ML20039C112

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Updated LER 81-011/03X-1:on 810507,leak Discovered in Socket Weld Reducing Fitting.Caused by Intergranular Stress Corrosion Cracking.All Similar Fittings Replaced W/Differently Designed Fitting Less Susceptible to Failure
ML20039C112
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 12/17/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20039C098 List:
References
LER-81-011-03X, LER-81-11-3X, NUDOCS 8112280418
Download: ML20039C112 (2)


Text

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14 75 REPORT C A. E $3 EVENT DESCRIPTION AND PROBABLE CONSECUENCES h t o 121 l Durine normal operation of the Reactor Water Cleanun System rmrfnn onernent  !

Io ja t t surveillance discovered a small leak in a 1" X 3/4" socket veld reducine fittine I lo 64I I in the tube-side drain line of Recenerative Heat Exchanger F-15-1A upstream of l 1o isi I valve V12-41A. There were no consequences adverse to the pualic health and l lo is l I safety as a result of this event. Similar previous occurrences were reported I lo t;} l to the Commission as LER 79-01. 80-37 and 80-41. I lots!I I SYSTEM CAUSE CAUSE COVP VA LV E COCE CCCE SL8COCE COMPONENT CCOE SU8CO DE SUSCOCE loi91 l Cl Gl h y h lD lh l PI I!P lE IX lX lh Wh dh 7 8 9 to 11 12 13 18 19 20

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1 CAUSE DESCRIPTION AND COFRECTIVE ACTIONS 4

The Reactor Water Cleanup System was . removed from service to l allow the degraded fitting to be replaced with an identical spare.

! The fitting was- sent to an independent laboratory where the mode of failure was determined to be intergranular stress corrosion crack-ing. During the 1981 refueling outage, this fitting and all similar fittings in the RWCU System were replaced with a differently designed.

reducing fitting which is less susceptible to this type of failure.

The laboratory analysis also revealed transgranular stress corrosion 4 cracking (not through wall) adjacent to the subject through wall crack on

the OD of the pipe. - The transgranular cracking was attributed ' to the
wetting of asbestos insulation with subsequent. leaking of chlorides to
the pipe surface.

As a result of this event and other transgranular cracking events, a- detailed plant review was performed to . determine if any other . insulated'

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high temperature stainless steel lines.have been subjected to wetting.

In addition, a field walkdown was performed to' identify sources or

! potential sources of wetting. .As a result of this. review, only the sus-  !

I pect piping and fittings in the, RWCU System were replaced during the 1981

  • efueling outage. . ,

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. Any future wetting will be followed-up byfinspections as required.

Purchase of all insulation and application of protective paints will be 4

continued with the emphasis on chloride control. Impicmentation of the-i aforementioned program and controls will reduce the potential for any.

future stress corrosion cracking.

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