IR 05000400/2025004

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Integrated Inspection Report 05000400/2025004
ML26020A041
Person / Time
Site: Harris 
Issue date: 01/22/2026
From: Matthew Fannon
NRC/RGN-II/DORS/PB2
To: Joseph C
Duke Energy Progress
References
IR 2025004
Download: ML26020A041 (0)


Text

SUBJECT:

SHEARON HARRIS NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000400/2025004

Dear Carolyne Joseph:

On December 31, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Shearon Harris Nuclear Plant. On January 14, 2026, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Shearon Harris Nuclear Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at Shearon Harris Nuclear Plant.

January 22, 2026 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Matthew S. Fannon, Chief Projects Branch 2 Division of Operating Reactor Safety Docket No. 05000400 License No. NPF-63

Enclosure:

As stated

Inspection Report

Docket Number:

05000400

License Number:

NPF-63

Report Number:

05000400/2025004

Enterprise Identifier:

I-2025-004-0020

Licensee:

Duke Energy Progress, LLC

Facility:

Shearon Harris Nuclear Plant

Location:

New Hill, NC

Inspection Dates:

October 1, 2025, to December 31, 2025

Inspectors:

M. Bates, Senior Operations Engineer

P. Boguszewski, Senior Resident Inspector

M. Kay, Resident Inspector

K. Kirchbaum, Senior Operations Engineer

Approved By:

Matthew S. Fannon, Chief

Projects Branch 2

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Shearon Harris Nuclear Plant, in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Evaluate Main Steam PORV Hydraulic Fluid Temperature Limits

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000400/2025004-01

Open/Closed

[H.13] -

Consistent

Process

71152A

A self-revealed Green finding and associated non-cited violation (NCV) of Title 10 of the Code

of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion III, Design Control, was

identified when the licensee failed to provide design control measures to maintain the main

steam (MS) power operated relief valve (PORV) operable. Specifically, the licensee failed to

include provisions to assure that appropriate quality standards were specified and

incorporated into design documents. The licensee did not control deviations from those

standards when they failed to evaluate the temperature limits of the MS PORV actuator

hydraulic fluid prior to using temporary heaters to keep the fluid warm. This resulted in

exceeding the temperature limits of the hydraulic fluid and the C MS PORV failing to stroke

open during surveillance testing on June 10, 2025.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On October 3, 2025, Unit 1 was

shutdown for a planned refueling outage. After completion of the refueling outage, operators

commenced reactor startup on November 2, 2025. Unit 1 was returned to rated thermal power

on November 5, 2025, and remained at or near rated thermal power for the remainder of the

inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix DProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 2515,</br></br>Appendix D" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Spent fuel pool cooling system after core offload while 'B' safety bus was out of

service on October 17, 2025

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated system configurations during a complete walkdown of the

high head safety injection system on December 3, 2025.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Reactor auxiliary building steam tunnel on October 2, 2025

(2)

Reactor containment building 221' and 236' elevations on October 8, 2025

(3)

Reactor containment building 261' and 286' elevations on October 8, 2025

(4)

'A' and 'B' 6.9kV switchgear rooms on December 16, 2025

(5)

Reactor auxiliary building 324' elevation on December 19, 2025

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

The licensee completed the annual requalification operating examinations required to be

administered to all licensed operators in accordance with Title 10 of the Code of Federal

Regulations 55.59(a)(2), "Requalification Requirements," of the NRC's "Operator's

Licenses." The inspector performed an in-office review of the overall pass/fail results of the

individual operating examinations, and the crew simulator operating examinations in

accordance with IP 71111.11, "Licensed Operator Requalification Program and Licensed

Operator Performance." These results were compared to the thresholds established in

Section 3.03, "Requalification Examination Results," of IP 71111.11.

(1)

The inspectors reviewed and evaluated the licensed operator examination failure

rates for the requalification annual operating exam completed on December 18, 2025.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1)

Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification

written examination completed on March 8, 2024.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification

operating test.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering

requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility

licensee is effectively evaluating their licensed operators for mastery of training

objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination

material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the

licensee and reviewed the adequacy of re-examinations for licensed operators who

did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators

met the conditions of their licenses.

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room

simulator in modeling the actual plant, and for meeting the requirements contained in

10 CFR 55.46.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2

Samples)

(1)

The inspectors observed and evaluated licensed operator performance in the control

room during a reactor shutdown for a planned refueling outage on October 3, 2025.

