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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6131994-04-29029 April 1994 LER 94-005-00:on 940330,fire Suppression Water Supply Sys Declared Inoperable.Caused by Inadequate Design of cross- Connection Portion of Svc Water Sys & Inadequate Procedures. Valve SW-8 Tagged Shut to Prevent re-opening.W/940429 Ltr ML20046B4901993-07-30030 July 1993 LER 93-008-00:on 930701,discovered That During Previous Surveillance Testing on 910515,pump Differential Pressure Entered IST Required Action Range Due to Personnel Error. Plant Procedure AP 0164 Will Be revised.W/930730 Ltr ML20046A1141993-07-16016 July 1993 LER 93-007-00:on 930609,determined That Daily Instrument Checks Required by TS Were Not Included in Operator Rounds. Caused by Mgt & Human Factors Weakness.Ts Proposed Change & Amend Issue Process Will Be performed.W/930716 Ltr ML20045G5991993-07-0707 July 1993 LER 93-001-02:on 921217,indeterminate Fire Penetration Seal Configuration Identified When Insulation Removed from Piping.On 930324,addl Indeterminate Seals Identified.Fire Watches Established & New Seals installed.W/930707 Ltr ML20045D9191993-06-24024 June 1993 LER 93-006-00:on 930527,both Core Spray Sys Trains a & B Declared Inoperable When Calibr Procedure Error Resulted in Setpoint Set Nonconservatively.Caused by Failure to Apply Head Correction Factor.Procedure corrected.W/930624 Ltr ML18100B2771992-05-20020 May 1992 LER 92-016-00:on 920422,discovered That TS Quarterly Flow Test Not Performed During safety-related HVAC Sys Surveillance of Chilled Water Pump.Caused by Personnel Error.Procedure Re Ref Valves revised.W/920520 Ltr ML18100B2761992-05-19019 May 1992 LER 92-015-00:on 920424,RCIC Sys Declared Inoperable When Sys Flow Controller Meter Indicated Approx 30 Gpm Flow W/ RCIC Not Operating.Caused by Setpoint Drift.Work Orders Initiated to Correct Meter indication.W/920519 Ltr ML20028H7501991-01-23023 January 1991 LER 91-001-00:on 910104,radiation Protection (RP) Technician Entered Posted High Radiation Area W/O Dose Rate Monitoring Device Due to Personnel Error.Technician Relieved of Further RP duties.W/910123 Ltr ML20043G5691990-06-15015 June 1990 LER 90-007-00:on 900515,determined That Concentration of Old Bottle of Ammonia Span Gas Not within Spec Causing Ammonia Trip Setting to Be Nonconservative.Caused by Incorrect Certification by Vendor.Bottle replaced.W/900615 Ltr ML20042F3611990-05-0202 May 1990 LER 90-006-00:on 900403,Tech Spec Surveillance Requirement Missed Due to Failure to Include Basis on Tracking List. Caused by Personnel Error.Changes to Master Surveillance List & Any Affected Procedures Will Be made.W/900502 Ltr ML20042F2231990-05-0202 May 1990 LER 90-006-01:on 900403,discovered That Flow Transmitters That Supply Advanced off-gas Sys Flow Indication Had Not Been Calibr.Caused by Failure to Include Procedure on Surveillance List.Personnel retrained.W/900503 Ltr ML20042E1691990-04-12012 April 1990 LER 90-003-00:on 900319,inadvertent Primary Containment Isolation Sys Actuation Occurred.Caused by Lack of Coordination Between Monitor Downscale Setpoint & Monitor Reading.Proper Coordination established.W/900412 Ltr ML20012E9301990-03-22022 March 1990 LER 90-002-00:on 900302,identified That Key Sprinkler Isolation Valve Not Adequately Surveilled.Caused by Personnel Error.Valve Verified as Sealed & Surveillances for Fire Protection Valves revised.W/900322 Ltr ML20012B6061990-03-0808 March 1990 LER-90-001-00:on 900209,primary Containment Isolation Sys Group III Isolation & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Personnel Error.Isolation Reset.Personnel Counseled on Proper procedures.W/900308 Ltr ML20012C4291990-03-0707 March 1990 LER 87-015-01:on 871003,reactor Scram Occurred as Result of Turbine Control Valves Rapid Opening & Subsequent Fast Closure.Caused by Flow Imbalance in Turbine Control Oil Sys. Turbine Startup Procedure revised.W/900207 Ltr ML20006B4701990-01-22022 January 1990 LER 89-026-00:on 891223 & 900105,primary Containment Isolation Sys Group III Isolation & Standby Gas Treatment Sys Initiations Occurred.Caused by Failure of Sensor Converter.Isolation Reset & Monitor bypassed.W/900122 Ltr ML20005E1511989-12-26026 December 1989 LER 89-025-00:on 891128,primary Containment Isolation Sys Group III & Standby Gas Treatment Sys Initiation Occurred. Caused by Failure of Reactor Bldg Ventilation Radiation Monitor/Sensor Converter.Converter replaced.W/891226 Ltr ML20011D4901989-12-20020 December 1989 LER 89-024-01:on 890913,while Reviewing RHR Sys Surveillance Procedure,Determined That Leak Testing of RHR Valve V10-18 Not Incorporated & Implemented in Rev 9.Caused by Incomplete Review.Event Reviewed w/personnel.W/891220 Ltr ML19327A8881989-10-13013 October 1989 LER 89-024-00:on 890913,noted That Requirement from Previous Inservice Test Program Rev 9 Re Leak Testing of Valve