ML023580127

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FENOC Meeting Handouts for Meetings with Individual Commissioners Regarding Davis-Besse Nuclear Power Station Reactor Pressure Vessel Head Issues
ML023580127
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 04/07/2002
From:
FirstEnergy Nuclear Operating Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML023580127 (10)


Text

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"* Visual inspections since 1988

"* Commitment to start refueling outage early

"* Compensatory measures until start of refueling outage

"* Most comprehensive inspection of reactor head in industry to date

- Hairline axial cracks found in 5 nozzles

"* Formation of FENOC Investigation Team

" Complete weld repairs on 3 nozzles 11'!

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Addressing the Problem

"* Special team formed to investigate root cause includes Framatome, EPRI, INPO, Oconee, MRP and other industry, experts

"* Team to create, repair plan

"* Safety Assessment submitted to NRC April 8 Plant operated safely during this condition

"* Repair plan to be submitted during April

"* Contingency plan available w New head previously ordered for i

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"* Probable Cause Through wall cracking of CRDM nozzle, resulting in boric acid corrosion of Reactor Pressure Vessel (RPV) head low-alloy steel.

"* Contributing Causes Failure to clean boric acid from RPV head Design of RPV service structure limited access for cleaning and inspections {)

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Deferral of modification to install portals to service structure to allow cleanings and inspections ,

- Deferral of head cleaning and inspecti,

FENOC Root Cause Summary (continued)

  • Causal Factors Acceptance of boric acid accumulation on RPV head from CRDM flange leakage Failure to recognize symptoms of leakage collected from Containment Building monitors Harsh environmental conditions

-Boric acid corrosion control program targeted CRDM flange leakage