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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6131994-04-29029 April 1994 LER 94-005-00:on 940330,fire Suppression Water Supply Sys Declared Inoperable.Caused by Inadequate Design of cross- Connection Portion of Svc Water Sys & Inadequate Procedures. Valve SW-8 Tagged Shut to Prevent re-opening.W/940429 Ltr ML20046B4901993-07-30030 July 1993 LER 93-008-00:on 930701,discovered That During Previous Surveillance Testing on 910515,pump Differential Pressure Entered IST Required Action Range Due to Personnel Error. Plant Procedure AP 0164 Will Be revised.W/930730 Ltr ML20046A1141993-07-16016 July 1993 LER 93-007-00:on 930609,determined That Daily Instrument Checks Required by TS Were Not Included in Operator Rounds. Caused by Mgt & Human Factors Weakness.Ts Proposed Change & Amend Issue Process Will Be performed.W/930716 Ltr ML20045G5991993-07-0707 July 1993 LER 93-001-02:on 921217,indeterminate Fire Penetration Seal Configuration Identified When Insulation Removed from Piping.On 930324,addl Indeterminate Seals Identified.Fire Watches Established & New Seals installed.W/930707 Ltr ML20045D9191993-06-24024 June 1993 LER 93-006-00:on 930527,both Core Spray Sys Trains a & B Declared Inoperable When Calibr Procedure Error Resulted in Setpoint Set Nonconservatively.Caused by Failure to Apply Head Correction Factor.Procedure corrected.W/930624 Ltr ML18100B2771992-05-20020 May 1992 LER 92-016-00:on 920422,discovered That TS Quarterly Flow Test Not Performed During safety-related HVAC Sys Surveillance of Chilled Water Pump.Caused by Personnel Error.Procedure Re Ref Valves revised.W/920520 Ltr ML18100B2761992-05-19019 May 1992 LER 92-015-00:on 920424,RCIC Sys Declared Inoperable When Sys Flow Controller Meter Indicated Approx 30 Gpm Flow W/ RCIC Not Operating.Caused by Setpoint Drift.Work Orders Initiated to Correct Meter indication.W/920519 Ltr ML20028H7501991-01-23023 January 1991 LER 91-001-00:on 910104,radiation Protection (RP) Technician Entered Posted High Radiation Area W/O Dose Rate Monitoring Device Due to Personnel Error.Technician Relieved of Further RP duties.W/910123 Ltr ML20043G5691990-06-15015 June 1990 LER 90-007-00:on 900515,determined That Concentration of Old Bottle of Ammonia Span Gas Not within Spec Causing Ammonia Trip Setting to Be Nonconservative.Caused by Incorrect Certification by Vendor.Bottle replaced.W/900615 Ltr ML20042F3611990-05-0202 May 1990 LER 90-006-00:on 900403,Tech Spec Surveillance Requirement Missed Due to Failure to Include Basis on Tracking List. Caused by Personnel Error.Changes to Master Surveillance List & Any Affected Procedures Will Be made.W/900502 Ltr ML20042F2231990-05-0202 May 1990 LER 90-006-01:on 900403,discovered That Flow Transmitters That Supply Advanced off-gas Sys Flow Indication Had Not Been Calibr.Caused by Failure to Include Procedure on Surveillance List.Personnel retrained.W/900503 Ltr ML20042E1691990-04-12012 April 1990 LER 90-003-00:on 900319,inadvertent Primary Containment Isolation Sys Actuation Occurred.Caused by Lack of Coordination Between Monitor Downscale Setpoint & Monitor Reading.Proper Coordination established.W/900412 Ltr ML20012E9301990-03-22022 March 1990 LER 90-002-00:on 900302,identified That Key Sprinkler Isolation Valve Not Adequately Surveilled.Caused by Personnel Error.Valve Verified as Sealed & Surveillances for Fire Protection Valves revised.W/900322 Ltr ML20012B6061990-03-0808 March 1990 LER-90-001-00:on 900209,primary Containment Isolation Sys Group III Isolation & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Personnel Error.Isolation Reset.Personnel Counseled on Proper procedures.W/900308 Ltr ML20012C4291990-03-0707 March 1990 LER 87-015-01:on 871003,reactor Scram Occurred as Result of Turbine Control Valves Rapid Opening & Subsequent Fast Closure.Caused by Flow Imbalance in Turbine Control Oil Sys. Turbine Startup Procedure revised.W/900207 Ltr ML20006B4701990-01-22022 January 1990 LER 89-026-00:on 891223 & 900105,primary Containment Isolation Sys Group III Isolation & Standby Gas Treatment Sys Initiations Occurred.Caused by Failure of Sensor Converter.Isolation Reset & Monitor bypassed.W/900122 Ltr ML20005E1511989-12-26026 December 1989 LER 89-025-00:on 891128,primary Containment Isolation Sys Group III & Standby Gas Treatment Sys Initiation Occurred. Caused by Failure of Reactor Bldg Ventilation Radiation Monitor/Sensor Converter.Converter replaced.W/891226 Ltr ML20011D4901989-12-20020 December 1989 LER 89-024-01:on 890913,while Reviewing RHR Sys Surveillance Procedure,Determined That Leak Testing of RHR Valve V10-18 Not Incorporated & Implemented in Rev 9.Caused by Incomplete Review.Event Reviewed w/personnel.W/891220 Ltr ML19327A8881989-10-13013 October 1989 LER 89-024-00:on 890913,noted That Requirement from Previous Inservice Test Program Rev 9 Re Leak Testing of Valve V10-18 Not Incorporated & Implemented.Caused by Incomplete Review & Omission.Procedure Changes implemented.W/891013 Ltr ML19325C7821989-10-11011 October 1989 LER 89-023-00:on 890911,discovered That Remote Indication to Valve RHR-20 Not Available from 890320-0912,when Supply Breaker Replaced.Caused by Lack of Personnel Recognition. Breaker Replaced & Indication restored.W/891011 Ltr ML20024A8681983-06-22022 June 1983 LER 83-015/01T-0:on 830608,error Discovered in Spacing Table Developed for Support of Copper Piping in Svc Water Sys.Addl Supports Required to Fully Comply W/Ansi B31.1.W/830622 Ltr ML20024A8311983-06-0909 June 1983 LER 83-015/01P-0:on 830608,Yankee Atomic Electric Co Informed Util That Addl Piping Supports Required to Support Piping in Svc Water Sys & Torus Attached Piping.Cause & Corrective Actions to Be Provided in Next