ML20202G473

From kanterella
Revision as of 11:18, 20 December 2021 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Insp Rept 50-331/98-02 on 971223-980204.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support
ML20202G473
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 02/06/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20202G435 List:
References
50-331-98-02, 50-331-98-2, NUDOCS 9802200137
Download: ML20202G473 (22)


See also: IR 05000331/1998002

Text

. _ _ _ _ _ _ _ _ - . _ _ _ _ - _ -

.

.

.

.- U. S. NUCLEAR REGULATORY COMMISSION

REGION lli

Docket No: 50 331

- Ucense No: DPR-49

.

Report No: 50-331/98002(DRP)

' Licensee: IES Utilities Inc.

200 First Street S.E.

P. O. Box 351.

Cedar Rapids, IA 52406 0351

Facility: . Duane Amold Energy Center

,

. Location: Palo, Iowa

Dates: December 23,1997 - February 4,1998

. Inspectors: C. Lipa, Senior Resident inspector

M. Kurth, Resident inspector

Approved by: R. D. Lanksbury, Chief

- Reactor Projects Branch 5

9002200137 990206

PDR ADOCK 05000331  ;

.O. PDR ,

_o

- - - - - - - - - - - - - - - - - - _ . -

,

EXECUTIVE SUMMARY

Duane Arnold Energy Center

NRC Inspection Report No. 50 331/98002(DRP)

This inspection report included resident inspectors' evaluation of aspects of licensee operations,

engineering, maintenance, and plant support.

Operations

l The conduct of operations continued to be professional, wit', appropriate focus on safety

as demonstrated by prompt identification of emergent equipment issues and the well-

controlled power reduction on January 22,1998. (Section 01.1).

l * The inspectors and licensee identified three instances where the limiting condition for

operation was exceeded for primary containment isolation valves. This resulted in three

violations. The inspectors were concerned that several discussions were necessary with

licensee personnel before a review of th6 issue was initiated. The inspectors concluded

that the licensed took the appropriate action following identification of the issue.

(Section 01.2).

and emergency diesel generator systems equipment was properly maintained.

Housekeeping within the plant was acceptable in most cases. (Section 02.1).

Maintenance

  • The inspectors identifbd weak controls in the testing and installation of standby liquid

control .ystem squib valve explosion charges. Specifically, there were no formal controls

to ensure that TS requirements regarding charges coming from the same batch would be

adhered to. (Section M1.2).

  • The licensee promptly resolved equipment issues that occurred during the inspection

period. Personnel from the maintenance and engineering departments provided good

support and exhibited good teamwork in resolong the issues. Additional efforts were

planned to reduce containment atmosphere monitor system leakage and prevent this

from continuing to be a recurring problem. (Section M2.1).

  • Corrective acthn following identification of an incorrect o-ring in a safety related chiller

was inadequate. There was no action taken to determine cause or prevent recurrence of

another failure, A non cited Wolation was identified. (Section M1.3).

Enaineenno

e The licenseo identified four examples where current surveillance testing did not meet

current TS. These were identified during a thorough review as part of the conversion to

improved TSs. This was a non-cited violation. (Section E8.16).

  • The inspectors identified that testing was performed on a safety related control building

chiller without a safety evaluation. A violation was identified. (Section E8.17).

2

,

- , .

.

Plant tunnort

e Radiation protection personnel provideo good support during the traversing incore probe

replacement. (Gection R1.1)

l.

1'

I

!

l

l

!

=

l

._

. _ =.=

3

.

_ .. ._

._ _ . _ _ . _ _ _ _ _ _ . . _ . _ . _ _ _ _ - _ _ _ _ _ . -

_ . _ .

'

l

!

l

Resort Details l

Summary of Plant Status  ;

The plant began this inspection period at 100 percent powe'. On December 24,1997, there was

a short power reduction for a control rod sequence exchange On January 22,1998, the plant

{

was reduced to approximately 75 percent reactor power for several hours for quarterty main i

steam isolation valve testing. The plant was operated at approximately 100 percent for the  !

remainder of the period.

I. Operations

01 Conduct of Operetiona

l

'

01.1 General Con ..s(71707). l

!

a. inanection Scone {

!

The inspectors followed the guidance of inspection Procedure 71707 and conducted  ;

frequent reviews of plant operations. This included observing routine control room {

activities, accompanying in plant opersbrs on daily rounds, reviewing system tegouts, j

attending shift tumovers and crew briefings, and performing panel walkdowns. ,

b,~ Observations and Findinas i

i

The conduct of operations was professional. The inspectors observed strict use of - I

procedures and thorough shift tumovers. Emergent equipment issues were promptly  !

'

-

addressed and cv,xiuot of operations was appropriately focussed on safety, The

inspectors observed a routine power reduction on January 22,1998. The evoluti9n was -

well-controlled.

I

c. Conclusions  !

The inspectors ccncluded that conduct of operations continued to be professional, with _  !

appropriate focus on safety.

01.2. Umitina condition for operation (LCO) Exceeded for Well Water Containment Isolation

-

Valves

a. Inspection Scope l

'i

The inspectors reviewed licensee corrective actions in response to inspection Followup

Item (IFI) 9600210. The inspectors had identified incorrect LCO durations when safety- i

related instrument air compressnrs were removed from service. The licenses

subsequently perfor ned a detailed evaluation per Action Request (AR) 971141. The - i

- 9 valuation concluded that LCO times had been exceeded for well water containment '

,

- isolation valves, and the licensee submitted Licensee Event Repor1 (LER) 9713.

t

-- -

_

..a ._.-m.-... . - _ _ _ ~ __

. - _ _ . - _ - - - _ - - -

.

1

4

4

b. Observations and Findinas

As discussed in inspection Report 50 331/96002, the inspectors identified that the

licensee used incorrect LCO duration when one of the safety related air compressors was

removed from service. The inspectors held several discussions with licensing and

engineering personnel before a detailed review was inillated in April 1997. The results of

the licensee's review and subsequent independent inspections by the inspectors are

detailed below.

