IR 05000261/2007003
Download: ML072110261
Text
July 27, 2007
Carolina Power and Light CompanyATTN:Mr. Tom WaltVice President - Robinson PlantH. B. Robinson Steam Electric Plant Unit 2 3851 West Entrance Road Hartsville, SC 29550
SUBJECT: H.B. ROBINSON STEAM ELECTRIC PLANT - NRC INTEGRATEDINSPECTION REPORT 05000261/2007003
Dear Mr. Walt:
On June 30, 2007, the US Nuclear Regulatory Commission (NRC) completed an inspection atyour H.B. Robinson reactor facility. The enclosed integrated inspection report documents the inspection findings, which were discussed on July 2, with Mr. E. Kapopoulos and other members of your staff. The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA by Scott Shaeffer Acting For/Randy Musser, ChiefReactor Projects Branch 4 Division of Reactor ProjectsDocket No.:50-261License No.:DPR-23
Enclosure:
Inspection Report 05000261/2007003
w/Attachment:
Supplemental Informationcc w/encl. (See page 3)
July 27, 2007Carolina Power and Light CompanyATTN:Mr. Tom WaltVice President - Robinson PlantH. B. Robinson Steam Electric Plant Unit 2 3851 West Entrance Road Hartsville, SC 29550SUBJECT:H.B. ROBINSON STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT05000261/2007003Dear M
SUMMARY OF FINDINGS
IR 05000261/2007-003, Carolina Power and Light Company; on 04/01/2007-06/30/2007; H.B.Robinson Steam Electric Plant, Unit 2.The report covered a three-month period of inspection by resident inspectors and announcedinspections by health physicists and reactor inspectors.. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649,
"Reactor Oversight Process," Revision 3, dated July 2000.A.NRC-Identified and Self-Revealing FindingsNone.
B. Licensee-Identified Violations
None.
Enclosure
REPORT DETAILS
Summary of Plant Status The unit began the inspection period operating at 92 percent of ratedthermal power as the unit was experiencing an end-of-cycle coastdown at the rate of approximately -1 percent of rated thermal power per day, in preparation for beginning a scheduled refueling outage. On April 7, with the reactor operating at approximately 4 percent power, the licensee manually tripped the reactor to begin that outage. The licensee restarted the reactor on May 12, re-connected the unit to the electrical grid on May 13, and began a routine post-outage power increase toward 100 percent. On May 15, with the unit operating at 82 percent of rated thermal power and ramping upward, the plant experienced an automatic reactor trip after an electrical fault associated with main transformer monitoring circuitry caused that circuitry to initiate a main generator lockout, which in turn caused a turbine trip and a subsequent reactor trip. After resolving trip-related issues, the licensee restarted the reactor and re-connected the unit to the electrical grid on May 17. The unit returned to full power on May 18, and operated at full power for the remainder of the inspection period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity1R04Equipment Alignment
a. Inspection Scope
Partial System Walkdowns:The inspectors performed the following three partial system walkdowns, while theindicated structures, systems, and/or components (SSCs) were out-of-service for maintenance and testing:System Walked DownSSC Out of ServiceDate InspectedTrain A motor driven auxiliaryfeedwaterTrain B motor drivenauxiliary feedwaterMay 24Trains B and C ChargingPumpsTrain A charging pumpMay 29A deepwell pumpD deepwell pumpJune 11To evaluate the operability of the selected trains or systems under these conditions, theinspectors compared observed positions of valves, switches, and electrical powerbreakers to the procedures and drawings listed in the Attachment.
b. Findings
No findings of significance were identified.
R05 Fire Protection
a. Inspection Scope
For the six areas identified below , the inspectors reviewed the control of transientcombustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures to verify that those items were consistent with UFSAR Section 9.5.1, Fire Protection System, and UFSAR Appendix 9.5.A, Fire Hazards
Analysis.
The inspectors walked down accessible portions of each area and reviewed results from related surveillance tests to verify that conditions in these areas were consistent with descriptions of the areas in the UFSAR. Documents reviewed are listed in the Attachment.The following areas were inspected:Fire ZoneDescription25F/25GTurbine building east/west mezzanine and operating deck1Diesel generator B room 20Emergency switchgear room and electrical equipment area 19Cable spread room 7Auxiliary building hallway 26Yard electrical transformers
b. Findings
No findings of significance were identified.1R08Inservice Inspection (ISI) Activities
a. Inspection Scope
The inspectors observed in-process ISI work activities, reviewed ISI procedures, andreviewed selected ISI records, associated with risk significant structures, systems, andcomponents during the outage. The observations and records were compared to the requirements specified in the Technical Specifications (TSs) and the ASME Boiler and Pressure Vessel Code, to verify compliance and to ensure that examination results were appropriately evaluated and dispositioned. The inspectors conducted an onsite review of nondestructive examination (NDE)activities to evaluate compliance with TSs, ASME Section XI, and ASME Section V requirements, to verify that indications and defects (if present) were appropriately evaluated and dispositioned in accordance with the requirements of ASME Section XI, IWB-3000 or IWC-3000 acceptance standards.
The inspectors observed and reviewed non-destructive examination (NDE) activities.Specifically, the inspectors observed the following examinations:Ultrasonic Testing (UT):*Main Feed water Pipe to Elbow Weld #: 216/07
- Residual Heat Removal Pipe Weld #s: 109/09, 109/08Magnetic Particle Testing (MT):*Main Feed Water Pipe Weld #s: 216/07Penetrant Testing (PT):*Residual Heat Removal Pipe Weld #s: 109/09, 109/08Specifically, the inspectors reviewed the following examination records:Magnetic Particle Testing (MT):*Main Feed Water Pipe Weld #: 216/08Ultrasonic Testing (UT):*Main Feed Water Elbow to Elbow Weld #: 216/011
- Main Feed Water Elbow to Pipe Weld #: 216/012Augmented Ultrasonic Testing (AUT):*Steam Generator (S/G) A Nozzle to Elbow Weld #: 215/79-13-A
- S/G B Nozzle to Elbow Weld #: 217/79-13-B
- S/G C Nozzle to Elbow Weld #: 217/79-13-CSpecifically, the inspectors reviewed the following examination records thatcontained recordable indications:*UT: Residual Heat Removal System # 109/08, 109/09*PT: Residual Heat Removal System # 109/08, 109/09
- VT: Spring Hanger, 3020-213C, 2080-247CQualification and certification records for examiners, inspection equipment, and consumables along with the applicable NDE procedures for the previously referenced ISI examination activities were reviewed and compared to requirements stated in ASME Section V, ASME Section XI, and other industry standards.From April 16-20, 2007, the inspectors reviewed the Boric Acid Corrosion Control(BACC) program to ensure compliance with commitments made in response to NRC Generic Letter 88-05, "Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants."The inspectors conducted an on-site record review as well as an independent walkdownof parts of the reactor building that are not normally accessible during at-power operations to evaluate compliance with licensee BACC program requirements and 10
CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. In particular,the inspectors verified that the visual examinations focused on locations where boric acid leaks can cause degradation of safety-significant components and that degraded or non-conforming conditions were properly identified in the corrective action system.
