ML20050B394

From kanterella
Jump to navigation Jump to search
LER 82-005/03L-0:on 820223,uninterruptible Ac Electric Power Sys Tripped & Lost Power to Motor Control Ctr 89B, Rendering Sys Inoperable.Caused by Shorted Out Transient Suppression Capacitor Due to Aging.Capacitor Replaced
ML20050B394
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 03/25/1982
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20050B384 List:
References
LER-82-005-03L, LER-82-5-3L, VTYS1, NUDOCS 8204050282
Download: ML20050B394 (2)


Text

-

(7 77)

- LICENSEE EVENT REPORT LER 82-5/3L CONTROL BLOCK; l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) t e i O l ai 9l l V lLICENSEE 1

T l VCODE l Y l S14 l 115l@l 0 l 0 l- lLICENSE o l0 NUYSER lo lo lo l- lo lo l@l 25 4 l 1LICENSE 26 l 1 l 1TYPE l 1JOl@l51 G Al T $8l@

CON'T l0lil 3y"'

l L }@l 0 ] 5 l 0 l 0 l0 l 2 l 7 l1 @l 0 l 2 l 2 l 3 l 8 l 2 l@l750 l 3 l 2 l 5 l 8 l280l@ 74 I d 60 61 DOCK ET NUVBER 68 69 EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h l o ;;; l With the plant at normal full power operation, Control Room personnel reported UPS B l yg,3, ;

tripped and lost power to MCC 89B. The Maintenance Department was immediately informed l

g y , y , and testing of the alternate system was commenced in accordance with Tech. Spec. ,

Sec.l

,g g ,3.5.A.4. UPS B was declared inoperable and alternate action taken in accordance with  ;

,g g ; Tech. Spec., Section 3.10.B.4. Maintenance tie breakers for MCC 89B were closed. Thereg g were no adverse consequences to public health and safety as a result of this event. l A similar event was reported as LER 82-2/3L.  ;

80 7 8 9 S4STEV CAUSE CAUSE COYP. VALVE CODE CODE SU8 CODE COVPONENT CODE SU8 CODE SUSCODE 10191 I a 1 El D l@ lE lh l Alh lX lX lX lX lX lX lh Wh lZlh 9 10 11 12 13 18 19 20 SEQUENTI AL OCCURRENCE REPORT REVISION CODE TYPE N O.

LED AO _EVENTvEAR RE PORT NO.

h y,cgaf l8 l2 l b l0l0l5l l/l l 0l 3l lLl [---] l0l J2

_ 21 22 2J 24 26 27 28 TJ 30 31 ACT!ON FUTURE EFFECT SHUTDOWN ATTACHVENT NP R O-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT VETHOD WOURS SU8MITTED FORM 4UB. SUPPLIER MANUFACTURER lJJA l@l34Z l@ l35Z l@ l36Z l@ l0l0l0l0l 3/ 40 lN 41 l@ lY 42

]@ lL 43 l@ l44E l 3 l 5 l 547 l@

CAU3E DESCRIPTION AND CORRECTIVE ACTIONS I

liloll lilil l See Attached. I I

l i l 71 l I

tilali l

1 i 141 I 80 7 8 9 ST S . POWER OTHER STATUS iSCO RY DISCOVERY CESCRiPTION I1 15 l l E l@ l 1l 0l 0lhl NA l l A l@l Alarm in Control Room l A[TIVtTY CO ENT RELE A$ED OF RELE ASE LOCATION OF RELE ASE Ii Ic l l9 z I @ Iz r

l@l AVOUNT NA OF ACTIVITY 44 l

45

@ l NA 80 l

et 10 11

  1. ERSONS.EL E xPOSURES NUY8ER TYPE D E SCRIPTION ji l 7 l l 0 l 0 l 0 l@l Z l@l NA PERSONNE L INJURIES NuvsER oESCRiptiON@

NA l

, ITI l 410

, 9 l 0101@l ,, 22 LOSS OF OR O AVAGE TO FACILITY TYPE DESCRIPTION NA  !

t 9 lZl@l 80 8204050282 820325 NRC USE ONLY PDR ADOCK 05000271 l

'S PDR NA l lllllllllllll$:

7 2 I

  • io 68 69 8 5
  • P PHONE:

(802) 257-7711 {

NAVE OF PREPARER

j VTVYS1

. 05000271 LER 82-5/3L t

1

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 4

A transcient suppression capacitor (GE 86F231L, 2900 MF) shorted out causing UPS B to trip. The capacitor malfunctioned due to aging. All 16 capacitors in the transcient suppression circuit were replaced. Also, all 16 capacitors in the UPS A transcient suppression circuit were replaced as preventive maintenance. The system was operationally tested and placed back in service. The current PM program will be reviewed and ' modified as appropriate in view of the recent UPS failures.

1 l

1

'i l

i 1

i

(

h l

i i

- . - - . . - - . - - . _ _ . - .-, .-