V10-18 Not Incorporated & Implemented.Caused by Incomplete Review & Omission.Procedure Changes implemented.W/891013 Ltr ML19325C7821989-10-11011 October 1989 LER 89-023-00:on 890911,discovered That Remote Indication to Valve RHR-20 Not Available from 890320-0912,when Supply Breaker Replaced.Caused by Lack of Personnel Recognition. Breaker Replaced & Indication restored.W/891011 Ltr ML20024A8681983-06-22022 June 1983 LER 83-015/01T-0:on 830608,error Discovered in Spacing Table Developed for Support of Copper Piping in Svc Water Sys.Addl Supports Required to Fully Comply W/Ansi B31.1.W/830622 Ltr ML20024A8311983-06-0909 June 1983 LER 83-015/01P-0:on 830608,Yankee Atomic Electric Co Informed Util That Addl Piping Supports Required to Support Piping in Svc Water Sys & Torus Attached Piping.Cause & Corrective Actions to Be Provided in Next rept.W/830609 Ltr ML20024A3441983-06-0707 June 1983 LER 83-014/03L-0:on 830510,discovered Surveillance Frequency for Svc Water Processs Monitor Exceeded Tech Specs.Caused by Schedule Error.Analysis Immediately Performed.Applicable Personnel reinstructed.W/830607 Ltr ML20024A4151983-05-13013 May 1983 LER 83-013/03L-0:on 830413,while Reactor Shutdown,Weekly Environ Air Sample for 830405-12 at Station AT1.3 Not Obtained.Caused by Technician Failure to Test for Sys Vacuum.Technician Reinstructed in procedure.W/830513 Ltr ML20023B4741983-04-25025 April 1983 LER 83-011/03L-0:on 830325,during Visual Insp,Shock Suppressor MS-6 on Main Steam a Piping Found W/No Visible Fluid in Sight Glass & Failed to Lock Up.Caused by Damaged Lenztee.Snubber Cleaned & Rebuilt ML20028F3741983-01-21021 January 1983 LER 83-002/02T-0:on 830108,discovered Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line.Cause Unknown.Leaking Elbow Replaced w/304L Type Stainless Steel Matl Per NUREG-0313 Requirements ML20028F3921983-01-19019 January 1983 LER 82-026/03L-0:on 821220,while Shifting from Reactor Bldg Closed Cooling Water HX B to A,Closed Cooling Water Temp Rapidly Dropped 20 F.Caused by Increased Efficiency of HX Upon Cleaning ML20028D5591983-01-10010 January 1983 LER 83-001/01P-0:on 830107,valves V-16-19-20 & 22B Failed to Close When Operator Attempted to Secure Nitrogen Flow.Caused by Accumulation of Iron Particles on Magnet Used to Provide Valve Position Indication.Valves Cleaned ML20028D5421983-01-10010 January 1983 LER 83-002/01P-0:on 830108,indication of Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line Found.Caused by Pipe Crack.Cause of Pipe Crack Unknown.Elbow Replaced w/304L Type Stainless Steel Matl ML20028A3601982-11-0303 November 1982 LER 82-022/03L-0:on 821005,diesel Generator a Failed to Reach Required Voltage & Frequency within Tech Spec Time Limit.Caused by Fuel Oil Return Line Check Valve Failure. Valve Replaced ML20052C0051982-04-23023 April 1982 LER 82-007/01T-1:on 820309,standby Liquid Control Storage Tank Level & Sodium Pentaborate Concentration Calculations Did Not Correctly Account for Specific Gravity of Sodium Pentaborate.Caused by Procedure Equation Errors ML20052C0451982-04-23023 April 1982 LER 82-003/01T-1:on 820220,boron Concentration Fell Below Tech Spec Requirement.Caused by Apparent Boron Loss Coupled W/Small Sodium Pentaborate Concentration Margin ML20050B3941982-03-25025 March 1982 LER 82-005/03L-0:on 820223,uninterruptible Ac Electric Power Sys Tripped & Lost Power to Motor Control Ctr 89B, Rendering Sys Inoperable.Caused by Shorted Out Transient Suppression Capacitor Due to Aging.Capacitor Replaced ML20050A9291982-03-23023 March 1982 LER 82-007/01T-0:on 820309,calculations of Standby Liquid Control Storage Tank Concentration Versus Tank Level Correlation Did Not Account for Specific Gravity of Sodium Penaborate.Procedures Corrected ML20050A3781982-03-21021 March 1982 LER 82-006/03L-0:on 820219,during Normal Surveillance on Differential Pressure Switches DPIS 2-120 A,B,C & D,Switches A,B & C Found to Be Out of Tech Spec Limits.Caused by Setpoint Drift.Switches Reset to within Required Tolerance ML20042B2361982-03-16016 March 1982 LER 82-004/03L-0:on 820216,discovered That Continuous Environ Air Sample Not Obtainable at Station AT1.4 Per Tech Spec.Caused by Solder Lug of Std 125V-8A Power Toggle Switch Parting at 90 Degree Bend.Faulty Switch Replaced ML20042A4111982-03-0909 March 1982 LER 82-007/01P-0:on 820309,error Revealed in Calculations of Sodium Pentaborate Concentration in SLC Tank.Caused by Specific Gravity of Solution Not Being Factored Into Weight Percent Calculation in Accordance W/Tech Specs ML20042A6031982-03-0606 March 1982 LER 82-003/01T-0:on 820208,sample of Standby Liquid Control Boron Concentration Below Tech Spec Limits.Investigation in Progress.Administrated Limit & Sampling Frequency Increased ML20041F9281982-03-0303 March 1982 LER 82-002/03L-0:on 820206,ac Ground & Blown Fuse Alarms Activated,Rendering Trouble Alarm UPS-B Inoperable.Caused by Blown Fuse