The inspectors reviewed a sample of engineering evaluations completed for boric acidfound on reactor coolant system piping and components to verify that the minimum design code-required section thickness had been maintained for the affected components. The inspectors also reviewed licencee corrective actions (NCRs) as well as corrosion assessments implemented for evidence of boric acid leakage to confirm that they were consistent with requirement. Specifically, the inspectors reviewed:*Work Order (WO) #: 990888, A Charging Pump inlet and outlet cover gasketsleak*WO #: 586874, Waste Decay tank Room Ceiling, boric acid on structural ceilingand walls.*WO #: 611353, B RHR Pump Seal Area
- NCR 20050914, discolored Boric Acid Buildup B Spray PP Seal
- NCR 20050917, Source of Boric Acid Leak Behind C RCP Not Identified
- NCR 20060109, Boric Acid Corrosion on SI-895L
- NCR 20070407, Wet Boric Acid On Tubing Downstream of CVC-310B
- NCR 20070409, Excess Letdown HX Boric Acid Leak
- 20070410, Boric Acid Found on RHR-HTX-B Flange and BoltingThe inspectors reviewed welding activities from the previous outage. The inspectorsreviewed drawings, work instructions, weld process sheets, weld travelers, pre-heat requirements and radiography records for welding of an ASME Class 2 pressure boundary weld.Specifically the inspectors reviewed:*Component Cooling Water Valve SW-6 Replacement
- Service Water Check Valve SW-75 Replacement
- Safety Injection System Valve SI-875J ReplacementThe inspectors reviewed the SG examination scope, expansion criteria, eddy currenttesting (ET) acquisition procedures, ET analysis procedures, the SG Operational Assessment, in-situ tube pressure testing procedures, and records and examination reports to confirm that:*The SG tube ET examination scope was sufficient to identify tube degradationconfirming that the ET scope completed was consistent with procedures and plant TS requirements. In addition, the inspectors reviewed the SG tube ET examination scope to determine that it was consistent with that recommended in EPRI
"Pressurized Water Reactor Steam Generator Examination Guidelines," Revision 6, and included tube areas which represent ET challenges, such as the tubesheet regions, expansion transitions and support plates.
- The ET probes and equipment configurations used to acquire ET data from the SGtubes were qualified to detect the known/expected types of SG tube degradation in accordance with Appendix H, "Performance Demonstration for Eddy Current Examination," of EPRI "Pressurized Water Reactor Steam Generator Examination Guidelines," Revision 6.*The licensee adequately evaluated for any contractor deviations from their ET dataacquisition or analysis procedures or EPRI "Pressurized Water Reactor Steam Generator Examination Guidelines," Revision 6.The inspectors performed a review of SG ISI-related problems that were identified bythe licensee and entered into the CAP. The inspectors reviewed these corrective action program (CAP) documents to confirm that the licensee had appropriately described the scope of the problems. In addition, the inspectors' review included confirmation that the licensee had an appropriate threshold for identifying issues and had implemented effective corrective actions. The inspectors evaluated the threshold for identifying issues through interviews with licensee staff and review of licensee actions to incorporate lessons learned from industry issues related to the ISI program. The inspectors performed these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements.
b. Findings
No findings of significance were identified.1R11Licensed Operator Requalification
a. Inspection Scope
The inspectors observed licensed-operator performance during requalification simulatortraining for crew 1 to verify that operator performance was consistent with expected operator performance, as described in Exercise Guide LOCT 01-6. This training tested the operators' ability to operate components from the control room, direct auxiliary operator actions, and determine the appropriate emergency action level classifications while responding to a failed pressurizer pressure transmitter, a leak in the south service water header, and a subsequent steam generator tube rupture without pressurizer pressure control. The inspectors focused on clarity and formality of communication, the use of procedures, alarm response, control board manipulations, group dynamics, and supervisory oversight. Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the two degraded SSC/function performance problems orconditions listed below to verify the appropriate handling of these performance problems or conditions in accordance with 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, and 10 CFR 50.65, Maintenance Rule. Documents reviewed are listed in theAttachment. The problems/conditions and their corresponding ARs were:ARPerformance Problem/Condition 216145Functional failures in the reactor protection system exceeded the corresponding Maintenance Rule performance criteria216382Guide ring found improperly setDuring the reviews, the inspectors focused on the following:*Appropriate work practices,*Identifying and addressing common cause failures,
- Scoping in accordance with 10 CFR 50.65(b),
- Characterizing reliability issues (performance),
- Charging unavailability (performance),
- Trending key parameters (condition monitoring),
- 10 CFR 50.65(a)(1) or (a)(2) classification and reclassification, and
- Appropriateness of performance criteria for SSCs/functions classified (a)(2) and/orappropriateness and adequacy of goals and corrective actions for SSCs/functions classified (a)(1).The inspectors reviewed the following ARs associated with this area to verify that thelicensee-identified and implemented appropriate corrective actions:*192736, Yellow [system health] status for Reactor Protection System*194211, Unanticipated [Limiting Condition for Operation] entry due to failure of [loop3 Tavg/Delta-T protection channel Thot average summator] TM-432N*205117, Unanticipated [Limiting Condition for Operation] 3.3.1 entry due to [steamgenerator B feedwater flow transmitter] FT-487 failure *213638, [low-pressure reactor trip protection signal lead/lag module] PM-455A foundout of tolerance during [surveillance test] MST-004.
b. Findings
No findings of significance were identified.1R13Maintenance Risk Assessments and Emergent Work Evaluation
a. Inspection Scope
For the three time periods listed below, the inspectors reviewed risk assessments andrelated activities to verify that the licensee performed adequate risk assessments and implemented appropriate risk-management actions when required by 10 CFR 50.65(a)(4). For emergent work, the inspectors also verified that any increase in risk was promptly assessed, and that appropriate risk-management actions were promptly implemented. Documents reviewed are listed in the Attachment. Those periods included the following:*May 14 - May 18, including a reactor trip and a subsequent plant startup
- May 18 - May 25, including testing of a Component Cooling Water to RegenerativeHeat Exchanger isolation valve concurrent with maintenance on a 115KV breaker*June 9 - June 15, including scheduled work involving the steam-driven auxiliaryfeedwater system
b. Findings
No findings of significance were identified.1R15Operability Evaluations
a. Inspection Scope
The inspectors reviewed the two operability evaluations associated with the ARs listedbelow. The inspectors assessed the accuracy of the evaluations, the use and control of any necessary compensatory measures, and compliance with the TS. The inspectors verified that the operability determinations were made as specified by Procedure OPS-NGGC-1305, Operability Determinations. The inspectors compared the justifications provided in the determinations to the requirements from the TS, the UFSAR, and associated design-basis documents, to verify that operability was properly justified and the subject components or systems remained available, such that no unrecognized increase in risk occurred.The inspectors also reviewed a licensee's response to NRC Information Notice 2006-20,"Foreign Material Found in the Emergency Core Cooling System", and in conjunction with licensee actions to resolve Generic Safety Issue 191, "Assessment of Debris Accumulation on PWR Sump Performance".