The licensee's review of this issue identified that TS the LCO for inoperable containment

isolation valves had been exceeded. When one of the safety related air compressors

(lK 3 or IK-4) was removed from servim, two well water containment isolation valves

were rendered inoperable. The plant was designed with only one well water containment

isolation valve at each drywell penetration because the piping inside the drywell was a

closed system. This design is consistent with 10 CFR Part 50, Appendix A, Criterion 57.

Technical Specifications 3.7.B.1,3.7.B.2, and 3.7.B.3 address primary containment valve

operability requirements and applicable action statements. With one vf the wulwater

isolation valves (CV5704A, CV5704B, CV5718A, or CV57188) inoperable, the roquired

action was to initiate an orderly shutdown and be in at least hot shutdown within the next

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and colo shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The licensee identified, in

LER 9713, one instance in January 1997 where IK 3 was out of service for 91.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />

(50-331/98002-01(DRP)). The inspectors identified two other Instances, in

January 1996, IK 4 was out of service for 58 hours6.712963e-4 days <br />0.0161 hours <br />9.589947e-5 weeks <br />2.2069e-5 months <br /> (50-331/98002 02(DRP)), and in

April 1997, IK 3 was out of service for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> (50-331/98002 03(DRP)). The three

instances described above represented three violations of TS.

The licensee planned to submit a TS change and to consider design modifications to

enable longer allowed outage times when IK 3 or IK-4 is removed from service for

maintenance.

c. .Qonclusions

The inspectors and licensee identified three instances where the limiting condition for

operation was exceeded for primary containment isolation valves. This resulted in three

violations. The inspectors were concemed that several discussions were necessary with

licensee personnel before a review of the issue was initiated. The inspectors concluded

that the licensee took the appropriate action following identification of the issue.

02 Operational Status of Facilities and Equipment

02.1 General Plant Tours and System Walkdowns (71707)

a. Inspection Scope

The inspectors followed the guidance of Inspection Procedure 71707 in walking down

accessible portions of several systems:

Residual heat removal service water (RHRSW)

6

__

_ - _ _ _ _ _ _ _ _ _ _ -

,

o Scram discharge volume

e Standby d;esel generators

e Standby gas treatment system

b. Observations and Findinas

Equipment operability and materiel condition were acceptable in all cases. Several minor

discrepancies were brought to the licensee's attention and were corrected. The

inspectors identified two instances where temporary equipment was tied off to r.onduits.

The licensee promptly corrected the two examples and initiated an AR to increase staff

awareness on appropriate methods of securing temporary equipment.

c. Conclusions

The inspectors conctuoed that plant equipment was properly maintained. Housekeeping

was acceptable in most cases.

02.2 Detailed Walkdown of Standby Llauld Control (SLC) System

i

a. Inspection Scope (71707)

,

During the inspection period, the inspectors followed the guidanco of Inspection

l Procedure 71707 and conducted a detailed walkdown of the standby lic;oid con'rol system

l to verify its standby readiness condition. The inspectors reviewed syatem diagrsms,

!

Operating instruction (01) 153, * Standby Liquid Control System," the Updated Fhal Safety

Analyc's Report (UFSAR) description, surveillance tests, operator logs, and maintenance

history. Ti:e inspectors also observed a routine quarterly surveillance test.

b. Observations and Findinas .

The inspectors varified that the SLC system was properly lined up and that test results

were satisfactory. The inspectors identKed only minor discrepancies betweea the 01,

operator logs, and surveillance tesi .cceedure. The licensee initiated AR 980268 and

promptly resolvec the discrepancies,

c. Conclusions

The inspectors concluded that the licensee maintained the SLC system in the proper

standby readiness condition.

07 Quality Assurar;ce in Operationu

07.1 Licensee Self Assessment Activities (71707)

During the inspection period, the inspee'. ,rs reviewed multiple licensee self assessment

activilles, Inc.luding:

  • Safety Committee Meeting

Action Request Screening Meetings

e Operations Com,witee Meeting

6

m

- .__ _ _ - - . _ -.

The inspectors observed active participal'on by plant management in the review of AR,

6afety Evaluations, root cause reports, and other acilvities. One concem is discussed in

Section M1.3. In Pia! Instance, corrective actions were not adequate to prevent

recurrence of a failure of safety related equipment. The inspectors concluded that, in

general, plant management established sufficient guidance and oversight to ensure

strong self assessment, and effective identification and resolution of problems.

08 Miscellaneous Operations issues (92700)

08.1 (Closed) IFI 50431/95006 01: Licensee Failed to Enter Applicable LCOs for Surveillance

Testing. The inspectors did not identify any cases where LOOS were exceeded during

surveillance testing. The licensee recognized NRC's position that exceeding TS LCOs,

even for surveillance testing, would nat be acceptable. This issue was still under review

by the Office of Nuclear Reactor Regulation (NRA) (AIT 96-0278). This IFl is closed and

the issue will be tracked by AIT 96 0278.

08.2 (Closed) Violation (VIO) 50-431/95008-01: Incorrect Tagout Restoration of Containment

Atmosphere Dilution (CAD) System, The inspectors reviewed corrective actions

described in the response letter dated November 20,1995. The inspectors also reviewed

improvements to Administrative Control Procedure (ACP) 1410.5, "Tagout Procedure."

The revised ACP provides additional controls on tagout activit}es, such as restoration of

valve position. The ACP requires that the required clearance position be stated on the

tagout form prior to releasing the tagout for clearance. The inspectors considered the

corrective actions to be appropriate. This item is closed.

08.3 (Closed) IFl 50 331/95008-02: Rope Found in Suction for Fuel Pool Cooling Pump. The

licensee recovered the rope and performed a root cause analysis. The licensee

determined that the rope had been trapped in the system since prior to 1992. Corrective

actions were appropriate and the inspectors had rio further concems. This item is closed.

08.4 (Closed) IFl 50-331/96002-10: Incorrect LCO Time When Instrument Air Compressor

Removed From Service. This item is closed to a violation as discussed in Section 01.2.

