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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000285/LER-1998-003, Re Individual Leaving High Radiation Area (HRA) Door Unlocked & Uncontrolled While in Hra. LER 98-003-00 Retracted1998-06-23023 June 1998 Re Individual Leaving High Radiation Area (HRA) Door Unlocked & Uncontrolled While in Hra. LER 98-003-00 Retracted 05000285/LER-1990-0071990-08-0101 August 1990 LER 90-007-02:on 900228,determined That Main Feedwater & Main Steam Piping Outside Design Basis.Caused by Design Deficiency & Failure of Engineer to Consider Loads Induced on Piping.Piping Supports modified.W/900801 Ltr 05000285/LER-1990-0101990-07-0303 July 1990 LER 90-010-01:on 900327,unplanned Attempted Start of Emergency Diesel Generator Occurred While Plant in Refueling Shutdown.Caused by Low Air Pressure in Diesel Start Sys. Instructions Re auto-start Signals changed.W/900703 Ltr ML20071G3271978-12-22022 December 1978 /03L-0 on 781124:during Shutdown Cooling Interlock Test Noted That PC-105B Was Not Operating.Caused by Valve Closing Relay 94-347/348 Not Being Wired to PC-105B; Inadvertently Disconnected in 1977 ML20071G2671978-12-22022 December 1978 /03L-0 on 781204:during Inspec of Discharged Fuel Assemblies,A Single Fuel Pin Was Observed to Have Failed, Assoc W/Manufacture & Exposure of Present Day Nuc Fuel ML20071G2381978-12-21021 December 1978 /03X-1 on 780918:during Refueling Outage,D Channel Hot Leg Temp Indication Was Investigated to Determine Cause of 780918 Failure.Failure Caused by Rosemount Model 104VC RTD Having Water in the Pothead ML20071G2201978-12-20020 December 1978 /03L-0 on 781122:noted That Level Transmiter for C Channel (C/LT-901) for Steam Generator RC-2A Level Instrumentation Not W/In Specs.Caused by Calibr Drift of Ge/Mac Model 555 Transmitter ML20071G2791978-12-19019 December 1978 /03L-0 on 781214:during 1978 Refueling Outage, Certain Surveillance Tests Req by Tech Specs Could Not Be Performed Because of Shutdown Condition.Facil Lic Change 77-11 Submitted to NRC on 781109 to Delete Requirements ML20071G0701978-12-12012 December 1978 /03L-0 on 781113:during Test of Ventilation Isolation Actuation Signal,Lockout 86B1/VIAS Did Not Trip. Cause Unidentified,Since Relay Retested & Found to Be Operating Normally.Relays Will Continue to Be Tested ML20071G0851978-12-0808 December 1978 /01T-0 on 781127:Diesel Generator 2 Failed to Auto Close Onto the Bus;Breaker Mode Switch Contracts 27-27c Failed to Make Contact.Caused by Contact Failure ML20071G1011978-12-0505 December 1978 /03L-0 on 781116:during Refueling,All Limitorque Valves Were Inspec for Proper Staking of the Lock Nut on the Motor operator.30 of 65 Valves Exhibited Unstaked Lock Nuts.Lock Nuts Were Staked IAW Manufacturer'S Instructions ML20071F9281978-11-27027 November 1978 /03L-0 on 781101:auxiliary Feedwater Check Valve FW-164 Found to Be Oriented in Wrong Position.Caused by Missing Valve Disk Plate Which Was Subsequently Located & Recovered ML20071F9061978-11-25025 November 1978 /03L-0 on 781026:repeated Tripping of Stack Particulate Process Monitor.Caused by Trip Set in Accordance W/Tech Specs Table 2-1 at 9.6x10-2,rather than More Conservative Release Rates 2x10-3 ML20071F8541978-11-0202 November 1978 /03L-0 on 781014:Reactor Coolant Cold Leg Temp Indicator B/122C Failed High Off Scale Because of an Open Circuited Rosemount Model 104VC Rtd.The RTD Will Be Replaced During Present Refueling Outage ML20071F4821978-10-0606 October 1978 /03L-0 on 780908:Inadvertent Radioactive Gas Release to Atmosphere Caused by Leakage Past Check Valve CH-284,HG-100 & Relief Valve HG-105.Valves Will Be Inspected & Replaced or Repaired During Next Refueling Outage ML20147B1901978-10-0303 October 1978 /01T-0 on 781003:During Oper Check on Auxiliary Steam Driven Feed Pump,The Steam Inlet Valve YCV-1045 Did Not Open Due to Closed Air Supply ML20071F4671978-09-27027 September 1978 /03L-0 on 780831:failure of Tri-x Weather Tower'S 100 Meter Delta-T Sensor Sys to Rept Stability Class Info. Calibrations Revised to Ensure