(2)

The inspectors observed and evaluated licensed operator performance in the control

room during reactor startup on November 1, 2025.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Elevated risk due to lowered inventory during refueling outage on October 6, 2025

(2)

Elevated risk due to 'B' safety bus outage during refueling outage on October 10,

2025

(3)

Elevated risk due to lowered inventory for reactor vessel head reinstall during

refueling outage on October 23, 2025

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (1 Sample)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

Refueling water storage tank header pipe broken variable spring support (Nuclear

Condition Report (NCR) 2571834) on December 3, 2025

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1

Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)

Engineering Change 420531, 'B' startup transformer replacement on October 14,

2025

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated refueling outage H1R26 activities from October 3, 2025, to

November 1, 2025.

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system

operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (5 Samples)

(1)

OST-1815, "Remote Shutdown: Test of Interposing MDR Relays Primary and Backup

Fuses," following transfer auxiliary relay TRA-1/1746 replacement on October 19,

2025

(2)

OST-1100, "Emergency Safeguards Sequencer 1B-SB Response Time Test,"

following maintenance on October 21, 2025

(3)

OST-1043, "Reactor Coolant System Vent Path Operability," following maintenance

on 1RC-905 on October 27, 2025

(4)

LP-L-0926, "Accumulator Tank B Level," following replacement of 'B' cold leg

accumulator level transmitter on December 15, 2025

(5)

OST-1824, "1B-SB Emergency Diesel Generator Operability Test," following multiple

relay replacements in the 'B' sequencer on December 19, 2025

Surveillance Testing (IP Section 03.01) (1 Sample)

(1)

LP-P-2001A/B, "Feedwater to Steam Generator A Pressure," loop calibration on

October 24, 2025

Containment Isolation Valve (CIV) Testing (IP Section 03.01) (1 Sample)

(1)

1ED-161, reactor coolant drain tank hydrogen supply and vent, local leak rate testing

during refueling outage on October 14, 2025

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS08: Heat Removal Systems (IP Section 02.07) (1 Sample)

(1)

October 1, 2024, through September 30, 2025

MS10: Cooling Water Support Systems (IP Section 02.09) (1 Sample)

(1)

October 1, 2024, through September 30, 2025

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1)

'C' Main Steam power operated relief valve (PORV) failure to stroke during

surveillance testing (NCR 02557590) on December 10, 2025

71152S - Semiannual Trend Problem Identification and Resolution

Semiannual Trend Review (Section 03.02) (1 Sample)

(1)

The inspectors reviewed the licensees corrective action program to identify potential

trends that might be indicative of a more significant safety issue.

INSPECTION RESULTS

Failure to Evaluate Main Steam PORV Hydraulic Fluid Temperature Limits

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000400/2025004-01

Open/Closed

[H.13] -

Consistent

Process

71152A

A self-revealed Green finding and associated non-cited violation (NCV) of Title 10 of the

Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion III, Design Control,

was identified when the licensee failed to provide design control measures to maintain the

main steam (MS) power operated relief valve (PORV) operable. Specifically, the licensee

failed to include provisions to assure that appropriate quality standards were specified and

incorporated into design documents. The licensee did not control deviations from those

standards when they failed to evaluate the temperature limits of the MS PORV actuator

hydraulic fluid prior to using temporary heaters to keep the fluid warm. This resulted in

exceeding the temperature limits of the hydraulic fluid and the C MS PORV failing to stroke

open during surveillance testing on June 10, 2025.

Description: Each main steam supply line is provided with one PORV, Harris has three main

steam lines and three associated MS PORVs. The safety-related MS PORVs are designed to

remove heat from the nuclear steam supply system when the main steam isolation valves are

closed. Additionally, in the event of a ruptured steam generator, the MS PORVs can be used

to depressurize the reactor coolant system so that residual heat removal can be placed in

service.

During routine surveillance testing in June 2025, the C MS PORV failed to stroke open when

the output was raised to 100% from the control room. Operations declared the C MS PORV

inoperable and commenced troubleshooting. Two solenoid valves, two pilot operated check

valves and one dual pilot check valve that are internal to the hydraulic actuator were

examined by the vendor. The vendor identified each solenoid valve had a varnished surface

and was sticky to the touch. The two solenoid valves identified as varnished are modulating

valves which permit movement of pressurized hydraulic fluid during operation which provides

a mode of force for the MS PORV to open or close. The vendor attributed the failure of the

solenoid valves to the varnished surface likely caused by overheating. A review of quarterly

maintenance on the PORVs identified that in January of 2025, as a result of temporary heater

installation, the C MS PORV actuator hydraulic fluid was subjected to 160 degrees F, which

is the maximum recommended operating temperature for the fluid. Due to being further away

from the heaters, the A and B MS PORV actuator hydraulic fluid temperature were

recorded to be 100 degrees F.

