GO2-83-815, Final Deficiency Rept 251 Re Limitorque Motor Operators W/ Motors from Baldor Electric Co Unqualified Per IEEE 382-1972.Initially Reported on 830422.Limitorque Will Replace Motors W/Units That Meet NUREG-0588 Requirements

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Final Deficiency Rept 251 Re Limitorque Motor Operators W/ Motors from Baldor Electric Co Unqualified Per IEEE 382-1972.Initially Reported on 830422.Limitorque Will Replace Motors W/Units That Meet NUREG-0588 Requirements
ML20078B170
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 09/08/1983
From: Carlisle C
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
RTR-NUREG-0588, RTR-NUREG-5688, RTR-NUREG-588 10CFR-050.55E, 10CFR-50.55E, 251, GO2-83-815, NUDOCS 8309260408
Download: ML20078B170 (2)


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Washington Public Power Supply System .

P.O. Box 968 3000 GeorgeWashingtonWay Richland, Washington 99352 (509)372 5b ,4 .N Docket No. 50-397 V.9

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Septeraber 8,1983 G02-83-815 Mr. J. B. Martin Regional Administrator U.S. Nuclear Regulatory Commission Region V 1450 Maria Lane, Suite 210 Walnut Creek, California 94596

Subject:

NUCLEAR PROJECT N0. 2 10CFR50.55(e) CONDITION #251, LIMITORQUE MOTOR OPERATORS WITH MOTORS FROM BALDOR ELECTRIC COMPANY

Reference:

Telecon QA2-83-059, dated April 22, 1983, L.C. Floyd to R. Dodds.

In accordance with the provisions of 10CFR50.55(e), your office was in-formed by telephone, of the above subject conditions. Attachment I pro-vides the Project's final report on Condition #251.

If you have any questions, contact Roger Johnson, WNP-2 Project QA Manager, at (509) 377-2501, extension 2712.

f Program Director, WNP-2 ,

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Attachment:

As stated cc: W.S. Chin, BPA N.D. Lewis, EFSEC A. Toth, NRC Resident Inspector Document Control Desk, NRC B309260408 830908 I PDR ADOCK 05000397 ,

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WASHINGTON PUBLIC POWER SUPPLY SYSTEM NUCLEAR PROJECT H0. 2 DOCKET NO. 50-397 LICENSE NO. CPPR-93 10CFR50.55(e) CONDITION #251 LIMITORQUE MOTOR OPERATORS WITH HOTORS FROM BALDOR ELECTRIC COMPANY FINAL REPORT Description of Deficiency i

Motor operated valves were received from the manufacturer with unqualified l

motors by Baldor Electric Company. Condition was discovered after valves were installed during equipment qualification group walkdown to obtain nameplate data on March 24, 1983. The valves involved are SW-H0-187A, -1878, -188A, and

-188B.

Safety Significance Valves SW-M0-187A and B and SW-M0-188A and B are Service Water System (SW) iso-lation valves at the interface with the Reactor Closed Cooling Water System (RRC) to provide an alternate cooling water source for the fuel pool cooling heat exchangers FPC-HX-1A and IB. The valves will allow utilization of the seismic Class I service water system for FPC cooling in the event of an earth-quake. Operation of the valves is not required for normal plant operations, but only under emergency conditions. The unqualified motors would have the potential for jeopardizing corrective action to meet emergency conditions and the deficiency is, therefore, considered reportable.

Cause for the Deficiency Error on the part of the manufacturer in that Limitorque supplied motor opera-tors to WNP-2 with motors that were not qualified to IEEE 382 - 1972.

Corrective Action The manufacturer, Limitorque, has been made aware that the motors were impro-perly supplied and is to replace the existing motors with units qualified to IEEE-382-1972 meeting requirements of NUREG-0588 Category II. Startup Defici-ency Reports (SDR) #8308, 8309, 8310, and 8312 have been issued to identify the deficient condition. The new qualified motors have been received from the manufacturer, but the physical replacement of the motors has been deferred until no later than the first refueling outage. This decision is based on the 4 ser-vice water valves identified are part of the fuel pool cooling modification, which has been deferred.

Action to Prevent Recurrence The vendor has pri. nary responsibility for assuring that components supplied correlate with the qualification records submitted to substantiate their suita-bility for the service designated.

The Supply System Equipment Qualification Program represents a complete review of safety-related equipment relative to environmental and seismic qualification.

This program assures that components are qualified for their design service conditions and will preclude unqualified components in completed plant installa-tions, unless justified by specific evaluation, such as the J10.

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