M Transient Suppression Circuit Due to Shorted Out Capacitor Off Board 2A 17 ML20041D7771982-02-25025 February 1982 LER 82-001/03L-0:on 820128,IRM Channel B Declared Inoperable.Caused by Failed Voltage Pre AMP (GE 112C-2218G001).Half Scram Manually Initiated.Component Will Be Repaired Prior to Entering IRM Range ML20041D4281982-02-22022 February 1982 LER 82-003/01P-0:on 820220,after Addition of Water to SLC Tank,Solution Sample Found Boron Concentration Below Required Amounts.Cause Unknown.Administrative Limit for Concentration Will Be Increased & Addl Sampling Conducted ML20040E2581982-01-26026 January 1982 LER 81-037/03L-0:on 811227,while Attempting to Start RHRSW Pump P-8-1A,breaker Tripped Contrary to Tech Specs.Caused by Worn Bushings on Operating Mechanism.Circuit Breaker Replaced.Breaker Mfg by Ge,Model Am 4.16 250-8HB ML20040C6971982-01-16016 January 1982 LER 81-036/03L-0:on 811217,containment Isolation Valve CU-15 Failed to Seat Satisfactorily Per Tech Spec 4.7.D.1 During Quarterly Surveillance Testing.Caused by Failure of Closing Torque Switch.Torque Switch Will Be Replaced Next Shutdown ML20040B1941981-12-30030 December 1981 Updated 81-028/03X-1:on 811017,field Breaker Failed to Open, Effectively Disabling Rrmg Set Recirculation Pump Trip Instrumentation.Caused by Binding of Operating Mechanism.New Breaker Installed ML20039F0101981-12-30030 December 1981 LER 81-035/03L-0:on 811204,during Core Spray Valve Test, Breaker for V14-11A Tripped & Reactor Shutdown Commenced. Caused by Breaker Not Latching When Closed,Allowing Breaker to Trip Below Setpoint.Breaker Replaced ML20039C2991981-12-18018 December 1981 LER 81-032/03L-0:on 811120,valves RWCU 68 & 15 Found to Have Seat Leakages Exceeding Tech Spec Range.Cause Not Stated. Disc Replaced & Valves Satisfactorily Retested ML20039C3071981-12-18018 December 1981 LER 81-034/03L-0:on 811121,operating Cycle Test of Standby Gas Treatment HEPA Filters Found Not to Have Been Done Since Sept 1979.Caused by Failure to Include Test on Dept Surveillance List.Test Completed & Schedule Revised ML20039C1121981-12-17017 December 1981 Updated LER 81-011/03X-1:on 810507,leak Discovered in Socket Weld Reducing Fitting.Caused by Intergranular Stress Corrosion Cracking.All Similar Fittings Replaced W/Differently Designed Fitting Less Susceptible to Failure ML20039C3821981-12-17017 December 1981 Updated LER 81-016/03X-1:on 810622,small Leak Found in Socket Weld Reducing Fitting in Vent Line of Regenerative Heat Exchanger E-15-1A.Caused by Intergranular Stress Corrosion Cracking Due to Wetting of Asbestos Insulation ML20039B1281981-12-0909 December 1981 LER 81-033/01T-0:on 811125,reactor Bldg Roof Hatch Opened by Work Crew W/O Notice to Supervisor Until Fire Permit for Welding Requested.Caused by Personnel Error.Personnel Reinstructed Re Procedural Requirement 1994-04-29
[Table view] Category:RO)
MONTHYEARML20029D6131994-04-29029 April 1994 LER 94-005-00:on 940330,fire Suppression Water Supply Sys Declared Inoperable.Caused by Inadequate Design of cross- Connection Portion of Svc Water Sys & Inadequate Procedures. Valve SW-8 Tagged Shut to Prevent re-opening.W/940429 Ltr ML20046B4901993-07-30030 July 1993 LER 93-008-00:on 930701,discovered That During Previous Surveillance Testing on 910515,pump Differential Pressure Entered IST Required Action Range Due to Personnel Error. Plant Procedure AP 0164 Will Be revised.W/930730 Ltr ML20046A1141993-07-16016 July 1993 LER 93-007-00:on 930609,determined That Daily Instrument Checks Required by TS Were Not Included in Operator Rounds. Caused by Mgt & Human Factors Weakness.Ts Proposed Change & Amend Issue Process Will Be performed.W/930716 Ltr ML20045G5991993-07-0707 July 1993 LER 93-001-02:on 921217,indeterminate Fire Penetration Seal Configuration Identified When Insulation Removed from Piping.On 930324,addl Indeterminate Seals Identified.Fire Watches Established & New Seals installed.W/930707 Ltr ML20045D9191993-06-24024 June 1993 LER 93-006-00:on 930527,both Core Spray Sys Trains a & B Declared Inoperable When Calibr Procedure Error Resulted in Setpoint Set Nonconservatively.Caused by Failure to Apply Head Correction Factor.Procedure corrected.W/930624 Ltr ML18100B2771992-05-20020 May 1992 LER 92-016-00:on 920422,discovered That TS Quarterly Flow Test Not Performed During safety-related HVAC Sys Surveillance of Chilled Water Pump.Caused by Personnel Error.Procedure Re Ref Valves revised.W/920520 Ltr ML18100B2761992-05-19019 May 1992 LER 92-015-00:on 920424,RCIC Sys Declared Inoperable When Sys Flow Controller Meter Indicated Approx 30 Gpm Flow W/ RCIC Not Operating.Caused by Setpoint Drift.Work Orders Initiated to Correct Meter indication.W/920519 Ltr ML20028H7501991-01-23023 January 1991 LER 91-001-00:on 910104,radiation Protection (RP) Technician Entered Posted High Radiation Area W/O Dose Rate Monitoring Device Due to Personnel Error.Technician