ML19094A560

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09/26/1977 Letter Proposed Design Change to Allow the Lhsi Discharge Valves to Be Remotely Throttled from the Control Room
ML19094A560
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/26/1977
From: Stallings C
Virginia Electric & Power Co (VEPCO)
To: Case E, Reid R
Office of Nuclear Reactor Regulation
References
Download: ML19094A560 (9)


Text

.

e VIRGINIA ELECTRIC AND POWER COMPANY RIOHMOND,VIRGINIA 23261 September 26, 1977 ..

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Mr. Edson* G. Case, Acting Director Serial No. 374B/082977 Nuclear Reactor Regulation PO&M/ALH:das U.S. Nuclear Regulatory Connnission Docket Nosw 50-280 Washington, ,D. C. 20555 50-281 License Nos. DPR-32 Attention: Mr. Robert W. Reid, Chief DPR-37 Operating Reactors Branch 4

Dear Mr. Case:

We submitted a proposed design change which would allow the LHSI discharge valves to be remotely throttled from the control room. We have recently comple-ted t~sts which provide information that will b~ helpful in your review. A com-plete tl;:scription of the tests along with an evaluation of the results is provid-ed in the attachment to this letter.

.Very truly yours, z;/'__-;_~ I ._,;/;~2 c:i~ ; c)

C. M. Stallings

  • Vice President-Power Supply and Production Operations Attachment cc: Mr. James P. O'Reilly

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SURRY POWER STATION UNIT NOS. 1 & 2 LHSI FLOW CONTROL TEST Purpose of Test Excessive LHSI pump flow during the recirculation phase of long term cooling can result in inadequate NPSH. This may cause pump cavitation and

'possible damage. A test was performed to show that LHSI pump flow could be satisfactorily controlled by throttling the gate valves in the pump dis-charge flow path. The test was also intended to show that the valves could be satisfactorily positioned electrically and that personnel could manually operate the valves in a reasonable ti.me period.

Test Description For test purposes, the hot leg injection valves (MOV 890 A&B) were se-lected to control flow. The attached SI flow diagram shows the test line-up. The cold leg valves were not used for the following reasons: 1) During the test, the reactor vessel head was partially lifted ancl cold leg inject-ion would subject core components to lift forces; 2) Cold leg injection would sweep crud deposits from core surfaces causing high levels of general area radiation and contamination to exist in the vicinity of the refueling cavity. Valve position during the test was controlled by manual operation of the valve handwheel and by electrically "jogging" the valve motor.

A "dry run" was performed prior to the flow test to simulate actual operator response during LOCA. This was to determine that sufficient time exists for an operator to manually position the injection valves between

e e the time an RWST low level alarm occurs and the time the minimum useable volume is reached.

Test Procedure and Results Initial conditions were established as follows: 1) Adequate RWST in-ventory and chemistry were verified; 2) Required electrical systems were verified operable; 3) Reactor cavity was made ready for flooding; 4) LHSI pump flow instrument calibration records' (attached) were checked; 5) Valve lineups were made to assure proper suction and discharge flow paths;

6) Reac_tor cavity was flooded* to a one foot level to verify _reactor cavity seal tightness.

Both LHSI pumps were started and flow ~stablished at 2100 +/-50 GPM per pump by manually positioning MOV 89U A&B .. Valve position was then varied to assure that flow could be changed in 100 GPM increments. During this phase of the test the operator did not experience any difficulty moving the valve even though high differential forces existed across the valve disc. There was no evidence of valve vibration or excessive flow noise during this test. Each valve was approximately 2 inches open with 2100

+/-50 GPM flow through each LHSI pump. The recirculation valves (MOV 885 A, B, C, D) were momentarily shut to verify that no measurable flow change*

would occur. As predicted the measured flow did not change noticeably.

This is due to the fact that recirculation line resistance is approximately 1000 times greater than injection line resistance, This is further verified by the monthly LHSI flow test where actual recirculation flow is measured at ~300 GPM with all other flow paths isolated. The recirculation valves were opened for the remainder of the testing.

The purpose of throttling flow to ~2100 GPM for two pump operation

e is to assure that loss of one LHSI pump doesn't result in excessive "run-out" flow on the remaining pump. Therefore, one LHSI pump was tripped to determine the effect on flow. -- When this occurred the flow on the opera-ting pump increased only by about 150 GPM. This seemed inconsistent with our predictions at f.irst, but-af--Eer--examining the differences between cold and hot leg injection piping it became obvious as to ,.,,why such a small flow change occurred. The cold leg injection piping is such that pump back pressure provides a significant portion of total system resistance in the two pump configuration. The pump discharge piping is joined together very near to the pumps. This would result in larger flow increases when one LSHI pump trips during cold leg injection. The hot leg i~jection piping is essentially two separate paths until it gets into the coolant loops and th1iA; pump back!:'rt::.s£ure would not be .:i. significE-nt. fac:t,-1.r i11 total system resistance. Tripping one LHSI pr.mp during hot leg j,jection should not re-sult in a significant increase of flow through the remaining pump.

In the single LHSI pump test configuration, flow was manually varied between 2100 GPM, and 3200 GPM to demonstrate flow control. Again the opera-tor had no difficulty operating the valve. As flow increased, it was noted that the instrumentation oscillated more widely until at 3200 GPM the varia~

tion was +/-150 GPM. The valve was approximately 2. 75 inches open at 3200+/-150 GPH, No noticeable vibration or excessive flow noise existed in thiP condi-tion.

The tests described above were then repeated and flow controlled by "jogging" the valve motor operator electrically, With. two LHSI pumps run-ning flow was controled at 2100+/-50 GPM with no difficulty. The operator was able to change flow in 100 GPM increments with no difficulty. With one

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pump running the operator varied flow from 2100+/-50 GPM to 3200+/-150 GPH with no difficulty. The time required to change flow from 2100+/-50 GPM to 3200+/-

150 GPM by valve "jogging" was less than one minute.

The flow test was concluded by opening MOV 890 A&B fully and running both LHSI pumps to fill the r~actor cavity in preparation for refueling.

11 The dry run" tests were performed by directing an operator to shut the fully open MOV 864 valves using the manual handwheels. Operator ac-tion was completed in less than six minutes for both valves. The LOCA procedure requires that LHSI flow be throttled to 2100 GPM for each pump commencing at the time au RWST low level alarm occurs (54,000 useable gal-lons remaining). If it is assumed that each LHSI pumps is operating at 4.000 GPM until its valve is in i_ts final position and that two EHSI are operating at 600 GPM each continuously, the operator would complete tbe valve operation with at least 4,500 useable gallons remaining in the RwST.

Conclusions The tests demonstrated that LHSI pump flow can be controlled by throt-tling the hot leg injection gate valves. Although flow testing through the cold leg injection valves was not performed, similar performance is expected due t6 valve similarity. The loss of one LHSI pump will not result in pump cavitation due to excessive flow "runout". No unusual or excessive forces are required to operate the valves even with high differential pressures ac-ross the discs. No excessive flow induced valve vibration will occur as a result of throttling. Electrical "jogging" of the valves was not difficult from the standpoint of positioning accuracy and it proved to be a very exped-itious method of valve operation.

It is concluded that manual valve throttling is a satisfactory method

e of controlling LHSI pump flow during LOCA, but electrical "jogging" is much'more appropriate since it can be done safely and quickly from the control room with minor electrical modifications.

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