rept.W/830609 Ltr ML20024A3441983-06-0707 June 1983 LER 83-014/03L-0:on 830510,discovered Surveillance Frequency for Svc Water Processs Monitor Exceeded Tech Specs.Caused by Schedule Error.Analysis Immediately Performed.Applicable Personnel reinstructed.W/830607 Ltr ML20024A4151983-05-13013 May 1983 LER 83-013/03L-0:on 830413,while Reactor Shutdown,Weekly Environ Air Sample for 830405-12 at Station AT1.3 Not Obtained.Caused by Technician Failure to Test for Sys Vacuum.Technician Reinstructed in procedure.W/830513 Ltr ML20023B4741983-04-25025 April 1983 LER 83-011/03L-0:on 830325,during Visual Insp,Shock Suppressor MS-6 on Main Steam a Piping Found W/No Visible Fluid in Sight Glass & Failed to Lock Up.Caused by Damaged Lenztee.Snubber Cleaned & Rebuilt ML20028F3741983-01-21021 January 1983 LER 83-002/02T-0:on 830108,discovered Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line.Cause Unknown.Leaking Elbow Replaced w/304L Type Stainless Steel Matl Per NUREG-0313 Requirements ML20028F3921983-01-19019 January 1983 LER 82-026/03L-0:on 821220,while Shifting from Reactor Bldg Closed Cooling Water HX B to A,Closed Cooling Water Temp Rapidly Dropped 20 F.Caused by Increased Efficiency of HX Upon Cleaning ML20028D5591983-01-10010 January 1983 LER 83-001/01P-0:on 830107,valves V-16-19-20 & 22B Failed to Close When Operator Attempted to Secure Nitrogen Flow.Caused by Accumulation of Iron Particles on Magnet Used to Provide Valve Position Indication.Valves Cleaned ML20028D5421983-01-10010 January 1983 LER 83-002/01P-0:on 830108,indication of Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line Found.Caused by Pipe Crack.Cause of Pipe Crack Unknown.Elbow Replaced w/304L Type Stainless Steel Matl ML20028A3601982-11-0303 November 1982 LER 82-022/03L-0:on 821005,diesel Generator a Failed to Reach Required Voltage & Frequency within Tech Spec Time Limit.Caused by Fuel Oil Return Line Check Valve Failure. Valve Replaced ML20052C0051982-04-23023 April 1982 LER 82-007/01T-1:on 820309,standby Liquid Control Storage Tank Level & Sodium Pentaborate Concentration Calculations Did Not Correctly Account for Specific Gravity of Sodium Pentaborate.Caused by Procedure Equation Errors ML20052C0451982-04-23023 April 1982 LER 82-003/01T-1:on 820220,boron Concentration Fell Below Tech Spec Requirement.Caused by Apparent Boron Loss Coupled W/Small Sodium Pentaborate Concentration Margin ML20050B3941982-03-25025 March 1982 LER 82-005/03L-0:on 820223,uninterruptible Ac Electric Power Sys Tripped & Lost Power to Motor Control Ctr 89B, Rendering Sys Inoperable.Caused by Shorted Out Transient Suppression Capacitor Due to Aging.Capacitor Replaced ML20050A9291982-03-23023 March 1982 LER 82-007/01T-0:on 820309,calculations of Standby Liquid Control Storage Tank Concentration Versus Tank Level Correlation Did Not Account for Specific Gravity of Sodium Penaborate.Procedures Corrected ML20050A3781982-03-21021 March 1982 LER 82-006/03L-0:on 820219,during Normal Surveillance on Differential Pressure Switches DPIS 2-120 A,B,C & D,Switches A,B & C Found to Be Out of Tech Spec Limits.Caused by Setpoint Drift.Switches Reset to within Required Tolerance ML20042B2361982-03-16016 March 1982 LER 82-004/03L-0:on 820216,discovered That Continuous Environ Air Sample Not Obtainable at Station AT1.4 Per Tech Spec.Caused by Solder Lug of Std 125V-8A Power Toggle Switch Parting at 90 Degree Bend.Faulty Switch Replaced ML20042A4111982-03-0909 March 1982 LER 82-007/01P-0:on 820309,error Revealed in Calculations of Sodium Pentaborate Concentration in SLC Tank.Caused by Specific Gravity of Solution Not Being Factored Into Weight Percent Calculation in Accordance W/Tech Specs ML20042A6031982-03-0606 March 1982 LER 82-003/01T-0:on 820208,sample of Standby Liquid Control Boron Concentration Below Tech Spec Limits.Investigation in Progress.Administrated Limit & Sampling Frequency Increased ML20041F9281982-03-0303 March 1982 LER 82-002/03L-0:on 820206,ac Ground & Blown Fuse Alarms Activated,Rendering Trouble Alarm UPS-B Inoperable.Caused by Blown Fuse M Transient Suppression Circuit Due to Shorted Out Capacitor Off Board 2A 17 ML20041D7771982-02-25025 February 1982 LER 82-001/03L-0:on 820128,IRM Channel B Declared Inoperable.Caused by Failed Voltage Pre AMP (GE 112C-2218G001).Half Scram Manually Initiated.Component Will Be Repaired Prior to Entering IRM Range ML20041D4281982-02-22022 February 1982 LER 82-003/01P-0:on 820220,after Addition of Water to SLC Tank,Solution Sample Found Boron Concentration Below Required Amounts.Cause Unknown.Administrative Limit for Concentration Will Be Increased & Addl Sampling Conducted ML20040E2581982-01-26026 January 1982 LER 81-037/03L-0:on 811227,while Attempting to Start RHRSW Pump P-8-1A,breaker Tripped Contrary to Tech Specs.Caused by Worn Bushings on Operating Mechanism.Circuit Breaker Replaced.Breaker Mfg by Ge,Model Am 4.16 250-8HB ML20040C6971982-01-16016 January 1982 LER 81-036/03L-0:on 811217,containment Isolation Valve CU-15 Failed to Seat Satisfactorily Per Tech Spec 4.7.D.1 During Quarterly Surveillance Testing.Caused by Failure of Closing Torque Switch.Torque Switch Will Be Replaced Next Shutdown ML20040B1941981-12-30030 December 1981 Updated 81-028/03X-1:on 811017,field Breaker Failed to Open, Effectively Disabling Rrmg Set Recirculation Pump Trip Instrumentation.Caused by Binding of Operating Mechanism.New Breaker Installed ML20039F0101981-12-30030 December 1981 LER 81-035/03L-0:on 811204,during Core Spray Valve Test, Breaker for V14-11A Tripped & Reactor Shutdown Commenced. Caused by Breaker Not Latching When Closed,Allowing Breaker to Trip Below Setpoint.Breaker Replaced ML20039C2991981-12-18018 December 1981 LER 81-032/03L-0:on 811120,valves RWCU 68 & 15 Found to