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Category:Letter
MONTHYEARML25058A3462025-02-28028 February 2025 Project Manager Assignment IR 05000261/20254042025-02-28028 February 2025 Material Control and Accounting Program Inspection Report 05000261 2025404 - Public ML25045A1622025-02-24024 February 2025 SLR Environmental Pre-Application Meeting Summary ML25006A0602025-01-0707 January 2025 2025 Requalification Program Inspection H.B. Robinson Nuclear Plant ML24353A3462025-01-0202 January 2025 Letter - U.S. Nuclear Regulatory Commission Feedback on White Papers Related to the Determination of T0 for H.B. Robinson Unit 2, Heat Number W5214 ML24323A2382024-12-0505 December 2024 Regarding Relief Request RA-23-0300 for the Fifth 10-Year Inservice Inspection Interval ML24320A0032024-12-0404 December 2024 Request for Withholding Information from Public Disclosure, H. B. Robinson Steam Electric Plant, Unit No. 2 IR 05000261/20240032024-10-30030 October 2024 Integrated Inspection Report 05000261/2024003 ML24297A2182024-10-28028 October 2024 – NRC Operator License IR 05000261/20244022024-10-16016 October 2024 – Security Target Set Baseline Inspection Report 05000261/2024402 IR 05000261/20244012024-09-11011 September 2024 Security Baseline Inspection Report 05000261/2024401 ML24242A2612024-08-29029 August 2024 Operator Licensing Examination Approval 05000261/2024301 IR 05000261/20240052024-08-22022 August 2024 Updated Inspection Plan for H.B. Robinson Steam Electric Plant - Report 05000261/2024005 ML24169A2712024-08-14014 August 2024 – Issuance of Amendment No. 280 to Adopt TSTF-258-A, Revision 4, Regarding Changes to Technical Specification 5.7, High Radiation Area IR 05000261/20240022024-08-0101 August 2024 Integrated Inspection Report 05000261/2024002 ML24183A0972024-07-12012 July 2024 ISFSI; Catawba 1, 2 & ISFSI; McGuire 1, 2 & ISFSI; Oconee 1, 2, 3 & ISFSI; Shearon Harris 1; H. B. Robinson 2 & ISFSI; and Radioactive Package Shipping Under 10 CFR 71 (71-266 & 71-345) – Review of QA Program Changes EPID L-2024-LLQ-0002 IR 05000261/20240112024-06-0303 June 2024 Focused Engineering Inspection- Commercial Grade Dedication Report 05000261/2024011 ML24114A0152024-06-0303 June 2024 Unit 2 – Issuance of Amendment No. 279 Regarding Application of Leak-Before-Break Methodology for Auxiliary Reactor Coolant System Piping IR 05000261/20240012024-05-0909 May 2024 Integrated Inspection Report 05000261/2024001 IR 05000261/20240102024-04-30030 April 2024 Biennial Problem Identification and Resolution Inspection Report 05000261/2024010 IR 05000261/20230062024-02-28028 February 2024 Annual Assessment Letter for H.B. Robinson Steam Electric Plant Unit 2 - Report 05000261-2023006 ML24072A2942024-02-0606 February 2024 – Notification of Licensed Operator Initial Examination 05000261/2024301 IR 05000261/20243012024-02-0606 February 2024 – Notification of Licensed Operator Initial Examination 05000261/2024301 ML24033A0592024-02-0202 February 2024 Response to Request for Additional Information License Amendment Request to Exclude the Dynamic Effects of Specific Postulated Pipe Ruptures from the Design and Licensing Basis Based on Leak-Before-Break Methodology IR 05000261/20230042024-01-31031 January 2024 Integrated Inspection Report 05000261/2023004 ML24009A2432024-01-25025 January 2024 Unit, No. 2 - Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0047 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML24009A2712024-01-24024 January 2024 Revision to Reactor Vessel Material Surveillance Capsule Withdrawal Schedule ML23354A0052024-01-0808 January 2024 Request for Withholding Information from Public