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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6131994-04-29029 April 1994 LER 94-005-00:on 940330,fire Suppression Water Supply Sys Declared Inoperable.Caused by Inadequate Design of cross- Connection Portion of Svc Water Sys & Inadequate Procedures. Valve SW-8 Tagged Shut to Prevent re-opening.W/940429 Ltr ML20046B4901993-07-30030 July 1993 LER 93-008-00:on 930701,discovered That During Previous Surveillance Testing on 910515,pump Differential Pressure Entered IST Required Action Range Due to Personnel Error. Plant Procedure AP 0164 Will Be revised.W/930730 Ltr ML20046A1141993-07-16016 July 1993 LER 93-007-00:on 930609,determined That Daily Instrument Checks Required by TS Were Not Included in Operator Rounds. Caused by Mgt & Human Factors Weakness.Ts Proposed Change & Amend Issue Process Will Be performed.W/930716 Ltr ML20045G5991993-07-0707 July 1993 LER 93-001-02:on 921217,indeterminate Fire Penetration Seal Configuration Identified When Insulation Removed from Piping.On 930324,addl Indeterminate Seals Identified.Fire Watches Established & New Seals installed.W/930707 Ltr ML20045D9191993-06-24024 June 1993 LER 93-006-00:on 930527,both Core Spray Sys Trains a & B Declared Inoperable When Calibr Procedure Error Resulted in Setpoint Set Nonconservatively.Caused by Failure to Apply Head Correction Factor.Procedure corrected.W/930624 Ltr ML18100B2771992-05-20020 May 1992 LER 92-016-00:on 920422,discovered That TS Quarterly Flow Test Not Performed During safety-related HVAC Sys Surveillance of Chilled Water Pump.Caused by Personnel Error.Procedure Re Ref Valves revised.W/920520 Ltr ML18100B2761992-05-19019 May 1992 LER 92-015-00:on 920424,RCIC Sys Declared Inoperable When Sys Flow Controller Meter Indicated Approx 30 Gpm Flow W/ RCIC Not Operating.Caused by Setpoint Drift.Work Orders Initiated to Correct Meter indication.W/920519 Ltr ML20028H7501991-01-23023 January 1991 LER 91-001-00:on 910104,radiation Protection (RP) Technician Entered Posted High Radiation Area W/O Dose Rate Monitoring Device Due to Personnel Error.Technician Relieved of Further RP duties.W/910123 Ltr ML20043G5691990-06-15015 June 1990 LER 90-007-00:on 900515,determined That Concentration of Old Bottle of Ammonia Span Gas Not within Spec Causing Ammonia Trip Setting to Be Nonconservative.Caused by Incorrect Certification by Vendor.Bottle replaced.W/900615 Ltr ML20042F3611990-05-0202 May 1990 LER 90-006-00:on 900403,Tech Spec Surveillance Requirement Missed Due to Failure to Include Basis on Tracking List. Caused by Personnel Error.Changes to Master Surveillance List & Any Affected Procedures Will Be made.W/900502 Ltr ML20042F2231990-05-0202 May 1990 LER 90-006-01:on 900403,discovered That Flow Transmitters That Supply Advanced off-gas Sys Flow Indication Had Not Been Calibr.Caused by Failure to Include Procedure on Surveillance List.Personnel retrained.W/900503 Ltr ML20042E1691990-04-12012 April 1990 LER 90-003-00:on 900319,inadvertent Primary Containment Isolation Sys Actuation Occurred.Caused by Lack of Coordination Between Monitor Downscale Setpoint & Monitor Reading.Proper Coordination established.W/900412 Ltr ML20012E9301990-03-22022 March 1990 LER 90-002-00:on 900302,identified That Key Sprinkler Isolation Valve Not Adequately Surveilled.Caused by Personnel Error.Valve Verified as Sealed & Surveillances for Fire Protection Valves revised.W/900322 Ltr ML20012B6061990-03-0808 March 1990 LER-90-001-00:on 900209,primary Containment Isolation Sys Group III Isolation & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Personnel Error.Isolation Reset.Personnel Counseled on Proper procedures.W/900308 Ltr ML20012C4291990-03-0707 March 1990 LER 87-015-01:on 871003,reactor Scram Occurred as Result of Turbine Control Valves Rapid Opening & Subsequent Fast Closure.Caused by Flow Imbalance in Turbine Control Oil Sys. Turbine Startup Procedure revised.W/900207 Ltr ML20006B4701990-01-22022 January 1990 LER 89-026-00:on 891223 & 900105,primary Containment Isolation Sys Group III Isolation & Standby Gas Treatment Sys Initiations Occurred.Caused by Failure of Sensor Converter.Isolation Reset & Monitor bypassed.W/900122 Ltr ML20005E1511989-12-26026 December 1989 LER 89-025-00:on 891128,primary Containment Isolation Sys Group III & Standby Gas Treatment Sys Initiation Occurred. Caused by Failure of Reactor Bldg Ventilation Radiation Monitor/Sensor Converter.Converter replaced.W/891226 Ltr ML20011D4901989-12-20020 December 1989 LER 89-024-01:on 890913,while Reviewing RHR Sys Surveillance Procedure,Determined That Leak Testing of RHR Valve V10-18 Not Incorporated & Implemented in Rev 9.Caused by Incomplete Review.Event Reviewed w/personnel.W/891220 Ltr ML19327A8881989-10-13013 October 1989 LER 89-024-00:on 890913,noted That Requirement from Previous Inservice Test Program Rev 9 Re Leak Testing of Valve V10-18 Not Incorporated & Implemented.Caused by Incomplete Review & Omission.Procedure Changes implemented.W/891013 Ltr ML19325C7821989-10-11011 October 1989 LER 89-023-00:on 890911,discovered That Remote Indication to Valve RHR-20 Not Available from 890320-0912,when Supply Breaker Replaced.Caused