- 235903, Loss of analog rod position indication on the main control board*230613, Foreign material in residual heat removal suction piping Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified. However, during a refueling outage on April22, 2007, the licensee used a remote video camera to visually inspect the two suction lines between the ECCS sump and RHR pumps A and B. Inspection of the first line revealed a piece of wire approximately 30 inches long, and inspection of the second line revealed a stainless steel insulation band and other smaller items of metallic debris.
These items were immediately removed. The licensee has not completed their engineering evaluations at the end of the inspection period. The inspectors determined that additional inspections are required to determine whether and to what extent the subject debris could have affected safety functions during a postulated event that includes recirculation flow from the ECCS sump. Therefore, this issue is identified asURI 05000261/2007003-01, Emergency Core Cooling Sump Piping Foreign Material.
This issue is in the CAP as AR 230613230613 1R19Post Maintenance Testing
a. Inspection Scope
For the five post-maintenance tests listed below, the inspectors witnessed the testand/or reviewed the test data to verify that test results adequately demonstrated restoration of the affected safety functions described in the UFSAR and TS. Documents reviewed are listed in the Attachment.The following tests were witnessed/reviewed:Test ProcedureTitleRelatedMaintenance ActivityDate InspectedOST-701-5Reactor CoolantSystem Inservice Valve TestValve maintenanceincluding limit switch adjustmentsApril 28OST-302-2Service Water PumpsC & D Inservice TestGrout repair on pumpand motor April 30OST-701-11Radiation MonitoringInservice Valve TestValve maintenanceincluding valve internal work and LLRT failureMay 1
1063174*Train "A" Motor DrivenAuxiliary Feedwater Pump Failed to AutostartReplaced the controlswitchMay 17OST-252-2Residual HeatRemoval System Valve Test Train "B"Valve maintenanceincluding motor torque adjustmentsMay 24* This post-maintenance test was described in the identified work order rather than in aprocedure.
b. Findings
No findings of significance were identified.1R20Refueling and Outage ActivitiesFor the outage that began on April 6 and ended on May 13, the inspectors evaluatedlicensee outage activities as described below to verify that licensees considered risk in developing outage schedules, adhered to administrative risk reduction methodologies they developed to control plant configuration, and adhered to operating license and technical specification requirements that maintained defense-in-depth. The inspectors also verified that the licensee developed mitigation strategies for losses of the following key safety functions:*decay heat removal*inventory control
- power availability
- reactivity control
- containmentIn addition, the inspectors completed their review of Operating Experience SmartSample (OpESS) FY2007-03, Crane and Heavy Lift Inspection, Supplemental Guidance for IP-71111.20. Documents reviewed are listed in the Attachment..1Review of Outage Plan
a. Inspection Scope
Prior to the outage, the inspectors reviewed the outage risk control plan to verify that thelicensee had performed adequate risk assessments, and had implemented appropriate risk-management strategies when required by 10 CFR 50.65(a)(4).
b. Findings
No findings of significance were identified..2Monitoring of Shutdown Activities
a. Inspection Scope
The inspectors observed portions of the cooldown process to verify that technicalspecification cooldown restrictions were followed.
b. Findings
No findings of significance were identified..3Licensee Control of Outage Activities
a. Inspection Scope
During the outage, the inspectors observed the items or activities described below toverify that the licensee maintained defense-in-depth commensurate with the outage risk-control plan for key safety functions and applicable technical specifications when taking equipment out of service.*Clearance Activities*Reactor Coolant System Instrumentation
- Electrical Power
- Decay Heat Removal (DHR)
- Spent Fuel Pool Cooling
- Inventory Control
- Reactivity Control
- Containment ClosureThe inspectors also reviewed responses to emergent work and unexpected conditions toverify that resulting configuration changes were controlled in accordance with the outage risk control plan, and to verify that control-room operators were kept cognizant of the plant configuration.
b. Findings
No findings of significance were identified..4Reduced-Inventory Conditions
a. Inspection Scope
The inspectors reviewed commitments from Generic Letter 88-17, and confirmed by
sampling that those commitments are still in place and adequate. Periodically duringthe reduced-inventory conditions, the inspectors reviewed system lineups to verify that the configuration of the plant systems are in accordance with those commitments.
During reduced-inventory operations, the inspectors observed operator activities to verify that unexpected conditions or emergent activities did not degrade the operators' ability to maintain required reactor vessel level.
b. Findings
No findings of significance were identified..5Refueling Activities
a. Inspection Scope
The inspectors observed fuel handling operations (removal, inspection, and insertion)and other ongoing activities to verify that those operations and activities were being performed in accordance with technical specifications and approved procedures. Also, the inspectors observed refueling activities to verify that the location of the fuel assemblies, including new fuel, was tracked from core offload through core reload.
b. Findings
No findings of significance were identified..6Monitoring of Heatup and Startup Activities
a. Inspection Scope
Prior to mode changes and on a sampling basis, the inspectors reviewed system lineupsand/or control board indications to verify that TSs, license conditions, and other requirements, commitments, and administrative procedure prerequisites for mode changes were met prior to changing modes or plant configurations. Also, the inspectors periodically reviewed RCS boundary leakage data, and observed the setting of containment integrity to verify that the RCS and containment boundaries were in place and had integrity when necessary. Prior to reactor startup, the inspectors walked down containment to verify that debris has not been left which could affect performance of the containment sumps. The inspectors reviewed reactor physics testing results to verify that core operating limit parameters were consistent with the design.
b. Findings
No findings of significance were identified.
.7 Identification and Resolution of Problems
a. Inspection Scope
Periodically, the inspectors reviewed the items that had been entered into the CAP toverify that the licensee had identified problems related to outage activities at an appropriate threshold and had entered them into the CAP. For the significant problems documented in the CAP and listed below, the inspectors reviewed the results of the investigations to verify that the licensee had determined the root cause and implemented appropriate corrective actions, as required by 10 CFR 50, Appendix B, Criterion XVI, Corrective Action.*230551, Damage to CVC-312B check valve seal cap*231270, Inadvertent spent fuel pool level decrease during refueling cavity draindown
- 231446, Water inadvertenly added to the reactor coolant system due tomaintenance on valve SI-870B*231589, Inadvertent start of emergency diesel generator A
- 232630, Deficiencies noted during NRC walkdown of containment A
- 232899, Technical specification interpretation relating to the steam-driven auxiliaryfeedwater pump
b. Findings
No findings of significance were identified.1R22Surveillance Testing
a. Inspection Scope
For the six surveillance tests listed below, the inspectors witnessed testing and/orreviewed the test data to verify that the systems, structures, and components involved in these tests satisfied the requirements described in the TS, the UFSAR, and applicable licensee procedures, and that the tests demonstrated that the SSCs were capable of performing their intended safety functions. Documents reviewed are listed in the
.Test ProcedureTitleDate InspectedOST-252-2RHR System Valve Test - Train BApril 4OST-703-2*Primary Side Inservice Valve Test for RHRSystemApril 26OST-253Comprehensive Flow test for Residual HeatRemovalApril 26
OST-151-4Comprehensive Flow Test for Safety InjectionPump AApril 28OST-411Emergency Diesel Generator BApril 29OST-163Safety Injection Test and Emergency DieselGenerator Auto Start on Loss of Power and Safety Injection (Refueling)May 3*This procedure included inservice testing requirements.
b. Findings
No findings of significance were identified.