08.5 (Closed) LER 50 331/96-05-00: Primary Containment isolation System (PCIS) Groups 3

and 5 Isolations. This occurred during a refueling outage. The licensee determined that

the likely cause was a voltage drop in a temporary power supply. This resulted in a loss

of power signal to logic for the Group 3 and 5 PCIS. The licensee reroved the temporary

power supply and restored normal source of power to the instrument AC systen prior to

plant start up. This item is closed.

08.6 (Closed) VIO 50-331/96005-01: Operating Procedure Deficiencies. The vidation

involved four examples of inadequate or deficient plant operating procedures. The

inspectors reviewed the corrective actions specified in the licensee's response letter,

dated September 27,1996. Each procedure was appropriately corrected. Additional

procedure deficiencies were identified during inspection 50-331/97006 and a violation

was cited (9700G-01a), item 96005-01 is closed. Corrective actions regarding prxedure

deficiencies will be reviewed during closure of Violation 50 331/97006-01a.

7

_ _ _ _ _ _ _ _ _ _ _ _ _ _

08.7 (Closed) VIO 50-331/96007-01: Failure to Follow Procedure During a Tagout Activity.

The inspectors reviewed the corrective actions specified in the licensee's response letter,

dated February 21,1997. The corrective actions were appropriate. This item is closed.

08.8 (Closed) VIO 50 331/97004 01: Residual Heat Removal Operating instruction (01) Not

Followed. The inspectors reviewed the licensee's ccrrective actions, which included:

1) revising the Ol to clarify the expectation, and 2) operations management issued a

memo to operations personnel reinforcing procedural compliance expectations. This item

is closed.

08.9 (Closed) VIO 50-331/97004 02: Diesel Generator Cooling Valve Found Mispositioned.

The inspectors identified a repeat occurrence of Valve V32170 being out of position on

July 23,1996. The licensee determined that the likely cause was that the valve handle

was bumped during routine oil cleanup. The handles for V32170 and other similar

valves were removed to prevent recurrence. This item is closed.

08.10 (Closed) VIO 50 331/97004 03: Annunciator Response Procedure (ARP) Not Promptly

Corrected. The inspectors reviewed the implementation of the corrective actions

described in the licensee's response letter dated May 21,1997. The inspectors had no

further concerns. This item is closed.

l

l

'

08.11 (Closed) VIO 50-331/97009-01: Inadequate Drywell spray Tagout. Plant management

reinforced expectations regarding preparation, installation, and removal of tagouts. The

inspectors considered corrective actions to be appropriate. This item is closed.

08.12 (Closed) VIO 50-331/97009-02: niver Water Selector Switch Found in Wrong Position.

The inspectors had identified this issue on May 12,1997. The licensee performed a root

cause analysis and implemented several corrective actions. The inspectors considered >

the corrective actions to be appropriate. This item Is closed,

ll. Maintenance

M1 Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707) (61726)

The inspectors observed or reviewed all or portions of the following work activities:

  • Standby diesel generator monthly fuel oil storage test, STP 48A003-M

e Daily instrument checks, STP 42A001

  • Instrument air compressor IK-4 air dryer maintenance, CMAR A40268
  • Traversing incore probe replacement
  • Dynamic VOTES test on M01939, EMP-M01939/1940 DV

8

, we -

.. .. .. -.- . .- - . . --- _ . . . . . . - . -.-- _ - -.

e Sts.ndby gas treatment rough filter clean and inspect, PMAR 1102802

>

e Standby liquid motor oil change, PMAR 1098488

, o Containment atmosphere monitor (CAM) system leakage walkdown,

STP 685007 CY

c. Conclusions

in general, the inspectors observed sound maintenknee practices, appropriate use of

procedures, and good coordination among departments. Concerns with corrective action

to prevent recurrence of a problem and controls over installation of squib valves are

discussed below.

M1.2 Weak Controls for Soulb Valve Exolosion Cheroe Testino and Installation

a. Inspection Scope (62707) -

The inspectors observed preventive maintenance action request (PMAR) 1099750. The

inspectors also reviewed other applicable documents, such as TS, UFSAR, maintenance

procedures, and surveillance test procedures.

b. Observations and Findinal

The inspectors identified that PMAR 109g750 required testing only one squib valve

explosion charge out of a batch of two charges. This was not consistent with

TS 4.4.A.2.b, which specifies that one of three charges from the same batch shall be

tested and the other two installed in the system. Through interviews, the inspectors

determined that the licensee had an extra explosion charge with a different manufacture

date in the warehouse that they planned to install during refueling outage (RFO) 15

(April 1998). The inspectors were concemed that theia were no formal controls in place

to ensure that the squib valve explosion charges installed during the upcoming RFO

would be from the same batch.

The inspectors verified that there was no present operability concem. The currently

installed valve charges were from the same batch as the charge that was tested in

preparation for RFO 14 (October 1996) and met TSs..

The licensee initiated AR 980263 and planned to correct the condition prior to RFO-15.

The licensee later found that the two different charges were from the same lot at the

manufacture and satisfied the TS requirement.

c. Conclusions

The inspectors identified weak controls in the testing and installation of SLC squib valve

explosion charges. Specifically, there were no formal controls to ensure that TS

requirements regarding charges coming from the same batch would be adhered to.

9-

_ _ . . _ _ __ ,_

_ _ - _ - _ - _ _ - _ _ - _ -

.. .. ..

. . .. .. .. ..

-

t

M1.3 Inadeauale Corrective Actions for incorrect o-rina In Control %Mna Chiller

a. Inmotion Scope (62707)

The inspectors observed maintenance on the 'B' control building chiller on Decemb$r 2,

1997. The licensee had declared the chiller inoperable after identification of a signiticant

'olileak and promptly entered the approoriate LCO, The inspectors discussed the

apparent cause of the failure with the mechanical maintenance technicians in the field.