Have Seat Leakages Exceeding Tech Spec Range.Cause Not Stated. Disc Replaced & Valves Satisfactorily Retested ML20039C3071981-12-18018 December 1981 LER 81-034/03L-0:on 811121,operating Cycle Test of Standby Gas Treatment HEPA Filters Found Not to Have Been Done Since Sept 1979.Caused by Failure to Include Test on Dept Surveillance List.Test Completed & Schedule Revised ML20039C1121981-12-17017 December 1981 Updated LER 81-011/03X-1:on 810507,leak Discovered in Socket Weld Reducing Fitting.Caused by Intergranular Stress Corrosion Cracking.All Similar Fittings Replaced W/Differently Designed Fitting Less Susceptible to Failure ML20039C3821981-12-17017 December 1981 Updated LER 81-016/03X-1:on 810622,small Leak Found in Socket Weld Reducing Fitting in Vent Line of Regenerative Heat Exchanger E-15-1A.Caused by Intergranular Stress Corrosion Cracking Due to Wetting of Asbestos Insulation ML20039B1281981-12-0909 December 1981 LER 81-033/01T-0:on 811125,reactor Bldg Roof Hatch Opened by Work Crew W/O Notice to Supervisor Until Fire Permit for Welding Requested.Caused by Personnel Error.Personnel Reinstructed Re Procedural Requirement 1994-04-29
[Table view] Category:RO)
MONTHYEARML20029D6131994-04-29029 April 1994 LER 94-005-00:on 940330,fire Suppression Water Supply Sys Declared Inoperable.Caused by Inadequate Design of cross- Connection Portion of Svc Water Sys & Inadequate Procedures. Valve SW-8 Tagged Shut to Prevent re-opening.W/940429 Ltr ML20046B4901993-07-30030 July 1993 LER 93-008-00:on 930701,discovered That During Previous Surveillance Testing on 910515,pump Differential Pressure Entered IST Required Action Range Due to Personnel Error. Plant Procedure AP 0164 Will Be revised.W/930730 Ltr ML20046A1141993-07-16016 July 1993 LER 93-007-00:on 930609,determined That Daily Instrument Checks Required by TS Were Not Included in Operator Rounds. Caused by Mgt & Human Factors Weakness.Ts Proposed Change & Amend Issue Process Will Be performed.W/930716 Ltr ML20045G5991993-07-0707 July 1993 LER 93-001-02:on 921217,indeterminate Fire Penetration Seal Configuration Identified When Insulation Removed from Piping.On 930324,addl Indeterminate Seals Identified.Fire Watches Established & New Seals installed.W/930707 Ltr ML20045D9191993-06-24024 June 1993 LER 93-006-00:on 930527,both Core Spray Sys Trains a & B Declared Inoperable When Calibr Procedure Error Resulted in Setpoint Set Nonconservatively.Caused by Failure to Apply Head Correction Factor.Procedure corrected.W/930624 Ltr ML18100B2771992-05-20020 May 1992 LER 92-016-00:on 920422,discovered That TS Quarterly Flow Test Not Performed During safety-related HVAC Sys Surveillance of Chilled Water Pump.Caused by Personnel Error.Procedure Re Ref Valves revised.W/920520 Ltr ML18100B2761992-05-19019 May 1992 LER 92-015-00:on 920424,RCIC Sys Declared Inoperable When Sys Flow Controller Meter Indicated Approx 30 Gpm Flow W/ RCIC Not Operating.Caused by Setpoint Drift.Work Orders Initiated to Correct Meter indication.W/920519 Ltr ML20028H7501991-01-23023 January 1991 LER 91-001-00:on 910104,radiation Protection (RP) Technician Entered Posted High Radiation Area W/O Dose Rate Monitoring Device Due to Personnel Error.Technician Relieved of Further RP duties.W/910123 Ltr ML20043G5691990-06-15015 June 1990 LER 90-007-00:on 900515,determined That Concentration of Old Bottle of Ammonia Span Gas Not within Spec Causing Ammonia Trip Setting to Be Nonconservative.Caused by Incorrect Certification by Vendor.Bottle replaced.W/900615 Ltr ML20042F3611990-05-0202 May 1990 LER 90-006-00:on 900403,Tech Spec Surveillance Requirement Missed Due to Failure to Include Basis on Tracking List. Caused by Personnel Error.Changes to Master Surveillance List & Any Affected Procedures Will Be made.W/900502 Ltr ML20042F2231990-05-0202 May 1990 LER 90-006-01:on 900403,discovered That Flow Transmitters That Supply Advanced off-gas Sys Flow Indication Had Not Been Calibr.Caused by Failure to Include Procedure on Surveillance List.Personnel retrained.W/900503 Ltr ML20042E1691990-04-12012 April 1990 LER 90-003-00:on 900319,inadvertent Primary Containment Isolation Sys Actuation Occurred.Caused by Lack of Coordination Between Monitor Downscale Setpoint & Monitor Reading.Proper Coordination established.W/900412 Ltr ML20012E9301990-03-22022 March 1990 LER 90-002-00:on 900302,identified That Key Sprinkler Isolation Valve Not Adequately Surveilled.Caused by Personnel Error.Valve Verified as Sealed & Surveillances for Fire Protection Valves revised.W/900322 Ltr ML20012B6061990-03-0808 March 1990 LER-90-001-00:on 900209,primary Containment Isolation Sys Group III Isolation & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Personnel Error.Isolation Reset.Personnel Counseled on Proper procedures.W/900308 Ltr ML20012C4291990-03-0707 March 1990 LER 87-015-01:on 871003,reactor Scram Occurred as Result of Turbine Control Valves Rapid Opening & Subsequent Fast Closure.Caused by Flow Imbalance in Turbine Control Oil Sys. Turbine Startup Procedure revised.W/900207 Ltr ML20006B4701990-01-22022 January 1990 LER 89-026-00:on 891223 & 900105,primary Containment Isolation Sys Group III Isolation & Standby Gas Treatment Sys Initiations Occurred.Caused by Failure of Sensor Converter.Isolation Reset & Monitor bypassed.W/900122 Ltr ML20005E1511989-12-26026 December 1989 LER 89-025-00:on 891128,primary Containment Isolation Sys Group III & Standby Gas Treatment Sys Initiation Occurred. Caused by Failure of Reactor Bldg Ventilation Radiation Monitor/Sensor Converter.Converter replaced.W/891226 Ltr ML20011D4901989-12-20020 December 1989 LER 89-024-01:on 890913,while Reviewing RHR Sys Surveillance Procedure,Determined That Leak Testing of RHR Valve V10-18 Not Incorporated & Implemented in Rev 9.Caused by Incomplete Review.Event Reviewed w/personnel.W/891220 Ltr ML19327A8881989-10-13013 October 1989 LER 89-024-00:on 890913,noted That Requirement from Previous Inservice Test Program Rev 9 Re Leak Testing of Valve V10-18 Not Incorporated & Implemented.Caused by Incomplete Review & Omission.Procedure Changes implemented.W/891013 Ltr ML19325C7821989-10-11011 October 1989 LER 89-023-00:on 890911,discovered That Remote Indication to Valve RHR-20 Not Available from 890320-0912,when Supply Breaker Replaced.Caused by Lack of Personnel Recognition. Breaker Replaced & Indication restored.W/891011 Ltr ML20024A8681983-06-22022 June 1983 LER 83-015/01T-0:on 830608,error Discovered in Spacing Table Developed for Support of Copper Piping in Svc Water Sys.Addl Supports Required to Fully Comply W/Ansi B31.1.W/830622 Ltr ML20024A8311983-06-0909 June 1983 LER 83-015/01P-0:on 830608,Yankee Atomic Electric Co Informed Util That Addl Piping Supports Required to Support Piping in Svc Water Sys & Torus Attached Piping.Cause & Corrective Actions to Be Provided in Next rept.W/830609 Ltr ML20024A3441983-06-0707 June 1983 LER 83-014/03L-0:on 830510,discovered Surveillance Frequency for Svc Water Processs Monitor Exceeded Tech Specs.Caused by Schedule Error.Analysis Immediately Performed.Applicable Personnel reinstructed.W/830607 Ltr ML20024A4151983-05-13013 May 1983 LER 83-013/03L-0:on 830413,while Reactor Shutdown,Weekly Environ Air Sample for 830405-12 at Station AT1.3 Not Obtained.Caused by Technician Failure to Test for Sys Vacuum.Technician Reinstructed in procedure.W/830513 Ltr ML20023B4741983-04-25025 April 1983 LER 83-011/03L-0:on 830325,during Visual Insp,Shock Suppressor MS-6 on Main Steam a Piping Found W/No Visible Fluid in Sight Glass & Failed to Lock Up.Caused by Damaged Lenztee.Snubber Cleaned & Rebuilt ML20028F3741983-01-21021 January 1983 LER 83-002/02T-0:on 830108,discovered Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line.Cause Unknown.Leaking Elbow Replaced w/304L Type Stainless Steel Matl Per NUREG-0313 Requirements ML20028F3921983-01-19019 January 1983 LER 82-026/03L-0:on 821220,while Shifting from Reactor Bldg Closed Cooling Water HX B to A,Closed Cooling Water Temp Rapidly Dropped 20 F.Caused by Increased Efficiency of HX Upon Cleaning ML20028D5591983-01-10010 January 1983 LER 83-001/01P-0:on 830107,valves V-16-19-20 & 22B Failed to Close When Operator Attempted to Secure Nitrogen Flow.Caused by Accumulation of Iron Particles on Magnet Used to Provide Valve Position Indication.Valves Cleaned ML20028D5421983-01-10010 January 1983 LER 83-002/01P-0:on 830108,indication of Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line Found.Caused by Pipe Crack.Cause of Pipe Crack Unknown.Elbow Replaced w/304L Type Stainless Steel Matl ML20028A3601982-11-0303 November 1982 LER 82-022/03L-0:on 821005,diesel Generator a Failed to Reach Required Voltage & Frequency within Tech Spec Time Limit.Caused by Fuel Oil Return Line Check Valve Failure. Valve Replaced ML20052C0051982-04-23023 April 1982 LER 82-007/01T-1:on 820309,standby Liquid Control Storage Tank Level & Sodium Pentaborate Concentration Calculations Did Not Correctly Account for Specific Gravity of Sodium Pentaborate.Caused by Procedure Equation Errors ML20052C0451982-04-23023 April 1982 LER 82-003/01T-1:on 820220,boron Concentration Fell Below Tech Spec Requirement.Caused by Apparent Boron Loss Coupled W/Small Sodium Pentaborate Concentration Margin ML20050B3941982-03-25025 March 1982 LER 82-005/03L-0:on 820223,uninterruptible Ac Electric Power Sys Tripped & Lost Power to Motor Control Ctr 89B, Rendering Sys Inoperable.Caused by Shorted Out Transient Suppression Capacitor Due to Aging.Capacitor Replaced ML20050A9291982-03-23023 March 1982 LER 82-007/01T-0:on 820309,calculations of Standby Liquid Control Storage Tank Concentration Versus Tank Level Correlation Did Not Account for Specific Gravity of Sodium Penaborate.Procedures Corrected ML20050A3781982-03-21021 March 1982 LER 82-006/03L-0:on 820219,during Normal Surveillance on Differential Pressure Switches DPIS 2-120 A,B,C & D,Switches A,B & C Found to Be Out of Tech Spec Limits.Caused by Setpoint Drift.Switches Reset to within Required Tolerance ML20042B2361982-03-16016 March 1982 LER 82-004/03L-0:on 820216,discovered That Continuous Environ Air Sample Not Obtainable at Station AT1.4 Per Tech Spec.Caused by Solder Lug of Std 125V-8A Power Toggle Switch Parting at 90 Degree Bend.Faulty Switch Replaced ML20042A4111982-03-0909 March 1982 LER 82-007/01P-0:on 820309,error Revealed in Calculations of Sodium Pentaborate Concentration in SLC Tank.Caused by Specific Gravity of Solution Not Being Factored Into Weight Percent Calculation in Accordance W/Tech Specs ML20042A6031982-03-0606 March 1982 LER 82-003/01T-0:on 820208,sample of Standby Liquid Control Boron Concentration Below Tech Spec Limits.Investigation in Progress.Administrated Limit & Sampling Frequency Increased ML20041F9281982-03-0303 March 1982 LER 82-002/03L-0:on 820206,ac Ground & Blown Fuse Alarms Activated,Rendering Trouble Alarm UPS-B Inoperable.Caused by Blown Fuse M Transient Suppression Circuit Due to Shorted Out Capacitor Off Board 2A 17 ML20041D7771982-02-25025 February 1982 LER 82-001/03L-0:on 820128,IRM Channel B Declared Inoperable.Caused by Failed Voltage Pre AMP (GE 112C-2218G001).Half Scram Manually Initiated.Component Will Be Repaired Prior to Entering IRM Range ML20041D4281982-02-22022 February 1982 LER 82-003/01P-0:on 820220,after Addition of Water to SLC Tank,Solution Sample Found Boron Concentration Below Required Amounts.Cause Unknown.Administrative Limit for Concentration Will Be Increased & Addl Sampling Conducted ML20040E2581982-01-26026 