Disclosure, H. B. Robinson Steam Electric Plant, Unit No. 2 ML23342A0902023-12-0808 December 2023 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection IR 05000261/20234202023-11-30030 November 2023 Security Baseline Inspection Report 05000261/2023420 (Cover Letter with Report) IR 05000261/20230102023-11-28028 November 2023 Fire Protection Team Inspection Report 05000261/2023010 ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000261/20230032023-11-0707 November 2023 – Integrated Inspection Report 05000261 2023003 and 07200060 2023001 ML23226A0862023-10-12012 October 2023 Issuance of Amendment No. 277 Regarding Revision of TSs to Add High-High Steam Generator Level Function to Table 3.3.2-1 and Remove Obsolete Content from TSs 2.1.1.1 and 5.6.5.b ML23346A1322023-10-0606 October 2023 Communication from C-10 Research & Education Foundation Regarding NextEra Common Emergency Fleet Plan License Amendment Request and Related Documents Subsequently Published ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds ML23195A0782023-08-29029 August 2023 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 ML23235A0552023-08-23023 August 2023 – Notification of an Fire Protection Team Inspection (FPTI) (NRC Inspection Report 05000261/2023010) and Request for Information (RFI) IR 05000261/20230052023-08-21021 August 2023 Updated Inspection Plan for H.B. Robinson Steam Electric Plant (Report 05000261/2023005) 05000261/LER-2023-002, Plant Trip During Reactor Protection System Testing2023-08-17017 August 2023 Plant Trip During Reactor Protection System Testing 05000261/LER-2023-001, Condition Prohibited by Technical Specification Due to Missed Entry Into Limiting Condition for Operation2023-08-10010 August 2023 Condition Prohibited by Technical Specification Due to Missed Entry Into Limiting Condition for Operation IR 05000261/20230022023-08-0707 August 2023 – Integrated Inspection Report 05000261/2023002 IR 05000261/20234022023-05-30030 May 2023 – Cyber Security Inspection Report 05000261/2023402 ML23145A1602023-05-25025 May 2023 Submittal of Updated Final Safety Analysis Report (Revision No. 30), Independent Spent Fuel Storage Installation Safety Analysis Report (Revision No. 28), Technical Specifications Bases Revisions, Quality IR 05000261/20230012023-05-0202 May 2023 Integrated Inspection Report 05000261/2023001 ML23118A0762023-05-0101 May 2023 Approval for Use of Specific Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI ML22332A4932023-03-10010 March 2023 William States Lee III 1 and 2 - Issuance of Amendments Regarding the Relocation of the Emergency Operations Facility IR 05000261/20220062023-03-0101 March 2023 Annual Assessment Letter for H.B. Robinson Steam Electric Plant, Unit 2 (Report 05000261/2022006) ML23047A4512023-02-21021 February 2023 Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection 05000261/2023402 ML23041A2272023-02-13013 February 2023 2022 Q4 Robinson_Workflow Final 2025-02-28
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000261/LER-2023-002, Plant Trip During Reactor Protection System Testing2023-08-17017 August 2023 Plant Trip During Reactor Protection System Testing 05000261/LER-2023-001, Condition Prohibited by Technical Specification Due to Missed Entry Into Limiting Condition for Operation2023-08-10010 August 2023 Condition Prohibited by Technical Specification Due to Missed Entry Into Limiting Condition for Operation RA-19-0384, LER 20190-001-00 for H.B. Robinson Steam Electric Plant, Unit 2, Turbine Trip/Reactor Trip Due to Main Generator Lockout2019-10-0909 October 2019 LER 20190-001-00 for H.B. Robinson Steam Electric Plant, Unit 2, Turbine Trip/Reactor