ML18113A976

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LER 79-006/03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control
ML18113A976
Person / Time
Site: Surry Dominion icon.png
Issue date: 04/04/1979
From: Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18113A975 List:
References
LER-79-006-03L-02, LER-79-6-3L-2, NUDOCS 7904060314
Download: ML18113A976 (3)


Text

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  • E ALL REQUIRED INFORMATION)

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@ .

~ I With* Unit /fl at power and Unit #2 shutdown, construction workers were iusta] 1 ing el ec

[2J]J trical cables as part of a plant improvement project. A fire seal in a fire harrjer

~ I penetration was removed to facilitate cable installation. Prior to reiustal 1 ing fire

[Q:li] seals, workers departed area. Also, a leak test was* not .Performed* after reinsta] 1 ing

~ fire* seals on three other penetrations which are reanired to perform a pressure sea]

~ ing function. This is contrary to Tech. Spec. 3.21.G and 4.18.H and reportable per

[Q))J I Tech. Spec. 6.6.2.b (3). The health and safety of the general public were oat affected 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

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32 ACTION FUTURE EFFECT SHUTDOWN ~ ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM SUB. SUPPLIER MANUFACTURER LU@~@

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)Upon discovery of the unsealed uenetration, a fire watch was immediate]y posted, ac-OJJJ Jtion was initiated to have the seal installed. A leak test was conducted on those

[I]}] I penetrations required to perform a pressure sealing function. The cause of this event I o:::II] 1was a lack of adequate administrative control over construction activities involving OJ1] lfire seals. Measures have been taken to prevent recurrence.

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W. L. Stewart NAME OF PRE PAR E R - - - - - - - - - - - - - - - - - - - PHON E:-(:..::8:..:0__;.4.:..)_35_7_-__:3..:::1..:.8..:.4_ _ __

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(Attachment, Page 1 of~

Surry Power Station, Unit 1 Docket No: 50-280 Report No: 79-006/03L-0 Event Date: 03-09-79 Unsealed Fire Penetration

1. Description of Event:

Construction personnel were installing electrical cables as a part of a plant improvement project. A fire seal in the fire barrier between the Auxiliary building and Unit One cable tunnel had been removed to facilitate the pulling of cables through the conduit. Due to administrative oversight, the fire barrier was not resealed prior to workers departing the area. This event is contrary to Technical Specification 3.21.G~

In another instance, after cables had been installed in penetrations of a fire barrier which is required to perform a pressure sealing function, the three penetrations involved were resealed but a local leakage test to verify operability was not conducted immediately. This is contrary to Tech-.

nical Specification 4.18.H.

2. Probable Consequences/Status of Redundant Systems:

The penetration of the fire barrier was unsealed for approximately 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />. In the event of a fire in the immediate vicinity, there was a remote possibility the fire could have traveled to the other side of the wall be-

' tween the Auxiliary building and Unit One cable tunnel.

The lack of a local leak test in the other wall prevented positive assurance of the pressure boundary.

3. Cause:

The cause of this event was a lack of adequate administrative control over construction activities involving fire seals. Appropriate corrective actions have been initiated.

4. Immediate Corrective Actions:

Upon discovery of the unsealed fire barrier, a fire watch was posted until the fire seal was reinstalled. A leak test was successfully conducted in the other case.

5. Scheduled Corrective Actions:

There is no corrective action required.

  • (Attqctrnent, page 2 of e S'urry Power.St;ation, Unit 1 Docket No: 50-28'0 Report No: 79-006/03L-0 Event Date: 03-09-79
6. Actions Taken to Prevent Recurrence:

The personnel involved have been reinstructed on the procedure require-ments. Additionally, a working log has been initiated to be time-dated and signed by the foreman which will insure continuity of sealing requirements are adhered to. Also, a VEPCO supervisor will be notified prior to and upon com-pletion of all work on fire seals. He will insure compliance with pertinent instructions.

7. Generic Implications:

There are no specific implications in this instance.