Instruments Detect Subsequent Sensor Sys Failures ML20071F4881978-09-15015 September 1978 /03L-1 on 780830:Bchannel RPS Variable Overpwr Trip Reset Demand Alarm Actuated & Would Not Reset.Then,Hi Pwr & Thermal Margin/Low Pressure Trip Units Failed,Both Due to Failure of Devar19-601A,18volt Pwr Supply 05000285/LER-1976-005, Suppl 1 to LER 76-05/03L:on 770210,recirculation Actuation Pressure Switches Found Out of Tolerance.Cause Not Stated. Switch Will Be Calibr Monthly Until New Switches Installed1977-02-10010 February 1977 Suppl 1 to LER 76-05/03L:on 770210,recirculation Actuation Pressure Switches Found Out of Tolerance.Cause Not Stated. Switch Will Be Calibr Monthly Until New Switches Installed 05000285/LER-1976-019, Suppl 1 to LER 76-19/03L:on 761001,five of 10 Valve Setpoints Drifted from Tech Spec Tolerance of Plus or Minus 1%.Caused by Change in Environ Condition.Valves Will Be Inspected During Refueling Outage1976-10-14014 October 1976 Suppl 1 to LER 76-19/03L:on 761001,five of 10 Valve Setpoints Drifted from Tech Spec Tolerance of Plus or Minus 1%.Caused by Change in Environ Condition.Valves Will Be Inspected During Refueling Outage 05000285/LER-1976-021, Suppl 1 to LER 76-21/03L:on 760802,timer Relays for SI-3A, AC-3B & SI-3B Failed to Time Out at Set Times.Caused by Binding Operating Mechanisms.Timers Tested Twice Weekly to Verify Operability Until Replacements Received1976-08-0909 August 1976 Suppl 1 to LER 76-21/03L:on 760802,timer Relays for SI-3A, AC-3B & SI-3B Failed to Time Out at Set Times.Caused by Binding Operating Mechanisms.Timers Tested Twice Weekly to Verify Operability Until Replacements Received 05000285/LER-1976-010, Suppl to LER 76-10/03L:on 760401,high Power Margin to Trip Meter B Drifted from 4.2% to 6% Power.Caused by Drift of Feed Back Limiter Module 19-317-2X.Module Calibr & Operated Satisfactorily1976-04-0808 April 1976 Suppl to LER 76-10/03L:on 760401,high Power Margin to Trip Meter B Drifted from 4.2% to 6% Power.Caused by Drift of Feed Back Limiter Module 19-317-2X.Module Calibr & Operated Satisfactorily 1998-06-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217B5401999-10-0606 October 1999 Safety Evaluation Supporting Amend 193 to License DPR-40 ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data LIC-99-0096, Monthly Operating Rept for Sept 1999 for Fcs,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Fcs,Unit 1.With ML20211J9321999-09-0202 September 1999 Safety Evaluation Concluding That Licensee Proposed Alternatives Provide Acceptable Level of Quality & Safety. Proposed Alternatives Authorized for Remainder of Third ten- Yr ISI Interval for Fort Calhoun Station,Unit 1 LIC-99-0084, Monthly Operating Rept for Aug 1999 for Fort Calhoun Station.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Fort Calhoun Station.With ML20216E6431999-08-26026 August 1999 Rev 19 to TDB-VI, COLR for FCS Unit 1 ML20210R1961999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Fcs,Unit 1 ML20210G2181999-07-27027 July 1999 Safety Evaluation Supporting Amend 192 to License DPR-40 ML20210D9951999-07-22022 July 1999 Safety Evaluation Supporting Amend 191 to License DPR-40 ML20216E6361999-07-21021 July 1999 Rev 18 to TDB-VI, COLR for FCS Unit 1 ML20210R2081999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Fcs,Unit 1 LIC-99-0065, Monthly Operating Rept for June 1999 for Fort Calhoun Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Fort Calhoun Station,Unit 1.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20210P5461999-06-0808 June 1999 Rev 0,Vols 1-5 of Fort Calhoun Station 1999 Emergency Preparedness Exercise Manual, to Be Conducted on 990810. Pages 2-20 & 2-40 in Vol 2 & Page 4-1 in Vol 4 of Incoming Submittal Not Included ML20195B4581999-05-31031 May 1999 Rev 3 to CE NPSD-683, Development of RCS Pressure & Temp Limits Rept for Removal of P-T Limits & LTOP Requirements from Ts ML20207H7401999-05-31031 May 1999 Performance Indicators Rept for May 1999 LIC-99-0053, Monthly Operating Rept for May 1999 for Fort Calhoun Station,Unit 