The technicians showed the inspectors a cut o-ring for the slide valve that they believed

was the wrong size and suspected to be the cause of the failure. -The incorrect o ring

l

had been insta' led in August 1997. The licensee subsequently replaced the o-ring with

the correct size and initiated AR 972760. Approximately one month later, the inspectors

followed up to see what the licensee determined to be the cause of the failure and the

cause of the incorrect o ring.

b. Observations andfindinns

The inspectors identified that AR 972760 had been closed and that no followup had

'

occurred to determins how the incorrect o-ring was installed. After discussion with plant

mana9ement, an addendum AR 972760.01 was initiated to determine when and how the

incorrect o-ring was installed on the chiller. The AR also assigned to the mainionance

department to initiate other corrective actions to prevent recurrence. The licensee also -

Initiated AR 980193 to review whether there was a possible break down in the normal -

corrective action process that allowed the original AR to be closed without appropriate

followup.

The failure to initiate corrective actions to prevent recurrence of the incorrect o rbg was a .

- violation of 10 CFR Part 50, Appendix B, Criterion XVI.- This was considered a minor

violation and is a non cited violation according to Section IV of the NRC Enforcement

Policy. (F0 331/98002-04(DRP)).

c. Conclualons

The inspectors concluded that licensee corrective actions were inadequate following

discovery of the incorrect o ring installation. There were no actions taken to prevent

recurrence of another failure.

'M2 - Maintenance and Materiel Condition of Facilities and Equipment

M2.1 Plant Materiel Conditiori

a.- Insoection Scope (62707)

The inspectors reviewed several emergent work items to ensure appropriate operability

evaluations were performed, TS were met, repairs were made, and root causes were

determined where appropriate.

?-+ = +

10

_

_

_ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _-

b. Observations and Findinas

The inspectors noted that there were several emement equipment issues during the

inspection period. The examples are listed below.-

  • On January 12,1998, a temperature switch for the drywell equipment drain sump

failed. The scensee promptly er.tered a 24-hour LCO. The temperature switch

was promptly replaced the same day. (AR 980028)

  • On January 17,1998, a *B" control building chiller trouble alarm was received in

the control room. The licensee entered a 30-day LCO. The cause was

determined to be a problem with the oil heater switch. The con)ponent was

repaired and the system tested satisfactorilylaterin the same day. (AR 980039)

e On January 22,1998, during a walkdown of the containment atmosphere monitor

(CAM) system (STP 685007-CY), the licensee identified a recurring problem with

leakage exceeding the allowable values in the STP. The licensee determined that

'

there was no oparability concern for the CAM system or other systems that use

the same piping. Also, the system engineer determined that the adualleakage

was greater than the administrative ilmit sr.t in the STP, but was within the overall

containment allowable leakage. The licensee had plans in place to perform

modifications to prevent recurrence of leakage problems with this system.

(AR 961802 and 980053, CMAR A32615A, and A37048A)

  • On January 28,1998, the 'A" train of the hydrogen and oxygen monitor was

declared inoperable when the system failed to pass routine surveillance test

STP 3.3.5.136. The licensee entered a 30-day LCO snd initiated repairs.

(AR 980286). Additional efforts were planned to reduce containment atmosphere

monitor system leakage and prevent this from continuing to be a recurring

problem.

t * On January 30,1998, during quarterly surveillance testing of the "B" core spray

f system, the minimum flow valve failed to open as expected. The licensee

promptly secured the pump and entered a seven-day LCO. Corrective

Maintenance Action Request (CMAR) A46905 was initiated and flow transmitter

FT2130 was re calibrated. The licensee's operability evaluation was approved by

the Operations Committee on February 1,1998, and the system was declared

operable. (AR 980298)

c. Conclusions

The licensee promptly resolved equipment issues that occurred during the inspection

period. Personnel from the maintenance and engineering departments provided good

support and exhibited good teamwork in resolving the issues.

M8 Miscellaneous Maintenance issues (92902)

M8.1 (Closed) IFl 60-331/95009-03: Plastic Shipping Plugs Installed in Transmitters. The

inspectors performed a walkdown of harsh environment areas during refueling outage 14

Ir, November 1996 and found no environmentally qualified transmitters with plastic plugs.

11

, l

___

.

The licensee subsequently revised transmitter calibra.lon procedures to require i

examination of plugs durin;; future calibrations and installation of new transmitters. The

procedures specified that metal plugs were to be installed if needed. The inspectors had  ;

no further concems. This item is closed. '

M8.2 (Closed) 1.ER 50-331/96-03-00: Primary Containment Isolation System Groups 1 )

Through 5 lsolations Due to Reactor Protection System Elactrical Protection Assembly l

Breaker Trip on Under Voltage. The licensee was not able to determine the cause. i

Temporary instrumentation was installed to monitor for possible voltage fluctuations. I

Components in the power supply were inspected and replaced. The inspectors l

considered the corrective actions to be thorough. This item is closed.

M8.3 (Closed) Unresolved item (URI) 50 331/96004 03: PoorTroubleshooting Activities. The

inspectors reviewed corrective actions following two instances where data was lost during

troubleshooting activities. The first instance was the failure of installed monitoring

equipment to record data following a trip of the "B" reactor recirculation motor generator

(RRMG). The licensee determined that the trigger points were not properly armed due to

a personal error during set up of the equipment. Training was provided to personnel.

The second instance involved damage to a transformer during troubleshooting. The

licensee determined that incorrect values were used for applying load during testing of

the transformer. The licensoe also developed a guideline to address calling people in for

after hours maintenance and troubleshooting. The Inspectors considered the corrective

actions to be appropriale. This item is closed.

MS.4 (Closed) URI 50-331/96006-06: Engineered Maintenance Action (EMA) Process Errors.

The licensee identified two instances where the EMA process was not effective l-

ensuring documentation was updated following maintenance. The licensee corrected the

documentation. The inspectors performed a detailed review of changes to the EMA

process as discussed in Section E8.3. The additional controls in the EMA process were

considered appropriate. Thia, item is closed.

