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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000281/LER-1992-001, Corrected Page 3 to LER 92-001-00 Re 920130 Mechanical Failure Due to Oil Leak from Charging Pump a Bearing & Damper Remaining Closed on Charging Pump B1992-03-26026 March 1992 Corrected Page 3 to LER 92-001-00 Re 920130 Mechanical Failure Due to Oil Leak from Charging Pump a Bearing & Damper Remaining Closed on Charging Pump B ML20245G9341989-06-16016 June 1989 Has Been Canceled.Resolution of LERs Missing from Lertrk/Scss/Dcs Discussed 05000000/LER-1986-022, Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation1987-02-20020 February 1987 Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation 05000000/LER-1986-030, Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted1986-12-16016 December 1986 Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted 05000000/LER-1986-026, Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed1986-12-0101 December 1986 Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed 05000000/LER-1986-023, Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation1986-11-21021 November 1986 Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation 05000000/LER-1986-024, Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access1986-11-18018 November 1986 Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access 05000000/LER-1986-052, Partially Withheld LER 86-052-01:on 860926,security Data Mgt Sys Computer Terminals Became Inoperable (Ref 10CFR73.21). Caused by Overload of Alarms & Sys Instability.Sys Restored by Placing Sys Multiplexers Online1986-11-13013 November 1986 Partially Withheld LER 86-052-01:on 860926,security Data Mgt Sys Computer Terminals Became Inoperable (Ref 10CFR73.21). Caused by Overload of Alarms & Sys Instability.Sys Restored by Placing Sys Multiplexers Online 05000000/LER-1986-007, Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected1986-10-0606 October 1986 Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected 05000000/LER-1986-021, Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced1986-09-15015 September 1986 Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced 05000000/LER-1986-020, Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised1986-08-15015 August 1986 Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised 05000000/LER-1986-004, Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause1986-06-11011 June 1986 Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause 05000000/LER-1986-016, Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made1986-05-0606 May 1986 Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made 05000000/LER-1986-015, Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired1986-05-0202 May 1986 Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000000/LER-1986-014, Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway1986-04-25025 April 1986 Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway 05000000/LER-1986-013, Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found1986-04-18018 April 1986 Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found 05000000/LER-1986-012, Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled1986-04-17017 April 1986 Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled 05000000/LER-1986-011, Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily1986-04-15015 April 1986 Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily 05000000/LER-1986-003, Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld1986-01-29029 January 1986 Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld 05000000/LER-1986-002, Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated1986-01-23023 January 1986 Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated 05000000/LER-1986-001, Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted1986-01-10010 January 1986 Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted 05000237/LER-1983-084, Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr1984-03-14014 March 1984 Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr 05000237/LER-1983-080, Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr1983-12-20020 December 1983 Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr ML20081M2021983-11-0202 November 1983 83-037/03L-0:on 831005,during Daily Battery Surveillance, 250-volt Battery Charger Float Voltage Indicated Improper Float Voltage.Caused by Defective Amplifier Board.Defective Board Replaced ML20078N5121983-10-14014 October 1983 LER83-043/03L-0:on 830914,following Reactor Trip,Flow Control Valve (FCV) Failed to Close Upon Receipt of Feedwater Isolation Signal.Caused by Malfunctioning Solenoid Valve & FCV-1488 Restricted by Antirotation Device 05000280/LER-1982-126, Updated LER 82-126/03X-1:on 821223,rod Position Indication for Control Rod F-4 Indicated Erratically & Fluctuated Greater than 12 Steps.Cause Unknown.Erroneous Signal Suspected of Being Inside Containment.Testing Underway1983-02-0808 February 1983 Updated LER 82-126/03X-1:on 821223,rod Position Indication for Control Rod F-4 Indicated Erratically & Fluctuated Greater than 12 Steps.Cause Unknown.Erroneous Signal Suspected of Being Inside Containment.Testing Underway 05000281/LER-1981-074, Updated LER 81-074/03X-1:on 811120,higher than Normal Activity Detected in Storm Drain Sys.Caused by Leaks from Stripper Feed Steam Heater Due to Failure of Heater Drain Receiver & Pumps to Prevent Overflow.Tubes Plugged1983-01-31031 January 1983 Updated LER 81-074/03X-1:on 811120,higher than Normal Activity Detected in Storm Drain Sys.Caused by Leaks from Stripper Feed Steam Heater Due to Failure of Heater Drain Receiver & Pumps to Prevent Overflow.Tubes Plugged 05000281/LER-1981-052, Updated LER 81-052/03X-1:on 810815,valve MOV-SW-202A Failed to Close Due to Grounded Motor.Grounding Caused by Flooding in Sump.Motor Replaced1983-01-31031 January 1983 Updated LER 81-052/03X-1:on 810815,valve MOV-SW-202A Failed to Close Due to Grounded Motor.Grounding Caused by Flooding in Sump.Motor Replaced 05000280/LER-1982-084, Updated LER 82-084/01X-1:on 820808,venting of a Charging Pump Resulted in Max Instantaneous Release Rate Being Exceeded.Caused by Failure to Change Radiation Monitor Setpoint Alarms to Reflect New Vent Sys Flow Rates1982-09-27027 September 1982 Updated LER 82-084/01X-1:on 820808,venting of a Charging Pump Resulted in Max Instantaneous Release Rate Being Exceeded.Caused by Failure to Change Radiation Monitor Setpoint Alarms to Reflect New Vent Sys Flow Rates 05000281/LER-1980-010, Updated LER 80-010/01X-1:on 800721,containment Gaseous & Particulate Radiation Monitor Found to Have One Automatic Function Incapable of Operating During Fuel Movement.Caused by Bypass of Containment Exhaust Fan Relay in Design1982-08-13013 August 1982 Updated LER 80-010/01X-1:on 800721,containment Gaseous & Particulate Radiation Monitor Found to Have One Automatic Function Incapable of Operating During Fuel Movement.Caused by Bypass of Containment Exhaust Fan Relay in Design Change 05000280/LER-1982-049, Updated LER 82-049/03X-1:on 820419,at 100% Power,Charging Pump Svc Water Pump 1-SW-P 10B Found W/Zero Discharge Pressure.Caused by Loss of Suction to Pumps Due to Increased Use of Svc Water by Chillers.Pump Operation Restored1982-08-0303 August 1982 Updated LER 82-049/03X-1:on 820419,at 100% Power,Charging Pump Svc Water Pump 1-SW-P 10B Found W/Zero Discharge Pressure.Caused by Loss of Suction to Pumps Due to Increased Use of Svc Water by Chillers.Pump Operation Restored 05000280/LER-1981-047, Updated LER 81-047/03X-1:on 810910,following Reactor Trip & While Returning to Power,Specific Activity of RCS Indicated Dose Equivalent I-131 Level Greater than Tech Spec Limit. Caused by Fuel Element Defect in Reactor Core1982-08-0303 August 1982 Updated LER 81-047/03X-1:on 810910,following Reactor Trip & While Returning to Power,Specific Activity of RCS Indicated Dose Equivalent I-131 Level Greater than Tech Spec Limit. Caused by Fuel Element Defect in Reactor Core 05000237/LER-1982-023, Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement1982-07-23023 