by Lack of Personnel Recognition. Breaker Replaced & Indication restored.W/891011 Ltr ML20024A8681983-06-22022 June 1983 LER 83-015/01T-0:on 830608,error Discovered in Spacing Table Developed for Support of Copper Piping in Svc Water Sys.Addl Supports Required to Fully Comply W/Ansi B31.1.W/830622 Ltr ML20024A8311983-06-0909 June 1983 LER 83-015/01P-0:on 830608,Yankee Atomic Electric Co Informed Util That Addl Piping Supports Required to Support Piping in Svc Water Sys & Torus Attached Piping.Cause & Corrective Actions to Be Provided in Next rept.W/830609 Ltr ML20024A3441983-06-0707 June 1983 LER 83-014/03L-0:on 830510,discovered Surveillance Frequency for Svc Water Processs Monitor Exceeded Tech Specs.Caused by Schedule Error.Analysis Immediately Performed.Applicable Personnel reinstructed.W/830607 Ltr ML20024A4151983-05-13013 May 1983 LER 83-013/03L-0:on 830413,while Reactor Shutdown,Weekly Environ Air Sample for 830405-12 at Station AT1.3 Not Obtained.Caused by Technician Failure to Test for Sys Vacuum.Technician Reinstructed in procedure.W/830513 Ltr ML20023B4741983-04-25025 April 1983 LER 83-011/03L-0:on 830325,during Visual Insp,Shock Suppressor MS-6 on Main Steam a Piping Found W/No Visible Fluid in Sight Glass & Failed to Lock Up.Caused by Damaged Lenztee.Snubber Cleaned & Rebuilt ML20028F3741983-01-21021 January 1983 LER 83-002/02T-0:on 830108,discovered Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line.Cause Unknown.Leaking Elbow Replaced w/304L Type Stainless Steel Matl Per NUREG-0313 Requirements ML20028F3921983-01-19019 January 1983 LER 82-026/03L-0:on 821220,while Shifting from Reactor Bldg Closed Cooling Water HX B to A,Closed Cooling Water Temp Rapidly Dropped 20 F.Caused by Increased Efficiency of HX Upon Cleaning ML20028D5591983-01-10010 January 1983 LER 83-001/01P-0:on 830107,valves V-16-19-20 & 22B Failed to Close When Operator Attempted to Secure Nitrogen Flow.Caused by Accumulation of Iron Particles on Magnet Used to Provide Valve Position Indication.Valves Cleaned ML20028D5421983-01-10010 January 1983 LER 83-002/01P-0:on 830108,indication of Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line Found.Caused by Pipe Crack.Cause of Pipe Crack Unknown.Elbow Replaced w/304L Type Stainless Steel Matl ML20028A3601982-11-0303 November 1982 LER 82-022/03L-0:on 821005,diesel Generator a Failed to Reach Required Voltage & Frequency within Tech Spec Time Limit.Caused by Fuel Oil Return Line Check Valve Failure. Valve Replaced ML20052C0051982-04-23023 April 1982 LER 82-007/01T-1:on 820309,standby Liquid Control Storage Tank Level & Sodium Pentaborate Concentration Calculations Did Not Correctly Account for Specific Gravity of Sodium Pentaborate.Caused by Procedure Equation Errors ML20052C0451982-04-23023 April 1982 LER 82-003/01T-1:on 820220,boron Concentration Fell Below Tech Spec Requirement.Caused by Apparent Boron Loss Coupled W/Small Sodium Pentaborate Concentration Margin ML20050B3941982-03-25025 March 1982 LER 82-005/03L-0:on 820223,uninterruptible Ac Electric Power Sys Tripped & Lost Power to Motor Control Ctr 89B, Rendering Sys Inoperable.Caused by Shorted Out Transient Suppression Capacitor Due to Aging.Capacitor Replaced ML20050A9291982-03-23023 March 1982 LER 82-007/01T-0:on 820309,calculations of Standby Liquid Control Storage Tank Concentration Versus Tank Level Correlation Did Not Account for Specific Gravity of Sodium Penaborate.Procedures Corrected ML20050A3781982-03-21021 March 1982 LER 82-006/03L-0:on 820219,during Normal Surveillance on Differential Pressure Switches DPIS 2-120 A,B,C & D,Switches A,B & C Found to Be Out of Tech Spec Limits.Caused by Setpoint Drift.Switches Reset to within Required Tolerance ML20042B2361982-03-16016 March 1982 LER 82-004/03L-0:on 820216,discovered That Continuous Environ Air Sample Not Obtainable at Station AT1.4 Per Tech Spec.Caused by Solder Lug of Std 125V-8A Power Toggle Switch Parting at 90 Degree Bend.Faulty Switch Replaced ML20042A4111982-03-0909 March 1982 LER 82-007/01P-0:on 820309,error Revealed in Calculations of Sodium Pentaborate Concentration in SLC Tank.Caused by Specific Gravity of Solution Not Being Factored Into Weight Percent Calculation in Accordance W/Tech Specs ML20042A6031982-03-0606 March 1982 LER 82-003/01T-0:on 820208,sample of Standby Liquid Control Boron Concentration Below Tech Spec Limits.Investigation in Progress.Administrated Limit & Sampling Frequency Increased ML20041F9281982-03-0303 March 1982 LER 82-002/03L-0:on 820206,ac Ground & Blown Fuse Alarms Activated,Rendering Trouble Alarm UPS-B Inoperable.Caused by Blown Fuse M Transient Suppression Circuit Due to Shorted Out Capacitor Off Board 2A 17 ML20041D7771982-02-25025 February 1982 LER 82-001/03L-0:on 820128,IRM Channel B Declared Inoperable.Caused by Failed Voltage Pre AMP (GE 112C-2218G001).Half Scram Manually Initiated.Component Will Be Repaired Prior to Entering IRM Range ML20041D4281982-02-22022 February 1982 LER 82-003/01P-0:on 820220,after Addition of Water to SLC Tank,Solution Sample Found Boron Concentration Below Required Amounts.Cause Unknown.Administrative Limit for Concentration Will Be Increased & Addl Sampling Conducted ML20040E2581982-01-26026 