M8,5 (Closed) VIO 50-331/96007-03: Improper Tagout Doundary Established. The licensee's

root cause debrmined that several barriers broke down during this event. There was

also a misunderstanding regarding the scope of the work to be performed. The

inspectors verified that the corrective actions were appropriate. This item is cleted.

M8.6 (Closed) VIO 50-331/96007 04: Incorrect Test Equipment installation. The licensee

determined the cause to be an inadequate procedure in that there were no specific

details regudin;, the location to connect recorder leads. The procedure was revised to

include specific information on the installation of recoroer leads. This itsm is closed.

M8.7 (Closed) VIO 50-331/96007 0); Failure to Llow Procedure During Calibration of

Inverter. The control room received 125 Vdc trouble annunciators during a calibration

activity. Fuses, capacitors, and resistors were found damaged. The licensee determined

the cause to be that the technician failed to follow the procedure and failed to use the

latest change to the procedure. Corrective actions included replacing the damaged

components, providing remedial training to the technician, and providing verification

training to plant personnel. This Cem is closed.

12

M8.8 (Closed) LER 50 331/96,0 % and (Closed) VIO 50-331/96007 01; High Pressure

Coolant injection (HPCI) Syn . - . Mon Due to Misplaced Relay Block. The licensee

determined the cause to be personnel error due to a break down in self checking and

dual verification. Meetings were held with all plant maintenance personnel following this

event to reinforce expectations. These items are closed.

M8.9 (Closed) IFl 50-331/96007-07: Reactor Core Isolation Cooling Flow Controller Concems. '

The licensee identified concems with the lasting of fiow controller FIC 2509. The

manufacturer recommended checking deviation meter movement during mode transf' of I

the controller from automatic to manual. Th9 calibration procedure was subsequently I

revised to ensure recommended testing is performed. The inpectors had no further I

concems. This item is closed.

M8.10 (Closed) VIO 50 331/9601101 and (Closed) VIO 50-331/97007 03
Document Change l

Form (DCF) Not incorporated During Diesel Surveillance Test and Repeat DCF

Control Problem. There were several examples discussed in inspec*'". Reports

Nos. 50-331/96011 and 50-331/97007 regarding problems with control of DCFs. The

inspectors reviewed the licensee's corrective actions as described in the licensee's

response letters dated February 26,1997, and June 9,1997. Procedure ACP 106.3 was

revised to prcvide better control of DCFs. Other plant procedures were also revised to

reflect changes made to ACP 106.3. The inspectors had no further concems. These

items are closed.

M8.11 (Closed) VIO 50-331/96013-02: Use of Uncontrolled Documents During TS Surveillance

Testing. The violation listed two examples where incorrect data from uncontrolled

documents were used during surveillance testing. There was little safety significance

associated with the examples. The licensee corrected the data on the documents and

provided additional controls to ensure that data used during surveillance tests is

controlled or maintained on controlled documents. Additionally, the licensee reviewed

other surveillance tests where supporting documents were used. The licensee corrected

several other cases where uncontrolled documenh were used. The inspectors

considered the corrective actions to be thorough. This item is closed.

M8.12 (Closed) LER 60 97-02-00: Both Standby Gas Treatment (SBGT) Trains Inoperable Due

to Low Carbon Bed Efficiencies. This was the subject of a violation in Inspection Report

No. 50-331/97004, as discussed in Section MS.13, below. The inspectors verified that

appropriate corrective acticns were implemented. The inspectors had no further

concems. This item is closed.

MB.13 LQlgyd) VIO 50-331/97004-01: Incorrect Evaluation of SBGT Test Results. The

inspectors had raised a concem in this case with the licensee inappropriately rounding up

a value to meet the TS, The licensee subsequently declared the system inoperable,

restored the syrtem to full compliance with TS, and made changes to improve carbon

bed efficiency in the future. Additionally, as discussed in the licensee's response letter

dated May 21,1997, plant management reinforced expectations to all plant personnel

regarding procedural adherence and verbatim compliance with TS. The inspectors had

no further concems. This item is closed.

M8.11 (Closed) VIO 50-331/97004 05: Incorrect Equation in SBGT Surveillance Test Procedure

(STP). The licensee verified that the correct equation had been used to arrive at the

13

l

. __

_ _ __ . _ _ . - _ _ - . _ . _ _ . . _ .-_ _ _ _ _ _ _ _ _ _ _ . _

.

.

values within the STP. The STP was subsequently revised. Addit:onally, plant

management reinforced procedural adherence expectations. Specifically addressed was

the need to stop and get the procedure corrected if it was found to be in error. The

inspectors had no further concems. This item is closed.

M8.15 iClosed) VIO 50 331/97007-01: Repeat Example of Incorrect ESW Acceptance Criteria.

The inspectors reviewed the licensees corrective actions as described in the licensee's

response letter dated June 9,1997. The licensee revised the surveillance test procedure

to record the data in the American Society of Mechanical Engineers (AGME) Data Book.

The inspectors have not. ldentified any similar Instances since the corrective action was

implemented. This item is closed.

M8.16 (Closed) VIO 50-331/97009-04: Failure to Spccify Post Maintenance Testing for

Ventilation Dampers. The inspectors reviewed the corrective actions specified in the

licensco's response letter dated July 28,1997. This included a quality assurance

department follow-up review to assess the effectiveness of the corrective actions. The

inspectors determined that the corrective actions were appropriate. This item is closed.

,

Ill. Enaineerina >

E1 Conduct of Engineering

a. Inspection Scope (37551)

The inspectors eveluated engineering involvement in resolution of emergent rNterial

condition problems and other routine activities. The inspectors reviewed areas such as

operability evaluations, root cause analyses, safety committees, and self assessments. *

The effectiveness of the licensee's controls for the identification, resolution, and

prevention of problems was also examined,

c. ,Q20 gly 3].qng

As discussed in Section M2.1, engineering personnel provided good support and

exhibited good teamwork with other departments in promptly resolving emergent

equipment issues. However, two concoms were noted. One violation was identified

regarding the failure to perform a safety evaluation prior to testing the control building

chiller, as discussed in Section E8.17. A non-cited violation was identified, as discussed

in Section M1.3 for inadequate corrective actions following identification of an incorrect o-

ring in a control building chiller.