11999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Fort Calhoun Station,Unit 1 ML20195B4521999-05-17017 May 1999 Technical Data Book TDB-IX, RCS Pressure - Temp Limits Rept (Ptlr) ML20206L4241999-05-10010 May 1999 Safety Evaluation Supporting Corrective Actions to Ensure That Valves Are Capable of Performing Intended Safety Functions & OPPD Adequately Addressed Requested Actions Discussed in GL 95-07 ML20206M2601999-05-0606 May 1999 SER Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & IPEEE Results Reasonable Given FCS Design,Operation & History LIC-99-0047, Monthly Operating Rept for Apr 1999 for Fort Calhoun Station Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Fort Calhoun Station Unit 1.With ML20195E8621999-04-30030 April 1999 Performance Indicators, for Apr 1999 ML20205Q5831999-04-15015 April 1999 Safety Evaluation Supporting Amend 190 to License DPR-40 ML20210J4331999-03-31031 March 1999 Changes,Tests, & Experiments Carried Out Without Prior Commission Approval for Period 981101-990331.With USAR Changes Other than Those Resulting from 10CFR50.59 ML20206G2641999-03-31031 March 1999 Performance Indicators Rept for Mar 1999 LIC-99-0034, Monthly Operating Rept for Mar 1999 for Fcs,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Fcs,Unit 1.With ML20205J8181999-02-28028 February 1999 Performance Indicators, for Feb 1999 LIC-99-0025, Monthly Operating Rept for Feb 1999 for Fort Calhoun Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Fort Calhoun Station,Unit 1.With ML20207F3291999-01-31031 January 1999 FCS Performance Indicators for Jan 1999 ML20203B0991998-12-31031 December 1998 Performance Indicators for Dec 1998 LIC-99-0026, 1998 Omaha Public Power District Annual Rept. with1998-12-31031 December 1998 1998 Omaha Public Power District Annual Rept. with LIC-99-0003, Monthly Operating Rept for Dec 1998 for Fort Calhoun Station.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Fort Calhoun Station.With ML20198S3771998-12-31031 December 1998 Safety Evaluation Supporting Amend 189 to License DPR-40 ML20198S4831998-12-31031 December 1998 Safety Evaluation Supporting Amend 188 to License DPR-40 ML20196G2251998-12-18018 December 1998 Rev 2 to EA-FC-90-082, Potential Over-Pressurization of Containment Penetration Piping Following Main Steam Line Break in Containment ML20198M3141998-11-30030 November 1998 Performance Indicators Rept for Nov 1998 LIC-98-0172, Monthly Operating Rept for Nov 1998 for Fort Calhoun Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Fort Calhoun Station,Unit 1.With LIC-98-0160, Special Rept:On 981113,MSL RM RM-064 Was Declared Inoperable Due to Leakage Past Isolation Valve HCV-922.Troubleshooting Has Indicated That Leakage Has Stopped & Cause of Leak Continues to Be Investigated1998-11-25025 November 1998 Special Rept:On 981113,MSL RM RM-064 Was Declared Inoperable Due to Leakage Past Isolation Valve HCV-922.Troubleshooting Has Indicated That Leakage Has Stopped & Cause of Leak Continues to Be Investigated ML20203B0721998-11-16016 November 1998 Rev 6 to HI-92828, Licensing Rept for Spent Fuel Storage Capacity Expansion ML20196E4981998-10-31031 October 1998 Performance Indicators Rept for Oct 1998 ML20196G2441998-10-31031 October 1998 Changes,Tests & Experiments Carried Out Without Prior Commission Approval. with USAR Changes Other than Those Resulting from 10CFR50.59 LIC-98-0154, Monthly Operating Rept for Oct 1998 for Fort Calhoun Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Fort Calhoun Station,Unit 1.With ML20154M4881998-10-19019 October 1998 Safety Evaluation Supporting Amend 186 to License DPR-40 ML20154N2411998-10-19019 October 1998 Safety Evaluation Supporting Amend 187 to License DPR-40 LIC-98-0136, Monthly Operating Rept for Sept 1998 for Fort Calhoun Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Fort Calhoun Station,Unit 1.With ML20155G4261998-09-30030 September 1998 Performance Indicators for Sept 1998 ML20154A1251998-08-31031 August 1998 Performance Indicators, Rept for Aug 1998 LIC-98-0122, Monthly Operating Rept for Aug 1998 for Fort Calhoun Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Fort Calhoun Station Unit 1.With ML20238F7231998-08-17017 August 1998 Owner'S Rept for Isis ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency 1999-09-30
