ML17354A452

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Submits Results of Inservice Insp SG Tube Plugging
ML17354A452
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 03/27/1997
From: Hovey R
FLORIDA POWER & LIGHT CO.
To: Reyes L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
L-97-084, L-97-84, NUDOCS 9704030004
Download: ML17354A452 (5)


Text

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REGULATd INFORMATION DISTRIBUTION ITEM (RIDE)

ACCESSION NBR:9704030004 DOC.DATE: 97/03/27 NOTARIZED: NO DOCKET FACIL:~>Wi-260'urkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH. NAME AUTHOR AFFILIATION HOVEY,R.J. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION REYES,L.A. Region 2 (Post 820201)

SUBJECT:

Submits results of inservice insp SG tube plugging.

DISTRIBUTION CODE: A047D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: OR Submittal: Inservice/Testing/Relief rom ASME Code GL-89-04 NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL E PD2-3 LA 1 1 PD2-3 PD 1 1 CROTEAUFR 1 1 INTERNAL: AEOD/SPD/RAB 1 1 CENTER 0 1 1 0 NRR/DE/EMEB 1 1 T 1 1 OGC/HDS3 1 0 RES/DET/EIB 1 1 RES/DET/EMMEB 1 1 EXTERNAL: LITCO ANDERSON 1 1 NOAC 1 1 NRC PDR 1 1 D

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N NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 13 ENCL 12

e~ '4 MAR 3 7 1997 APL L-97-084 10 CFR 50.36 Luis A. Reyes Regional Administrator U. S. Nuclear Regulatory Commission 101 Marietta Street, N.W., Suite 2900 Atlanta, Georgia 30323

Dear Mr. Reyes:

Re: Turkey Point Unit 3 Docket No. 50-250 In accordance with Turkey Point Technical Specification 4.4 '.5.a, the subject Special Report is submitted pursuant to Specification 6.9.2 for Turkey Point Unit 3 as a result of the End-of-Cycle 15 inservice inspection of steam generator tubes.

The Turkey Point Unit 3 steam generators were inspected from March 13, 1997, through March 19, 1997. There were 3 steam generator 'I tubes plugged in steam generator 3A as a result of the inspection bringing the total tubes plugged in 3A to 20. There were 9 tubes plugged in steam generator 3B bringing the total tubes plugged in 3B to 27 'here were 2 tubes plugged in steam generator 3C bringing the total tubes plugged in 3C to 35. The attachment to this letter provides additional Unit 3 steam generator tube plugging details.

Should there be any questions, please contact us.

Very truly yours, R. J. Hove Vice President Turkey Point Plant MSD cc: USNRC, Document Control Desk, Washington, D.C.

T. PE Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9704030004 970327

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Attachment to L-97-084 End-of-Cycle 15 (NOTE: Technical Specification represented as TS below) 13 5 Defective per TS 4.4.5.4.a 31 18 Defective per TS 4.4.5.4.a 44 36 Defective per TS 4.4.5.4.a 37 20 Defective per TS 4.4.5.4.a 42 38 Defective per TS 4.4.5.4.a 39 39 Defective per TS 4.4.5.4.a 44 40 Defective per TS 4.4.5.4.a 23 41 Defective per TS 4.4.5.4.a 44 41 Defective per TS 4.4.5.4.a 41 44 Defective per TS 4.4.5.4.a 45 41 Preventively Plugged*

45 42 Preventively Plugged*

33 66 Defective per TS 4.4.5.4.a 30 48 Preventively Plugged**

  • Tubes adjacent to a foreign object were preventively plugged
    • Tube was preventively plugged due to wear at the anti-vibration bar