Relieved of Further RP duties.W/910123 Ltr ML20043G5691990-06-15015 June 1990 LER 90-007-00:on 900515,determined That Concentration of Old Bottle of Ammonia Span Gas Not within Spec Causing Ammonia Trip Setting to Be Nonconservative.Caused by Incorrect Certification by Vendor.Bottle replaced.W/900615 Ltr ML20042F3611990-05-0202 May 1990 LER 90-006-00:on 900403,Tech Spec Surveillance Requirement Missed Due to Failure to Include Basis on Tracking List. Caused by Personnel Error.Changes to Master Surveillance List & Any Affected Procedures Will Be made.W/900502 Ltr ML20042F2231990-05-0202 May 1990 LER 90-006-01:on 900403,discovered That Flow Transmitters That Supply Advanced off-gas Sys Flow Indication Had Not Been Calibr.Caused by Failure to Include Procedure on Surveillance List.Personnel retrained.W/900503 Ltr ML20042E1691990-04-12012 April 1990 LER 90-003-00:on 900319,inadvertent Primary Containment Isolation Sys Actuation Occurred.Caused by Lack of Coordination Between Monitor Downscale Setpoint & Monitor Reading.Proper Coordination established.W/900412 Ltr ML20012E9301990-03-22022 March 1990 LER 90-002-00:on 900302,identified That Key Sprinkler Isolation Valve Not Adequately Surveilled.Caused by Personnel Error.Valve Verified as Sealed & Surveillances for Fire Protection Valves revised.W/900322 Ltr ML20012B6061990-03-0808 March 1990 LER-90-001-00:on 900209,primary Containment Isolation Sys Group III Isolation & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Personnel Error.Isolation Reset.Personnel Counseled on Proper procedures.W/900308 Ltr ML20012C4291990-03-0707 March 1990 LER 87-015-01:on 871003,reactor Scram Occurred as Result of Turbine Control Valves Rapid Opening & Subsequent Fast Closure.Caused by Flow Imbalance in Turbine Control Oil Sys. Turbine Startup Procedure revised.W/900207 Ltr ML20006B4701990-01-22022 January 1990 LER 89-026-00:on 891223 & 900105,primary Containment Isolation Sys Group III Isolation & Standby Gas Treatment Sys Initiations Occurred.Caused by Failure of Sensor Converter.Isolation Reset & Monitor bypassed.W/900122 Ltr ML20005E1511989-12-26026 December 1989 LER 89-025-00:on 891128,primary Containment Isolation Sys Group III & Standby Gas Treatment Sys Initiation Occurred. Caused by Failure of Reactor Bldg Ventilation Radiation Monitor/Sensor Converter.Converter replaced.W/891226 Ltr ML20011D4901989-12-20020 December 1989 LER 89-024-01:on 890913,while Reviewing RHR Sys Surveillance Procedure,Determined That Leak Testing of RHR Valve V10-18 Not Incorporated & Implemented in Rev 9.Caused by Incomplete Review.Event Reviewed w/personnel.W/891220 Ltr ML19327A8881989-10-13013 October 1989 LER 89-024-00:on 890913,noted That Requirement from Previous Inservice Test Program Rev 9 Re Leak Testing of Valve V10-18 Not Incorporated & Implemented.Caused by Incomplete Review & Omission.Procedure Changes implemented.W/891013 Ltr ML19325C7821989-10-11011 October 1989 LER 89-023-00:on 890911,discovered That Remote Indication to Valve RHR-20 Not Available from 890320-0912,when Supply Breaker Replaced.Caused by Lack of Personnel Recognition. Breaker Replaced & Indication restored.W/891011 Ltr ML20024A8681983-06-22022 June 1983 LER 83-015/01T-0:on 830608,error Discovered in Spacing Table Developed for Support of Copper Piping in Svc Water Sys.Addl Supports Required to Fully Comply W/Ansi B31.1.W/830622 Ltr ML20024A8311983-06-0909 June 1983 LER 83-015/01P-0:on 830608,Yankee Atomic Electric Co Informed Util That Addl Piping Supports Required to Support Piping in Svc Water Sys & Torus Attached Piping.Cause & Corrective Actions to Be Provided in Next rept.W/830609 Ltr ML20024A3441983-06-0707 June 1983 LER 83-014/03L-0:on 830510,discovered Surveillance Frequency for Svc Water Processs Monitor Exceeded Tech Specs.Caused by Schedule Error.Analysis Immediately Performed.Applicable Personnel reinstructed.W/830607 Ltr ML20024A4151983-05-13013 May 1983 LER 83-013/03L-0:on 830413,while Reactor Shutdown,Weekly Environ Air Sample for 830405-12 at Station AT1.3 Not Obtained.Caused by Technician Failure to Test for Sys Vacuum.Technician Reinstructed in procedure.W/830513 Ltr ML20023B4741983-04-25025 April 1983 LER 83-011/03L-0:on 830325,during Visual Insp,Shock Suppressor MS-6 on Main Steam a Piping Found W/No Visible Fluid in Sight Glass & Failed to Lock Up.Caused by Damaged Lenztee.Snubber Cleaned & Rebuilt ML20028F3741983-01-21021 January 1983 LER 83-002/02T-0:on 830108,discovered Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line.Cause Unknown.Leaking Elbow Replaced w/304L Type Stainless Steel Matl Per NUREG-0313 Requirements ML20028F3921983-01-19019 January 1983 LER 82-026/03L-0:on 821220,while Shifting from Reactor Bldg Closed Cooling Water HX B to A,Closed Cooling Water Temp Rapidly Dropped 20 F.Caused by Increased Efficiency of HX Upon Cleaning ML20028D5591983-01-10010 January 1983 LER 83-001/01P-0:on 