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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20092G0111995-09-11011 September 1995 Ro:On 950801,loss of One Channel of Reactor Vessel Level Sys Occurred.Reactor Water Level Instrument LE-0101A & signal-&-power Cable Will Be Replaced During Next Refueling Outage ML20198H3691983-11-14014 November 1983 Ro:On 831003,results of as-found Tests Indicated Crosby Main Steam Relief Valves Had Lift Points Exceeding Tech Spec Limits.Valves Disassembled & Rebuilt by Mfg ML20081H3471983-10-25025 October 1983 Telecopy Ro:During Ae Analysis,Design Deficiency in Support Configuration for 1-inch Diameter Fill & Drain Piping to T-82D (Safety Injection Tank D) Discovered.Supports Will Be Redesigned & Installed During Current Outage ML20080R0971983-10-0707 October 1983 Telecopy Ro:On 831006,walkdown of Safety Injection Sys Pipe Hangers Revealed Overloaded Condition on Base Plate & Anchor Bolts of Hanger H214.Caused by Error in Design Analysis.Hanger Support to Be Redesigned ML20080P8341983-10-0303 October 1983 Supplemental RO 82-034:panel C-47 Will Be Modified & Fire Deluge Sys Reflash Capability Will Be Provided for Panel C-13 ML20076C5671983-08-12012 August 1983 Telecopy Ro:On 830811,safety Injection Tank Boron Found Below Tech Spec Limits for Tanks T-82D & T-82B.No Cause Stated.Both Tanks Inoperable at Same Time for 1 Minute ML20076A9031983-08-0808 August 1983 Telecopy Ro:On 830806,sample from T-82D Showed Boron Concentration to Be 1,712 Ppm Which Is Below Tech Spec Limit of 1,720 Ppm Boron.Safety Injection Tank Restored to Operability W/Boron Concentration of 1,753 Ppm ML20076A6241983-08-0505 August 1983 Telecopy Ro:On 830804,safety Injection (SI) Tank T-82B Became Inoperable Due to Low Level,While SI Tank T-82D Inoperable Due to Routine Sampling.Si Tank T-82B Restored to Operability within 5 Minutes ML20077G8201983-07-20020 July 1983 Telecopy Ro:On 830719,discovered Current from 125-volt Dc Sys Short Circuit Will Result in Temp of Associated Conductors,Exceeding FSAR Value.Sample Boron Concentration Could Not Be Restored within 1 H ML20090F2461983-06-23023 June 1983 Telecopy Ro:On 830531,auto & Manual Indication Lights for FIC-0737A & HIC-0737A (Controllers for CV-0737A-auxiliary Feedwater) Discovered Out.Caused by Blown Fuse in Control Circuitry ML20073T0831983-05-0202 May 1983 Telecopy Ro:On 830429,sample from T-82D (Safety Injection Tank D) Showed Boron Concentration Below Tech Spec Limit. While Attempting to Increase Boron Level,Addl Safety Injection of T-82B occurred.T-82D & T-82B Restored ML20079P6851983-04-28028 April 1983 Updated RO 83-06:evaluation of Discrepancies Between as- Built & Actual Design of Safety Injection Refueling Water Tank Support Structure Indicated Sufficient Capacity to Resist Loadings.Schedule for Mods & Design Review Submitted ML20073Q8501983-04-26026 April 1983 Telecopy Ro:On 830425,two Safety Injection Tanks Inoperable. Caused by Low Level & Routine Testing.Tank Level Restored ML20073R3501983-04-25025 April 1983 Telecopy Ro:On 830423,safety Injection Tank Inoperable Due to Routine Sampling.Additionally,Another Tank Became Inoperable Due to Low Level ML20069K4911983-04-18018 April 1983 Telecopy Ro:On 830415,safety Injection Tank T-82D Fell Below Tech Spec Level Requirements.No Cause Stated.Level Restored ML20072F3461983-03-14014 March 1983 Telecopy Ro:On 830312,w/safety Injection Tank T-82D Inoperable Due to Low Boron Concentration,Addl Safety Injection Tank T-82B Became Inoperable Due to Low Boron Level.Operability Restored ML20070W0541983-02-10010 February 1983 Telecopy Ro:On 830129,operators Discovered Thermal Overloads for One Room Cooler Fan in Each of Engineered Safeguards Rooms Tripped & Wired Incorrectly on 830131.Fan Wiring Corrected ML20071A0201983-02-0707 February 1983 Telecopy Ro:On 830204,number of Openings in Safety Injection Refueling Water Tank Support Structure Unaccounted for & Only One Fan