Trip Due to Main Generator Lockout 05000261/LER-2018-001, Valid Actuation of Emergency Diesel Generator2019-01-16016 January 2019 Valid Actuation of Emergency Diesel Generator 05000261/LER-1917-002, Regarding Plant Vital Area Security Vulnerability Discovered Without Compensatory Security Measures2017-12-14014 December 2017 Regarding Plant Vital Area Security Vulnerability Discovered Without Compensatory Security Measures 05000261/LER-1917-001, Regarding Auxiliary Feedwater System Actuation During Surveillance Testing2017-06-0101 June 2017 Regarding Auxiliary Feedwater System Actuation During Surveillance Testing 05000261/LER-2016-005, Regarding Reactor Trip and Automatic System Actuation Due to Weather-Related Loss of Offsite Power2016-12-0505 December 2016 Regarding Reactor Trip and Automatic System Actuation Due to Weather-Related Loss of Offsite Power 05000261/LER-2016-004, Regarding Reactor Trip During the Performance of a Visual Inspection of the Main Turbine Trip Block2016-10-21021 October 2016 Regarding Reactor Trip During the Performance of a Visual Inspection of the Main Turbine Trip Block 05000261/LER-2016-003, Regarding Failure of Lake Robinson Tainter Gates to Fully Open During Performance of Functionality Testing2016-10-10010 October 2016 Regarding Failure of Lake Robinson Tainter Gates to Fully Open During Performance of Functionality Testing 05000261/LER-2016-002, Unit No. 2, Regarding Unanalyzed Condition Related to Main Steam Line Break Inside Containment2016-06-13013 June 2016 Unit No. 2, Regarding Unanalyzed Condition Related to Main Steam Line Break Inside Containment 05000261/LER-2016-001, Regarding Inoperability of Motor-Driven Auxiliary Feedwater Pumps Due to Insufficient Lube Oil Cooling2016-03-21021 March 2016 Regarding Inoperability of Motor-Driven Auxiliary Feedwater Pumps Due to Insufficient Lube Oil Cooling 05000261/LER-2015-004, Regarding Refueling Water Storage Tank (RWST) Discharge Valve Failed to Close on Demand2015-08-26026 August 2015 Regarding Refueling Water Storage Tank (RWST) Discharge Valve Failed to Close on Demand 05000261/LER-2015-003, Regarding Failed Surveillance on Station Battery Charger A-12015-06-0909 June 2015 Regarding Failed Surveillance on Station Battery Charger A-1 05000261/LER-2015-002, Regarding Pressurizer Power Operated Relief Valve (PORV) Limit Switches Qualified Life Exceeded Due to Miscalculation2015-05-15015 May 2015 Regarding Pressurizer Power Operated Relief Valve (PORV) Limit Switches Qualified Life Exceeded Due to Miscalculation 05000261/LER-2015-001, Regarding Reactor Protection and DC Electrical System Inoperability Due to Inadvertant Parallel Connection of Safety Trains2015-03-30030 March 2015 Regarding Reactor Protection and DC Electrical System Inoperability Due to Inadvertant Parallel Connection of Safety Trains 05000261/LER-2014-002, Regarding Technical Specification Violation Due to Incorrect Procedural Guidance2015-01-23023 January 2015 Regarding Technical Specification Violation Due to Incorrect Procedural Guidance NG-75-1158, Abnormal Occurrence Report 50-261/75-14 Regarding Failure of Auxiliary Feedwater Pump Discharge Valve V2-14B2014-07-25025 July 2014 Abnormal Occurrence Report 50-261/75-14 Regarding Failure of Auxiliary Feedwater Pump Discharge Valve V2-14B 05000261/LER-2014-001, Regarding Reactor Trip Due to a Two-out-of-Three Logic Signal from Steam Generator Water Level Protection Train B Logic Matrix2014-03-10010 March 2014 Regarding Reactor Trip Due to a Two-out-of-Three Logic Signal from Steam Generator Water Level Protection Train B Logic Matrix 05000261/LER-2013-003, Regarding Reactor Trip on 4KV Bus