July 1982 Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement 05000280/LER-1982-0711982-07-16016 July 1982 LER 82-071/03L-0:on 820618,motor Operated valve-1536 Pressure Power Operated Relief Block Valve Was Cycled Open But Failed to Close Fully,Remotely or Manually.Cause Undetermined.Valve Closed Electrically 05000280/LER-1982-0731982-07-16016 July 1982 LER 82-073/03L-0:on 820622,charging Pump Svc Water Pump 1-SW-P-10B Failed to Develop Adequate Discharge Pressure. Caused by Insufficient Npsh.Svc Water to Chillers Throttled to Provide Sufficient NPSH 05000280/LER-1980-059, Updated LER 80-059/01X-1:on 801016,util Informed of Potential for Loss of Auxiliary Feedwater Flow Following Steamline Rupture.Caused by Original Design Allowing Pump Runout & Subsequent Tripping of Sys Pump Motors1982-07-15015 July 1982 Updated LER 80-059/01X-1:on 801016,util Informed of Potential for Loss of Auxiliary Feedwater Flow Following Steamline Rupture.Caused by Original Design Allowing Pump Runout & Subsequent Tripping of Sys Pump Motors 05000280/LER-1979-045, Updated LER 79-045/01X-1:on 791228,air Would Not Flow Through Filters If Consequence Limiting Safeguards hi-hi Signal Removed from Control Circuit of Safeguards Area Exhaust Ventilation Dampers.Caused by Design Deficiency1982-07-15015 July 1982 Updated LER 79-045/01X-1:on 791228,air Would Not Flow Through Filters If Consequence Limiting Safeguards hi-hi Signal Removed from Control Circuit of Safeguards Area Exhaust Ventilation Dampers.Caused by Design Deficiency 05000280/LER-1982-0681982-07-14014 July 1982 LER 82-068/03L-0:on 820614,fire Detection Sys Discovered to Have Lost Program,Rendering Sys Inoperable.Probably Caused by Voltage Spike in Sys Resulting in Loss of Program.Sys Reprogrammed & Verified Operational 05000280/LER-1982-0361982-07-0909 July 1982 LER 82-036/03L-0:on 820611,motor Operated Valve CS-203C Failed to Close During Performance of PT-17.1.Caused by Loose Field Wiring Disconnect Device at Motor Control Ctr Cubicle.Plug Reinserted & Valve Returned to Svc 05000280/LER-1982-0741982-07-0909 July 1982 LER 82-074/03L-0:on 820618,following Check of Svc Water Piping,Pump 1-SW-P-10B Failed to Auto Start.Caused by Drift of Low Pressure Setpoint of Pressure Switch PS-SW-105.Switch Replaced 05000280/LER-1982-0261982-07-0909 July 1982 LER 82-026/03L-0:on 820618,electrical Penetration Found Improperly Sealed.Caused by Personnel Failure to Restore Penetration to Original State Following Cable Installation. Penetration Sealed 05000280/LER-1982-0351982-07-0202 July 1982 LER 82-035/03L-0:on 820607,w/unit at Full power,TV-IA-201A Would Not Remain Closed After High Radiation Test Signal Cleared.Caused by Incomplete Valve Contact Due to Loosened Limit Switch Mounting Plate.Plate Secured 05000280/LER-1982-0651982-07-0202 July 1982 LER 82-065/03L-0:on 820609,w/unit at 100% Power,Core Cooling Monitor Channel B Failed,Resulting in Spurious Alarms.Caused by Faulty Thermocouple Input.Input Replaced 05000280/LER-1982-0611982-07-0202 July 1982 LER 82-061/03L-0:on 820606,w/unit at 100% Power,Core Cooling Monitor a Showed Erratic Indication & Was Removed from Svc. Caused by Failed Printed Circuit Board.Board Replaced 05000280/LER-1982-0701982-06-28028 June 1982 LER 82-070/03L-0:on 820604,containment Spray Pump 1-CS-P-1A Failed to Start During Performance Testing 17.1.Caused by Pump Motor Breaker.Breaker Replaced & Pump Tested Satisfactorily 05000280/LER-1982-0661982-06-28028 June 1982 LER 82-066/03L-0:on 820602,steam Driven Auxiliary Feed Pump Started Automatically Due to Failure of Time Delay Relay Coil.Caused by Open Circuit in Coil.Defective Relay Replaced 05000280/LER-1982-0321982-06-28028 June 1982 LER 82-032/03L-0:on 820531,pressure in Nitrogen Bottle Supplying Emergency Air to PCV-MS-202A & B Found Below Tech Spec Limit.Caused by Fitting Leaks in Air Lines.Fittings Tightened & Pressurized Bottle Installed 05000280/LER-1982-0291982-06-14014 June 1982 LER 82-029/03L-0:on 820518,during Periodic Test 2-PT-39B-2 Snubbers 2-RC-HSS-162 & 163 Found to Have Empty Remote Reservoir.Caused by Damaged O Ring on Common Valve Block. O Ring Replaced 05000280/LER-1982-0621982-06-14014 June 1982 LER 82-062/03L-0:on 820520,PT-27 Revealed Low Ampere Readings for Circuit 7A in Panels 8 & 9,contrary to Tech Spec.Caused by Damaged Tapes.Tapes Replaced 1992-03-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML20249C8491999-09-30030 September 1999 1999 Third Quarter Rept of Completed Changes,Tests & Experiments Evaluated,Per 10CFR50.59(b)(2), for Dresden Nuclear Power Station. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML20210R6081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Dresden Nuclear Power,Units 1,2 & 3.With ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML20209E1291999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20210D3071999-06-30030 June 1999 Corrected Page 8 to MOR for June 1999 for DNPS Unit 3 ML20209J3481999-06-30030 June 1999 1999 Second Quarter Rept of Completed Changes,Tests & Experiments, Per 10CFR50.59.With ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML20195G6381999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML20206N2821999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML20205N7491999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20206B1901999-03-31031 March 1999 First Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 for Dresden Nuclear Power Station. with ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML20207M6921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML20199C8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20199D3261998-12-31031 December 1998 10CFR50.59 SER for 1998-04 Quarter, of Changes,Tests & Experiments.With ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML20197G8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Dresden Nuclear Power Station.With ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML20196J0061998-11-19019 November 1998 Rev 66 to Topical Rept CE-1-A, QA Program ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr 1999-09-30
[Table view] |
LER-2050-237, Updated LER 50-237/01L:on 760406,unacceptable Ultrasonic Indication Found on Isolation Condenser safe-end.Caused by Cracks in safe-ends.Cracked safe-end Removed & Sent to Bmcl for Metallographic Analysis |
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h ~ l 25 X o S rrNr /* or nsir ris'rrontre >?rM/ Al I Y-t')t*//~ 7/TTD C A Ac t' A T THf" 17'nn PM STA S % POWIR DTHER STATUS O CO InY DIOCOVERY DESCR;PilON I
- dE 0 9 lL/J l of of o I I 'N4 I LsJ l "4 7 10 12 13 44 45 46 L:
ACT!vrT Y COdTENT =
Ef tIASfD Of PFLFASE AMOUNT OF t':TNTTY IE
' O 9 LzJ lLJ 10 l ne i I #4 LOCATON OF RELEASE 11 44 45 0 PERSONNEL EXPOSURES . -
NUV8tA TYPE IBU9lol ol cl [2] l OtSCAPTON
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11 12 13 0
PERSONNEL INJUR:ES NUMutR DESCOTTION
- 15 1:010101 09 IHA 11 12 S OTTSrTE CONSEOUENCES
- 15) I il A O9 =
Di LOSS OR OAMAGE TO FACILITY
IE 12J UU l eM 10 El PUullCrTY iB0Dl NA G
ADDmONAL FACTORS 8403020366 760902 1511 N// gDRADOCK 05000 8 CD 6'
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, FYEfiT DESCRIllIOv- Continued) ,
s of cracking in furnace-sensitized stainless steci forgingshave occurred on'
, both Unit-2 core spr.;y loops as well as on the !!PCI steam line.-
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- The safe-end (which was SA-182 F316 stainicss steel) was replaced with one forged from SA-182 F316L stainless ste'e1. -(50-237/1976-21) ,, ,
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l CAUSE DESCRIPTION (Continued) ,
and four axially-oriented cracks at the 1:00, 4:00, 4:45, and 5:00 positions. The depth of the circumferential crack was found to be 0.261 inches, while the axial cracks ranged in depth from 0.255 to 0.500 inches. The circumferential crack was located approximately 3/8 inch from the safe-end-to-pipe weld and was 0.60 inches long at the I.D. surface. The axial cracks ranged from 0.23 to 0.43 inches in length and extended to within 1/16 inch of the safe-end-to-pipe weld.