830107,valves V-16-19-20 & 22B Failed to Close When Operator Attempted to Secure Nitrogen Flow.Caused by Accumulation of Iron Particles on Magnet Used to Provide Valve Position Indication.Valves Cleaned ML20028D5421983-01-10010 January 1983 LER 83-002/01P-0:on 830108,indication of Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line Found.Caused by Pipe Crack.Cause of Pipe Crack Unknown.Elbow Replaced w/304L Type Stainless Steel Matl ML20028A3601982-11-0303 November 1982 LER 82-022/03L-0:on 821005,diesel Generator a Failed to Reach Required Voltage & Frequency within Tech Spec Time Limit.Caused by Fuel Oil Return Line Check Valve Failure. Valve Replaced ML20052C0051982-04-23023 April 1982 LER 82-007/01T-1:on 820309,standby Liquid Control Storage Tank Level & Sodium Pentaborate Concentration Calculations Did Not Correctly Account for Specific Gravity of Sodium Pentaborate.Caused by Procedure Equation Errors ML20052C0451982-04-23023 April 1982 LER 82-003/01T-1:on 820220,boron Concentration Fell Below Tech Spec Requirement.Caused by Apparent Boron Loss Coupled W/Small Sodium Pentaborate Concentration Margin ML20050B3941982-03-25025 March 1982 LER 82-005/03L-0:on 820223,uninterruptible Ac Electric Power Sys Tripped & Lost Power to Motor Control Ctr 89B, Rendering Sys Inoperable.Caused by Shorted Out Transient Suppression Capacitor Due to Aging.Capacitor Replaced ML20050A9291982-03-23023 March 1982 LER 82-007/01T-0:on 820309,calculations of Standby Liquid Control Storage Tank Concentration Versus Tank Level Correlation Did Not Account for Specific Gravity of Sodium Penaborate.Procedures Corrected ML20050A3781982-03-21021 March 1982 LER 82-006/03L-0:on 820219,during Normal Surveillance on Differential Pressure Switches DPIS 2-120 A,B,C & D,Switches A,B & C Found to Be Out of Tech Spec Limits.Caused by Setpoint Drift.Switches Reset to within Required Tolerance ML20042B2361982-03-16016 March 1982 LER 82-004/03L-0:on 820216,discovered That Continuous Environ Air Sample Not Obtainable at Station AT1.4 Per Tech Spec.Caused by Solder Lug of Std 125V-8A Power Toggle Switch Parting at 90 Degree Bend.Faulty Switch Replaced ML20042A4111982-03-0909 March 1982 LER 82-007/01P-0:on 820309,error Revealed in Calculations of Sodium Pentaborate Concentration in SLC Tank.Caused by Specific Gravity of Solution Not Being Factored Into Weight Percent Calculation in Accordance W/Tech Specs ML20042A6031982-03-0606 March 1982 LER 82-003/01T-0:on 820208,sample of Standby Liquid Control Boron Concentration Below Tech Spec Limits.Investigation in Progress.Administrated Limit & Sampling Frequency Increased ML20041F9281982-03-0303 March 1982 LER 82-002/03L-0:on 820206,ac Ground & Blown Fuse Alarms Activated,Rendering Trouble Alarm UPS-B Inoperable.Caused by Blown Fuse M Transient Suppression Circuit Due to Shorted Out Capacitor Off Board 2A 17 ML20041D7771982-02-25025 February 1982 LER 82-001/03L-0:on 820128,IRM Channel B Declared Inoperable.Caused by Failed Voltage Pre AMP (GE 112C-2218G001).Half Scram Manually Initiated.Component Will Be Repaired Prior to Entering IRM Range ML20041D4281982-02-22022 February 1982 LER 82-003/01P-0:on 820220,after Addition of Water to SLC Tank,Solution Sample Found Boron Concentration Below Required Amounts.Cause Unknown.Administrative Limit for Concentration Will Be Increased & Addl Sampling Conducted ML20040E2581982-01-26026 January 1982 LER 81-037/03L-0:on 811227,while Attempting to Start RHRSW Pump P-8-1A,breaker Tripped Contrary to Tech Specs.Caused by Worn Bushings on Operating Mechanism.Circuit Breaker Replaced.Breaker Mfg by Ge,Model Am 4.16 250-8HB ML20040C6971982-01-16016 January 1982 LER 81-036/03L-0:on 811217,containment Isolation Valve CU-15 Failed to Seat Satisfactorily Per Tech Spec 4.7.D.1 During Quarterly Surveillance Testing.Caused by Failure of Closing Torque Switch.Torque Switch Will Be Replaced Next Shutdown ML20040B1941981-12-30030 December 1981 Updated 81-028/03X-1:on 811017,field Breaker Failed to Open, Effectively Disabling Rrmg Set Recirculation Pump Trip Instrumentation.Caused by Binding of Operating Mechanism.New Breaker Installed ML20039F0101981-12-30030 December 1981 LER 81-035/03L-0:on 811204,during Core Spray Valve Test, Breaker for V14-11A Tripped & Reactor Shutdown Commenced. Caused by Breaker Not Latching When Closed,Allowing Breaker to Trip Below Setpoint.Breaker Replaced ML20039C2991981-12-18018 December 1981 LER 81-032/03L-0:on 811120,valves RWCU 68 & 15 Found to Have Seat Leakages Exceeding Tech Spec Range.Cause Not Stated. Disc Replaced & Valves Satisfactorily Retested ML20039C3071981-12-18018 December 1981 LER 81-034/03L-0:on 811121,operating Cycle Test of Standby Gas Treatment HEPA Filters Found Not to Have Been Done Since Sept 1979.Caused by Failure to Include Test on Dept Surveillance List.Test Completed & Schedule Revised ML20039C1121981-12-17017 December 1981 Updated