Undervoltage During Load Transfer2014-01-0202 January 2014 Regarding Reactor Trip on 4KV Bus Undervoltage During Load Transfer 05000261/LER-2013-002, Regarding Automatic Actuation of the Auxiliary Feedwater System Due to Main Feed Pump Trip2014-01-0202 January 2014 Regarding Automatic Actuation of the Auxiliary Feedwater System Due to Main Feed Pump Trip 05000261/LER-2013-001, Regarding Non-Environmentally-Qualified Splice Rendered Post Accident Monitoring (PAM) Instrumentation Channel Inoperable2013-12-0505 December 2013 Regarding Non-Environmentally-Qualified Splice Rendered Post Accident Monitoring (PAM) Instrumentation Channel Inoperable 05000261/LER-2011-001-01, Regarding Condition Prohibited by Technical Specifications When Non-Seismic System Was Aligned to Refueling Water Storage Tank Due to Regulatory Requirements Not Adequately Incorporated in Plant Documentation2012-08-10010 August 2012 Regarding Condition Prohibited by Technical Specifications When Non-Seismic System Was Aligned to Refueling Water Storage Tank Due to Regulatory Requirements Not Adequately Incorporated in Plant Documentation 05000261/LER-2012-004, For H.B. Robinson Unit 2, Regarding Reactor Tripped Due to a Turbine Trip Caused by a Feedwater Isolation Signal from Steam Generator B High Level2012-05-23023 May 2012 For H.B. Robinson Unit 2, Regarding Reactor Tripped Due to a Turbine Trip Caused by a Feedwater Isolation Signal from Steam Generator B High Level 05000261/LER-2012-002, Regarding Unplanned LCO 3.5.4 Entry Due to RWST Alignment to Purification2012-05-0909 May 2012 Regarding Unplanned LCO 3.5.4 Entry Due to RWST Alignment to Purification 05000261/LER-2012-003, Regarding a Plant Modification Interference with Operation of the Containment Wide Range Level Indicator2012-05-0707 May 2012 Regarding a Plant Modification Interference with Operation of the Containment Wide Range Level Indicator 05000261/LER-2012-001, Regarding Technical Specification Required Plant Shutdown Due to Missed Surveillance and Operation Prohibited by Technical Specifications2012-03-14014 March 2012 Regarding Technical Specification Required Plant Shutdown Due to Missed Surveillance and Operation Prohibited by Technical Specifications 05000261/LER-2011-002, Regarding Reactor Trip Due to a Failed Relay Coil on RCP-3-X(B) and Actuation of Auxiliary Feedwater System2011-11-15015 November 2011 Regarding Reactor Trip Due to a Failed Relay Coil on RCP-3-X(B) and Actuation of Auxiliary Feedwater System RNP-RA/11-0057, Regarding Condition Prohibited by Technical Specifications When Non-Seismic System Was Aligned to Refueling Water Storage Tank Due to Regulatory Requirements Not Adequately Incorporated in Plant Documentation2011-06-30030 June 2011 Regarding Condition Prohibited by Technical Specifications When Non-Seismic System Was Aligned to Refueling Water Storage Tank Due to Regulatory Requirements Not Adequately Incorporated in Plant Documentation 05000261/LER-2010-007, Regarding Reactor Trip Due to a Degraded Connection on a Circuit Board in the Electro-Hydraulic Control Cabinet2010-11-0505 November 2010 Regarding Reactor Trip Due to a Degraded Connection on a Circuit Board in the Electro-Hydraulic Control Cabinet 05000261/LER-2010-006, Pressurizer Heaters Inoperable Longer than Allowed Due to Inadequate Procedure2010-10-0404 October 2010 Pressurizer Heaters Inoperable Longer than Allowed Due to Inadequate Procedure 05000261/LER-2010-005, Regarding Emergency Diesel Generator Inoperable Due to Inverter Failure2010-08-23023 August 2010 Regarding Emergency Diesel Generator Inoperable Due to Inverter Failure 05000261/LER-2010-003, Potential Loss