January 1982 LER 81-037/03L-0:on 811227,while Attempting to Start RHRSW Pump P-8-1A,breaker Tripped Contrary to Tech Specs.Caused by Worn Bushings on Operating Mechanism.Circuit Breaker Replaced.Breaker Mfg by Ge,Model Am 4.16 250-8HB ML20040C6971982-01-16016 January 1982 LER 81-036/03L-0:on 811217,containment Isolation Valve CU-15 Failed to Seat Satisfactorily Per Tech Spec 4.7.D.1 During Quarterly Surveillance Testing.Caused by Failure of Closing Torque Switch.Torque Switch Will Be Replaced Next Shutdown ML20040B1941981-12-30030 December 1981 Updated 81-028/03X-1:on 811017,field Breaker Failed to Open, Effectively Disabling Rrmg Set Recirculation Pump Trip Instrumentation.Caused by Binding of Operating Mechanism.New Breaker Installed ML20039F0101981-12-30030 December 1981 LER 81-035/03L-0:on 811204,during Core Spray Valve Test, Breaker for V14-11A Tripped & Reactor Shutdown Commenced. Caused by Breaker Not Latching When Closed,Allowing Breaker to Trip Below Setpoint.Breaker Replaced ML20039C2991981-12-18018 December 1981 LER 81-032/03L-0:on 811120,valves RWCU 68 & 15 Found to Have Seat Leakages Exceeding Tech Spec Range.Cause Not Stated. Disc Replaced & Valves Satisfactorily Retested ML20039C3071981-12-18018 December 1981 LER 81-034/03L-0:on 811121,operating Cycle Test of Standby Gas Treatment HEPA Filters Found Not to Have Been Done Since Sept 1979.Caused by Failure to Include Test on Dept Surveillance List.Test Completed & Schedule Revised ML20039C1121981-12-17017 December 1981 Updated LER 81-011/03X-1:on 810507,leak Discovered in Socket Weld Reducing Fitting.Caused by Intergranular Stress Corrosion Cracking.All Similar Fittings Replaced W/Differently Designed Fitting Less Susceptible to Failure ML20039C3821981-12-17017 December 1981 Updated LER 81-016/03X-1:on 810622,small Leak Found in Socket Weld Reducing Fitting in Vent Line of Regenerative Heat Exchanger E-15-1A.Caused by Intergranular Stress Corrosion Cracking Due to Wetting of Asbestos Insulation ML20039B1281981-12-0909 December 1981 LER 81-033/01T-0:on 811125,reactor Bldg Roof Hatch Opened by Work Crew W/O Notice to Supervisor Until Fire Permit for Welding Requested.Caused by Personnel Error.Personnel Reinstructed Re Procedural Requirement 1994-04-29
[Table view] Category:RO)
MONTHYEARML20029D6131994-04-29029 April 1994 LER 94-005-00:on 940330,fire Suppression Water Supply Sys Declared Inoperable.Caused by Inadequate Design of cross- Connection Portion of Svc Water Sys & Inadequate Procedures. Valve SW-8 Tagged Shut to Prevent re-opening.W/940429 Ltr ML20046B4901993-07-30030 July 1993 LER 93-008-00:on 930701,discovered That During Previous Surveillance Testing on 910515,pump Differential Pressure Entered IST Required Action Range Due to Personnel Error. Plant Procedure AP 0164 Will Be revised.W/930730 Ltr ML20046A1141993-07-16016 July 1993 LER 93-007-00:on 930609,determined That Daily Instrument Checks Required by TS Were Not Included in Operator Rounds. Caused by Mgt & Human Factors Weakness.Ts Proposed Change & Amend Issue Process Will Be performed.W/930716 Ltr ML20045G5991993-07-0707 July 1993 LER 93-001-02:on 921217,indeterminate Fire Penetration Seal Configuration Identified When Insulation Removed from Piping.On 930324,addl Indeterminate Seals Identified.Fire Watches Established & New Seals installed.W/930707 Ltr ML20045D9191993-06-24024 June 1993 LER 93-006-00:on 930527,both Core Spray Sys Trains a & B Declared Inoperable When Calibr Procedure Error Resulted in Setpoint Set Nonconservatively.Caused by Failure to Apply Head Correction Factor.Procedure corrected.W/930624 Ltr ML18100B2771992-05-20020 May 1992 LER 92-016-00:on 920422,discovered That TS Quarterly Flow Test Not Performed During safety-related HVAC Sys Surveillance of Chilled Water Pump.Caused by Personnel Error.Procedure Re Ref Valves revised.W/920520 Ltr ML18100B2761992-05-19019 May 1992 LER 92-015-00:on 920424,RCIC Sys Declared Inoperable When Sys Flow Controller Meter Indicated Approx 30 Gpm Flow W/ RCIC Not Operating.Caused by Setpoint Drift.Work Orders Initiated to Correct Meter indication.W/920519 Ltr ML20028H7501991-01-23023 January 1991 LER 91-001-00:on 910104,radiation Protection (RP) Technician Entered Posted High Radiation Area W/O Dose Rate Monitoring Device Due to Personnel Error.Technician Relieved of Further RP duties.W/910123 Ltr ML20043G5691990-06-15015 June 1990 LER 90-007-00:on 900515,determined That Concentration of Old Bottle of Ammonia Span Gas Not within Spec Causing Ammonia Trip Setting to Be Nonconservative.Caused by Incorrect Certification by Vendor.Bottle replaced.W/900615 Ltr ML20042F3611990-05-0202 May 1990 LER 90-006-00:on 900403,Tech Spec Surveillance Requirement Missed Due to Failure to Include Basis on Tracking List. Caused by Personnel Error.Changes to Master Surveillance List & Any Affected Procedures Will Be made.W/900502 Ltr ML20042F2231990-05-0202 May 1990 LER 90-006-01:on 900403,discovered That Flow Transmitters That Supply Advanced off-gas Sys Flow Indication Had Not Been Calibr.Caused by Failure to Include Procedure on Surveillance List.Personnel retrained.W/900503 Ltr ML20042E1691990-04-12012 April 1990 LER 90-003-00:on 