of Relay Mechanism by Dirt or Corrosion.Breaker Replaced.Periodic Insp Initiated | | | 05000311/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-002-03, /03L-0:on 830314,discovered Pressurizer Code Safety Valves 2PR3,2PR4 & 2PR5,tested by Wyle Labs During 830224-25,lifted Below 2,485 Psig Plus/Minus 1% Pressure Range & Displayed Heavy Audible & Visual Seat Leakage | /03L-0:on 830314,discovered Pressurizer Code Safety Valves 2PR3,2PR4 & 2PR5,tested by Wyle Labs During 830224-25,lifted Below 2,485 Psig Plus/Minus 1% Pressure Range & Displayed Heavy Audible & Visual Seat Leakage | | | 05000272/LER-1983-002-01, /01T-0:on 830106,station Power Transformer 12 de-energized for Planned Maint.Loss of Power to Automatic Starting Feature on Both Diesel Fire Pumps Resulted.Caused by Oversight Due to Human Error.Personnel Counseled | /01T-0:on 830106,station Power Transformer 12 de-energized for Planned Maint.Loss of Power to Automatic Starting Feature on Both Diesel Fire Pumps Resulted.Caused by Oversight Due to Human Error.Personnel Counseled | | | 05000272/LER-1983-003, Forwards LER 83-003/04L-0.Detailed Event Analysis Encl | Forwards LER 83-003/04L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-003-04, /04L-0:on 830121,during Commencement of Refueling Shutdown for Unit 2,Unit 1 Restart Delayed Approx 7 Wks. Caused by Problems W/Steam Generator Nozzle Dams & Degradation of Welds in Svc Water Piping | /04L-0:on 830121,during Commencement of Refueling Shutdown for Unit 2,Unit 1 Restart Delayed Approx 7 Wks. Caused by Problems W/Steam Generator Nozzle Dams & Degradation of Welds in Svc Water Piping | | | 05000311/LER-1983-003-03, /03L-0:on 830111,rod Position Indicator Channel 1SA2 Indicated Approx Half Scale,Contrary to Flux Map Indication That No Change in Rod Position Occurred.Caused by Failed Signal Conditioner.Module Replaced | /03L-0:on 830111,rod Position Indicator Channel 1SA2 Indicated Approx Half Scale,Contrary to Flux Map Indication That No Change in Rod Position Occurred.Caused by Failed Signal Conditioner.Module Replaced | | | 05000311/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-004-04, /04L-0:on 830317,during Gaseous Effluent Testing, Iodine/Particulate Collection Device Sample Pump Deenergized.Caused by Not Including Pump on Electrical Distribution List.Tagging Sys Will Be Revised | /04L-0:on 830317,during Gaseous Effluent Testing, Iodine/Particulate Collection Device Sample Pump Deenergized.Caused by Not Including Pump on Electrical Distribution List.Tagging Sys Will Be Revised | | | 05000311/LER-1983-004, Forwards LER 83-004/04L-0.Detailed Event Analysis Encl | Forwards LER 83-004/04L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-004, Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-004-03, /03L-0:on 830124,equipment Operator Discovered Leak on Diesel Generator 1B Jacket Water Sys.Caused by Cracked Piping Nipple Due to Personnel Standing on Jacket Water Sys Piping.Cracked Nipple Replaced | /03L-0:on 830124,equipment Operator Discovered Leak on Diesel Generator 1B Jacket Water Sys.Caused by Cracked Piping Nipple Due to Personnel Standing on Jacket Water Sys Piping.Cracked Nipple Replaced | | | 05000311/LER-1983-005-03, /03X-1:on 830122,both Channels of Pressurizer Overpressurization Protection Sys Declared Inoperable Due to Leakage in Pressurizer Relief Lines.Porv Plugs Replaced & PORV Circuitry Modified | /03X-1:on 830122,both Channels of Pressurizer Overpressurization Protection Sys Declared Inoperable Due to Leakage in Pressurizer Relief Lines.Porv Plugs Replaced & PORV Circuitry Modified | | | 05000311/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-005-03, /03L-0:on 830121,RHR Sys Automatic Isolation Function Not Tested Prior to Placing RHR Sys in Operation. Caused by Procedure Problems & Personnel Inexperience. Procedures Revised | /03L-0:on 830121,RHR Sys Automatic Isolation Function Not Tested Prior to Placing RHR Sys in Operation. Caused by Procedure Problems & Personnel Inexperience. Procedures Revised | | | 05000311/LER-1983-006-04, /04L-0:on 830408,decreased Sensitivity of Channel 2R41C Plant Vent Noble Gas Monitor Rendered Waste Gas Discharge Line Automatic Isolation Feature Inoperable.Caused by Leakage on Monitor Sample Lines & Internal Connections | /04L-0:on 830408,decreased Sensitivity of Channel 2R41C Plant Vent Noble Gas Monitor Rendered Waste Gas Discharge Line Automatic Isolation Feature Inoperable.Caused by Leakage on Monitor Sample Lines & Internal Connections | | | 05000311/LER-1983-006, Forwards LER 83-006/04L-0.Detailed Event Analysis Encl | Forwards LER 83-006/04L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-006-03, /03L-0:on 830126 & 28 Nonseismically Qualified Components & Power Boxes Discovered Installed in Dc Control Power Feeds to Emergency Diesel Generators.Caused by Personnel Oversight.Power Box Components Replaced | /03L-0:on 830126 & 28 Nonseismically Qualified Components & Power Boxes Discovered Installed in Dc Control Power Feeds to Emergency Diesel Generators.Caused by Personnel Oversight.Power Box Components Replaced | | | 05000272/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-007, Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days | Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days | | | 05000272/LER-1983-007-03, /03L-0:on 830129,control Room Operator Discovered Low Flow Through Number 14 Reactor Coolant Loop Resistance Thermometer Detector Bypass.Caused by Obstruction in Hot Leg Flowpath.Hot Leg Cycled & Bypass Flow Restored to Norm | /03L-0:on 830129,control Room Operator Discovered Low Flow Through Number 14 Reactor Coolant Loop Resistance Thermometer Detector Bypass.Caused by Obstruction in Hot Leg Flowpath.Hot Leg Cycled & Bypass Flow Restored to Normal | | | 05000272/LER-1983-007, Forwards LER 83-007/03L-0.Detailed Event Analysis Encl | Forwards LER 83-007/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-007-01, /01T-0:on 830210 & 11,during Routine Surveillance Testing,Two Steam Generator Snubbers Failed to Meet Acceleration & Bleed Test Requirements.Caused by Aging of Snubber Piston Seal Rubber Matl.Seals Will Be Rebuilt | /01T-0:on 830210 & 11,during Routine Surveillance Testing,Two Steam Generator Snubbers Failed to Meet Acceleration & Bleed Test Requirements.Caused by Aging of Snubber Piston Seal Rubber Matl.Seals Will Be Rebuilt | | | 05000272/LER-1983-008, Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating Conditions | Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating Conditions | | | 05000272/LER-1983-008-03, /03L-0:on 830311,discovered Pressurizer Code Safety Valves Tested for Lift Set Pressure & Seat Leakage by Wyle Labs During 821102-13 Lifted in Excess of Tech Specs & Exhibited Heavy Seat Leakage.Cause Undetermined | /03L-0:on 830311,discovered Pressurizer Code Safety Valves Tested for Lift Set Pressure & Seat Leakage by Wyle Labs During 821102-13 Lifted in Excess of Tech Specs & Exhibited Heavy Seat Leakage.Cause Undetermined | | | 05000311/LER-1983-008-99, /99X-0:on 830218,diesel Generator Area Low Pressure Carbon Monoxide Sys Automatic Initiation Feature Disabled & Tagged Out for Planned Maint.Continuous Fire Watch Established.On 830131,event Became Reportable | /99X-0:on 830218,diesel Generator Area Low Pressure Carbon Monoxide Sys Automatic Initiation Feature Disabled & Tagged Out for Planned Maint.Continuous Fire Watch Established.On 830131,event Became Reportable | | | 05000311/LER-1983-008, Forwards LER 83-008/99X-0.Detailed Event Anaysis Encl | Forwards LER 83-008/99X-0.Detailed Event Anaysis Encl | | | 05000272/LER-1983-009-99, /99X-0:on 830130,during Routine Plant Cooldown, Inadvertent Safety Injection Occurred Due to Low Pressurizer Pressure.Caused by Operator Overlooking Decreasing Pressure. All safety-related Equipment Functioned as Designed | /99X-0:on 830130,during Routine Plant Cooldown, Inadvertent Safety Injection Occurred Due to Low Pressurizer Pressure.Caused by Operator Overlooking Decreasing Pressure. All safety-related Equipment Functioned as Designed | | | 05000272/LER-1983-009, Forwards LER 83-009/99X-0.Detailed Event Analysis Encl | Forwards LER 83-009/99X-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-009, Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-009-03, /03L-0:on 830203,during Shutdown Operation,Sample Analysis of RCS Boron Concentration Revealed Concentration Less than Tech Spec Limit.Caused by Hydrolazing Steam Generators.Rcs Boration Performed to Maintain Concentration | /03L-0:on 830203,during