LER 81-011/03X-1:on 810507,leak Discovered in Socket Weld Reducing Fitting.Caused by Intergranular Stress Corrosion Cracking.All Similar Fittings Replaced W/Differently Designed Fitting Less Susceptible to Failure ML20039C3821981-12-17017 December 1981 Updated LER 81-016/03X-1:on 810622,small Leak Found in Socket Weld Reducing Fitting in Vent Line of Regenerative Heat Exchanger E-15-1A.Caused by Intergranular Stress Corrosion Cracking Due to Wetting of Asbestos Insulation ML20039B1281981-12-0909 December 1981 LER 81-033/01T-0:on 811125,reactor Bldg Roof Hatch Opened by Work Crew W/O Notice to Supervisor Until Fire Permit for Welding Requested.Caused by Personnel Error.Personnel Reinstructed Re Procedural Requirement 1994-04-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8831999-10-21021 October 1999 Safety Evaluation Supporting Proposed Alternatives to Code Requirements Described in RR-V17 & RR-V18 ML20217G2041999-10-13013 October 1999 Safety Evaluation Supporting Amend 179 to License DPR-28 BVY-99-127, Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With ML20212C2551999-09-17017 September 1999 Safety Evaluation Supporting Amend 175 to License DPR-28 BVY-99-112, Monthly Operating Rept for Aug 1999 for Vermont Yankee.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Vermont Yankee.With BVY-99-109, Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 9908311999-08-19019 August 1999 Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 990831 BVY-99-102, Monthly Operating Rept for July 1999 for Vermont Yankee. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Vermont Yankee. with ML20209J0081999-07-14014 July 1999 Special Rept:On 990615,diesel Driven Fire Pump Failed to Achieve Rated Flow of 2500 Gallons Per Minute.Pump Was Inoperable for Greater than 7 Days.Corrective Maint Was Performed to Reset Pump Lift Setting BVY-99-090, Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With ML20196G5071999-06-23023 June 1999 Vynp Assessment of On-Site Disposal of Contaminated Soil by Land Spreading BVY-99-077, Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With BVY-99-068, Monthly Operating Rept for Apr 1999 for Vynp.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Vynp.With ML20206E8741999-04-29029 April 1999 SER Determined That Flaw Evaluation Meets Rules of ASME Code & Assumed Crack Growth Rate Adequate for Application ML20206D9301999-04-27027 April 1999 1999 Emergency Preparedness Exercise 990427 Exercise Manual (Plume Portion) ML20205S4211999-04-16016 April 1999 Non-proprietary Version of Revised Page 4-3 of HI-981932 Technical Rept for Vermont Yankee Spent Fuel Pool Storage Expansion ML20205K7581999-04-0707 April 1999 Safety Evaluation Supporting Alternative Proposal for Reexamination of Circumferential Welds with Detected Flaw Indications in Plant RPV BVY-99-046, Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With ML20205F6631999-03-0404 March 1999 Jet Pump Riser Weld Leakage Evaluation BVY-99-035, Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With ML20205P8241999-02-28028 February 1999 Rev 2 to Vermont Yankee Cycle 20 Colr ML20203H9881999-02-18018 February 1999 SER Accepting Alternative to 10CFR50.55a(g)(6)(ii)(A) Augmented Reactor Vessel Exam at Vermont Yankee Nuclear Power Station.Technical Ltr Rept Encl ML20203A6951999-02-0404 February 1999 Revised Rev 2,App B to Vermont Yankee Operational QA Manual (Voqam) ML20199K7151999-01-21021 January 1999 Corrected Safety Evaluation Supporting Amend 163 Issued to FOL DPR-28.Pages 2 & 3 Required Correction & Clarification ML20199K6991999-01-20020 January 1999 Safety Evaluation Concluding That Request to Use YAEC-1339, Yankee Atomic Electric Co Application of FIBWR2 Core Hydraulics Code to BWR Reload Analysis, at Vermont Yankee Acceptable ML20199L5951999-01-14014 January 1999 Safety Evaluation Accepting Licensee Proposed Alternative to Code Requirement,Described in Rev 2 to Pump Relief Request RR-P10 Pursuant to 10CFR50.55a(a)(3)(i) BVY-99-071, Corp 1998 Annual Rept. with1998-12-31031 December 1998 Corp 1998 Annual Rept. with BVY-99-001, Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station ML20198H5481998-12-23023 December 1998 Rev 2 to Vermont Operational QA Manual,Voqam ML20196H8641998-12-0101 December 1998 Cycle 19 Operating Rept BVY-98-163, Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With ML20195C4161998-11-0909 November 1998 SER Accepting Request That NRC Approve ASME Code Case N-560, Alternative Exam Requirement for Class 1,Category B-J Piping Welds BVY-98-154, Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With ML20155B6471998-10-26026 October 1998 Safety Evaluation Accepting Jet Pump Riser Insp Results & Flaw Evaluation,Conducted During 1998 Refueling Outage ML20154N0891998-10-16016 October 1998 Rev 1 to Vermont Operational QA Program Manual (Voqam) ML20154B6951998-10-0101 October 1998 