The metallographic exanination revealed similar. features in both the axial and circumferential cracks: initiation at the I. D. surface, and .
intergranular propagation in a heavily-sensitized microstructure. Microprobe analyses of fracture surfaces and cross sections of the cracks indicated no chlorides, fluorides, sulfides, or other possible corrosives. Moderate residual l stresses from welding and possibly from inner surface grinding (up to 5 mils of cold working were observed) may also have been contributing factors. The mechanism I
of cracking is the'same as that experienced in'the HPCI safe-end, the 10-inch core spray piping, and the 4-inch recirculation bypass piping.
The cracked safe-end was manufactured from'SA-182 F316 stain 1 css steel and was unclad. It was approximately 5 inches long, with a 14-inch 0.D. at the piping end (0.56-inch wall thickness) end a 16-inch 0.D. at the nozzle end (1.08-inch wall thickness). The safe-end was furnace-sensitized during the post-weld stress relief treatment of the pressure vessel. .
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BBS Ltr. #76-531 ' July 14, 1976 h (, g
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(- A 10 l Mr. James.C. Keppler, Regional Director 9,l s ' -
j Directorate of Regulatory Operations - Region III %
- U. S. Nuc1 cur Kegulatory Commission g, ,
799 Roosevcit Road s p /
, Glen Ellyn, Illinois 60137
) .
Enclosed pleaset find an update report to Reportable Occurrence report
, number 50-237/1976-21. This report is being submitted to your office in accordance with the Srcsden Nuc1 car Power Station Technical Specifications, Section 6.6.B.
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. 'S t ep)ienson Station Superintendent Dresden Nuclear Power Station BBS:jo Enclosure .-
cc: Director of Inspection & Enforcement -
Director of Management Information & Program Control i
File /NRC s
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COPY SENT REGION
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~T mnE-st-76-io !
() LICENSEE EVENT REPOPN V
..w CONTROL BLOCK l l l l l l l (PLEASE PflNT Att RECulRED INFCRMATl!N) 1 6
t Cf N51 tVlN1 L CE *.M t TYPE fvPE NtWI tiCENGE NUV0t R
[@] Iv la I s I el s1_d lo lo I-I ol ol ol ol 01-101025I I2641 i i t t i l o30l I31ol 31 32 7 09 14 1S Af ecur cart twtNT Dart CAfincur [vY hIN 1013 Io00Cair Nuvotn 1-1 c 12.181 oj i ol 7121317 I 674: Lol 8! 0121716 00 J 0 i Coat in 11J LtJ LIJ 60 61 68 69 7b 7 0 S7 68 09 FVENT DESCR!PilON
}
O IDuring the preparations to test the startinn of #1 cmernency diesel neverator (EDC). BO 7 oo diesel nenerator was fr=ediatej
@ l water was detected in #7 cylinder. The backup ernernency 60 7 H9 h { ly tested satisf actorily_and the repfi rs cormence) on #1 EDG. The _ engine was re.pnited 80 l 7 o9 l
@ [by replacing the cylinder head _ and 13 3 d gasket. This is a reportable cecurrenceJ n CO 7 tl 9 l
@ laccordance with Technical Specification _{t.6.2h (2). (lfSRE S1-76-lo) 80 p.,vr 7 u9 ccwn Nt councNtsr s,su v C .ta s. min Mar.ur Ac Tu.* n votAYON CDOf CCDF COVPON' NT CODE h l E l [E_j IE IM i Cl I! NI El17 d43 44 iElIl4l7l 47
[MJ 48 7 09 10 11 12 CAUSL DECCRPTION crack in S7 cylinder head whic!}
@ [EMD-G51 Turbo Vee _20, 3810 Bhn diesci onnine surtained a 60 7 H9 inc ke t;. Thets w.3terfroml iextendedbetweentwoexhaustvalveseatsandthrounhthewater 60 l HH }
it.he Sylindet head unter Jacket u n porriittted to drip int _o the cylinder. (Continued) c-VI1HDD Of f AOut y DiSCG.f4v O'SCOvE nY Ot ECD'PflON
% I'OWin 01stn STAfus EE) stArus
[2J Lo_LsIol I n/^ l LaJ l n/i 00 I
12 13 44 45 46 7 u 9 10 senu OF LOCATON OF Pf tf ASE AVOUNT OF AC Ylvit y ttti E.( D Of rit f 5!