The temporary heaters were previously installed near the MS PORV actuators in April 2024

while Harris Unit 1 was in a refueling outage. During a refueling outage there is no steam in

the main steam lines and therefore the steam tunnel experiences colder temperatures. Based

on previous issues with MS PORV operations during outages, the vendor recommended

keeping the actuator hydraulic fluid temperature above 70 degrees. This was being

accomplished with the use of temporary heaters. The heaters were installed using licensee

procedure AP-301 Seasonal Weather Preparations and Monitoring, but there is no record

(work request or work order) that controlled installation of the heaters. The licensee placed

the unit online on May 12, 2024. However, the heaters remained powered and unmonitored.

This resulted in the uncontrolled addition of heat to the MS PORV hydraulic fluid ultimately

resulting in the C MS PORV failing to stroke open from the main control room on June 10,

2025.

Per licensee procedure AP-301, drawing/checklist 7-S-5917, Seasonal HVAC Equipment

Installations, should have been completed prior to installing the temporary heaters. The

licensee failed to complete the checklist, which would provide guidance on whether

installation of temporary heater warrants an Engineering Change product. Duke Energy

performed a causal evaluation and determined that licensee procedure AP-301 and drawing

7-S-5917 were inadequate to ensure evaluation of the temperature impacts on components

are evaluated prior to placement of temporary heaters.

Corrective Actions: The licensee entered the condition into their corrective action program,

performed corrective actions to restore operability of the C MS PORV which included a

complete actuator replacement during the most recent refueling outage in October 2025, and

completed a causal evaluation. The licensee also established administrative limits for the total

acid number based on vendor recommendation which is an indicator of the potential for

varnish formation on internal components. The licensee has planned corrective actions to

revise AP-301 and drawing 7-S-9517 to ensure that potential temperature impacts on

components (including internal fluids and environmental quality temperature impacts) are

evaluated prior to use of temporary heaters. Additionally, the licensee plans to revise the

vendor manual and preventive maintenance procedure for the MS PORV actuators to include

more detailed tracking of MS PORV actuator hydraulic fluid health.

Corrective Action References: NCR 02557590

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensees failure to provide

design control measures for installation of temporary heaters to maintain the MS PORV

actuators operable was a performance deficiency that was within the licensees ability to

foresee and correct.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Design Control attribute of the Mitigating Systems

cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the licensee failed to evaluate the temperature limits of the MS

PORV hydraulic fluid prior to the placement of temporary heaters. This affected the

availability and reliability of the MS PORVs.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., The Significance Determination Process for Findings At-Power. The inspectors

determined a detailed risk evaluation (DRE) was required. A regional Senior Reactor Analyst

(SRA) performed a DRE using SAPHIRE 8 Version 8.2.11 and the Harris SPAR Model

Version 8.83 dated September 21, 2023. The exposure time was considered to be T/2 since

the last successful valve opening test was completed on December 5, 2024, and the date of

the failed test occurred on June 10, 2025 (188 days/2), plus repair time until June 30, 2025,

when the PORV was returned to service. This is a total of 114 days. The SRA modelled the

condition by setting MSS-ARV-CC-MS62 SG 1C PORV MS-62 FAILS TO OPEN, to TRUE.

The dominant accident sequence was a steam generator tube rupture, with a failure of

auxiliary feedwater, main feedwater, and a failure of operators to isolate the affected steam

generator. The change in core damage frequency was less than 1 E-6 corresponding to a

finding of very low safety significance (GREEN).

Cross-Cutting Aspect: H.13 - Consistent Process: Individuals use a consistent, systematic

approach to make decisions. Risk insights are incorporated as appropriate. Specifically, the

licensee failed to follow procedure AP-301 and subsequently drawing 7-S-9517 to evaluate

the impact of temporary heaters on the MS PORV actuator hydraulic fluid. An upper

temperature limit was not established due to inadequate control of temporary heaters.

