ML20041B404

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Updated LER 81-030/03L-0:on 811211,during Testing,Degraded Voltage Relay 27A1/B25 Found W/Voltage Setpoint Outside Allowable Band.Exact Cause Unknown.Relays Recalibr & Found to Operate Correctly
ML20041B404
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 02/12/1982
From: Musolf D
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20041B393 List:
References
LER-81-030-03L, LER-81-30-3L, NUDOCS 8202230610
Download: ML20041B404 (1)


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? 8 60 61 DOCK ET NLM8 ER 68 69 EVENT DATE 74 75 83 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo121lDuring surveillance test, degraded voltage relay 27A1/B25 was found with l 1 o l a i I a voltage setpoint outside of the allowable band. A setpoint of 90 plus or l l o I A I I minus 2 percent is specified. The as-found setpoint was 93 percent. The time l 10isl 1 delay was within the specified 6 plus or minus 2 seconds. Technical Specification ;

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