900319,inadvertent Primary Containment Isolation Sys Actuation Occurred.Caused by Lack of Coordination Between Monitor Downscale Setpoint & Monitor Reading.Proper Coordination established.W/900412 Ltr ML20012E9301990-03-22022 March 1990 LER 90-002-00:on 900302,identified That Key Sprinkler Isolation Valve Not Adequately Surveilled.Caused by Personnel Error.Valve Verified as Sealed & Surveillances for Fire Protection Valves revised.W/900322 Ltr ML20012B6061990-03-0808 March 1990 LER-90-001-00:on 900209,primary Containment Isolation Sys Group III Isolation & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Personnel Error.Isolation Reset.Personnel Counseled on Proper procedures.W/900308 Ltr ML20012C4291990-03-0707 March 1990 LER 87-015-01:on 871003,reactor Scram Occurred as Result of Turbine Control Valves Rapid Opening & Subsequent Fast Closure.Caused by Flow Imbalance in Turbine Control Oil Sys. Turbine Startup Procedure revised.W/900207 Ltr ML20006B4701990-01-22022 January 1990 LER 89-026-00:on 891223 & 900105,primary Containment Isolation Sys Group III Isolation & Standby Gas Treatment Sys Initiations Occurred.Caused by Failure of Sensor Converter.Isolation Reset & Monitor bypassed.W/900122 Ltr ML20005E1511989-12-26026 December 1989 LER 89-025-00:on 891128,primary Containment Isolation Sys Group III & Standby Gas Treatment Sys Initiation Occurred. Caused by Failure of Reactor Bldg Ventilation Radiation Monitor/Sensor Converter.Converter replaced.W/891226 Ltr ML20011D4901989-12-20020 December 1989 LER 89-024-01:on 890913,while Reviewing RHR Sys Surveillance Procedure,Determined That Leak Testing of RHR Valve V10-18 Not Incorporated & Implemented in Rev 9.Caused by Incomplete Review.Event Reviewed w/personnel.W/891220 Ltr ML19327A8881989-10-13013 October 1989 LER 89-024-00:on 890913,noted That Requirement from Previous Inservice Test Program Rev 9 Re Leak Testing of Valve V10-18 Not Incorporated & Implemented.Caused by Incomplete Review & Omission.Procedure Changes implemented.W/891013 Ltr ML19325C7821989-10-11011 October 1989 LER 89-023-00:on 890911,discovered That Remote Indication to Valve RHR-20 Not Available from 890320-0912,when Supply Breaker Replaced.Caused by Lack of Personnel Recognition. Breaker Replaced & Indication restored.W/891011 Ltr ML20024A8681983-06-22022 June 1983 LER 83-015/01T-0:on 830608,error Discovered in Spacing Table Developed for Support of Copper Piping in Svc Water Sys.Addl Supports Required to Fully Comply W/Ansi B31.1.W/830622 Ltr ML20024A8311983-06-0909 June 1983 LER 83-015/01P-0:on 830608,Yankee Atomic Electric Co Informed Util That Addl Piping Supports Required to Support Piping in Svc Water Sys & Torus Attached Piping.Cause & Corrective Actions to Be Provided in Next rept.W/830609 Ltr ML20024A3441983-06-0707 June 1983 LER 83-014/03L-0:on 830510,discovered Surveillance Frequency for Svc Water Processs Monitor Exceeded Tech Specs.Caused by Schedule Error.Analysis Immediately Performed.Applicable Personnel reinstructed.W/830607 Ltr ML20024A4151983-05-13013 May 1983 LER 83-013/03L-0:on 830413,while Reactor Shutdown,Weekly Environ Air Sample for 830405-12 at Station AT1.3 Not Obtained.Caused by Technician Failure to Test for Sys Vacuum.Technician Reinstructed in procedure.W/830513 Ltr ML20023B4741983-04-25025 April 1983 LER 83-011/03L-0:on 830325,during Visual Insp,Shock Suppressor MS-6 on Main Steam a Piping Found W/No Visible Fluid in Sight Glass & Failed to Lock Up.Caused by Damaged Lenztee.Snubber Cleaned & Rebuilt ML20028F3741983-01-21021 January 1983 LER 83-002/02T-0:on 830108,discovered Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line.Cause Unknown.Leaking Elbow Replaced w/304L Type Stainless Steel Matl Per NUREG-0313 Requirements ML20028F3921983-01-19019 January 1983 LER 82-026/03L-0:on 821220,while Shifting from Reactor Bldg Closed Cooling Water HX B to A,Closed Cooling Water Temp Rapidly Dropped 20 F.Caused by Increased Efficiency of HX Upon Cleaning ML20028D5591983-01-10010 January 1983 LER 83-001/01P-0:on 830107,valves V-16-19-20 & 22B Failed to Close When Operator Attempted to Secure Nitrogen Flow.Caused by Accumulation of Iron Particles on Magnet Used to Provide Valve Position Indication.Valves Cleaned ML20028D5421983-01-10010 January 1983 LER 83-002/01P-0:on 830108,indication of Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line Found.Caused by Pipe Crack.Cause of Pipe Crack Unknown.Elbow Replaced w/304L Type Stainless Steel Matl ML20028A3601982-11-0303 November 1982 LER 82-022/03L-0:on 821005,diesel Generator a Failed to Reach Required Voltage & Frequency within Tech Spec Time Limit.Caused by Fuel Oil Return Line Check Valve Failure. Valve Replaced ML20052C0051982-04-23023 April 1982 LER 82-007/01T-1:on 820309,standby Liquid Control Storage Tank Level & Sodium Pentaborate Concentration Calculations Did Not Correctly Account for Specific Gravity of Sodium Pentaborate.Caused by Procedure Equation Errors ML20052C0451982-04-23023 April 1982 LER 82-003/01T-1:on 820220,boron Concentration Fell Below Tech Spec Requirement.Caused by Apparent Boron Loss Coupled W/Small Sodium Pentaborate Concentration Margin ML20050B3941982-03-25025 March 1982 LER 82-005/03L-0:on 