Operating for Each Room Cooler.Caused by Loss of Offsite Power & Diesel Generator Failure ML20067C8451982-12-0303 December 1982 Ro:On 821203,safety Injection Tank T-828 Boron Concentration Fell Below Tech Specs & Could Not Be Restored within Required 1-h Limit ML20066A8651982-11-0101 November 1982 Telecopy Revised RO Initially Reported on 821025:on 821022, Boron Concentration in Safety Injection Tank T-82B Restored in 1-h.Initially Reported That Concentration Less than Tech Specs for Over 1-h ML20065T3841982-10-25025 October 1982 Telecopy Ro:On 821022,23, & 25,safety Injection Tank T-82B Boron Concentration Fell Below Tech Spec Limit & Could Not Be Restored within 1-h as Required ML20063E8211982-08-16016 August 1982 Telecopy Message of Ro:On 820814,containment Integrity Momentarily Lost.Caused by Failed Gasket on Escape Air Lock ML20084U6011977-12-0808 December 1977 Telecopy RO 77-056:on 771129,main Exhaust Fan Stopped During Gaseous Waste Release,Exceeding Tech Spec 3.9.15.Release Terminated.No Waste Gas Monitor Alarms Received or Discharge Limits Exceeded ML20084U6191977-11-28028 November 1977 Telecopy RO 77-055:on 771125,offsite Power Lost,Resulting in Loss of Main Condenser Cooling Water.Plant Stabilized in Hot Condition & Borated.Letdown Line Developed Leak.Leakage Exceeded Tech Spec 3.1.5 Limits.Leak Isolated & Repaired ML20084U6641977-09-26026 September 1977 Telecopy Ro:On 770924,station Power & Startup Power Lost. Caused by Lightning Storm ML20084U6831977-09-0909 September 1977 Telecopy Ro:On 770908,turbine Load Limiter Lower Switch Stuck Closed,Causing Turbine to Run Back to 43% Power.Caused by Control Rods Inserting Below pre-power & Power Dependent Insertion Limits to Maintain Primary Coolant Temp ML20084U7051977-07-19019 July 1977 Telecopy RO ER-76-036:on 770719,C SI Bottle Found Out of Specs & Level Transmitter Failed.Instrument Calibr,Repaired & Returned to Svc ML20084U2341977-02-0808 February 1977 Telecopy RO ER-77-014:on 770107,intake/discharge Water Temp Delta Temp Limit Exceeded Twice ML20084U2491977-02-0101 February 1977 Telecopy RO 77-009:on 770130,intake/discharge Water Delta Temp Limit Exceeded Twice,Violating Tech Specs 3.9 & 4.1 ML20084U7131977-02-0101 February 1977 Telecopy Ro:On 770131,transmission Towers & Conductors Between Plant & Switchyard Found Heavily Loaded W/Ice Deposited by Cooling Tower Plume.North Cooling Tower Placed on Bypass to Reduce Further Ice Formation ML20084U7281977-01-18018 January 1977 Telecopy Ro:On 770117,discharge/lake Delta Temp Exceeded Twice & Control Rod Misaligned During Withdrawal for Critical Approach ML20084U3031977-01-14014 January 1977 Telecopy RO 77-004:on 770111 & 12,intake/discharge Temp 5 F Limit Exceeded During Plant Trip Startup Conditions ML20085E6331977-01-0404 January 1977 Telecopy RO 77-001:control Rod Drive Mechanism 4 Declared Inoperable Due to Seal Leakage ML20085E4321976-12-10010 December 1976 Telecopy Ro:On 761209,one Sequencer in Left Channel Failed to Run Completely Through During Safeguards Sys Online Tests.Caused by Improper Sequencer Resetting ML20085E5881976-08-27027 August 1976 Telecopy Ro:On 760823,sequencer Improperly Operated.W/All Rods Withdrawn,Group 4 Select Light Energized When Group 3 Selected.Transmittal Sheet Encl ML20085E4801976-08-19019 August 1976 Telecopy RO ER-PAL-76-026:on 760817,cooling Tower Basin Level Exceeded Normal Elevation During Attempted Modified Mode of Circulating Water Sys Operation ML20085E5221976-05-17017 May 1976 Telecopy RO 76-016:on 760514,MSIV Integrity May Be Lost After Main Steam Line Break.Fsar Review Indicates That Steam Line Rupture Incident Assumed Complete Steam Generator Blowdown ML20085E5311976-05-11011 May 1976 Telecopy RO PAL-ER-014;on 760511,1-1 Diesel Generator Removed from Svc W/One High Pressure Safety Injection Pump Inoperable.Caused by Greater than Tech Spec Limiting Condition for Operation ML20085E5361976-05-11011 May 1976 Telecopy RO 76-013:during