Cornerstone:
Emergency Preparedness1EP6 Drill Evaluation
a. Inspection Scope
On June 18, the inspectors observed an emergency preparedness drill to verify licenseeself-assessment of classification, notification, and protective action recommendation development in accordance with 10 CFR 50, Appendix E. The inspectors also attended the post-drill critique to verify that the licensee properly identified failures in classification, notification and protective action recommendation development activities.
Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.2.RADIATION SAFETYCornerstone: Occupational Radiation Safety2OS1Access Control To Radiologically Significant Areas
a. Inspection Scope
Licensee activities for monitoring workers and controlling access to radiologicallysignificant areas were reviewed. The inspectors evaluated procedural guidance and directly observed implementation of administrative and physical controls; appraised radiation worker and technician knowledge of, and proficiency in implementing, radiation protection program activities; and assessed worker exposures to radiation and radioactive material.
Radiological postings and material labeling were directly observed during tours of theUnit 2 (U2) reactor auxiliary building, U2 containment, and radwaste processing areas.
The inspectors conducted independent surveys in these areas to verify posted radiation levels and to compare with current licensee survey records. During plant tours, control of locked high radiation area (LHRA) and very high radiation area (VHRA) keys and the physical status of LHRA doors and accessible VHRA access points were examined. Inaddition, the inspectors observed radiological controls for non-fuel radioactive material stored in the spent fuel pool. The inspectors also reviewed selected radiological control procedures and radiation work permits (RWPs), and discussed current access control program implementation with health physics supervisors.During the inspection, radiological controls for work activities in high radiation areas(HRA) were observed and discussed. The inspectors attended pre-job briefings for radiography and core reload, evaluating the communication of RWP requirements, radiological conditions, and operating experience. The inspectors directly or by remote monitoring observed work activities associated with steam generator (S/G) sludge lancing, S/G eddy current testing, emergency core cooling system (ECCS) sump modification, scaffolding, and various ongoing maintenance activities in the U2 containment. The inspectors directly observed licensee posting and control of boundaries during radiographic operations. The inspectors observed workers' adherence to RWP guidance and health physics technician (HPT) proficiency in providing job coverage. Controls for limiting exposure to airborne radioactive material were reviewed, and operation of ventilation units and positioning of air samplers were also observed. The inspectors evaluated electronic dosimeter alarm setpoints for consistency with radiological conditions in containment and the reactor auxiliary building. In addition, the inspectors interviewed workers in the reactor auxiliary building and containment to assess knowledge of RWP requirements.The inspectors evaluated worker exposures through review of data associated withdiscrete radioactive particle and dispersed skin contamination events. The inspectors also evaluated licensee procedure and process for evaluating internal doses, including review of select internal dose assessments. Controls used for monitoring extremity dose and the placement of dosimetry when work involved significant dose gradients were reviewed. Health Physics Program activities were evaluated against 10 CFR Part 20; TechnicalSpecification (TS) Sections 5.4, Procedures, and 5.7, HRA; Regulatory Guide 8.38, Control of Access to High and Very High Radiation Areas in Nuclear Power Plants; and approved licensee procedures. Licensee guidance documents, records, and data reviewed are listed in the report Attachment.Problem Identification and Resolution An audit, three self-assessments, and twobenchmark reports related to access controls to radiologically significant areas were reviewed. Additionally, select Nuclear Condition Reports (NCRs) associated with radiological controls, personnel monitoring, and exposure assessments were reviewed and discussed with health physics supervisors. The inspectors assessed the ability to identify, characterize, prioritize, and resolve the identified issues in accordance with
Procedure CAP-NGGC-0200, Corrective Action Program , Rev. 18. Specific documentsreviewed are listed in the report Attachment.The inspectors completed 21 of the specified line-item samples detailed in InspectionProcedure (IP) 71121.01.
b. Findings
No findings of significance were identified.2OS2ALARA Planning and Controls
a. Inspection Scope
ALARA The inspectors evaluated ALARA program guidance and its implementation forrefueling outage 24 (RO-24). The inspectors reviewed, and discussed with licensee staff, ALARA work plan (AWP) documents including dose estimates and prescribed ALARA controls for selected outage work activities that incurred significant collective doses. The inspectors reviewed the integration of AWP requirements into work procedures and RWPs. The inspectors reviewed the interfaces between plant departments in regard to implementation of the ALARA program. These elements of the ALARA program were evaluated for consistency with the methods and practices delineated in applicable licensee procedures.The inspectors reviewed the site collective exposure estimates and their bases forcalendar year 2007 and RO-24. The inspectors compared select person-hour estimates provided by maintenance and other planning groups with actual work activity time requirements, evaluated the accuracy of the estimates, and discussed identified differences with the ALARA staff. Changes to dose budgets relative to changes in job scope also were identified and discussed.The inspectors reviewed select shielding request packages with respect to dose ratereduction goals and the associated engineering reviews, as applicable. The inspectors reviewed pre-installation and post-installation radiation surveys associated to shielding request packages to determine the consistency between dose reduction goals and results achieved. Selected work activities were observed for evaluating the use of ALARA controls. Activities observed included: ECCS sump modification, S/G eddy current testing, S/G sludge lancing, and industrial radiography. The inspectors evaluated if the AWP considerations, including engineering controls, were implemented appropriately during job performance. The inspector determined if workers were aware of low dose waiting areas, their electronic dosimeter set points, and the radiological conditions in the area ofwork. The inspectors evaluated whether radiation workers adhered to AWP and RWP requirements, and if radiation worker practices demonstrated the ALARA philosophy. In addition, the inspectors evaluated HPT proficiency in providing pre-job briefings and job coverage.
The inspectors reviewed the controls employed by the licensee for declared pregnantwomen with respect to the requirements of 10 CFR Part 20.ALARA program activities and their implementation were evaluated against 10 CFR19.12; 10 CFR Part 20, Subparts B, C, F, G, H, and J; and approved licensee procedures. In addition, licensee performance was evaluated against Regulatory Guide 8.8, Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear Power Stations will be As Low As Reasonably Achievable. Procedures and records reviewed within this inspection area are listed in the Attachment.Problem Identification and Resolution Licensee CAP documents associated withALARA activities were reviewed and assessed. The inspectors evaluated the ability to identify, characterize, prioritize, and resolve issues in accordance with CAP requirements. Specific assessments, audits, and NCR documents reviewed and evaluated in detail for this inspection area are identified in the Attachment.The inspectors completed ten of the specified line-item samples detailed in IP 71121.02. Together with the sixteen samples documented in IR 05000261/2006003, IP 71121.02 is complete.
b. Findings
No findings of significance were identified.