of Residual Heat Removal System Safety Function in Modes 3 and 4 Due to Void Formation2010-06-28028 June 2010 Potential Loss of Residual Heat Removal System Safety Function in Modes 3 and 4 Due to Void Formation 05000261/LER-2010-004, Regarding Clearance Error Results in the a Emergency Diesel Generator Becoming Inoperable2010-06-24024 June 2010 Regarding Clearance Error Results in the a Emergency Diesel Generator Becoming Inoperable 05000261/LER-2010-002, For H. B. Robinson, Unit 2, Regarding Plant Trip Due to Electrical Fault2010-05-27027 May 2010 For H. B. Robinson, Unit 2, Regarding Plant Trip Due to Electrical Fault 05000261/LER-2010-001, For H.B. Robinson, Unit 2, Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Completion Time Due to Output Breaker Failure2010-04-22022 April 2010 For H.B. Robinson, Unit 2, Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Completion Time Due to Output Breaker Failure 05000261/LER-2009-003, For H.B. Robinson, Unit 2, Regarding Manual Reactor Trip Due to Failure of a Steam Generator Level Module2010-01-0505 January 2010 For H.B. Robinson, Unit 2, Regarding Manual Reactor Trip Due to Failure of a Steam Generator Level Module 05000261/LER-2009-002, Failure to Complete Technical Specifications Required Action within the Allowed Completion Time2009-08-26026 August 2009 Failure to Complete Technical Specifications Required Action within the Allowed Completion Time 05000261/LER-2009-001, Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time2009-06-18018 June 2009 Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time 05000261/LER-2008-002, Regarding Manual Reactor Trip Due to High Turbine Vibrations2009-01-15015 January 2009 Regarding Manual Reactor Trip Due to High Turbine Vibrations 05000261/LER-2008-001, Regarding Appendix R Pathway Impassable Due to Lock Configuration2008-07-21021 July 2008 Regarding Appendix R Pathway Impassable Due to Lock Configuration 05000261/LER-2007-001, From H. B. Robinson Steam Electric Plant, Unit 2, Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry2007-07-11011 July 2007 From H. B. Robinson Steam Electric Plant, Unit 2, Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry 05000261/LER-2006-001, Re Manual Reactor Trip Due to Failure of a Turbine Governor Valve Electro-Hydraulic Control Card2006-12-21021 December 2006 Re Manual Reactor Trip Due to Failure of a Turbine Governor Valve Electro-Hydraulic Control Card 05000261/LER-2004-002, Entry Into Mode 3 with the Steam Driven Auxiliary Feedwater Pump Flowpath Inoperable2004-07-21021 July 2004 Entry Into Mode 3 with the Steam Driven Auxiliary Feedwater Pump Flowpath Inoperable 05000261/LER-2004-001, Regarding Both Trains of High Pressure Safety Injection Inoperable for Approximately 25 Minutes2004-05-26026 May 2004 Regarding Both Trains of High Pressure Safety Injection Inoperable for Approximately 25 Minutes 05000261/LER-2003-003, Unit N0. 2, Regarding Discovery of Two New Appendix R Safe Shutdown Vulnerabilities2004-01-20020 January 2004 Unit N0. 2, Regarding Discovery of Two New Appendix R Safe Shutdown Vulnerabilities 05000261/LER-2003-002, Regarding Failure of Automatic Containment Ventilation Isolation During Containment Pressure Relief2003-07-31031 July 2003 Regarding Failure of Automatic Containment Ventilation Isolation During Containment Pressure Relief 05000261/LER-2003-001, For H. B. Robinson Unit 2 Regarding Failure to Complete Technical Specifications Required Action within the Allowed Completion Time2003-04-23023 April 2003 For H. B. Robinson Unit 2 Regarding Failure to Complete Technical Specifications Required Action within the Allowed Completion Time 05000261/LER-2002-001, From H.B. Robinson, Unit 2 Regarding Four Main Steam Safety Valves Failure to Meet Acceptance Criteria During Lift Pressure Testing2002-12-0909 December 2002 From H.B. Robinson, Unit 2 Regarding Four Main Steam Safety Valves Failure to Meet Acceptance Criteria During Lift Pressure Testing 2023-08-17