January 1982 LER 81-037/03L-0:on 811227,while Attempting to Start RHRSW Pump P-8-1A,breaker Tripped Contrary to Tech Specs.Caused by Worn Bushings on Operating Mechanism.Circuit Breaker Replaced.Breaker Mfg by Ge,Model Am 4.16 250-8HB ML20040C6971982-01-16016 January 1982 LER 81-036/03L-0:on 811217,containment Isolation Valve CU-15 Failed to Seat Satisfactorily Per Tech Spec 4.7.D.1 During Quarterly Surveillance Testing.Caused by Failure of Closing Torque Switch.Torque Switch Will Be Replaced Next Shutdown ML20040B1941981-12-30030 December 1981 Updated 81-028/03X-1:on 811017,field Breaker Failed to Open, Effectively Disabling Rrmg Set Recirculation Pump Trip Instrumentation.Caused by Binding of Operating Mechanism.New Breaker Installed ML20039F0101981-12-30030 December 1981 LER 81-035/03L-0:on 811204,during Core Spray Valve Test, Breaker for V14-11A Tripped & Reactor Shutdown Commenced. Caused by Breaker Not Latching When Closed,Allowing Breaker to Trip Below Setpoint.Breaker Replaced ML20039C2991981-12-18018 December 1981 LER 81-032/03L-0:on 811120,valves RWCU 68 & 15 Found to Have Seat Leakages Exceeding Tech Spec Range.Cause Not Stated. Disc Replaced & Valves Satisfactorily Retested ML20039C3071981-12-18018 December 1981 LER 81-034/03L-0:on 811121,operating Cycle Test of Standby Gas Treatment HEPA Filters Found Not to Have Been Done Since Sept 1979.Caused by Failure to Include Test on Dept Surveillance List.Test Completed & Schedule Revised ML20039C1121981-12-17017 December 1981 Updated LER 81-011/03X-1:on 810507,leak Discovered in Socket Weld Reducing Fitting.Caused by Intergranular Stress Corrosion Cracking.All Similar Fittings Replaced W/Differently Designed Fitting Less Susceptible to Failure ML20039C3821981-12-17017 December 1981 Updated LER 81-016/03X-1:on 810622,small Leak Found in Socket Weld Reducing Fitting in Vent Line of Regenerative Heat Exchanger E-15-1A.Caused by Intergranular Stress Corrosion Cracking Due to Wetting of Asbestos Insulation ML20039B1281981-12-0909 December 1981 LER 81-033/01T-0:on 811125,reactor Bldg Roof Hatch Opened by Work Crew W/O Notice to Supervisor Until Fire Permit for Welding Requested.Caused by Personnel Error.Personnel Reinstructed Re Procedural Requirement 1994-04-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8831999-10-21021 October 1999 Safety Evaluation Supporting Proposed Alternatives to Code Requirements Described in RR-V17 & RR-V18 ML20217G2041999-10-13013 October 1999 Safety Evaluation Supporting Amend 179 to License DPR-28 BVY-99-127, Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With ML20212C2551999-09-17017 September 1999 Safety Evaluation Supporting Amend 175 to License DPR-28 BVY-99-112, Monthly Operating Rept for Aug 1999 for Vermont Yankee.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Vermont Yankee.With BVY-99-109, Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 9908311999-08-19019 August 1999 Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 990831 BVY-99-102, Monthly Operating Rept for July 1999 for Vermont Yankee. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Vermont Yankee. with ML20209J0081999-07-14014 July 1999 Special Rept:On 990615,diesel Driven Fire Pump Failed to Achieve Rated Flow of 2500 Gallons Per Minute.Pump Was Inoperable for Greater than 7 Days.Corrective Maint Was Performed to Reset Pump Lift Setting BVY-99-090, Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With ML20196G5071999-06-23023 June 1999 Vynp Assessment of On-Site Disposal of Contaminated Soil by Land Spreading BVY-99-077, Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With BVY-99-068, Monthly Operating Rept for Apr 1999 for Vynp.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Vynp.With ML20206E8741999-04-29029 April 1999 SER Determined That Flaw Evaluation Meets Rules of ASME Code & Assumed Crack Growth Rate Adequate for Application ML20206D9301999-04-27027 April 1999 1999 Emergency Preparedness Exercise 990427 Exercise Manual (Plume Portion) ML20205S4211999-04-16016 April 1999 Non-proprietary Version of Revised Page 4-3 of HI-981932 Technical Rept for Vermont Yankee Spent Fuel Pool Storage Expansion ML20205K7581999-04-0707 April 1999 Safety Evaluation Supporting Alternative Proposal for Reexamination of Circumferential Welds with Detected Flaw Indications in Plant RPV BVY-99-046, Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With ML20205F6631999-03-0404 March 1999 Jet Pump Riser Weld Leakage Evaluation BVY-99-035, Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With ML20205P8241999-02-28028 February 1999 Rev 2 to Vermont Yankee Cycle 20 Colr ML20203H9881999-02-18018 February 1999 SER Accepting Alternative to 10CFR50.55a(g)(6)(ii)(A) Augmented Reactor Vessel Exam at Vermont Yankee Nuclear Power Station.Technical Ltr Rept Encl ML20203A6951999-02-0404 February 1999 Revised Rev 2,App B to Vermont Yankee Operational QA Manual (Voqam) ML20199K7151999-01-21021 January 1999 Corrected Safety Evaluation Supporting Amend 163 Issued to FOL DPR-28.Pages 2 & 3 Required Correction & Clarification ML20199K6991999-01-20020 January 1999 Safety Evaluation Concluding That Request to Use YAEC-1339, Yankee Atomic Electric Co Application of FIBWR2 Core Hydraulics Code to BWR Reload Analysis, at Vermont Yankee Acceptable ML20199L5951999-01-14014 January 1999 Safety Evaluation Accepting Licensee Proposed Alternative to Code Requirement,Described in Rev 2 to Pump Relief Request RR-P10 Pursuant to 10CFR50.55a(a)(3)(i) BVY-99-071, Corp 1998 Annual Rept. with1998-12-31031 December 1998 Corp 1998 Annual Rept. with BVY-99-001, Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station ML20198H5481998-12-23023 December 1998 Rev 2 to Vermont Operational QA Manual,Voqam ML20196H8641998-12-0101 