820223,uninterruptible Ac Electric Power Sys Tripped & Lost Power to Motor Control Ctr 89B, Rendering Sys Inoperable.Caused by Shorted Out Transient Suppression Capacitor Due to Aging.Capacitor Replaced ML20050A9291982-03-23023 March 1982 LER 82-007/01T-0:on 820309,calculations of Standby Liquid Control Storage Tank Concentration Versus Tank Level Correlation Did Not Account for Specific Gravity of Sodium Penaborate.Procedures Corrected ML20050A3781982-03-21021 March 1982 LER 82-006/03L-0:on 820219,during Normal Surveillance on Differential Pressure Switches DPIS 2-120 A,B,C & D,Switches A,B & C Found to Be Out of Tech Spec Limits.Caused by Setpoint Drift.Switches Reset to within Required Tolerance ML20042B2361982-03-16016 March 1982 LER 82-004/03L-0:on 820216,discovered That Continuous Environ Air Sample Not Obtainable at Station AT1.4 Per Tech Spec.Caused by Solder Lug of Std 125V-8A Power Toggle Switch Parting at 90 Degree Bend.Faulty Switch Replaced ML20042A4111982-03-0909 March 1982 LER 82-007/01P-0:on 820309,error Revealed in Calculations of Sodium Pentaborate Concentration in SLC Tank.Caused by Specific Gravity of Solution Not Being Factored Into Weight Percent Calculation in Accordance W/Tech Specs ML20042A6031982-03-0606 March 1982 LER 82-003/01T-0:on 820208,sample of Standby Liquid Control Boron Concentration Below Tech Spec Limits.Investigation in Progress.Administrated Limit & Sampling Frequency Increased ML20041F9281982-03-0303 March 1982 LER 82-002/03L-0:on 820206,ac Ground & Blown Fuse Alarms Activated,Rendering Trouble Alarm UPS-B Inoperable.Caused by Blown Fuse M Transient Suppression Circuit Due to Shorted Out Capacitor Off Board 2A 17 ML20041D7771982-02-25025 February 1982 LER 82-001/03L-0:on 820128,IRM Channel B Declared Inoperable.Caused by Failed Voltage Pre AMP (GE 112C-2218G001).Half Scram Manually Initiated.Component Will Be Repaired Prior to Entering IRM Range ML20041D4281982-02-22022 February 1982 LER 82-003/01P-0:on 820220,after Addition of Water to SLC Tank,Solution Sample Found Boron Concentration Below Required Amounts.Cause Unknown.Administrative Limit for Concentration Will Be Increased & Addl Sampling Conducted ML20040E2581982-01-26026 January 1982 LER 81-037/03L-0:on 811227,while Attempting to Start RHRSW Pump P-8-1A,breaker Tripped Contrary to Tech Specs.Caused by Worn Bushings on Operating Mechanism.Circuit Breaker Replaced.Breaker Mfg by Ge,Model Am 4.16 250-8HB ML20040C6971982-01-16016 January 1982 LER 81-036/03L-0:on 811217,containment Isolation Valve CU-15 Failed to Seat Satisfactorily Per Tech Spec 4.7.D.1 During Quarterly Surveillance Testing.Caused by Failure of Closing Torque Switch.Torque Switch Will Be Replaced Next Shutdown ML20040B1941981-12-30030 December 1981 Updated 81-028/03X-1:on 811017,field Breaker Failed to Open, Effectively Disabling Rrmg Set Recirculation Pump Trip Instrumentation.Caused by Binding of Operating Mechanism.New Breaker Installed ML20039F0101981-12-30030 December 1981 LER 81-035/03L-0:on 811204,during Core Spray Valve Test, Breaker for V14-11A Tripped & Reactor Shutdown Commenced. Caused by Breaker Not Latching When Closed,Allowing Breaker to Trip Below Setpoint.Breaker Replaced ML20039C2991981-12-18018 December 1981 LER 81-032/03L-0:on 811120,valves RWCU 68 & 15 Found to Have Seat Leakages Exceeding Tech Spec Range.Cause Not Stated. Disc Replaced & Valves Satisfactorily Retested ML20039C3071981-12-18018 December 1981 LER 81-034/03L-0:on 811121,operating Cycle Test of Standby Gas Treatment HEPA Filters Found Not to Have Been Done Since Sept 1979.Caused by Failure to Include Test on Dept Surveillance List.Test Completed & Schedule Revised ML20039C1121981-12-17017 December 1981 Updated LER 81-011/03X-1:on 810507,leak Discovered in Socket Weld Reducing Fitting.Caused by Intergranular Stress Corrosion Cracking.All Similar Fittings Replaced W/Differently Designed Fitting Less Susceptible to Failure ML20039C3821981-12-17017 December 1981 Updated LER 81-016/03X-1:on 810622,small Leak Found in Socket Weld Reducing Fitting in Vent Line of Regenerative Heat Exchanger E-15-1A.Caused by Intergranular Stress Corrosion Cracking Due to Wetting of Asbestos Insulation ML20039B1281981-12-0909 December 1981 LER 81-033/01T-0:on 811125,reactor Bldg Roof Hatch Opened by Work Crew W/O Notice to Supervisor Until Fire Permit for Welding Requested.Caused by Personnel Error.Personnel Reinstructed Re Procedural Requirement 1994-04-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8831999-10-21021 October 1999 Safety Evaluation Supporting Proposed Alternatives to Code Requirements Described in RR-V17 & RR-V18 ML20217G2041999-10-13013 October 1999 Safety Evaluation Supporting Amend 179 to License DPR-28 BVY-99-127, Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With ML20212C2551999-09-17017 September 1999 Safety Evaluation Supporting Amend 175 to License DPR-28 BVY-99-112, Monthly Operating Rept for Aug 1999 for Vermont Yankee.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Vermont Yankee.With BVY-99-109, Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 9908311999-08-19019 August 1999 Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 990831 BVY-99-102, Monthly Operating Rept for July 1999 for Vermont Yankee. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Vermont Yankee. with ML20209J0081999-07-14014 July 1999 Special Rept:On 990615,diesel Driven Fire Pump Failed to Achieve Rated Flow of 2500 Gallons Per Minute.Pump Was Inoperable for Greater than 7 Days.Corrective Maint Was Performed to Reset Pump Lift Setting BVY-99-090, Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With ML20196G5071999-06-23023 June 1999 Vynp Assessment of On-Site Disposal of Contaminated Soil by Land Spreading BVY-99-077, Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With BVY-99-068, Monthly Operating Rept for Apr 1999 for Vynp.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Vynp.With ML20206E8741999-04-29029 April 1999 SER Determined That Flaw Evaluation Meets Rules of ASME Code & Assumed Crack Growth Rate Adequate for Application ML20206D9301999-04-27027 April 1999 1999 Emergency Preparedness Exercise 990427 Exercise Manual (Plume Portion) ML20205S4211999-04-16016 April 1999 Non-proprietary Version of Revised Page 4-3 of HI-981932 Technical Rept for Vermont Yankee Spent Fuel Pool Storage Expansion ML20205K7581999-04-0707 April 1999 Safety Evaluation Supporting Alternative Proposal for Reexamination of Circumferential Welds with Detected Flaw Indications in Plant RPV BVY-99-046, Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With ML20205F6631999-03-0404 March 1999 Jet Pump Riser Weld Leakage Evaluation BVY-99-035, Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With ML20205P8241999-02-28028 February 1999 Rev 2 to Vermont Yankee Cycle 20 Colr ML20203H9881999-02-18018 February 1999 SER Accepting Alternative to 10CFR50.55a(g)(6)(ii)(A) Augmented Reactor Vessel Exam at Vermont Yankee Nuclear Power Station.Technical Ltr Rept Encl ML20203A6951999-02-0404 February 1999 Revised Rev 2,App B to Vermont Yankee Operational QA Manual (Voqam) ML20199K7151999-01-21021 January 1999 Corrected Safety Evaluation Supporting Amend 163 Issued to FOL DPR-28.Pages 2 & 3 Required Correction & Clarification ML20199K6991999-01-20020 January 1999 Safety Evaluation Concluding That Request to Use YAEC-1339, Yankee Atomic Electric Co Application of FIBWR2 Core Hydraulics Code to BWR Reload Analysis, at Vermont Yankee Acceptable ML20199L5951999-01-14014 January 1999 Safety Evaluation Accepting Licensee Proposed Alternative to Code Requirement,Described in Rev 2 to Pump Relief Request RR-P10 Pursuant to 10CFR50.55a(a)(3)(i) BVY-99-071, Corp 1998 Annual Rept. with1998-12-31031 December 1998 Corp 1998 Annual Rept. with BVY-99-001, Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station ML20198H5481998-12-23023 December 1998 Rev 2 to Vermont Operational QA Manual,Voqam ML20196H8641998-12-0101 December 1998 Cycle 19 Operating Rept BVY-98-163, Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With ML20195C4161998-11-0909 November 1998 SER Accepting Request That NRC Approve ASME Code Case N-560, Alternative Exam Requirement for Class 1,Category B-J Piping Welds BVY-98-154, Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With ML20155B6471998-10-26026 October 1998 Safety Evaluation Accepting Jet Pump Riser Insp Results & Flaw Evaluation,Conducted During 1998 Refueling Outage ML20154N0891998-10-16016 October 1998 Rev 1 to Vermont Operational QA Program Manual (Voqam) ML20154B6951998-10-0101 October 1998 SER Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Vermont Yankee Nuclear Power Station BVY-98-149, Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With ML20239A1361998-09-0202 September 1998 SER Re License Request for NRC Review & Concurrence W/Changes to NRC-approved Fire Protection Program BVY-98-135, Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With ML20151U0361998-08-28028 August 1998 Non-proprietary Rev 1 to Holtec Rept HI-981932, Vermont Yankee Nuclear Power Station Spent Storage Expansion Project ML20237E9221998-08-20020 August 1998 Vynp 1998 Form NIS-1 Owners Summary Rept for ISI, 961103-980603 BVY-98-122, Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station ML20205F6491998-07-31031 July 1998 Rev 1 to GE-NE-B13-01935-02, Jet Pump Assembly Welds Flaw Evaluation Handbook for Vermont Yankee ML20236G0011998-06-30030 June 1998 Individual Plant Exam External Events BVY-98-098, Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station ML20248C5081998-05-31031 May 1998 Rev 2 to 24A5416, Supplemental Reload Licensing Rept for Vermont Yankee Nuclear Power Station Reload 19 Cycle 20 ML20248C4951998-05-31031 May 1998 Rev 1 to Vermont Yankee Nuclear Power Station Cycle 20 Colr BVY-98-081, Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station ML20247J8341998-05-31031 May 1998 Peak Suppression Pool Temp Analyses for Large Break LOCA Scenarios, for May 1998 ML20247G4001998-05-12012 May 1998 Interview Rept of Ej Massey ML20247E6351998-04-30030 April 1998 Rev 1 to GE-NE-B13-01935-LTR, Jet Pump Riser Welds Allowable Flaw Sizes Ltr Rept for Vermont Yankee 1999-09-30
[Table view] |
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,. o VERMONT YANKEE NUCLEAR PowEn CORPORATION P. O. DOX 157 ,
l GOVERNOR HUNT TtOAD VERNON, VERMONT 05354 December'20, 1989 !