Cornerstone:
Public Radiation Safety4.OTHER ACTIVITIES 4OA2Identification and Resolution of Problems.1Routine Review of ARsTo aid in the identification of repetitive equipment failures or specific humanperformance issues for followup, the inspectors performed frequent screenings of items entered into the CAP. The review was accomplished by reviewing daily AR reports..2Annual Sample Review
a. Inspection Scope
The inspectors selected AR 200586200586for detailed review. The inspectors selected this ARbecause it relates generally to the Mitigating Systems Cornerstone, in that it involves the reliability and availability of the D instrument air compressor. The inspectors reviewed this report to verify:*complete and accurate identification of the problem in a timely manner;*evaluation and disposition of performance issues;
- evaluation and disposition of operability and reportability issues;*consideration of extent of condition, generic implications, common cause, andprevious occurrences;*appropriate classification and prioritization of the problem;
- identification of root and contributing causes of the problem;
- identification of corrective actions which were appropriately focused to correct theproblem; and*completion of corrective actions in a timely manner.The inspectors also reviewed this AR to verify compliance with the requirements of theCAP as delineated in Procedure CAP-NGGC-0200, Corrective Action Program, and 10 CFR 50, Appendix B. Documents reviewed are listed in the Attachment.
b. Observations and Findings
No findings of significance were identified..3Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of the CAP and associated documents to identifytrends that could indicate the existence of a more significant safety issue. The inspector's review focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1, licensee trending efforts, and licensee human performance results. The inspector's review considered the six-month period of January, 2007, through June, 2007. The review included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the latest monthly and quarterly trend reports.
Corrective actions associated with a sample of the issues identified in the trend reports were reviewed for adequacy. The specific documents reviewed are listed in the
.The inspectors also evaluated the trend reports against the requirements of the CAP asspecified in 10 CFR 50, Appendix B, Criterion XVI, and in Procedures CAP-NGGC-0200, CAP-NGGC-0206, Corrective Action Program Trending and
Analysis.
b.Assessment and ObservationsNo findings of significance were identified. The inspectors evaluated trendingmethodology and observed that the licensee had performed detailed reviews. The licensee routinely reviewed cause codes, involved organizations, key words, and system links to identify potential trends in their CAP data. The inspectors compared the licensee process results with the results of the inspectors' daily screening, and did not
identify any discrepancies or potential trends in the CAP data that the licensee hadfailed to identify.4OA3Event Follow-up.1May 15 Reactor Trip
a. Inspection Scope
Following the reactor trip that occurred on May 15, the inspectors reviewed the status ofmitigating systems and fission product barriers, equipment and personnel performance, and related plant management decisions to assist NRC management in making an informed evaluation of plant conditions. The inspectors also reviewed post-trip activities to verify that the licensee identified and resolved event-related issues prior to restarting the plant. Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.4OA5Other Activities.1(Closed) Temporary Instruction (TI) 2515/166, Pressurized Water Reactor ContainmentSump Blockage (NRC Generic Letter 2004-02)
a. Inspection Scope
The inspectors reviewed Unit 2 implementation of commitments documented in their September 1, 2005, response to Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized Water Reactors. These commitments included the permanent modification of the Containment Building ECCS sump strainer assembly. The inspectors reviewed the sump strainer assembly Engineering Change package (EC), corresponding 10 CFR 50.59 evaluation, and ECCS sump inspection requirements in the Plant Operating Manual. The inspectors conducted a visual walkdown to verify the installed strainer assembly configuration was consistent with drawings and specifications provided in the engineering change packages. The inspectors determined the following answers to the Reporting Requirementsdetailed in TI 2515/166-05 issued 3/16/06:*The licensee implemented plant modifications and procedure changescommitted to in their GL 2004-02 response for Unit 2.*The licensee updated its licensing bases to reflect the corrective actions taken in response to GL 2004-02.
b. Findings and Observations
No findings of significance were identified..2Independent Spent Fuel Storage Installation (ISFSI) Radiological Controls
a. Inspection Scope
The inspectors reviewed gamma-ray, neutron, and contamination surveys of the twoISFSI facilities, 7P-ISFSI (docket No. 72-3) and 24P-ISFSI (docket No. 72-60).
Inspectors also observed performance of routine gamma and neutron surveys, and compared the results to previous surveys and TS limits. The inspectors evaluated implementation of radiological controls, including labeling and posting, and discussedcontrols with health physics supervisory staff. Environmental monitoring results for direct radiation from the ISFSI were reviewed, and inspectors observed the placement of thermoluminescent dosimeters around the facilities.Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20,10 CFR Part 72, radioactive materials license SNM-2502 TS, and NUHOM Certificate of Compliance No. 1004 TS details. Documents reviewed are listed in section
4OA5 of the
report Attachment. The inspectors completed the radiation protection line-item sample activities specified in IP 60855.
b. Findings