December 1998 Cycle 19 Operating Rept BVY-98-163, Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With ML20195C4161998-11-0909 November 1998 SER Accepting Request That NRC Approve ASME Code Case N-560, Alternative Exam Requirement for Class 1,Category B-J Piping Welds BVY-98-154, Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With ML20155B6471998-10-26026 October 1998 Safety Evaluation Accepting Jet Pump Riser Insp Results & Flaw Evaluation,Conducted During 1998 Refueling Outage ML20154N0891998-10-16016 October 1998 Rev 1 to Vermont Operational QA Program Manual (Voqam) ML20154B6951998-10-0101 October 1998 SER Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Vermont Yankee Nuclear Power Station BVY-98-149, Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With ML20239A1361998-09-0202 September 1998 SER Re License Request for NRC Review & Concurrence W/Changes to NRC-approved Fire Protection Program BVY-98-135, Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With ML20151U0361998-08-28028 August 1998 Non-proprietary Rev 1 to Holtec Rept HI-981932, Vermont Yankee Nuclear Power Station Spent Storage Expansion Project ML20237E9221998-08-20020 August 1998 Vynp 1998 Form NIS-1 Owners Summary Rept for ISI, 961103-980603 BVY-98-122, Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station ML20205F6491998-07-31031 July 1998 Rev 1 to GE-NE-B13-01935-02, Jet Pump Assembly Welds Flaw Evaluation Handbook for Vermont Yankee ML20236G0011998-06-30030 June 1998 Individual Plant Exam External Events BVY-98-098, Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station ML20248C5081998-05-31031 May 1998 Rev 2 to 24A5416, Supplemental Reload Licensing Rept for Vermont Yankee Nuclear Power Station Reload 19 Cycle 20 ML20248C4951998-05-31031 May 1998 Rev 1 to Vermont Yankee Nuclear Power Station Cycle 20 Colr BVY-98-081, Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station ML20247J8341998-05-31031 May 1998 Peak Suppression Pool Temp Analyses for Large Break LOCA Scenarios, for May 1998 ML20247G4001998-05-12012 May 1998 Interview Rept of Ej Massey ML20247E6351998-04-30030 April 1998 Rev 1 to GE-NE-B13-01935-LTR, Jet Pump Riser Welds Allowable Flaw Sizes Ltr Rept for Vermont Yankee 1999-09-30
[Table view] |
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3 VERMONT YANKEE NUCLEAR POWER' CORPORATION P.O. Box 157, Governor Hunt Road 3; s
'/ \ Vernon, Vermont 05354-0157
.( Y I .'
- x. _-( (802) 257-7711 3 ,.-
July 16, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
REFERENCE:
Operating License DPR-28 Docket No. 50-271 Reportable Occurrence No. LER 93-07 Dear Sirst As defined by 10 CFR 50.73, we are reporting the attached Reportable Occurrence as LER 93-07. A seven-day extension was granted on 7/9/93 by Eugene Kelley of Region I for this LER.
Very truly yours, VERMONT YANKEE NUCLEAR POWER CORPORATION
/ .
Robert Wanczyk r Plant lianager cc: Regional Administrator USNRC Region I 475 Allendale Road King of Prussia, PA 19406 230040 9307260212 930726 PDR S
ADOCK 05000272 pon I.1
//)Vh i
2 1 i
g,3
WRC Form 366 U.S. NUCLEAR SEGULATORY COMMISSION APP 30VED OMS No. 3150-0104- I (6-89) EXP!2ES 4/30/92 ESTIMATED BURDEN PER RESPONSE TO C0t; PLY WITH THIS ]
INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD i COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P 350), U.S. NUCLEAR PEGULATORY COMMISSION, WASHINGTON DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.
FACILITY NAME (1) DOCKET NO. (2) PAGE (3)
VERMONT (ANKEE NUCLEAR POWER $ FAT 10N Ol5j.0l0l0l2l7l1 0 1 OF 0 4 TITLE (4)
FAILURE TO PERFORM DAILY INSTRUMENT CHECKS DUE TO MANAGEMENT AND HUMAN FACTORS WEAKNESS EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEQ # REV # MONTH DAY YEAR FACILITY NAMES DOCKET NO (S) ,
0 5 0 0 0 !
l 0 6 0 9 9 3 9 3 -
0 0 7 -
0 0 0l7 1 6 9 3 0 5 0 0 0 !
OPERATING THIS REPORT IS SUBMITTED PURSUANT TO REQ'MTS OF 10 CFR i: CHECK ONE OR MORE (11)
CloDE (9) N 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) )
LEVEL (10) 100 j 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vil) OTHER: 1
. . ... . . ... 20.405(a)(1)(lii) X 50.73(a)(2)(i) 50.73(a)(2)(viii)(A)
. . . . . . 20.405(a)(1)(iv) 50.73(a)(2)(fi) 50.73(a)(2)(viii)(B)
...... . .. . 20.405(a)(1)(v) 50.73(a)(2)(lii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NO.
AREA CODE ROBERT J. WANCZYK, PLANT MANAGER 8l0l2 2lSl7l-l7l7l1l1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYST COMPONENT MFR REPORTABLE CAUSE SYST COMPONENT MFR REPORTABLE TO NPROS .. TO NPRDS .... ;
NA NA ... NA NA .... l l { l l l l l l l l l l l l 1
l l l l 1 SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MO DAY YR I SUBMISSION i DATE (15) !
YES (!f yes, complete EXPECTED SUBMISSloN DATE) X NO l l l ABSTRACT (Limit to 1400 spaces, i.e., approx. fif teen single-space typewritten lines) (16)
On June 9,1993 it was determined that the Daily Instrument Checks required by Technical Specifications Table 4.2.1~were not included in the Operators Rounds for the Auxiliary Power Monitor and the Pump Bus Power Monitor for the Core Spray system and the Low Pressure Coolant injection system. On June 21,1993 additional Daily Check omissions from the Operator Rounds were found in Table 4.2.1 for the High Drywell Pressure instrumentation in the Emergency Cote Cooling System, and on June 23,1993 in Table 4.2.2 for the High Drywell Pressure instrumentation in the Primary Containment Isolation System and Table 4.2.9 for the Reactor Core isolation Cooling Lcgic Bus Power Monitor.
The root cause of these events has been determined to be Management weakness in evaluating surveillance requirements with contributing causes of Human Factors and Personnel Error due to a lack of instrument tag numbers in the Tech Spec Tables.