VYV 89-261 U.S. Nuclear Regulatory Commission-Document Control Desk Washington, D.C. 20555-
REFERENCE:
Operating License DPR-28 !
Docket No. 50-271 Reportable Occurrence No. LER 89-24
[
Dear _ Sirs:
As defined by 10CFR50.73, we are reporting the attached Reportable j Occurrence as LER 89-14 Rev. 1. This revision was issued based on additional information obtained during a subsequent documentation review.
Very truly yours, 1-i VERMONT YANKEE NUCLEAR POWER CORPORATION '
James P. Pelletier Plant Manager ,
cc: Regional Administrator USNRC l Region I l 475 Allendale Road ;
King of Prussia, PA- 19406 >
v I
?
L 8912270316 891220
.S-PDR- ADOCK 05000271 ' ' - 8 $
PDC < >
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NRC Form 384 U.S. NUCL EAR REGULATORY COMMISSION (9-83) APPROVED OMS NO.3150-0104 LICENSEE EVENT REPORT (LER) EXPIRES 8/31/96 FACILITY NAME (5) DOCKET NO. e) PAGE (8)
VERMONT YANKEE NUCLEAR POWER STATION O l 5 l 0 l 0 l(0 l 2 l 70 ll 1 1 l 0F l 0 l 3 TITLE (*) MISSED RESIDUAL HEAT REMOVAL SYSTEM VALVE LEAKAGE SURVEILLANCE DUE TO INCOMPLETE PROCEDURE REVIEW.
EVENT DATE (*) LER NUMBER (5) REPORT DATE (?) OTHER FACILITIES INVOLVED (*)
MONTH DAY YEAR YEAR SEO # REV# MONTH DAY YEAR FACILITY NAMES DOCKET NO.(S)
NA 0 5 0 0 0 1 0l9 1__[3 _ 819 8l9 -
0l2l4 -
0l1 1l2 2l0 8l9 NA 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO REQ'MTS OF 10CFR 6: / ONE OR MORE ('1)
MODE (*) N 20.402(b) __ 20.405(c) __ 50.73(a)(2)(iv) __ 73.71(b)
POWER __ 20.405(a)(1)(I) __ 50.36(c)(1) __ 50.73(a)(2)(v) __ 73.71(c)
LEVEL (t*) 1l d 0 20.405(a)(1)(II) ._ 50.36(c)(2) __ 50.73(a)(2)(vii) __
OTHER:
............... __ 20.405(a)(1)(III) _X 50.73(a)(2)(I) __ 50.73(a)(2)(viii)(A)
............... __ 20.405(a)(1)(iv) __ 50.73(a)(2)(II) __ 50.73(a)(2)(viii)(B)
............... 20.405(a)(1)(v) 50.73(a)(2)(III) 50.73(a)(2)(x) '
LICENSEE CONTACT FOR THIS LER (ie)
NAME TELEPHONE NO. ~ '
AREA CODE JAMES P. PELLETIER, PLANT MANAGER 8ld22l5l7[-l7l7lIl1 ;
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (18) ;
CAUSE SYST COMPNT MFR REPORTABLE ..... CAUSE SYST COMPNT MFR REPORTABLE ...... i TO NPRDS ..... TO NPRDS ......
NA l lll lll ll. NA l lll lll .
NA l lll lll . .l NA l lll lll SUPPLEMENTAL REPORT EXPECTED ('*) EXPECTED M0 DA YR SUBMISSION
~~l YES (If ves, complete EXPECTED SUBMISSION DATE) 'X1 NO DATE (15) l l l ABSTRACT (Limit to 1400 spaces, i.e., approx. fifteen single-space typewritten lines) ('*)
In order to implement the recently developed Revision 10 of the Vermont Yankee Intervice Testing (IST) program, various system surveillance procedures were being revised to incorporate program changes. On 9/13/89, while reviewing the Residual Heat Removal _(RHR)
(EIIS=BO) System surveillance procedure, it was noted that a requirement from previous IST Program Revision 9 concerning leak testing of RHR valve V10-18 had not been incorporated and izplemented.
The root cause of this event has been determined to be incomplete review and omission of the V10-18 leak test requirement during RHR System implementing procedure development. j Vermont Yankee's subsequent documentation review reveals that per VY's design basis (i.e., Technical Specifications, B 31.1 - 1967) and Generic Letter 89-04, that RHR-18 did not require IST testing. Based on this investigation the IST Program requirement to leak tett RHR-18 will be removed from the program.
To preclude recurrence of a similar event, future changes to implementing procedures involving IST Program testing will be routed to the IST Program Coordinator for a complete rsview.
Previous similar events have been reported to the Commission, in the last five years, as LER 87-04 and LER 89-20.