SER Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Vermont Yankee Nuclear Power Station BVY-98-149, Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With ML20239A1361998-09-0202 September 1998 SER Re License Request for NRC Review & Concurrence W/Changes to NRC-approved Fire Protection Program BVY-98-135, Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With ML20151U0361998-08-28028 August 1998 Non-proprietary Rev 1 to Holtec Rept HI-981932, Vermont Yankee Nuclear Power Station Spent Storage Expansion Project ML20237E9221998-08-20020 August 1998 Vynp 1998 Form NIS-1 Owners Summary Rept for ISI, 961103-980603 BVY-98-122, Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station ML20205F6491998-07-31031 July 1998 Rev 1 to GE-NE-B13-01935-02, Jet Pump Assembly Welds Flaw Evaluation Handbook for Vermont Yankee ML20236G0011998-06-30030 June 1998 Individual Plant Exam External Events BVY-98-098, Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station ML20248C5081998-05-31031 May 1998 Rev 2 to 24A5416, Supplemental Reload Licensing Rept for Vermont Yankee Nuclear Power Station Reload 19 Cycle 20 ML20248C4951998-05-31031 May 1998 Rev 1 to Vermont Yankee Nuclear Power Station Cycle 20 Colr BVY-98-081, Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station ML20247J8341998-05-31031 May 1998 Peak Suppression Pool Temp Analyses for Large Break LOCA Scenarios, for May 1998 ML20247G4001998-05-12012 May 1998 Interview Rept of Ej Massey ML20247E6351998-04-30030 April 1998 Rev 1 to GE-NE-B13-01935-LTR, Jet Pump Riser Welds Allowable Flaw Sizes Ltr Rept for Vermont Yankee 1999-09-30
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VERMONT YANKIcic NUCLEAR POWER CORPORATION P. O. BOX 157 GOVEltNOR !!UNT ROAD VERNON, VERMONT 05354 June 15, 1990 VYV# 90-208 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
REFERENCE:
Operating License DPR-28 Docket No. 50-271 Reportable Occurrence No. LER 90 07
Dear Sirs:
9 As defined by 10CFR50.73, we are reporting the attached Reportable Occurrence as LER 90-07.
Very truly yours, VERMONT YANKEE NUCLEAR POWER CORPORATION Donald A. Reid Plant Manager cc: Regional Administrator USNRC Region I 475 Allendale Road King of Prussia, PA 19406 9006200442 900615 PDR S
ADOCK 05000271 PDC
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NRC F rm* 366 U.S. NUCLEAR REGULATORY COMMISSION APkROVED OMS NO.3150-0104 (6-89)
- EXPIRES 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTU REGARDING t LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. DC 20603.
FACILITY NAME (5) DOCKET NO. (8) PAGE (*)
VERMONT YANKEE NUCLEAR POWER STATION Ol5l0l010l2l7l1 0 l 110F l 0 l 4 TITLE (*) Toxic Gas Monitor Ammonia Gas Trip Point Error Due to Wrong Concentration in Span Gas Bottle EVENT DATE (5) LER NUMBER (*) REPORT DATE (') OTHER FACILITIES INVOLVED (*)_
MONTH DAY YEAR YEAR SEQ. # REV# MONTH DAY YEAR FACILITY NAMES DOCKET NO.(S) 0 5 0 0 0 0l5 1l5 9l0 9l0 -
010l7 -
0l0 0l6 1l5 9l0 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PURGUANT TO REQ'MTS OF 10CFR 4: / ONL OR MORE ()
MODE (*) N 20.402(b) __ 20.405(c) __ 50.73(a)(2)(iv) __ 73.71(b)
POWER __ 20.405(a)(1)(I) __ 50.36(c)(1) __ 50.73(a)(2)(v) __ 73.71(c) >
LEVEL ($*) Il d 0 20.405(a)(1)(II) __ 50.36(c)(2) __ 50.73(a)(2)(vii) __
OTHER:
............... _ 20.405(a)(1)(III) _x 50.73(a)(2)(I) __ 50.73(a)(2)(viii)(A)
............... ._ 20.405(a)(1)(iv) __ 50.73(a)(2)(II) __ 50.73(a)(2)(viii)(B)
,.,............ 20.405(a)(1)(v) 50.73(a)(2)(III) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (se)
NAME TELEPHONE NO.
AREA CODE JAMES P. PELLETIER, PLANT MANAGER dd2 2ld7l-l7l7l1l1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT ('*)
CAUSE SYST COMPNT MFR REPORTABLE ..... CAUSE SYGT COMPNT MFR REPORTABLE ......
TO NPRDS ..... TO NPRDS ......
N/A l lll lll l N/A l lll lll ll N/A l lll lll l . N/A l lll lll . l SUPPLEMENTAL REPORT EXPECTED ($*) EXPECTED M0 DA YR SUBMISSION
~~l YES (If ves, complete EXPECTED SUDMISSION DATE) x l NO DATE ($5) l l l ABSTRACT (Limit to 1400 spaces, i.e., approx. fifteen single-space typewritten lines) ($*)
On 4/19/90, with the plant at 100% steady state power, Instrument and Control spe-cialists were performing an ammonia span gas bottle changeout for the toxic gas monitor (EIIS=45) (TGM). Once the new bottle was in place, the concentration of the gas was me: Cured. The measured concentration of the new span gas bottle was less than its certified c ncentration and outside of the allowable tolerance. The old bottle was placed back in c rvice and the new bottle sent out for analysis.
The results of the analysis on the new bottle confirmed that the concentration was within the tolerance allowed and was subsequently returned for use. Based upon this, on 5/15/90, it was determined that the concentration of the old bottle was not within speci-fication which caused the ammonia trip setting to be non-conservative from the period 1-29-90 to 5-14-90.