E8 Miscellaneous Engineering lasues (92902)

E8.1 (Clo$ed) 1.ER 95-013-00 and 01: HPCI System inoperable Due to Water in Turbina

Steam Exhaust Line. The licensee's corrective actions described in the LER were

verified to be completed. In addition, a modification was performed in October 1996 to

prevent recurrence. The details of the originalissue and modification are currently under

review by NRR (AITS96-254, Revision 1). The issue will continue tu be tracked by

AITS96-254, Revision 1. This LER is closed.

14

- - - - - - -

- - _ . - - - -- . .. - .-.

l

E8.2 (Closed) LER 50 331/96-0100.01. and 02: Core Average Control Rod Scram Time

'

Exceeding TS Limit. The licensee performed to:, ting in March 1996 in response to

industry operating experience regarding problems with Viton scram solenoid pilot valve

(SSPV) diaphragms. The condition was promptly corrected and a program to monitor

, degradation in response times was initiated. During the October 1996 refueling cutage,

the licensee replaced the Viton diaphragms with Buna N diaphragms. The licensee

planned to test a sample of SSPVs during the April 1998 outage to ensure continued

satisfactory operation of the Buna N diaphragms. Also, scram time testing will be

performed prior to start up as required by TS. This item is closed.

E8.3 (Closed) VIO 50 331/96002 07: Failure to Correct Weak Controls in EMA Process. The

inspectors reviewed the licensee's corrective actions as described in their resp >nse

letter, dated M6y 9,1996. Also, the current EMA process procedure, Administrative

<

Control Procedure 109.1, Revision 6, was reviewed to verify added controls. The

inspectors concluded that corrective actions were appropriate and had no further

concems. This item is closed.

E8.4 (Closed) IFl 50-331/96002 08: Inconsistency of Valve Closure Time in UFSAR. This item

iitvolved the licensee's position that the Update Final Safety Analysis Report (UFSAR)

values are considered " nominal design values." The inspectors reviewed this issue

further in inspection Report No,50 331/97006, Section M3.1, and identified several

additional discrepancies. The inspectors concluded that the failure to ensure design

acceptance criteria as described in the UFSAR were incorporated into surveillance testing

was a violation (50-331/97006-03(DRS)). This item (50 331/96002 08) is closed to the

violation cited in Inspection Report No. 50 331/97006.

E8.5 {C1gjed) URI 50-331/96003-01: Potential for Pressure Locking of Drywell Spray Valve.

'

The licensee's initial review of M01902 did not document the basis for operability. A

phone conf 6rence was held between the licensee, the NRC resident inspectors, and NRC

staff at the Office of Nuclear Reactor Regulation (NRR) on August 1,1996, to discuss the

inspectors' concoms. The licensee subsequently prepared a detailed engineering

evaluation that provided appropriate justification for operability. Also, the valve was

modified on October 27,1996, to relieve the potential pressure locking concem

(CMAR A23968). The inspectors had no further concems. This item is closed.

. E8.6 (Closed) VIO 50-331/96005 03: Inadequate 10 CFR 50.59 Safety Evaluation (SE) for

Emergency Service Water Make up to Spent Fuel Pool. The inspectors reviewed the

implementation and adequacy of corrective actions specified in the licensee's response

letter dated September 27,1996. The inspectors also reviewed revised SE 95-06,

Revision 1. The inspectors concluded that corrective actions were appropriate. This item

is closed.

E8.7 (Closed) URI 50-331/9601105: Configuration Control of Temporary Modifications (T M).

The inspectors reviewed other open and closed TMs and had no concems. The TM fom,

requires: 1) installation signature and verification; 2) removal signature and verification;

3) installation prerequisi'es, sequence constraints, and post-installation test requirements;

and 4) post removal test requirements. Procedure ACP 1410.6 contains adequate

controls of plant configuration. This item is closed.

15

_ .

_ __

____________ - __ _ __ _ -

.

E8.8 (Closed) URI 50-331/96011-07; Drywell Seismic Monitor Design Temperature Exceeded.

The licensee identified this condition and took action to ensure design temperature would

not be exceeded in the future. The licensee plans a modification du,ing the next refueling

outage to install additional insulation and a cooling air duct for the monitor. The

inspectors determined that the UFSAR was correcl and the licensee took appropriate

action to restore the degradod equipment. This item is closed.

E8.9 (CJ81ed) URI 50 331/9501108: Implementation of 10 CFR 50.73 Reportability

Requirements. The licensee had already submitted " voluntary" LER 96 07, Revision 00,

regarding main steam safety valves that failed to meet TS setpoints. The inspectors

were concemed that an LER was required and was not voluntary. After further

discussions, the licensee reviewed the reportability practices of other plants. The

licensee determ!ned that the failures were reportable under 10 CFR 50.73(a)(2)(vil) and

issued Revision 01 to LER 96 07. Additionally, the licensee provided reportabil!!y training

to licensing personnel. The inspectors did not identify any other concems with the

licensee's reportability practices. This item is closed,

i

E8.10 {plosed) URI 50 331/97004 07: Use of * Nominal" Values for TS Setpoints. The

inspectors had identified that actualinstrument setpoints were not all on the preferred

side of the inequality sign glven in TS. The licensee promptly reviewed all TS instmments

and reset severalinstruments to ensure compliance with TS. A commitment letter was

submitted to the NRC on February 25,1997, which detailed tne licensee's plans to ensure

l continued compliance with the TS values. Final resolution of this issue will be addressed

'

in the improved Technical Specifications, which are currently with NRR for review. This

item is closed.

E8.11 (Closed) VIO $0-331/97004-08: Failure to Perform an SE When Cha.4 ") Room

Temperature for GLC System. The licensee subsequently performed a SE to document

the basis for the determination that no unreviewed safety question was involved. Also,

( the licensee revised their 10 CFR 50.59 process to ensure SEs are performed when

changes are made to the UFSAR. This item is closed.