Plant Startup,Cooling Tower Drained to Repair Leaking Condenser Tube,Resulting in Temp Differential Above Tech Spec Limits ML20085E5561976-05-0303 May 1976 Telecopy Ro:On 760430,during Mods Re Boron Recrystallization,Vendor Reported That Case Code Allowable Stress May Be Exceeded at Valve body-to-bonnet Flange.Valves within Code Limits for Present Operating Pressure ML20085E5691976-04-23023 April 1976 Telecopy RO 76-011:penetration 46 Containment Vent Header Exceeded Allowable Limits During Leak Testing ML20085E5821976-04-12012 April 1976 Telecopy RO 76-008:on 760409,waste Gas Tank T-101A Inadvertently Partially Released.No Limits Exceeded or Approached ML20085E6011976-02-11011 February 1976 Telecopy RO 76-004:on 760210,abnormal Degradation of Steam Generator Tubes/Reactor Pressure Boundary Suspected.Data Evaluation in Progress ML20085E6131976-02-10010 February 1976 Telecopy RO ER-76-003:on 760209,eddy Current Testing Revealed Greater than Expected Steam Generator Tube Degradation ML20085E6281976-01-12012 January 1976 Telecopy RO 76-001:investigation of Unusual Noise Revealed That Sirw Tank Slightly Dented & Vent Partially Plugged W/Ice & Snow.Lpsi Pump Stopped & Reactor Cavity Secured. Investigation Continues ML20085E7621975-12-22022 December 1975 Telecopy Message of Ro:On 751221,plant Discharge Water Temp Exceeded 5-degree Temp Differential During Plant Cooldown & Removal of a Cooling Tower from Svc ML20085E7701975-12-10010 December 1975 Telecopy Message Ro:On 751208,Tech Specs Apparently Violated Re Discharge Water Ph.Caused by Misinterpretation of Sample Data.Ro Negated & Problem Handled Through Plant Corrective Action Sys ML20085F9021975-12-10010 December 1975 Corrected AO 75-014 Re Previous Insp of 2,400-volt Breaker on Bus 1D ML20085E7731975-11-21021 November 1975 RO 75-026:on 751113,containment Purge Exhaust Valve Leaked Excessively During Local Leak Test.Caused by Improper Seat Alignment of Upstream Valve Due to Deformation by 46 Psig Pressure.Valves Tagged Closed ML20085E8641975-10-14014 October 1975 RO UE-75-010:on 751002,poison Rod Axial Growth Found in Facility Fuel.Possibly Caused by Radiation Induced Gowth. Power Level Limited to 80% & Primary Coolant Gross Gamma Radioactivity Monitored by Daily Samples 1995-09-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18066A6901999-11-0101 November 1999 Rev 5 to Palisades Nuclear Plant Colr. ML18066A6761999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Palisades Nuclear Plant ML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6351999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Palisades Nuclear Plant ML18066A6771999-08-31031 August 1999 Operating Data Rept Page of MOR for Aug 1999 for Palisades Nuclear Plant ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A6061999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Palisades Nuclear Plant.With 990803 Ltr ML18066A5201999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Palisades Nuclear Plant.With 990702 Ltr ML18066A4841999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Palisades Nuclear Plant.With 990603 Ltr ML18066A6371999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant ML18068A5941999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant.With 990503 Ltr ML18066A4161999-04-0101 April 1999 Rev 4 to COLR, for Palisades Nuclear Plant ML18066A4501999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Palisades Nuclear Plant.With 990402 Ltr ML18066A4671999-03-31031 March 1999 Rev 0 to SIR-99-032, Flaw Tolerance & Leakage Evaluation Spent Fuel Pool Heat Exchanger E-53B Nozzle Palisades Nuclear Plant. ML18068A5351999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Palisades Nuclear Plant.With 990302 Ltr ML18066A3931999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Palisades Nuclear Plant.With 990202 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML18066A3651998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Palisades