The new span gas bottle was immediately installed and the instruments recalibrated.
The root cause of the event is the incorrect certification by the vendor of the con-centration of ammonia in the span aas previous 1v supplied.
NRC Form 366 (6-09)
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. t NRC F;rm,366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO.3150-0104 l (6-89) EXPIRES 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY i
WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTS REGARDING LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS TEXT CONTINUATION MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.
UTILITY NAME (') DOCKET NO. (8) LER NUMBER (*) PAGE (*)
YEAR SEO. # REV#
t VERMONT YANKEE _ NUCLEAR POWER STATION d d d d d 2l 7l 1 9l0 -
0l0l7 -
0l0 d2 0F d4 TEXT (If more space is required, use additional NRC Form 366A) (5')
DESCRIPTION OF EVENT On 4/19/90, Instrument and Control specialists were performing a changeout of the ammonia span gas bottle for the toxic gas monitor system. Prior to the changeout, the ana-lyzer was calibrated to the standard that was currently in use, which was certified to 266 ppm ammonia.
A new spar gas bottle was installed which was certified to contain 277 ppm ammonia.
Per procedure, the new span gas is compared to the old standard before the analyzers are r calibrated. From that comparison, it was determined that the new span gas concentration was reading 211 ppm 24% lower than it was certified for.
The new ammonia span gas bottle was returned to the vendor for retesting. On 5/14/90, the. retested bottle was released f rom Quality Control with a re-certification of 281 ppm ammonia. This bottle was again installed in the toxic gas monitor and when compared to the old span gas bottle it indicated 213 ppm which is also 24% lower than it was cer-tified for.
Based on this, on 5/15/90 it was determined that the old span gas bottle was incorrectly certified. This resulted in a non-conservative indication and trip setting, of the toxic gas monitor.
A similar problem with span gas concentration had previously been identified during bottle changeout in 1989. At that time one of the corrective actions was to revise the pro-
-c: dure to require a calibration to the old standard before the change and a comparison of th) analyzer indication af ter change of the span gas. This revision was in review at the time the span gas was changed in January but had not yet been approved and no comparison was performed at that time.
CAUSE OF EVENT The root cause of the event is the incorrect certification by the vendor of the con-c;ntration of ammonia in the span gas previously supplied.
A major contributing f actor in the event is the reactivity of the ammonia gas which C;kes analysis of the gas at the low concentrations required extremely difficult.
Another contributor was that the procedure revision initiated due to prior concerns with the concentration of new span gas bottles was not in place at the time of the span gas rcplacement in January. At that time there were no procedural requirements to compare span NRC Form 366A (6-89) -
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NRC FCr3 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO.3150-0104 (6-89) ' EXPIRES 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY !
f WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTS REGARDING LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS TEXT CONTINUATION MANAGEMENT BRANCH (P-530), U.S. NUCLEAR l REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.
UTILITY NAME (') DOCKET NO. (*) LER_ NUMBER (*) PAGE (a)
YEAR SEO. # REV#
VERMONT YANKEE NUCLEAR POWER STATION d d d d d 2l 7l 1 910 -
0l0l7 -
0l0 d3 0F d4 TEXT (If more space is required, use additional NRC Form 366A) ()
gases during bottle replacement and subsequently the difference in concentration was not identified when the span gas was replaced. This revision since has been approved and was re:ponsible for the identification of this event.
ANALYSIS OF EVENT The discrepancy in the gas concentration of the original bottle caused the alarm set-p int to be greater than that allowed by tech specs. The tech spec. requirement is for the toxic gas monitor to alarm at a concentration of 75 ppm of ammonia gas. With the lower thin certified gas concentration, the actual trip point was 80.87 ppm, While the setpoint was above the tech, spec, requirement, the toxicity level as rcferenced by Reg. Guide 1.78 is 100 ppm for ammonia. Therefore, the toxic gas monitor system would have tripped and performed its function well before any toxic ammonia gas levels were reached.
Based on the above, there were no potential health or safety implications to plant-personnel or the public.
CORRECTIVE ACTIONS The immediate corrective actions were:
- 1. The span gas bottle was changed with the new one that had been tested, and verified by a second test to be correct.
- 2. The instruments were recalibrated to agree with the concentration in the new span gas.
Long term corrective actions:
- 1. Return the bottle that was removed to the vendor for further testing to determine the actual concentration.
- 2. Complete a vendor evaluation, by our Quality Assurance Department, to determine the continuing acceptability of their product.
- 3. Pursue an evaluation to justify the elimination of the toxic gas monitor system.
This subject has already been discussed with NRR. -
NRC Form 366A (6-89)
r;
. , *o NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO.3150-0104 (6-89)' EXPIRES 4/30/92
- ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTS REGARDING LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS TEXT CONTINUATION MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION P90 JECT (3160-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.
UTILITY NAME (') DOCKET NO. g*) LER NUMBER (*) PAGE (*)
YEAR SEQ. # REV#
VERMONT YANKEE NUCLEAR POWLR STATION d d d d d 2l 7] I 9l0 -
0l0l7 -
0l0 d4 0F d4 TEXT (If more space is required, use additional NRC Form 366A)-(i')
Since the corrective actions implemented due to previously identified discrepancies in gas concentration were inst!wmental in identifying this event, they are felt to be suf-ficient to prevent recurrence and no additional corrective actions besides those above are necessary.
ADDITIONAL INFORMATION A similar incident was reported in 1987 as LER BT-03.
i NRC Form 366A (6-89)
I