No findings of significance were identified.4OA6 Meetings, Including ExitOn April 20, the inspectors discussed results of the onsite radiation protection inspectionwith Mr. T. Walt and other staff members. The inspectors noted that personally identifiable information was reviewed during the course of the inspection but would not be included in the documented report. On April 20, the inspectors discussed results of the inspection described in section 1R08with Mr. C. Baucom and other staff members. The inspectors confirmed that proprietary information was not provided or examined during the inspection. On May 10, the inspectors conducted via telephone a formal exit for the inspectiondescribed in section 4OA5.1, with Mr. T. Walt and other staff members.On July 2, the resident inspectors presented additional inspection results to Mr. E.Kapopoulos and other staff members. The inspectors confirmed that proprietary information was not provided or examined during the inspection.ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- C. Baucom, Acting Manager, Support Services - Nuclear
- L. Baxley, Radiation Control Supervisor
- D. Blakeney, Outage and Scheduling Manager
- B. Clark, Training Manager
- W. Farmer, Engineering Manager
- D. Foster, Acting Operations Manager
- J. Huegel, Maintenance Manager
- E. Kapopoulos, Plant General Manager
- J. Lucas, Nuclear Assurance Manager
- T. Tovar, Radiation Protection Superintendent
- T. Walt, Vice President, Robinson Nuclear Plant
- S. Wheeler, Supervisor, Regulatory Support
NRC personnel
- R. Musser, Chief, Reactor Projects Branch 4
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened05000261/2007003-01URIEmergency Core Cooling Sump Piping ForeignMaterial (Section 1R15)
Closed
- 05000261/2515/166TIPressurized Water Reactor Containment SumpBlockage (NRC Generic Letter 2004-02) (Section
- 4OA5.1)
- Attachment
LIST OF DOCUMENTS REVIEWED
1R04Equipment AlignmentPartial System WalkdownMotor Driven Auxiliary Feedwater system:Drawing G-190197, Feedwater, Condensate and Air Evacuation System Flow Diagram, sheet 1of 4, Rev. 77Drawing G-190197, Feedwater, Condensate and Air Evacuation System Flow Diagram, sheet 4of 4, Rev. 55Procedure
- OP-402, "Auxiliary Feedwater System," Rev. 67Charging system:Drawing 5379-685, "Chemical and Volume Control System Purification and Makeup FlowDiagram, Sheet 2, Rev. 57Deepwell pumps:Procedure
- OP-402, "Auxiliary Feedwater System," Rev. 67
Procedure
- OMM-007, "Equipment Inoperable Record", Rev. 70
- Drawing G-190202, "Primary and Makeup Water System Flow Diagram", Sheet 3, Rev. 301R05Fire ProtectionUFSAR Section3.1.5.6 Fire Zone 20 - Emergency Switchgear Room and Electrical Equipment Area3.7.5 Fire Zone 25F - Turbine Building East Mezzanine
- 3.7.6 Fire Zone 25F - Turbine Building West Mezzanine
- 3.7.7 Fire Zone 25G - Turbine Building Operating Deck
- 3.1.1 Fire Zone 1 - Diesel Generator "B" Room
- 3.1.3.2 Fire Zone 7 - Auxiliary Building HallwayResults from Completed ProceduresOST-627, Functional Test of the Emergency Diesel Generators CO2 Cardox SuppressionSystem (Annual), Rev. 29, dated 1/29/07OST-621, Diesel Generator CO2 System Cylinder Wight Test (Semi-Annual), Rev. 23, dated4/2/07OST-611-1, Low Voltage Fire Detection and Actuation System Zones 1 & 2 (Semi-Annual),Rev. 5, dated 2/17/07OST-611-11, Low Voltage Fire detection and Actuation System Zones 19 & 20 (Semi-Annual),Rev. 4, dated 12/9/06OST-620, Carbon Dioxide Suppression System Weight Test (Semiannual), Rev. 23, dated2/9/07OST-624, Fire Damper Inspection (18-Month), Rev. 20, dated 3/21/06
- OST-628, Function Test of the Halon 1301 System (Annual), Rev. 28, dated 9/5/06
- OST-630, Halon 1301 Suppression System Weight Test (Semi-Annual), Rev. 22, dated 4/1/07
- OST-611-6, Low Voltage Fire Detection and Actuation System Zone 11 & 13 (Semi-Annual),Rev. 3, dated 12/27/06
- A-3AttachmentOST-611-7, Low Voltage Fire Detection and Actuation System Zone 12 (Semi-Annual), Rev. 2,dated 11/29/061R08Inservice Inspection ActivitiesProceduresENG-NGGC-0207, Boric Acid Corrosion Control, Rev. 1TMM-104, System Walkdown Procedure, Rev. 18
- NDEP-2001, Liquid Penetrant Examination (visible, dye, solvent removeable)
- NDEP-0301, Magnetic particle Examination, Rev. 15
- NDEP-0437, Ultrasonic Examination Procedure for Ferritic Pipe Welds, Rev. 1
- TMM-020, Inservice Pressure Testing Program, Rev. 16OtherInservice Inspection Report, Interval 4, Period 2, Online (2006 On-Line)ISI Self-Assessment Report, 8/1-4/2005
- NRC 229085, Procedure use expectations not met
- NCR 228991, VT1 qualified inspector not used for lift rig inspection
- NCR 229555, SG 'B' secondary manway degraded gasket seating surfaces1R11Licensed Operator RequalificationExercise Guide LOCT 06-01Continuing Training Simulator Option form, "[Operating Experience] and additional malfunctionsfor LOCT 01-6 in Cycle 07-1", 5/17/071R12Maintenance EffectivenessAction Requests192736, Yellow [system health] status for Reactor Protection System194211, Unanticipated [Limiting Condition for Operation] entry due to failure of [loop 3Tavg/Delta-T protection channel Thot average summator]
- TM-432N205117, Unanticipated [Limiting Condition for Operation] 3.3.1 entry due to [steam generator Bfeedwater flow transmitter]
- FT-487 failure
- 213638, [low-pressure reactor trip protection signal lead/lag module]
- PM-455A found out oftolerance during [surveillance test]
- MST-004.216145, System 1080 [Maintenance Rule] performance criteria exceeded216382, Guide ring found improperly setOther DocumentsAction Plan [in accordance with procedure
- PLP-121, Troubleshooting Guidelines] for Return ofSystem 1080 to GREENProcedure
- PLP-121, Troubleshooting Guidelines, Rev. 5
- System 1080 health report
Procedure
- CM-102, Nozzle Relief Valve Maintenance, Rev. 36
- A-4AttachmentProcedure
- EST-111, Safety Pressure Relief & Vacuum Breaker Valve Test Selection andVerification (Refueling Shutdown and As Needed After Maintenance), Rev. 14Procedure
- EST-112, Pressure Safety and Relief Valve Bench Testing, Rev. 23Maintenance Rule DocumentsFor system 1080, Reactor Protection System:*Event List for December, 2005 - June, 2007
- Scoping and Performance Criteria
- Monitoring Status1R13Maintenance Risk Assessments and Emergent Work EvaluationProcedure
- OMM-048, Work Coordination and Risk Assessment, Rev. 28
- 1R15Operability EvaluationsAction Requests230613,
- Foreign material in residual heat removal suction piping CorrespondenceLetter from A. Schwencer (NRC) to Mr. J.A. Jones dated 10/29/1979NO-80-1133, Request for Technical Specification Change Rod Position Indication System,August 1, 1980GD-79-3214, letter to NRC from E.E. Utley, dated December 14, 1979
- NLU-80-465, [Amendment No. 48]ProceduresOST-020, Shiftly Surveillances, Rev. 28EST-139, [Emergency Core Cooling System] Sump Inspection, Rev. 2
- PLP-047, Foreign Material Exclusion Area Program, Rev. 11Other DocumentsEngineering Service Request 97-00611, Rod Position Indication Drift, Rev. 1TS 3.1.7, Rod Position Indication and Bases Operator log entries from 5/27/2007,
