ML19296B363

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LER 80-004/03L-0:on 800118,discovered That Loop a Steam Flow Transmitter Had Drifted Out of Spec.Caused by Failure of Differential Pressure Unit in Barton Flow Transmitter Model 384.Pressure Unit Replaced,Transmitter Recalibr
ML19296B363
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 02/15/1980
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19296B361 List:
References
LER-80-004-03L, LER-80-4-3L, NUDOCS 8002200467
Download: ML19296B363 (1)


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y LICENSEE EVENT REPORT CONTROL 8 LOCK: l l l l l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 lo l1l8 lM 7 9

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NUMBEH 26 26 LICENSE TYPE JO $7 CAT $8 CON'T 7

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74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l Main s te m flow tr,nn-it tor FT-465 u,c fnnna en hwn Arirend c i , r. h that reactor trip o 3 l input and steam line isolation input from this channel would have occurred outside 1 o 4 l Tech Spec limits. Tech Specs 2.3.A.3.c and Table 3.5-1 apply. No effect on oublic j o 13 l l health and safety since redundant instruments were all operable. I o s l l jOl7l l 0 8 l 7 8 9 80 SYSTEM CAUSE CAUSE COVP. VALVE CODE CODE SUSCODE COMP 0NENT CODE SUSCODE SU8 CODE g l Il A]h yh l Elh lIl Nl S l Tl Rl Ulh Wh Wh 7 8 9 10 11 12 13 18 19 20

_ SEQUENTI AL OCCURRENCE REPORT REVISION LE R,RO JVENT YE AR R EPORT NO. CODE TYPE N O.

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_2n 22 23 24 26 27 28 29 30 31 32 TAKEN A ON ON PLANT M T D HOURS SP IT D FO 8. SUPPLI R MAN FACT RER l33 A l@W@ 34 W@

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42 W@ lIl21014lh 4J 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h l i l o l l Failure of the dif ferentini nressurn unir in , n,renn unan1 uA Flow Transmitter. I li lil Differential pressure unit was replaced and transmitter recalibrated.

I 2 l 1 i a l I i 4 I l 7 8 9 80 ST S  % POWE R OTHER STATUS O S OV RY DISCOVERY DESCRIPTION l1 I 5 l [E j@ l 1 l 0 l 0 l@l NA l W @l Operator observation l ACTivlTY CO TENT AMOUNT OF ACTIVITY LOC ATION OF RELE ASE i 6 RELE ASE@D OF RELE ASE@l NA l l NA l 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DE SCRIP TION i 7 l 0 l 0 [0 l@y@l NA l

' ' ' ,E RSO~ d'IN>uL S NUV8t R DESCRIPTION i a NA 8 9 l 0 l 0 l 0 l@l12 l 7 11 80 LOSS TYPE OF OR DAMAGE TO FACILITY Q DESCRIPTION  %./

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I DESCRIPTIO*d *

@ [SSUEN_jhl NA l llll l llllll5 7 8 9 10 68 69 80 E NAME OF PREPARER

. . unStad PHONE:

612-388-4767 2 8002200 h