Immed: ate corrective actions consisted of revisions to the " Conduct of Operations and Operator Rounds
of Standing Order # 8, and expanded review for potential problems with other Daily Instrument Checks in this TS Section. A 1 continuing effort will review all other TS Sections and will result in issuance ci an LER supplement and TS revisions if required.
NRC Form 366 ]
(6 89) .
1
w NCC Form 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO. 3150-0104 (6 89)' EXP!RES 4/30/92 4
ESTIMATED BURDEN PE2 RESPONSE TO COMPLY WITH THIS .
-INFORMATION COLLECTION REoVEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REcARDING BURDEN ESTIMATE TO THE RECORDS AND TEXT CONTINUATION REPORTS MANAGEMENT BRANCH (P-350), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.
FACILITY NAME (1) DOCKET No (2) LER NUMBER (6) PAGE (3)
YEAR SEQ # REV #
VERMONT YANKEE NUCLEAR POWER CoRPORAT!oN 9 3 -
0 0 7 -
0 0 0l5l0l0l0l2l7l1 0l2 0F 0l4 TEXT (If more space is required, use additional NRC Form 366A) (17)
Descrmtion of Event On June 9,1993 it was determined that the Daily instrument Checks required by Vermont Yankee Technical Specifications (TS)
Table 4.2.1 for the Auxiliary Power Monitor relay and the one of the two Pump Bus Power Monitor relays for the Core Spray system (CS) (Ells =BM) and the Low Pressure Coolant injection system (LPCI) (Ells = BO) were not being met by the daily check being conducted under the Operator Rounds. The CS Pump Bus Monitor consists of relays 14-K3 A&B and 14-K4 A&B, the CS Aux. Power Monitor consists of relays 14-K1 A&B. The LPCI Pump Bus Power Monitor consists of relays 10-K3 A&B and 10-K4 A&B, the LPCI Aux. Power Monitor consists of relays 10-K1 A&B. This concem was identified during a Biennial review of a Maintenance relay cal;bration procedures.
On June 21,1993 during a follow up engineering review, it was determined that the Daily Instrument Checks in accordance with TS Table 4.2.1 for the High Drywell Pressure instruments in the Emergency Core Cooling System (ECCS) (Ells = BO) were also not included in the Operators Rounds. The ECCS High Drywell Pressure instruments consists of Analog Trip Cards for PT.10-101 A(M) through D(M).
On June 23,1993 during additional engineering review, it was determined that the Daily Instrument Checks in accordance with TS 4.2.2 for the High Drywell Pressure instruments in the Primary Containment Isolation System (PCIS) (Ells =BD) were also not being performed. The PCIS High Drywell Pressure instruments consists of Analog Trip Cards for PT-5-12 A(M) through.
D(M). At the same time it was determined that the Daily instrument Check in accordance with TS Table 4.2.9 were not being performed for the Reactor Core isolation Cooling system (RCIC) (Ells = BN) Logic Bus Power Monitor. The RCIC Logic Bus Power Monitor consists of relay 13-K36.
The Daily Instrument Checks of the Aux Power Monitor and Pump Bus Power Monitors in the CS, and LPCI systems were thought to be satisfied by checking the annunciator for Bus / Logic Fail, a further review determined that the relays in question did not feed the annunciator window, these relays are original plant equipment since start-up in 1972. The High Drywell Pressure instrument checks in the PCIS and ECCS systems were installed in 1984 under the Analog Trip modification Phase 11 and were not identified in the Operator Round. The RCIC Logic Bus Power Monitor table was added to the TS Tables in November 1988 under Amendment 111, this relay is annunciated in the Control Room, but was not listed in the Operators P.ounds for daily checks.
Cause of Event These events will be discussed in three separate areas for specific root cause evaluation. The first concern is the Aux and Pump Bus Power Monitors. These daily instrument check requirements are original requirements from initial plant start-up. The root cause most applicable to these checks is due to misinterpretation in that the opetators were checking an annunciator to satisfy this requirement and were not aware that the second Pump Bus Power Monitor relay or the Aux Power relay did not feed the annunciator window. This alarm window is fed from the first of two Pump Bus Power Monitor relays and is not associated with the Aux Power Monitor relay.
The second concern is the Drywell Pressure instrumentation for the ECCS and PCIS Analog Trip systems. These instruments were installed in 1984 as the second phase of the Analog Trip system. The initial Analog Trip system design change added several daily instrument checks on the Operators Round Sheets. However, this phase of design provided revised TS Tables requirements for the additional daily instrument checks but did not list the Operators Round Sheet procedure as affected by the design. The Proposed TS Change No.103 and Plant Design Change 82-08 which implemented the new daily instrument checks received a detailed review dunng the design review process which did not discover the missing procedure requirements.
This root cause is that the level of review in 1982 was not adequate to locate the missing procedure change for daily instrument checks. The required functional and Cahbrations procedure changes were adequately addressed during the review process and were implemented in the Surveillance Tracking system.
NRC Form 366A (6-89) =
- l. . .. . _.
,- . +
NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO. 3150 0104 (6-89) EXP]RES 4/30/92 3
. ESilMATED BURDEN PER RESPONSE TO COMPLY WITH THIS l
- INFDRMATt0N COLLECTION REQUEST: 50.0 HRS. FORWARD .
LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND TEXT CONTINUATION REPORTS MANAGEMENT BRANCH (P 350), U.S. NUCLEAR REGULATORY COMMISSloN, WASHINGTON DC 20555, AND To THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.
FACILITY NAME (1) DOCKET NO (2) LER NUMBER (6) PAGE (3)
YEAR SEo # REV #
9 7 0 3 0 0 0 0l3 0F 0l4 VERMONT YANKEE NUCLEAR POWER CORPORATION 0l5l0l0j0j2l7l1 TEXT Of more space is required, use additional NRC Form 366A) (17)
The third concem is the RCIC Logic Bus Power Monitor. This TS change was driven by an NRC requirement to establish a new TS Table for RCIC actuation logic surveillance requirements in 1988. This requirement which added a daily instrument check had not existed prior to this time, however, the annunciator for the RCIC Logic Bus Power Monitor was original plant design.
These changes in the new TS Table were reviewed under the TS Proposed Change No.145, however the review did not identify the need to add the Daily instrument Check to the Operator Round Sheet procedure. This relay is annunciated in the Control Room as a valid indication of availability and equipment operability however the specific daily instrument check in the TS tables was not documented in the Operators Rounds sheets. This root cause is attributed to personnel error in that when the revision was made to TS, the daily check requirement was not incorporated into plant procedures.
