ML20052B273

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LER 82-005/03L-0:on 820322,review of Chemistry Logs Showed That Boric Acid Tank 11 Had Not Been Sampled.Caused by Communication Breakdown.Tank Sampled & Involved Personnel Will Review Rept
ML20052B273
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 04/21/1982
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20052B271 List:
References
LER-82-005-03L, LER-82-5-3L, NUDOCS 8204300244
Download: ML20052B273 (1)


Text

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LICENSEE EVENT REPORT

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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo ltl8 lM 7 9

!N LICENSEE l P lI CODE lN l 1 l@l 14 0 l 0 l - l 0 l LICENSE 15 0 l 0 NUMBER l 0 l 0l -l 0 l 0 25l@l 264 l1LICENSE l 1 l 1TYPE l 1JOl@l57 CATl 58 l@

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dl 0 l 5 l 0 l 0 l 0 l7 l g l 9 l@l 01312 69 l 2 l a l 2 l@l 075 l 4REPORT 74 l ? l DATE 1 l R l 802 lh 7 8 60 61 DOCKET NUMBER 68 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l Routine review of Chemistry Logs showed No. 11 Boric Acid Tank was not sampled twice ;

l o 13 l l the previous week. ' Subsequent sampling showed the tank to be within specifications, g

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lo g4; l and since there were no transfers of fluid to or from the tank during the period it 13 I

No Ioisl l felt the tank was in spec during the period. Recent similar event was R0 81-19. g o e i effect on public health and safety. Tech Spec Table 4.1-2B, Item 10, applies.  ;

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10181 l CODE C0DE sis 8 CODE COMPONENT CODE SUBC DE S E O 9 lP lC l@ ]@ {@ l Z l Z l Z l Z l Z l Z [Q {g ]g 9 12 13 18 19 20 7 8 to 11 SEQUENTIAL OCCURRENCE REPCRT REVISION EVENT YE AR REPORT NO. CODE TYPE NO.

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]g 42 lZ lg lZ l9 l 9 l 9[g 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l

L'Lo_] I cnmmuniention breakdown between Radiation Protection Specialist and Control Room 1 1 l nnorntor. Upon discovery the tank was immediate1v sampled. Involved versonnel i 1

1 7 I will review this report.

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  • 8 PHONE:

612-388 1121 NAME OF PREPARER