E8.12 (Closed) LER 50 331/97-06-00; inadequate Functional Test of the HPCI System Steam

Leak Detection Time Delay. The surveillance test was revised and alllogic performed as

required when tested. This was part of the non-cited violation (NCV) discussed in

Sectien E8.16. This item is closed.

E8.13 (Closed) LER 50-331/97 07-00: Inadequate Test of Reactor Mode Switch to Shutdown

Position Rod Block Function and Rod Block Monitor. The inspectors verified that

corrective actions were completed and that the testing required by TS was satisfactorily

completed. This issue was part of a NCV as discussed in Section E8.16. This item is

closed.

EB.14 (Closed) VIO 50-331/97007-02: Residual Heas %moval Service Water (RHRSW)

Surveillance Test Not Consistent With Design Basis. The inspectors had identified that

the licensee closed a normally open back wash valve during this test. This prevented

accounting for diverted flow during quarterly surveillance testing. The licensee

determined that there was no operability concem after a review of pump performance

data. The STP was promptly revised to test the system correctly. This item is closed.

16

i

l

.- . . _ _- ---

E8.15 [Qlosed) LER 50 331/97-09-00: Inadequate Survelllance Testing of Reactor Water

Cleanup (RWCU) Area Differential Temperature Isolation Logic. The inspectors reviewed

corrective actions and virified that required testing was completed as required by TS.

This item was the subject of an NCV as discussed in Section E8.16. This item is closed.

E8.10 frosed) Unresolved item fURI) 50 331/97010-03: Inadequate TS Surveillance Test

identified During Licensee's improved TS Project. Inspection Report No. 50 331/97010

discusses three examples 2nd Inspection Repori No. 50-331/97012 discusses an

additional example. The fu.r examples were identified by the licensee as part of the

improved TS Project. The inspectors verified that, in each case, the sumeillance tests

were properly revised and performed satisfactorily as required. The licensee submitted

licensee event reports as required by 10 CFR 50.73. The failure of the surveillance tests

to adequately perform the testing required by TS was a violation. This non rnpetitive,

licensee-identified and correried violation is being treated as an NCV consistent with

Section Vll.B.1 of the NRC Enforcement Policy 30-331/98002 05(DRP)). This item is

closed.

E8.17 (Q sed) URI 50 331/97017 03: Testing on Control Building Chiller Without a Safety

Evaluation (SE). The inspectors reviewed the details of the chiller 100 percent load test

performed on November 19,1997. The licensee had used Tagout Number 971369 to fall

open a control valve in the heating loop in order to increase the heat in the control

building. The control building ventilation system serves the control room, cable spreading

room, safety related battery rooms, and essential switch gear rooms. The inspectors

were concerned that no safety evaluation was performed prior to the test to determine

what effect the testing could have on safety-related components within the control

building. Part 50.59 of 10 CFR required that a written safety evaluation be performed for

a test that is not described in the safety analysis report, and that the SE provides the

bases for the determination that the test does not involve en unreviewed safety question.

The failure to perform an SE in this case was a violation (50-331/98002 06(DRP)).

IV. Plant Supped

R1 Radiological Protection and Chemistry Controls

R11 Good Radiation Protection Support for Transversina incore Probt(TIP) Replacement

a. Inspection Scope f71750)

The inspectors reviewed the adequacy of radiological controls in accordance with

inspection Procedure 71750. This included observing radiological work practices

supporting the January 8,1998, TIP replacement.

b. Observations and Findinas

On January 8,1998, the inspectors observed portions of the *C" TIP replacement. The

inspectors observed radiation protection personnel providing good support during the

replacement process. Radiation protection personnelwere performing numerous

exposure rate surveys in the TIP toom and the surrounding area to ensure exposure rate

levels were not in excess of established limits. Upon removal of the "C" TIP, radiation

17

_

_ _ - . . .

.. ,

,

protection personnel placed it and its cable in containers for transfer to the radweste

building. The inspectors noted good area controls by radiation protection personnel to

ensure no personnel would com3 in close proximity to the containers during their transfer

from the TIP room to the radwaste building,

c. Conclusions

Radiation protection personnel provided good support during the TIP replacement,

I

V. Mananoment Meetinos

, a

X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on February 4,1998. The licensee acknowledged the

findings presented.

The inspecte t asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

. _ _

_

18

u i

. . . _ . - - _ . _ .

.__ _- . _ _.__

_ _ _ . _ __;

.- ,

e

PARTIAL LIST OF PERSONS CONTACTED

Licensee l

!

J. Franz, Vice President Nuclear

G. Van Middlesworth, Plant Manager

. R. Anderson, Manager, Outage and Support

J. Bjorseth, Mair:tenance superintendent

D. Curtland, Operations Manager i

R. Hite, Manager, Radiation Protection  !

M. McDermot, Manager, Engineering ,

K. Poveler, Manager, Regulatory Performance  !

i

5

i

!

.

k

?

.'

i

e

I

i

1

i'

t

h

r

/

- - -

- _ _ _

L

.

- - , - -- -,- ,,,v., ,,-.,2,-b,~w..  % v

'

+ - - - - - . ,,---,n.e.,r.,-, - ,,m , , _ , -, , , , , - - - , , - w, . . , . c-mo,.- , . , - ,-,m--- , - , , ,,.-f..--y,_,_

.  !

INSPECTlON PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observation

IP 62707: Mair,tenance Observation

IP 71707: Piant Operations

IP 71750: plant Support

IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Powu Reactor

Facilities

IP 92901: Followup Operetions

IP 92902: Fol!owup Engineering

IP 92903: Followup Maintenance

IP 93702: Prompt Onsite Response to Events at Operating Power Reactors

ITEM 8 OPENED, CLO8ED, AND DISCUSSED

Opened

50-331/98002 01 NOV LCO time exceeded for well water containment isolation valves

50-331/98002 4 2 NOV LCO time exceeded for wsll water containment isolation valves

50 331/98002 03 NOV LCO time exceeded for well water containment isolation valves *

50-331/98002 04 NCV Inadequate corrective actions for incorrect o ring

50-331/98002 05 NCV inadequate TS surveillances

50 331/98002 06 NOV Testing on chiller without a safety evaluation

Closed

50 331/95006-01 IFl Licensee failed to enter applicable LCOs for surveillance testing

50 331/95006-01 VIO Incorrect tagout restoration of CAD system .