Nuclear Plant.With 990105 Ltr ML18066A3421998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Palisades Nuclear Plant.With 981202 Ltr ML18066A3301998-11-11011 November 1998 Part 21 Rept Re Potential Safety Hazard Associated with Wrist Pin Assemblies for FM-Alco 251 Engines at Palisades Nuclear Power Plant.Caused by Insufficient Friction Fit Between Pin & Sleeve.Supplier of Pin Will No Longer Be Used ML18068A4921998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Palisades Nuclear Plant.With 981103 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A3181998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Palisades Nuclear Plant ML18066A2901998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Palisades Nuclear Power Plant.With 980903 Ltr ML18066A3191998-08-31031 August 1998 Revised Monthly Operating Rept Data for Aug 1998 for Palisades Nuclear Plant ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237E0301998-07-31031 July 1998 ISI Rept 3-3 ML18066A2701998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Palisades Nuclear Plant.W/980803 Ltr ML18066A2311998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Palisades Nuclear Plant ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A3061998-06-18018 June 1998 SG Tube Inservice Insp. ML20249C4951998-06-17017 June 1998 Rev 1 to EA-GEJ-98-01, Palisades Cycle 14 Disposition of Events Review ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18066A1711998-06-0101 June 1998 Part 21 Rept Re Impact of RELAP4 Excessive Variability on Palisades Large Break LOCA ECCS Results.Change in PCT Between Cycle 13 & Cycle 14 Does Not Constitute Significant Change Per 10CFR50.46 ML18066A1741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Palisades Nuclear Plant.W/980601 Ltr ML18066A2321998-05-31031 May 1998 Revised MOR for May 1998 for Palisades Nuclear Plant ML18068A4701998-05-31031 May 1998 Annual Rept of Changes in ECCS Models Per 10CFR50.46. ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18066A2331998-04-30030 April 1998 Revised MOR for Apr 1998 for Palisades Nuclear Plant ML18068A3461998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Palisades Nuclear Plant.W/980501 Ltr ML18066A3411998-04-22022 April 1998 Rev 0 to EMF-98-013, Palisades Cycle 14:Disposition & Analysis of SRP Chapter 15 Events. ML18065B2071998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Palisades Nuclear Plant.W/980403 Ltr ML20217C2741998-03-31031 March 1998 Independent Review - Is Consumers Energy Method (W Method) of Determining Palisades Nuclear Plant Best Estimate Fluence by Combining Transport Calculation & Dosimetry Measurements Technically Sound & Does It Meet Intent of Pts ML18066A2341998-03-31031 March 1998 Revised MOR for Mar 1998 for Palisades Nuclear Plant ML18068A3041998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Palisades Nuclear Plant.W/980302 Ltr ML18066A2351998-02-28028 February 1998 Revised MOR for Feb 1998 for Palisades Nuclear Plant ML18065B1641998-02-0505 February 1998 Rev 0 to Regression Analysis for Containment Prestressing Sys at 25th Year Surveillance. ML18067A8211998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Palisades Nuclear Plant.W/980203 Ltr 1999-09-30
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General Officos: 212 W est Michigan Avenue, Jackson, Michigan 49201. Araya Code $17 788-0550 December 16, 1971 Dr. P. A. Morris, Director Re: Docket 50-255 Division of Reactor Licensing License DFR-20 United States Atomic Energy Co:enission Washington, DC 2051+5
Dear Dr. Morris:
This is to inform you of two unusual problems that cccur-red during t.nd as a result cf the maintenance activities that have been performed during the previous month at the Palisades Flant.
Tuese two problems are the bending of nut capture devices on the Type A fuel bundles and the continuous outward driving of a control rod drive mechanism (CRDM) motor package while it was disconnected from the remainder of the CRDM.