NRC Form 384 -
(9-83)
]
NRCForb384A U.S. NUCLEAR REGULATORY COMMISSION (9-83) APPROVED OMS NO.3150-0104 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION EXPIRES 8-31-96 UTILITY NAME (i) DOCKET NO. (e) LER NUMBER (*) PAGE (8)
YEAR SEQ. # REV#
VERMONT YANKEE NUCl. EAR POWER STATION d d d d d 2l711 8l9 -
0l2l4 -
0l1 d2 0F d3 TEXT (If more space is required, use additional NRC Form 384A) ( ') ,
DESCRIPTION OF EVENT In order to implement the recently developed Revision 10 of the Vermont Yankee Intervice Testing (IST) Program, various system surveillance procedures were being revised to incorporate program changes. On 9/13/89, while reviewing the Residual Heat Removal (RHR)
(EIIS=BO) System surveillance procedure, it was noted that a requirement from previous IST Program Revision 9 had not been incorporated and implemented.
Revision 9 of the IST Program, which was approved on 7/28/88 and implemented on 1/17/89, added a requirement for leak testing RHR valve V10-18 during each refueling outage.
(NOTE: Valve V10-18 is the inboard Shutdown Cooling Suction Valve.) It was noted that-this tasting had not been performed during the 1989 refueling outage because it had not been cdded to the RHR system surveillance procedure.
Vermont Yankee's subsequent investigation into this event revealed that the requirement to leak test the V10-18 valve does not belong in the IST program.
When Vermont Yankee was licensed, ASME B31.1 1967 Edition, required only one valve at a high pressure to low pressure boundary. This valve needed to be qualified to the higher of tha two pressures. This requirement is currently met. Additionally, the Code required prcrsure relief valve is provided along with pressure monitoring of the low pressure side of tha piping that alarms in the Control Room. Pressure Isolation Valves (PIV's) were not a d2 sign bases that was addressed in the Technical Specifications.
Generic Letter 89-04 " Guidance on Developing Acceptable Inservice Testing (IST)
Programs" requires those PIVs listed in plant Technical Specifications to be listed in the IST program. Since Vermont Yankee's investigation revealed that this valve is not a PIV Vsrmont Yankee plans to remove the requirement to test V10-18 valves from the IST program.
l CAUSE OF EVENT l
After completion of program changes by the IST Program coordinator, Revision 9 of the IST Program was tracked on the Vermont Yankee commitment system and forwarded, with all chtnges identified, to the Operations Department to allow for revision of implementing pro-crdures. During revision of the RHR system implementing procedure, the' subject valve leak tset was omi,tted. The Operations department developed the procedure revision and provided for its internal review. Although not specifically required, the IST Program coordinator w:s then requested to provide additional review. The IST Program coordinator provided a curzory review of this and all other procedures necessary to implement Revision-9 of the program. All procedure changes covered by this random review were found to be complete and to adequately reflect program testing requirements. However, the subject valve leak test His not included in the scope of the review. This, coupled with the initial omission of the l leak test during procedure development, is determined to be the root cause of this event.
i l ANALYSIS OF EVENT The subject valve, V10-18, is the inboard valve of the Primary Containment Isolation Valve pair for the RHR Shutdown Cooling Suction line penetration. Valve V10-18 and j V10-17, the outboard valve at this penetration, have the additional function of providina a NRC Form 384A (9-83)
NgC-For's 384A U.S. NUCLEAR REGULATORY COMMISSION (9-83) APPROVED OMS NO.3150-0104 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION EXPIRES 8-31-96 UTILITY NAME (5) DOCKET NO. (*) LER NUMBER (*) PAGE (a)
YEAR SEO, # REV#
VERMONT YANKEE NUCLEAR POWER STATION d d d d d 2l7]1 8l9 -
0l2l4 -
0l1 ,d3 0F d3 ,
TEXT (If more space is required, use additional NRC Form 384A) ( ')
ANALYSIS OF EVENT (Continued) piping pressure specification separation. These valves separate Reactor Coolant Pressure
.from RHR System piping. Although these valves act as Pressure Isolation Valves (PIV's),
thsy have no specific requirement for leak testing in Tech. Spec. Section 3.7.D concerning Primary Containment.
In addition, it should be noted that although the recently self imposed IST Program lack test requirement was not performed, valve stroke time testing was accomplished. Review of this stroke time data shows no indication of valve operator degradation. It should also be noted that in the worst case scenario of valve V10-18 being inoperable in the fully open position, reactor operation is permitted if the next valve downstream is closed.
During development of Revision 9 of the IST Program, Vermont Yankee committed to leak tcst valve V10-18 during each refueling outage to determine any gross leakage. Corrective Ection would then be taken per ASME Section XI requirements. Since ASME Section XI testing is referenced in Tech. Spec. 4.6.E.2, this event can be considered a missed Tech. Spec. sur-vaillance. Although the leak test was not performed, system pressure indication downstream of the subject containment penetration has been normal during the current operating cycle.
Based on the above, it is concluded that the integrity of the corresponding Primary Containment penetration is assured via closure of valve V10-17 and continuous pressure tonitoring.
Therefore, during the events of this report and for the remainder of the current operating cycle, there is reasonable assurance that there are no adverse safety implications to plant equipment, personnel, or to the public.
CORRECTIVE ACTION l Based on the guidance provided in GL 89-04, and review of the design basis for the V10-18 valve, the requirement to leak test RHR-18 valves will be removed from the IST program.
A review has been completed and all other IST Program implementing procedures adequately l address all testing required by the program. In addition, this event has been reviewed with L th3 affected personnel responsible for procedu're development and review.
To further preclude recurrence of a similar event, future changes to implementing pro-i c dures involving IST Program revisions will be routed to the IST Program Coordinator for l c complete review.
ADDITIONAL INFORMATION Previous similar events have been reported to the Commission, in the last five years, L as LER 87-04 and LER 89-20.
NRC Form 384A L
(9-83) l-