Severat efforts have been initiated since 1988 to ensure that the required TS surveillance requirements are being performed.
The Technical Specsfications tables were extensively reviewed by outside contractors for compliance with the surveillance requirement as a result of an NRC Inspection. However, the objective of the review was to ensure that all surveillance procedures addressed the tests requinng scheduling. These procedures are specifically listed in the 4000 series procedures for
" Surveillance Procedures" The daily instrument checks are listed in the General Plant Administrative and Operating Procedure 1 as AP 0150 and since the daily checks are not scheduled they were not included in this review. This effort did not identify the need to address the daily instrument checks due to human factors in that the efforts was originated with concerns on the Surveillance List which is governed by the 4000 series surveillance procedures.
In 1992, in response to LER 91-16 Operations performed a review of all Operations Department Daily Instrument Checks to verify that the specific instruments identified in the TS were the instruments actually being checked. This review was performed using the Operations procedure as the starting point to insure that specific instruments would be cross referenced in the procedure with the appropriate TS table reference. This ef fort did not identify the need to add the missing instrument checks due to human f actors weakness in that the clear definition of the device to be checked is not specified in the TS Tables.
The root cause of these events has been determined to be Management weakness in evaluating surveillance requirements with contnbuting causes of Human Factors and Personnel Error due to a lack of instrument tag numbers in the Tec.i Spec Tables.
Anafysis of Event The CS and LPCI system Aux. Bus Power Monitor relays are not annunciated in the Control Room, therefore a f ailure of these relays would not be immediately identified. However, if they were to fail, the result would be a initiation of the 0,5, or 10 second time delay start upon initiation of the ECCS pumps. The f ailure of these relays will not stop the pump from running as expected. These time delays are initiated to allow Dieselloading and are considered in our design basis for Loss of Normal j Power operation, l The CS and LPCI system Pump Bus Power Monitor relays have one of the two relays annunciated in the Control Room. The loss of the un annunciated relay would not be immediately identified. The loss of the un annunciated relay would not stop the pump start operation because both relay contacts are in parallel, either relay would allow pump start. The loss of both would be alarmed in the Control Room The ECCS High Drywell Pressure Master Trip Cards are located in the ECCS Cabinets in the Reactor Building on the 280 foot elevation. Each Trip Card has two annunciator alarms irt the Control Room. The two alarms are High Pressure and Gross Failure of the card. If the trip card drif ted high an alarm would annunciate in the Control Room, if the card failed an alarm would also annunciate and the card would need to be checked to determine the f ailure. However, if the card should drif t low, no alarm would be annunciated and the card must be checked to verify accurate pressure indicat;on. These cards are redundant to each other on the two different trains of ECCS, therefore the single f ailure of one card would still allow high drywell pressure initiation for the ECCS system. )
1 I
NRC Form 366A (6-89)
I
- 4
- NRC ]Pora 366A U.S. NUCLEAR REGULA'! DRY COMMISSION APPROVED OMS NO. 3150-0104 i (6-69) ~
EXPIRES 4/30/92 ESTIMATED BURDEN PER RESPONSE 'ID COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD
' LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE 'ID THE RECORDS AND TEXT CONTINUATION REPORTS MANAGEMENT BRANCH (P-350), U.S. NUCLEAR REGULA'! DRY COMMISSION, WASHINGTON T 20555, AND 'ID THE PAPERWORK REDUCTION PRCkrECT (316, 3104), OFFICE OF MANAGEMENT AND BUDGET, WASHING'!DN, DC 20603.
FACILITY NAME 11) DOCKET NO (2) LER NUMBER (6) PAGE 13)
YEAR SEQ t REV 6 VERNONT YANKEE NUCLEAR POWER CORPORATION 0l5l0l0l0l2l7l1 9l3 -
0l0l7 -
ol0 0l4 or 0l4 TEXT (if more space is required, use additional NRC Form 366A) (17)
The PCIS High Drywell Pressure Master Trip Cards are located in the RPS Cabinets in the Reactor Building on the 280 foot elevation. Each Trip Card has two annunciator alarms in the Control Room. The two alarms are High Pressure and Gross Failure of ths card, if the trip card drifted high an alarm would annunciate in the Control Room, if the card failed an alarm would also annunciate and the card would need to be checked to determine the failure. However, if the card should drift low, no alarm would be annunciated and the card must be checked to verify accurate pressure indication. These cards are redundant to each other on the different trains of PCIS, therefore the single failure of one card would still allow high dryweX pressure initiation for the PCIS system.
The RCIC Logic Bus Power Monitor relay is annunciated in the Control Room and its failure would be known immediately, Corrective Actions immediate Corrective Actions
- 1. On June 9,1993 the Operations Dept. issued Standing Order No. 8 to visually verify the relay status daily for the CS and LPCI Pump Bus Power Monitor and Aux. Power Monitor relays.
- 2. On June 10,1993 the Operations Dept. revised procedure AP 0150 to include standing order No. 8 for the Aux Power Monitor and Pump Bus Power Monitor.
- 3. On June 21,1993 Procedure AP 0150 was revised to include ECCS High Drywell Pressure instrumentation daily checks for PT-10-101 A through D.
- 4. On June 23,1993 Procedure AP 0150 was revised to include PCIS High Drywell Pressure instrumentation daily checks for PT-5-12 A through D. In addition AP 0150 was also revised to include verification of annunciator window 4-V.5 for the RCIC Logic Bus Power Monitor is de-energized.
Lona Term Corrective Actions
- 5. All Daily instrument Checks listed in TS Tables will be verified as being performed, with respect to the appropriate device or instrument. This verification will be completed by 8/31/93.
- 6. If the above review finds any other Daily Instrument Checks that are not been performed, a supplement to this LER will be submitted if required.
- 7. A review of the TS required Calibrations and Daily Instrument Checks applied to devices which are not instruments will be performed and appropriate TS revisions will be submitted as required.
B. A review of the Design Change process, Technical Specification Proposed Change and Amendment issue process will be performed to establish a formal review process to ensure appropriate procedures are revised. This review will be completed by 2/28/94
- 9. In response to a previous concern we wiu perform a review of procedures that implement TS surveillance requirements to ensure management's expectations in this area are being met. This review will begin in the near future and will address such items as the intent of the TS surveillance requirements, assumptions, trending, administrative limits and clarity of procedural instructions.
Additional Information A review of past LER's for five years for similar occurrences identified LER 91-16 " Failure to Perform Daily Instrument Checks Due to Tech Spec Human Factors Weakness".
NRC Form 366A (6-89)
L