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criterion III, "Design Control," states in part that

measures shall be established to assure that applicable regulatory requirements and the

design basis, as defined in § 50.2 and as specified in the license application, for those

structures, systems, and components to which this appendix applies are correctly translated

into specifications, drawings, procedures, and instructions. These measures shall include

provisions to ensure that appropriate quality standards are specified and included in design

documents and that deviations from such standards are controlled. Measures shall also be

established for the selection and review for suitability of application of materials, parts,

equipment, and processes that are essential to the safety-related functions of the structures,

systems and components.

Contrary to the above, from April 2024 to June 2025, the licensee failed to assure that

appropriate quality standards related to the MS PORV actuator hydraulic fluid were specified

and that any deviations are controlled.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On January 14, 2026, the inspectors presented the integrated inspection results to

Carolyne Joseph and other members of the licensee staff.

On December 18, 2025, the inspectors presented the biennial licensed operator

requalification inspection results to Kevin O'Brien, Training Manager, and other members

of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NCR 2577396

WR 20298507

Corrective Action

Documents

WRs

20296239

20296240

20753755

20296243

20296240

5-S-0550

Simplified Flow Diagram Containment Spray System Unit 1

Revision 18

5-S-1304

Simplified Flow Diagram Chemical and Volume Control

System Sheet 2

Revision 14

5-S-1305

Simplified Flow Diagram Chemical and Volume Control

System Unit 1

Revision 30

5-S-1308

Simplified Flow Diagram Safety Injection System

Revision 12

5-S-1309

Simplified Flow Diagram Safety Injection System Sheet 2

Unit 1

Revision 21

5-S-1310

Simplified Flow Diagram Safety Injection System Sheet 3

Unit 1

Revision 14

Drawings

5-S-1324

Simplified Flow Diagram Residual Heat Removal System

Unit 1

Revision 12

71111.04

Procedures

OP-110

Safety Injection

Revision 53

CSD-HNP-PFP-

CNMT

Containment Building Pre-Fire Plan

Revision 0

CSD-HNP-PFP-

RAB-261

Reactor Auxiliary Building Elevation 261 Pre-Fire-Plan

Revision 4

CSD-HNP-PFP-

RAB-286

Reactor Auxiliary Building Elevation 286 Pre-Fire Plan

Revision 4

71111.05

Procedures

CSD-HNP-PFP-

RAB-305-324

Reactor Building Elevations 305 and 324 Pre-Fire Plan

Revision 6

Drawings

TK-1-261-1-CT-

H-201

Containment Spray

5/D

71111.15

Procedures

DBD-106

Containment Spray System

Revision 19

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

5-S-1309

Simplified Flow Diagram Safety Injection System

Revision 23

6-B-401 Sheet

1148

Emergency Load Sequencer ESS Cabinet 1B-SB

Revision 14

6-B-401 Sheet

1165

Emergency Load Sequencer ESS Cabinet 1B-SB Sh. 20

Revision 15

6-B-401 Sheet

1750

Emergency Diesel Generator 1B-SB Breaker 126SB Sh. 2

Revision 12

6-B-401 Sheet

1752

6.9 KV Emer Bus 1B-SB to Aux Bus 1E Tie BKR 125 SB Sh.

Revision 11

6-B-401 Sheet

2008

Diesel Generator 1B-SB Engine Control Sh. 1

Revision 15

6-B-401 Sheet

2304

ESW Aux Reservoir Bay No. Traveling Screen 1B-SB

Revision 13

Drawings

6-B-401 Sheet

3290

Emer Service Water Intake Structure Elec Equipment Room

Supply Fan AH-86(1B-SB)

Revision 13

Engineering

Changes

EC 424373

Accumulator Transmitter Upgrade to Rosemount

Revision 12

EST-212

Type C Local Leak Rate Tests

Revision 6

Procedures

LP-P-0926

Accumulator Tank B Level

Revision 8

71111.24

Work Orders

20681859

NCR 2557590

Corrective Action

Documents

NCRs 2505389

2505381 2512233

2512232 2518442

2526518 2547223

2537547

5-S-0542

Simplified Flow Diagram Main Steam System Unit 1

Revision 28

Drawings

7-S-9517

Seasonal HVAC Equipment Installations

Revision 3

Miscellaneous

VM-OSO

Operators

Revision 22

AD-MN-ALL-0800

Temporary Power

Revision 3

AP-301

Seasonal Weather Preparations and Monitoring

Revision 89

OP-126

Main Steam, Extraction Steam, and Steam Dump Systems

Revision 45

71152A

Procedures

OST-1191

Steam Generator PORV and Block Valve Operability Test

Revision 33