50-331/95006 02 IFl Rope in fuel pool cooling pump

50 331/95009-03 IFl Plastic shipping plugs installed in transmitters

50 331/95-13 00,01 LER- HPCI system inoperable due to water in turbine sieam exhauct line

50 331/96-01 00, LER Core average control rod scram time exceeding TS limit 01,02

50 331/96002 07 VIO Failure to correct weak controls in EMA process

50 331/96002-08 IFl Inconsistency of valve closure time in UFSAR

50 331/96002 10- IFl incorrect LCO time when instrument air compressor taken out of

service

50-331/96-03 00 LER PCIS Groups 1 through 5 isolations

50 331/96003-01 URI Potential for pressure locking of drywell spray volve

50 331/96-04-00 LER HPCI system isolation due to misplaced relay block

50-331/96004-03 URI Poor troubleshooting activities

.50 331/96-05-00 LER PCIS Groups 3 and 5 isolations

50-331/96005-01 VIO Operating procedure deficiencies

50-331/96005-03 VIO Inadequate 10 CFR 50,59 SE for emergency service water maka-

up to spent fuel pool

50 331/96006-06 URI EMA process errors

50 331/96007 01 VIO Failure to follow procedure during a tagout activity

50-331/96007-C3 VIO Improper tagout boundary established

50-331/96007-04 VIO Incorrect test equipment installation

20

.. .

. . . . . . . . . . . . . . . . .

. . . .

. .

.. . .

. . . . . . .. __;

_ _ - _ _ _ _ _ _ _ _ _ - _ _ - --

.

50-331/96007-05 VIO Failure to follow procedurm during calibration of inverier

50 331/96007 06 VIO HPCI system isolation due to misplaced relay block

50 331/96007-07 IFl Reactor core isolation cooling flow controller cor.cerns

50 331/96011 01 VIO DCF not incorporated during diesel surveillance test

50 331/96011 05 URI Configuration control of TMs

50 331/96011 07 URI Drywell seismic monitor design temperature exceeded

50-331/96011 08 URI implementation of 10 CFR 50.73 reportability requirements

50 331/96013-02 VIO Use of uncontrolled documents during TS surveillance testing

50 331/97-02 00 LER Both SBGT trains Inoperable due to low carbon bed efficiencies

50 331/97004 01 VIO Residual heat removal Ol not followed

50 331/97004 02 VIO Diesel generator cooling vaive found mispositioned

50 331/97004 03 VIO ARP not promptly corrected

50-331/97004 04 VIO incorrect evaluation of SBGT test results

50-331/97004 05 VIO Incorrect equation in SBGT STP

l

50 331/97004-07 URI Use of " nominal" values for TS setpoints

i

50 331/97004-08 VIO Failure to perform an SE when changing room temperature for SLC

system

,

50-331/97 06-00 LER Inadequate functional test of the HPCI system steam leak detection

I time delay

50-331/97 07 00 LER inadequate test of reactor mode switch to shutdown position

50-331/97007 01 VIO Repeat example of incorrect ESW acceptance criteria

50 331/97007 02 VIO RHRSW surveillance test on consistent with design basis

50-331/97007 03 VIO Repeat DCF control problem

50-331/97-09-00 LER inadequate surveillance testing of RWCU area differential

temperature isolation logic

50 331/97009 01 VIO Inadequate drywell spray tagout

50-331/97009-02 VIO River water selector switch found in wrong position

l.

i 50 331/97009 04 VIO Failure to specify post maintenance testing

50 331/97010 03 URI Inadequate TS surveillance tests identified during licensee's ITS

project

50 331/97017-03 URI Testing or' control building chiller without a sa fety evaluation

50-331/98002-04 NCV Inadequate corrective actions for incorrect o-ring

50-331/98002-05 NCV Inadequate TS surveillances

.

21

Y

- - _ _ - . - _ . - . -_ . . _ _ _ _ _ . _ .- - . . .-. ...

.

M

^

LIST OF ACRONYMS USED

ACP Administrative Control Procedure

AR - Action Request

ARP Annunciator Response Procedure

ASME American Socir' ,. Aechanical Engineers

CAD Containment atmosphere dilution

CAM Con'ainment atmosphere monitor

CFR Coda of Federal Regulations

CMAR Corrective Maintenance Action Request

DAEC Duane Amold Energy Center

DCF Document change form

EMA Engineered maintenance action

ESW Emergency service water

.HPCI High Pressure Coolant injection

'

.

IFl Inspection followup item

IP inspection procedure ,

IR ' Inspection report

LCO - Limiting Condition for Operation

LER Licensee Event Report

, NCV Non-cited violation

NOV Notice of vlotation

NRC. Nuclear Regulatory Commission

NRR Office of Nuclear R; actor Regulation

01 Operating Instruction .

9

PCIS Primary containment isolation sy tem

PMAR Preventive maintenance action request

RFO Refuel Outage

RHR- Residual heat removal

RHRSW Residual heat removal service water

RPS Reactor protection system

RRMG Reactor recirculation motor generator

RWCU Reactor water cleanup

SAR' Safety analysis report

SBDG Standby diesel generator

SBGT Standby gas treatment system

SE Safety evaluation

SLC S'andby liquid control

SSPV Leam solenold pilot valve

STP Surveillance Test Procedure-

'

TIP Traversing incore probe

TM Temporary modifications

TS Technical Specification.

UFSAR Updated Final Safety Analysis Report

URI Unresolved item

VIO Violation

_ _

22

i

. _ . _ _ _ . , _ . - _ _