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LICENSEE EVENT RF. PORT
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3 60 61 DCOKET NLMBER 68 69 EV ENT O ATE 74 75 AE809T OATE dJ EVENr DESCRIPTION AND PRC8 ABLE CONSECUENCES h l o' 6 2 l lDuring the parfor w ce of shutdown cooling interlock test (ST-SDC-1) it was discoveredt i o e a i I that PC-1053 was not operating. Further investigation showed relay 9h-3h7/3h8 (the l I o i A I l valve closing relay) was not vired to PC-1053 and was inoperable since the 1977 l lo46; } Refueling Outage. The redundant shutdown cooling interloch PC-105 was operable duringl l0t6l l this period. l l 017 l l l t o ia l ! - I
- es 3 SYSTEM CAUSE CAUSE COMP. vatyE CODE COCE SUSCOCE COMPCNENT CODE SueCODE SUBCOCE
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_i 22 :2 24 a :: := a ao si :2 ACTtON . FUTURE EpsECT SMUT 0cWN ATTACMMENT N*m O 4 PatME COMP. COM*CNEN*
TAKEN ACTICN ON PLANT METHCO hours -- SUSMITTED FORM aus. SUP*LIEm MANUS AC 1,;RER IFl@izl@ Izl@ 12 l@ I o 10 l o l o l I44 Yl@ Ll1@ l43Al@ l ci of 81 (47 3-33 34 25 . 36 de_ 40 42 ais CAUSE CESORIPTION AND CORRECTIVE AC*lCNS h ji i o , l During installation of Pcver Operated Felief Valve Modification du-ine the icT" !
- i,., Irefueling cutare, relay 9h-3h7/?h6 was inadve- entiv disee ne ai f-rn 00-102 . *4e 1 l
t., il error vas not .Stected prier te subsecuent unit operatien since it was no- kncv- a- I
[- j jthe a -kat the shutdevn cocline pressu~e interlock sve-a- kd keen effected. U:c- f i .! Idiscovery redundant interlock vas provided and both inter 10cks tested satisfactorilv. I 7 3 3 40 pactLITV a ME* WOO C8 STATUS %PCWER QTHER STATUS - CISCOV ERY OISCOVERY OES0miPTICN 4-i li i t al 5W@ l 01010 7 to l@l HA 12 is 44 l3l@l as as Surveillance '"est so l
ACTIVITY CONTENT
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1 lIR 78-Oh2 0-^a Public Power District Fort Calhoun Station Unit ilo. 1-Docket No. 05000285
- i. Attachment No. 1 Safet1 Analysis The Fort Calhoun Station Unit No.1 safety syste= is so designed that no l
single inoperable channel can prevent the perfomance of a safety function if j required. During the ti=e in which PC-105B was inoperable, Plos, the redund-ant channel was operable.
I The function of the shutdown cooling interlock is to provide automatic isolation of the shutdevn cooling isolation valves HCV-3kT and ECV-3h8 to protect the safety injection piping in the event the reactor coolant loop
( pressure' exceeds 250 psia while on the shutdown ecoling decay heat renoval syste=. Operator action and the auto =atic operation of P105 intericek pro-vided adequate protection'of the piping during the ti=e PC-1053 was inoperable.
It should be noted that .HCV-3kT'and ECV-3h8 are locked closed during power operation. Opening these valves when reactor coolant system pressure is greater than 250 psia is prevented bf:
- 1. Ad=inistrative control of key operated control switch,
- 2. P-105 pressure interlock, and ,
3 PC-1053 pressure switch interlock.
PC-1053 was incapable cf perfor-4ng its interlock function as a result of this incident. Pressure channel 113/115 nov perfor=s this interlock function 4
in conforance with the design package.
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~IF. 78-Ch2 C=aha Public Pcver District Fort Calhoun Station Uni,:Ic. 1 tocket UO. 050002B5
. Attach =ent No. 2 Corrective Action to P-event Rececu-rence Adherence to the recently revised Station Modi'.ication Control Procedure should prevent reoccurrence of this type incident.
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7.2?. 7S-ch2 C=aha Public Power Distric:
Fort Calhoun Station Unit No. 1 Docket No. 03000233
- Attachnent No. 3 Failure Dsts This is the first installation e - -epor.able at the Fort Calhoun Statics Unit no. 1.
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