- UFSAR section 7.7.1.1.5.1, Analog [Rod Position Indication] System
[Residual Heat Removal] Suction Debris Action Items, Rev. 0, 6/7/2007
- Installation Data Report for S-143, 3/29/98Work Request/Job Orders97-AEUU1, Install the [emergency core cooling system] sump screens, S-143-1 thru S-143-10per [Engineering Service Request] 96-00671 and drawing
- SK-9600671-C-100097-AEUU3, Remove, bag, tag and store approx. 2 [linear feet] of insulation on line 3/4-CH-11A/Inspect and repair insulation in the ECCS sump area for line 3/4-CH-11A97-AEUU4, Support [Engineering Service Request] 96-00671 by setting up [foreign materialexclusion area], remove 2 screens, pump down [residual heat removal] suction piping, install
- A-5Attachmentcover plates over [residual heat removal] pipe and relocate [foreign material exclusion area]to cover plates97-ACCN1, Prepare and paint [emergency core cooling system] sump area ...1R19Post Maintenance TestingProceduresOST-151-4, Comprehensive Flow Test for Safety Injection Pump "A", Rev. 8OST-302-2, Service Water Pumps C & D Inservice Test, Rev. 42
- OST-701-5, Reactor Coolant System Inservice Valve Test, Rev. 18
- OST-701-11, Radiation Monitoring Inservice Valve Test, Rev. 8
- OST-707-11, Radiation Monitoring Valve Position Indication Verification, Rev. 4
- OST-258-2, Residual Heat Removal Valve Position Indicator Verification Train "B", Rev 7
- OST-252-2, Residual Heat Removal System Valve Test Train "B", Rev 16Drawings5379-1082, Safety Injection System Flow Diagram, Sheet 1 of 5, Rev. 435379-1082, Safety Injection System Flow Diagram, Sheet 4 of 5, Rev. 298-190628, Sheet 651, Control Wiring Diagram / [Auxiliary] Feedwater Pump "A", Rev. 255379-376, Component Cooling Water System Flow Diagram, Sheet 2 of 4, Rev 33
- OtherEngineering Change 66771,
- SI-869 Motor Replacement, Rev. 0Work Order
- 01063174, "A" [Motor Driven Auxiliary Feedwater Pump] Failed to Autostart, tasks02 & 031R20Refueling and Outage ActivitiesDrawingsHBR2 10305, Reactor Containment Building Safe Load Path Internals and [Reactor Vessel]Head, Sheet 1, Rev. 4HBR2 10305, Reactor Containment Building Safe Load Path Internals and [Reactor Vessel]Head, Sheet 2, Rev. 4HBR2 10306,
- Reactor Containment Building Safe Load Path Reactor Coolant Pumps andMisc. Loads, Rev. 7HBR2 10307, Fuel Handling Building Safe Load Paths, Rev. 3ProceduresCM-603, Disassembly and Assembly of the Containment Equipment Hatch and Missile Barrier,Rev. 28FMP-019, Fuel and Insert Shuffle, Rev. 34
- GP-007, Plant Cooldown From Hot Shutdown to Cold Shutdown, Rev. 71
- GP-008, Draining the Reactor Coolant System, Rev. 58
- GP-009-2, Filling the Refueling Cavity with Reactor Defueled
- GP-010, Refueling, Rev. 63
- MMM-009, Operation, Testing and Inspection of Cranes and Material Handling Equipment, Rev.57
- A-6AttachmentMRP-004, Reactor Vessel Head Removal and Installation, Rev. 20
- OMM-033, Implementation of CV Closure, Rev. 13
- OMM-033, Implementation of CV Closure, Rev. 18
- OMP-003, Shutdown Safety Function Guidelines, Rev. 21
- OMP-003, Shutdown Safety Function Guidelines, Rev. 27
- OMP-003, Shutdown Safety Function Guidelines, Rev. 29
- OMP-004, Outage Risk Assessment, Rev. 20
- OP-603, Electrical Distribution, Rev. 76
- PLP-006, Containment Vessel Inspection/Closeout, Rev. 61
- PLP-006, Containment Vessel Closeout Inspection, Rev. 71
- PM-125, Crane Hook Inspection Annual, Rev. 23
- PM-132, Containment Polar Gantry Crane Semiannual at Hot or Cold Shutdown Rev. 15
- PRO-NGGC-0200, Procedure Use and Adherence, Rev. 8CorrespondenceGD-78-2207, CP&L to NRC, "Control of Heavy Loads Near Spent Fuel", August 9, 1978NRC letter, "Control of Heavy Loads", dated December 12, 1980
- NO-81-1336, CP&L to NRC, "Control of Heavy Loads", August 12, 1981
- Un-numbered letter, CP&L to NRC, "Control of Heavy Loads -
- NUREG-0612", December 15,1982NLS-85-032, CP&L to NRC, "Control of Heavy Loads", January 30, 1985
- Training PlansMEI0006R, Lift Coordinator
- ME217G, Overhead Crane Operation, Rev. 3
- MEI0005R,
- MMM-009 Operation, Testing, and Inspection of Cranes and Material HandlingEquipment, Rev. 1ME210G, Hydraulic Crane Operation, Rev. 6OtherANSI N14.6 1978, "Standard For Special Lifting Devices tor Shipping Containers Weighing10,000 Pounds (4500 kg) or More For Nuclear Materials" ANSI N14.5-1977, "American National Standard for Leakage Tests on Packages for Shipmentof Radioactive Materials"AR
- 175608, Heavy load lifts outside
- NUREG-0612 guidelines Engineering Change 66104, Best Estimate Time to Boil Calculation for Early Equipment HatchRemovalGID/R87038/0007, Generic Issues Document Hazards Analysis, Rev. 5
- NUREG-0612, Control of Heavy Loads at Nuclear Power Plants
- OMM-001-6 Post-Trip/Safeguards Review Report, dated 5/15/07
- Self-Assessment Report
- 176381, RNP Rigging and Lifting Program, October 2-6, 2006
- SFP Level and Temperature Monitoring Contingency Plan, Rev. 0
- Technical Evaluation Report]-C5506-389, "Control of Heavy Loads - Phase I Safety EvaluationReport"Work Order
- 00767045, Inspection of the [Containment Vessel] Polar Crane and Hooks,completed 04/09/07Work Order
- 00767046, Containment Polar Crane Inspection, completed 04/07/07
- A-7Attachment1R22Surveillance TestingProceduresOST-252-2, RHR System Valve Test - Train B, Rev. 16OST-703-2, Primary Side Inservice Valve Test for RHR System, Rev. 5
- OST-253, Comprehensive Flow test for Residual Heat Removal, Rev. 41
- OST-411, Emergency Diesel Generator "B" (Twenty-Four Hour Load Test), Rev. 33
- OST-163, Safety Injection Test and Emergency Diesel Generator Auto Start on Loss of Power and Safety Injection (Refueling), Rev. 441EP6 Drill EvaluationEmergency Response Organization Exercise, June 18, 2007Emergency Operating Procedure logic diagram
- PATH-1, Rev. 18
- Emergency Action Level diagram
- EAL-1, Rev. 14
- NEI-99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 4
- 2OS1Access Controls to Radiologically Significant AreasProcedures, Manuals, and Guidance DocumentsPLP-031, Contamination Monitoring Program for Personnel/Personal Effects, Rev. 31
- HPS-NGGC-0016, Access Control, Rev. 3
- HPS-NGGC-0014, Radiation Work Permits, Rev. 4HPS-NGGC-0013, Personnel Contamination Monitoring, Decontamination, and Reporting, Rev.6HPS-NGGC-005, Skin Dose from Contamination, Rev. 8
- HPS-NGGC-0003, Radiological Posting, Labeling, and Surveys, Rev. 10