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(_~ DUKE ENERGY Date: August 17, 2023 Serial: RA-23-0203 United States Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001 H. B. ROBINSON STEAM ELECTRIC PLANT, UNIT NO. 2 DOCKET NO. 50-261/RENEWED LICENSE NO. DPR-23 Subject: LICENSEE EVENT REPORT NO. 2023-002-00:
Laura A. Basta H. B. Robinson Steam Electric Plant Unit 2 Site Vice President Duke Energy 3581 West Entrance Road Hartsville, SC 29550 0 : 843 9511701 Laura.Basta@duke-energy.com 10 CFR 50.73 PLANT TRIP DURING REACTOR PROTECTION SYSTEM TESTING Ladies and Gentlemen:
Pursuant to 10 CFR 50. 73, Duke Energy Progress, LLC is submitting the attached Licensee Event Report. There are no unresolved corrective actions necessary to restore compliance with NRC requirements. Please direct any questions regarding this submittal to Phillip D. Mason, Manager Nuclear Support Services, at (843) 951-5797.
This document contains no new regulatory commitments.
Sincerely, Laura A. Basta Site Vice President LAB/mjh Attachment c:
Region Administrator, NRC, Region II NRC Resident Inspectors, HBRSEP Mr. Luke Haeg, NRC Project Manager, NRR
United States Nuclear Regulatory Commission Attachment to Serial: RA-23-0203 4 Pages (including this page)
H. B. ROBINSON STEAM ELECTRIC PLANT, UNIT NO. 2 LICENSEE EVENT REPORT NO. 2023-002-00:
PLANT TRIP DURING REACTOR PROTECTION SYSTEM TESTING
Abstract
At 10:35 hours Eastern Daylight Time on 06/22/2023, with Unit 2 in Mode 1 at 100% power, H. 8. Robinson Steam Electric Plant, Unit 2 (H8RSEP2), experienced an automatic turbine trip followed by an automatic reactor trip during the performance of reactor protection logic testing. Subsequent to the reactor trip, the auxiliary feedwater system actuated as expected on low steam generator level. There were no other equipment performance issues.
The cause of this event is attributed to pre-existing flaws with reactor trip breaker cubicle design that allowed for the flexing of the cell switch support structure, which resulted in the failure of the cell switch to change state and preclude a turbine trip or reactor trip when the 'B' reactor trip bypass breaker was racked in to position during testing. The trip was not complex, with all systems responding normally.
This event is reportable under 10 CFR 50. 73(a)(2)(iv)(A) due to the event resulting in an automatic actuation of the reactor protection system and auxiliary feedwater system. This event did not impact the health and safety of the public.
BACKGROUND
- 2. DOCKET NUMBER
- 3. LER NUMBER I
00261 D
NUMBER NO.
I YEAR SEQUENTIAL REV
~-I 002 1-G At the time of this event, H. B. Robinson Steam Electric Plant, Unit No. 2, (HBRSEP2) was operating in Mode 1 at approximately 100 percent power. No structures, systems, or components were out of service at the time of this event that contributed to the event. This event is reportable under 10 CFR 50.73(a)(2)(iv)(A) due to the automatic actuation of the reactor protection system (RPS) [AA] and auxiliary feedwater system (AFW) [BA].
The RPS monitors all parameters related to the safe operation of the reactor. The system is designed to protect the core against fuel rod cladding damage caused by departure from nucleate boiling, and to protect the reactor coolant system [AB] against damage caused by overpressure.