In order to perform the inspectiona of the control blade upper end fittings described in Special Report-1, " Description of Cause and Correction of Damage to Control Rod Drive Mechanisms at the Palisades Nuclear Plant" submitted December 3, 1971, it was necessary to remove the control blades frem the core through the upper guide structure to the refueling canal. This work was per-formed using the auxiliary hook on the polar crane complete with a load cell to detect any binding of control blades that might occur during removal or reinstallation. This work proceeded smoothly until it was noticed that one blade wac binding slight'ly as it van being reinstalled in the core.
The control blade was removed and inspected. It showed <
very light scratching of the stainless steel control blade claddin6 ;f Further inspections revealed that the cause of the binding to be _l the guide rod nut capture devices on two Type A fuel bundles adjacent id to this control blade being bent such that they interfered with the Y
( control blade during its reinstallation.
4 A review of the design of the locking tabs revealed that these nut capture devices are raised slightly e.bove the upper end of N. the threaded portion of the Type A fuel assemblies' guide rods. The
- Pif same tabs on the Type B and Type C fuel have the upper end of the
' j 'b threaded portion of guide rod inserted through the hole in the nut 4 capture device (refer to attached sketch, Figure 1). '
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. December 1971 As this control blade did not show any sign of scratching during its inspection prior to being reinstalled in the core, it was concluded that the damage to the nut capture device occurred when reinstalling the control blade. The work was being done with the auxiliary crane and it was very difficult to obtain the required alignment such that the control blade could be lowered without catch-ing" on the edges of fuel assemblies. The nut capture devices are
) .060 inch thick and bend very casily.
The upper guide structure was removed and all nut capture devices were inspected. Twenty nut capture devices,were found bent, all on Type A fuel bundles. These 20 nut capture devices were straightened and visually inspected at 2X magnification for any signs of cracking. There were no signs of cracking.
- This type of problem will not reoccur during plant operation because the control rod blades cannot be withdrawn far enough to allow the tips to engage the nut capture devices. If further maintenance or core alteration activities take place prior to discharge of the Type A fuel assemblies that have the potential for bending these nut ,
capture devices, they wi.'ll be inspected at the completion of these
!. activities pricr to returning the plant to service.
The continuous outward driving of CRDM No 18 motor package occurred while the motor packade was removed to rezero primary rod po-
- . sition indication synchros following rework of the clutch by the manu-
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i facturer. Electrically, the motor package was connected as it would be during normal plant operations. During the zeroing of this synchro-nous unit, the following sequence of events occurred:
1.
From the control room the motor was driven-in the raise direction starting from zero indication. Manual individual J control was selected for CRR4 No 18, Group B.
- 2. The control room operator released the " raise" control switch but observed that raise motion was still indicated. Motion was confirmed by electricians on the reactor head observing l CRDM No 18 package. The control cable was disconnected at
- the CRDM and motion stopped.
s 3 The control cable was reconnected at the CRDM. Indicating
[ lights were restored but no motion occurred.
- 4. The control room operator again drove CRDM No 18 in the raise l
direction. Upon releasing the raise control switch, up motion again continued. This was interrupted by disconnecting the cable at the reactor head once again. ,
5 No other CRDM package could be made to continue to drive upwards after releasing ~the " raise" control switch.
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- 6. The control cable between CRDM No 18 and the junction box at 649' level was replacca by a spare cable.
7 CRDM No 18 now performed normally when driven up or down.
No unintentional motion could be made to occur.
- 8. The suspect control cable terminations were inspected re-vealing the following (refer to attached Figure 2):
- a. No grounds detected.
b ._ CRDM end termination: No shorts between pins and no broken connections.
- c. At junction box termination (straight end), the insu-lation on Pins L and G was either deteriorated or mis-sing such that the bare conductors and a piece of solder had caused a short circuit between these pins.
The effect of a short circuit from Pins L to G was studied to determine if it cculd cauce continuous driving of the motor package in the outward direction. This study assumed the conditions were the same as when the continuous driving occurred: namely, the mode selection switch was positioned to MI ranual indiviaual.; the group selection switch to Group B; and rod selection switch to No 18; the circuit is made up from the manual rod control switch, through Pin L; LS-1 (the upper limit switch) and B 18 raise contactor coil to neutral.