- DOS-NGGC-0007, Internal Dose Calculations, Rev. 9
- AP-031, Administrative Controls for Entry into Locked and Very High Radiation Areas, Rev. 41
- HPP-500-4, Health Physics - Conduct of Pre-Job Briefings, Rev. 10
- HPP-105, Airborne Radioactivity Surveillance, Rev. 30
- HPP-009, Control of Radiographic Operations, Rev. 19
- HPP-008, Steam Generator Inspection and Maintenance, Rev. 25
- HPP-006, Radiation Work Permits, Rev. 70
- HPP-003, Control of Hot Particles, Rev. 12
- HPP-001, Radiologically Controlled Area Surveillance Program, Rev. 88Records and Data ReviewedRWP 3998, S/G Eddy Current Support ActivitiesRWP 3997, Remove/Install S/G Primary Manways and Diaphragms
- RWP 3996, S/G Sludge Lance Activities
- RWP 3999, S/G Eddy Current and Tube Plugging Activities
- RWP 3567, Filter Changeouts
- RWP 3588, Radiography Activities
- RWP 4078, S/G Eddy Current Support Activities
- RWP 3576, Reactor Head Disassembly/Reassembly/Cavity Activities Penetration E-5 Radiography Plan, 4/17/07
- A-8AttachmentSurvey
- 041807-56, CV First Level, RoutineSurvey
- 041207-29, CV First Level at Head Storage Survey
- 041007-27, CV First Level at RHR Line Survey
- 040707-54, CV Second Level, Initial Radiation Survey Survey
- 041807-37, CV Second Level, Routine Survey
- 041607-36, CV Third Level, Post Cavity Drain Survey
- 041807-43, CV Third Level, Routine Survey
- 041907-28, CV Third Level, Clean Reactor Studs/Nuts Survey
- 041507-33, "C" S/G Platform, Initial Survey Following Draining of Secondary Side Survey
- 041707-41, CV Level 2 Overhead Feedwater Piping Survey PassPort Dose Report, 8/1/06-4/14/07
- DRD Alarm Evaluations, 8/1/06-4/18/07
- Contamination Occurrence Log, 8/15/06-4/17/07
- Internal Dose Assessment, intake date 4/8/07 19:53
- Personnel Contamination Event Record (Event 1, 4/16/06; Event 2, 4/17/07)
- U2 Hot Particle Gamma Scan, 4/17/07Audits and Self-AssessmentsR-RP-06-01, Robinson Nuclear Plant Radiation Protection Assessment Report, 11/16/06Self-Assessment
- 176400, Radiation Work Permits, 7/28/06
- Self-Assessment
- 176399, Radioactive Material Storage in Outside Areas, 7/20/06
- Benchmark
- 176323, 12/18/06
- Benchmark
- 176321, 10/28/06Nuclear Condition Reports (NCRs)209651, R-RP-06-01 NAS Assessment Weakness #3, 10/18/06200725, Weakness #2 - Self-assessment #176399, 7/20/06
- 200726, Weakness #3 - Self-assessment #176399, 7/20/06
- 23190, Evaluate applicability: Riverbend NCV on alpha survey, 2/20/07
- 216862, Increase negative observations in radworker practices, 12/18/06
- 2219, Self-assessment #176400, weakness #1 - worker's RWP knowledge, 8/3/06
- 2223, Self-assessment #176400, weakness #2, 8/3/06
- 208287, LHRA key box lock is not uniquely keyed, 10/4/06
- 216960, Personnel contamination occurrences during filter change, 12/19/06
- 24163, Individuals entered a RMA without electronic dosimetry, 3/1/072OS2ALARA Planning and ControlsProcedures and Guidance DocumentsADM-NGGC-0105, ALARA Planning, Rev. 7ERC-004, Setup and Use of Temporary ALARA Equipment, Rev. 12
- MNT-NGGC-0003, Radiation Shielding Use, Rev. 10
- HPP-500-3, Radiation Control Work Planning Process, Rev. 15
- HPP-252, Spent Resin Transfer to Waste Processing Containers, Rev. 18
- A-9AttachmentHPS-NGGC-0014, Radiation Work Permits, Rev. 4NGGM-PM-0002, Radiation Control & Protection Manual, Rev. 35
- DOS-NGGC-0004, Administrative Dose Limits, Rev.9
- CAP-NGGC-0200, Corrective Action Program, Rev. 19
- PLP-016, Radiation Work Permit Program, Rev. 29
- Records and DataProgress Energy, H. B. Robinson Nuclear Plant, 2006 ALARA Report, 02/28/2007
- Radiation Work Permit (RWP) 3586, Scaffolding Activities (ALARA Task
- 864212 09 01)
- 772582 01 01)
- 864212 20 05)
- 864212 29 01)
- 864212 29 02)
- 864212 33 02)
- 864212 29 03)
- 864212 29 17)
- 864212 29 22)
- 864212 31 04)
- 86421220 03)Temporary Shielding Request (TSR)07-045, Excess Letdown Heat Exchanger, Rev. 0
- TSR 07-049, Bottom of "C" Pump Bay on line 10-SI-54, Rev. 0
- TSR 07-046, Excess LD Hx,
- CVC 200 Valves, & RCDT, Rev. 0
- TSR 07-042, Grating at "A" RCP Pump Platform, Rev. 0
- TSR 07-041, Floor Grating at Seal Table Room, Rev. 0
- In-progress ALARA Evaluations #24-027,24-007, 24-007,24-011, 24-026 dated 04/16/07,04/10/07, 04/19/07, 04/18/07, and 04/18/07 respectively.2007 Projected and Actual monthly dose by unit reports (document not dated)
e-mail message from G. Kirven to
- RNP-Site Wide Re: March 2007 Site Dose Status, datedApril 3, 2007ALARA Work Plan (AWP)24-036, Check Valve Inspections/Radiography, Rev. 0
- AWP 24-019, Reactor Head Work and Refueling Activities, Rev. 0
- AWP 24-020, Scaffolding, Rev. 0
- AWP 24-027,
- RO-24 S/G Sludge Lance Project, Rev. 0
- RO-24 Daily RC Status Reports dated April 18-20, 2007
- ALARA Review Status Reports dated April 18-20, 2007Nuclear Condition Reports203613, Excessive Dose Received During Resin HIC Shipment, 8/17/06216069, ALARA Self-Assessment Issue #1, 12/11/06
- 20183, "C" Steam Generator Repair Dose Exceeds Projection, 1/24/07
- 217272, RNP NAS
- RO-24 Pre-Outage Assessment, 12/22/06
- A-10Attachment172133,
- HPP-252, Rev. 17, Spent Resin Transfer to Waste Processing Containers, 10/10/05200180,
- HPP-252, Rev. 18, Spent Resin Transfer to Waste Processing Containers, 7/14/06
- 4OA2Identification and Resolution of ProblemsNuclear Condition Report
- AR 200586200586 Second trip of the "D" [instrument air compressor], afterrepairs had been completedProcedure
- CAP-NGGC-0205, Significant Adverse Condition Investigations, Rev. 54OA3Event Follow-upProcedure
- OMM-001-6, Operations Assessments, Rev. 17Post Trip/Safeguards Review Report, dated 5/15/07 and prepared in accordance withprocedure
- OMM-001-6Work Order
- 01063174-03, "A" [Motor Driven Auxiliary Feedwater] Pump Failed to Autostart4OA5Other ActivitiesProceduresRST-025, Surveillance of the 7P-Independent Spent Fuel Storage Installation, Rev. 13
- RST-030, Surveillance of the 24P-Independent Spent Fuel Storage Installation, Rev. 2
- HPP-010, Control of Radioactive Materials Outside of the Primary Radiation Control Area, Rev.18EST-139, ECCS Containment Sump Inspection, Rev. 8Documents/RecordsRC-05-002, Evaluation of Dose Impacts from Dry Fuel Storage Activities and New SiteFacilities, 1/3/07Area TLD Trending Results, 10/3/06-1/10/07RST-025, performed 9/1/06 and 1/29/07RST-030, performed 9/12/06, 12/4/06, and 2/27/07
- 176330, Cross-Function Review of the ISFSI Program/System, 7/13/06
- AR 231689231689 10
- CFR 50.59 Evaluation for EC 63481