HBRSEP2 reactor trip breakers (RTBs) and reactor trip bypass breakers (BYBs) are DB-50 breakers originally supplied from Westinghouse Electric Corporation. Cell switches are designed to externally indicate the change of state as a breaker moves from the CONNECT position to the TEST position and vice versa within the cell compartment. The switches are designed to mount on a channel at the bottom rear of the breaker compartment. Each switch contains eight switch contacts.
On 06/22/2023 at 13:50 hours Eastern Daylight Time, Event Notification#56585 was made to the Nuclear Regulatory Commission (NRC) Operations Center under 10 CFR 50.72(b)(2)(iv)(B), due to the automatic actuation of the RPS, and under 10 CFR 50. 72(b)(3)(iv)(A)(B)(6), due to the valid actuation of the AFW system. This criterion requires a licensee event report (LER) be submitted within 60-days of the event date.
EVENT DESCRIPTION
At 10:35 hours on 06/22/2023, an automatic turbine [TRB] trip and a subsequent automatic reactor [RCT] trip occurred.
Subsequent to the reactor trip, the auxiliary feedwater system actuated as expected on low steam generator level.
Maintenance and operations personnel were performing at-power reactor protection logic train 'B' testing. Per the test procedure, the 'B' reactor trip bypass breaker [BKR] was racked in and closed to permit the testing of the 'B' reactor trip breaker. This action should have caused the cell switch [33] contact (52H) for the 'B' reactor trip bypass breaker to open to allow testing and prevent the logic necessary for a turbine control system-actuated [TG] turbine trip signal. However, due to flexure in the breaker cell switch mounting support [SPT] the cell switch experienced enough displacement as the bypass breaker was racked into position to cause the switch to remain closed. The result was generation of a turbine trip signal to the turbine control system, subsequent turbine trip, reactor trip and auxiliary feedwater system actuation when the 'B' RTB was opened for testing.
CAUSAL FACTORS An in-depth evaluation of the automatic turbine trip followed by the automatic reactor trip has concluded that the direct cause of the turbine trip signal was a design characteristic of the cubicle design that allowed for the flexing of the cell switch support structure, which resulted in the failure of the switch to change state and prevent a turbine trip and reactor trip. An extent of condition review was performed on the remaining reactor trip breakers and bypass breaker. The same design vulnerability was determined to exist on the 'B' reactor trip breaker, requiring additional support shims be installed.
CORRECTIVE ACTIONS
- 2. DOCKET NUMBER
- 3. LER NUMBER I
00261 D
NUMBER NO.
I YEAR SEQUENTIAL REV
~-I 002 1-0 An engineering change was implemented to install support shims beneath the breaker cell switches of the subject reactor trip and bypass breakers to correct the condition and prevent recurrence. Procedure changes to Reactor Protection Logic Train Testing At-Power maintenance test procedures have been initiated to utilize turbine control system sliding links eliminating trips due to cell switch contact failure during testing. Any changes to the corrective actions or completion schedules will be made in accordance with the site's corrective action program.
SAFETY ANALYSIS
The reactor was operating at full power during the Reactor Protection Logic Train 'B' At Power Testing when an automatic reactor trip occurred. The mitigating equipment (RPS and AFW) functioned as expected and plant shutdown proceeded normally without further challenge. The cause of the plant trip is attributed to a design characteristic of the cubicle design that allowed for the flexing of the breaker cell switch support structure, which resulted in the failure of the switch to change state. The RPS trip logic performed as designed and there were no other equipment performance issues. Therefore, this event had very low safety significance based on a successful reactor trip with no equipment or operational challenges.
This event resulted in no impact to the health and safety of the public.
ADDITIONAL INFORMATION
An operating experience search was conducted and there are no prior events at HBRSEP2 involving inadvertent actuation of the reactor protection system due to reactor trip bypass breaker cell switch malfunction within the past five years.
Energy Industry Identification System (EIIS) codes for systems and components relevant to this event are identified in the text of this document within brackets [ ]. Page 3
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