Shutdown Operation,Sample Analysis of RCS Boron Concentration Revealed Concentration Less than Tech Spec Limit.Caused by Hydrolazing Steam Generators.Rcs Boration Performed to Maintain Concentration | | | 05000272/LER-1983-010-03, /03L-0:from 821016-830205,during Testing of Type B & C Components,Three Containment Isolation Valves Exhibited Leakage Rates in Excess of Test Equipment Range. Valves 1CC215 & 1VC8 Restroked.Valve 14GB4 Reworked | /03L-0:from 821016-830205,during Testing of Type B & C Components,Three Containment Isolation Valves Exhibited Leakage Rates in Excess of Test Equipment Range. Valves 1CC215 & 1VC8 Restroked.Valve 14GB4 Reworked | | | 05000311/LER-1983-010-03, /03L-0:on 830126,during Shutdown Operations, Control Air Header 21 Isolated & Tagged for Leak Rate Testing.Porv 2PR1 Closed Resulting in Loss of RCS Vent Path. Caused by Surge in Header 22 Due to Failed Valve | /03L-0:on 830126,during Shutdown Operations, Control Air Header 21 Isolated & Tagged for Leak Rate Testing.Porv 2PR1 Closed Resulting in Loss of RCS Vent Path. Caused by Surge in Header 22 Due to Failed Valve | | | 05000311/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-011, Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-011-03, /03L-0:on 830401,discovered That Monthly Testing of Control Room Emergency Air Conditioning Sys Was Overlooked.Caused by Insp Order Sys Card Requiring Testing Being Erroneously Stated.Card Revised | /03L-0:on 830401,discovered That Monthly Testing of Control Room Emergency Air Conditioning Sys Was Overlooked.Caused by Insp Order Sys Card Requiring Testing Being Erroneously Stated.Card Revised | | | 05000311/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-012-01, /01T-0:on 830222,during Startup,Reactor Manually Tripped.Caused by Rapidly Decreasing Steam Generator Levels. Manual Trip Obscured Failure of Trip Breakers to Open Automatically.Plant Cooldown Commenced | /01T-0:on 830222,during Startup,Reactor Manually Tripped.Caused by Rapidly Decreasing Steam Generator Levels. Manual Trip Obscured Failure of Trip Breakers to Open Automatically.Plant Cooldown Commenced | | | 05000311/LER-1983-012-03, /03L-0:on 830406,10-ton Cardox Sys Pilot Valve Found in Closed Position & All Low Pressure Sys Declared Inoperable.Caused by Inadequacies in Sys Recharging Operation on 830304.Procedures Revised | /03L-0:on 830406,10-ton Cardox Sys Pilot Valve Found in Closed Position & All Low Pressure Sys Declared Inoperable.Caused by Inadequacies in Sys Recharging Operation on 830304.Procedures Revised | | | 05000311/LER-1983-012, Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-013, Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1983-013-99, /99T-0:on 830215,calculated Moderator Temp Coefficient (Mtc) Value for All Control Rods Withdrawn Found More Positive than Tech Spec Allowance But within Expected Deviation.Limitation on Withdrawal Will Be Maintained | /99T-0:on 830215,calculated Moderator Temp Coefficient (Mtc) Value for All Control Rods Withdrawn Found More Positive than Tech Spec Allowance But within Expected Deviation.Limitation on Withdrawal Will Be Maintained | | | 05000311/LER-1983-013-03, /03L-0:on 830409,during Routine Shutdown,Lube Oil Temp Increases Observed on Charging Pump 22.Caused by Restricted Svc Water Flow to Pump Due to Oyster Shells & Miscellaneous Mollusks.Shells Removed | /03L-0:on 830409,during Routine Shutdown,Lube Oil Temp Increases Observed on Charging Pump 22.Caused by Restricted Svc Water Flow to Pump Due to Oyster Shells & Miscellaneous Mollusks.Shells Removed | | | 05000272/LER-1983-013, Forwards LER 83-013/99T-0.Detailed Event Analysis Encl | Forwards LER 83-013/99T-0.Detailed Event Analysis Encl | | | 05000311/LER-1983-014-03, /03L-1:on 830413 & 18,operating Loads on 2A 4kV & 460-volt Vital Buses Observed to Trip.Caused by Spurious Operation of Safeguards Equipment Control Sys Due to Design Deficiencies.Equipment Restarted | /03L-1:on 830413 & 18,operating Loads on 2A 4kV & 460-volt Vital Buses Observed to Trip.Caused by Spurious Operation of Safeguards Equipment Control Sys Due to Design Deficiencies.Equipment Restarted | | | 05000272/LER-1983-014, Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | |
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