l 1 1 N/A I I N/A 80 10 11 44 45 7 0 9 PERSONNEL EXPOSURES Novi t n tiiE of SCn+1:oN I 1
Lo I o I of LzJ Lt4LA- 60 7 89 11 1H 13 PIHSONNEL INJURES NuVel H DESCn P h0N I EE] Io l o l ol I n/A 80 7 39 11 12 OfISl!E CONSLOUENCCS I
@l 7 09 N/A 60 LOSS On DAMAGE TO rACillTY ivrt Di SChPf ION l b (Zj i N/A _
60 7 89 10 PUUUCliY () h# l 3i N/A
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SO 7 0 11 ADDITIONAL i ACIOHS 3 IThe hackup enernency diesel rencrator was demonstrated _to be operable. eO Therefor 7 89 l
1- Isafety systems would have functioned if they had been requ_ ired. (Continued) eo 7 U9 T. I,. Ilaticota PHONE: (804) 357-3184 NAME. G9 0 801 961
CAUSE DESCRIPTION (CONTINUED)
Inspection of the engine prior to starting permitted detection of the water and prevented further damage to the engine.
This is the sixth cylinder head on this engine to be found with a crack, in a tima frame of juct over three months. USRE S1-76-07 listed the other incidents and Indicated the probabic cause as either a cylinder heat imbalance or a heat stresF as a result of an engine overheat condition at some previous time.
The location of /S head on the engine does not conform to the previous pattern and tends to eliminate a cylinder heat imbalance as the probable cause. It appears that a previous engine overheat condition has heat stressed the cylinder heads to such a point that premature metal f atigue f rom vibration is causing the cracks to appear between the exhaust valve seats. This is an area of high heat and vibration stress.
To ensure the reliability of this engine, the weekly testing of thic engine as outlined in USRE S1-76-07 will continue. New cylinder heads have been ordered and total replacement should preclude any additional failure. This course of action has been thoroughly discussed with the manufacturer's representative who concurs with this procedure.
ADDITIONAL FACTORS (CO:TTINUED)
Accordingly, no hazard to the safety or health of the generai public existed.
4
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VIMOINI A ELI:CTHIC AND l'OWHH COMI*ANh p Hica:Moxn.V HO M A nUM61 1
August 4, 1976 11 . 5 , + s
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'll s3 Mr. Normn C. !!oscley, Director Scrial No.173 Office of Inspection and Enforcement P0&M/ALil:jlf U. S. Nuclear Regulatory Comission Region II - Suite 818 Docket No. 50-280 230 Peacht.rce Street, Northwest License No. DPR-32 Atlanta, Georgia 30303
Dear Mr. Moscicy:
i Pursuant to Surry Power Station Technical Specification '6.6.2, the Virginia Electric and Power Company hereby submits a copy of Licensco Event Report No. USRE-S1-76-10.
1 The substance of this report has been reviewed by the Station Nuclear Safety and Operating Comittee and will be placed on the agenda' for the next meeting of the Syctem Nuclear Rafety and operating Comittee.
Very truly yours, 26.D7.ssaa:;,y l C. M. Stallings Vice President-Power Supply and Production Operations Enclosure -
I cc: tir. Robert W. Reid, Chief (40 copics)
Operating Reactors Branch 4 i
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