- 1. . A manual raise signal from the control room will energize B 18 " raise" contactor coil. This switches the 120-volt a-c supply to the CRDM windings, with a series capacitor in one circuit. The reversing interlock contact in the " lower" contactor coil circuit is opened. The motor will start and run up to speed, driving in the " raise" direction.
- 2. The short circuit between Pins L and G places in parallel with the circuit through LS-3 and B 1B raise contactor coil, a second circuit thz ough the control cable back to C-15, through the 6 pF capacitor and the No 3 contact of the " raise" contactor, throuch the c.ctar fuse to the 120-volt supply neutral.
3 This capacitive shunt across B 18 raf ce coil certainly did not prevent it fram remaining energizied.
- h. The same short circuit from Pins L to G means that with the upper electrical limit Switch LS-1 c1:osed (rod anywhere from "O" to 131"), the " raise" contactor Cbil B 18 has scaled it-self in through the Motor Winding T3 - Th in series with the raise coil.
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4 December 16, 1971- ,
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5 Releasing the manual raise control switch thus will not stop raise motion. The sealed in coil holds open the re-versing interleck contact preventing a " lower" signal for B 18. It also holds closed the No 1, No 2 and No 3 contacts of the " raise" contactor cupplying full volts to the T6 -
T7 motor winding and the T3 - T4 phase shifted winding.
Motion will continue'until the LS-1 limit switch opens at inches withdrawal.
- 6. The anergency off selector switch will interrupt this sneak circuit to stop raise motion.
Th'e cause of the degradation of the cable termination was at-tributed to the many times the cable had been handled in the past. This handling coupled with the stray piece of solder allowed the cable in-sulation to deteriorate and a sneak circuit to develop.
A complete single failure analysis of the cable terminations was perfonned. This analysis assumes that pin-to-pin sneak circuits could develop chnilar to the one described above. The results of this single failure analysis revealed that the L to G sneak circuit is the only failure that allows outward motion of CRH4 motor that cannot be stopped with the manual rod control switch. This metion is not self-initiating; it only commences if the rod control switch is positioned to raise. Shorts between other adjacent pins could cause the CRDM to respond in a variety of ways, including a dropped rod, continuous in-ward motion after releasing the rod control switch, wrona direction _of rgd motion or no effect. There were no defects that could cause the failure of a CRDM to trip and only two (both previously discussed) which would allow rod motion that an operator would not be able to stop with the manual rod control switch. This motor motion can be halted by the
" emergency off" switch.
Wiring modifications are being made that relocate the Pin L function to Pin C, which was previously unused. This eliminates the
)
two single failure sneak circuits that result in continued rod motion after releasing the rod control switch. A study of the modified wiring was made assuming that a single failure was again to occur. It was concluded from this study that further single failures of the nature described above would not cause any occurrences that were detrimental to reactor safety.
The equipment involved in this failure involved multiconductor cable,16AWG,25-1/C,1X3/CtriplexedandshieldedcableandaCannon MS 3106 E-32-7P. J Even if a failure of the nature experienced above were to occur with the CRDM assembled and the reactor operating, the control room op-erators would have been quickly alerted to the continued CRDM motion by the two rod deviation alarms (Rod Position Deviation Lo Limit); one when the affected CRDM deviates four inches from its group average and #
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. December 16, 1971 the second alarm (Rod Position Deviation Lo Lo) at an eight-inch de-viation. This would allow the operators to stop the continued rod motion very quickly with the " emergency off" switch. The uncontrolled rod withdrawal accident has been analyzed from a low initial and high-power level assuming the operator takes no corrective action. These analyses are presented in the Final Hazards Summary Report and show that in the unlikely event of a control rod withdrawal incident with the conditions varying from source level to full-power operation, the core and primary coolant system is protected by the high neutron flux trips, the high pressurizer trip, the thermal margin trip or the manual trip. The minimum DHB ratio is greater than 1.3 in all cases.
Based on the foregoing, it is concluded that the continued driving of the CRDM motor package does not involve an unreviewed safety question. In addition, the potential for recurrence through a similar failure has been eliminated for all CRDM by the wiring modifications described earlier in this letter.
Yours very truly, Robert L. Haueter (Signed)
RBS/dmb Robert L. Haveter Electric Production CC: Boyce H. Grier, Superintendent - Huclear
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