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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20042F9581990-05-0707 May 1990 LER 90-001-01:on 900124,shift Surveillance Log Did Not Meet Requirements of Tech Specs.Caused by Deficient Procedure. Surveillance Log Revised to Include Daily Instrument Check. W/900507 Ltr ML19332E7591989-11-27027 November 1989 LER 89-008-00:on 891027,primary Containment Isolation Sys Group II & III Isolations Occurred When Spurious Reactor Low Level Signal Sensed by Instruments.Possibly Caused by Air Bubble in Sensing Lines.Line backfilled.W/891127 Ltr ML20024A4251983-05-26026 May 1983 LER 83-010/03L-0:on 830427,sample Line Flow Meter Indicated No Flow & 3-way Selector Valve SV-2524 Found Stuck.Caused by Dirt Buildup Inside Solenoid Valve, (Asco Model S-36-734). Valve Tapped & Flow Returned ML20027E6441982-11-0505 November 1982 Revised LER 82-021/01P:on 821101,3A Reactor Bldg Vent Stack Radiation Monitor Found to Have Less than Desired Sensitivity.Caused by Drift in Channel Voltage Plateau. Monitor Calibr & Returned to Svc ML20027D9201982-10-28028 October 1982 LER 82-019/03L-0:on 820928,floor Cable Penetration Found W/ 1.5-square-inch Gap Due to Broken Marinite Barrier Board. Probably Caused by Impact to Kick Plate Encompassing Cable Tray Penetration.Board Repaired ML20027B1771982-09-0707 September 1982 LER 82-022/03L-0:on 820820,main Control Room Intake Air Radiation Monitor B Failed Downscale.Caused by Defective Geiger-Mueller tube,194X927GO11.Tube & Associated Electronics Replaced.Detector Recalibr ML20003C3281981-02-23023 February 1981 LER 81-008/03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 ML20003C3331981-02-23023 February 1981 LER 81-014/03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 ML19318D1051980-06-30030 June 1980 LER 80-031/03L-0:on 800605,during Surveillance Test,Pressure Switch Ps 3 5 12C Found 0.3 Psig Above Tech Spec Limit. Caused by Setpoint Drift.Switch Recalibr,Tested & Returned to Svc ML19331C7811980-06-19019 June 1980 LER 80-012/03L-0:on 800520,during Full Power Operation, Routine Testing Revealed Pressure Switch 5121B Setpoint at 700 Psi Above Tech Spec.Caused by Personnel Error.Setpoint Adjusted.Technician Instructed ML19323F2081980-05-21021 May 1980 LER 80-010/03L-0:on 800421,while Performing Surveillance Test,Lpci Injection valve,MO-3-10-25B,failed to Open.Caused by Lack of Guide Clearance Between Valve Disc & Valve Guide. Valve Was Repaired & Stroked Satisfactorily ML19305A9071980-03-0606 March 1980 LER 80-004/03L-0:on 800205 During Plant Startup,Reactor Water Conductivity Increased & Exceeded Tech Spec Limits. Caused by Resin Injection.Reactor Was Shut Down & Primary Coolant Chemistry Brought within Tech Spec Limits ML20008D6821979-12-21021 December 1979 LER 79-053/01T-0:on 791207,jumper,installed to Restore Manual Operation to Recirculation Sys Sample Isolation Valve That Failed to Open,Was Found to Inhibit Automatic Isolation.Caused by Technical Personnel Error ML19291B9611979-12-0505 December 1979 LER 79-051/01T-0:on 791121,fire Pump Controls Removed from Svc to Permit Mod on Fire Header.Diesel Pump Found to Be Inoperable.Caused by Dirty Relay Contacts in Regulator Circuit.Contacts Cleaned & Pump Returned to Svc ML19210D6251979-11-16016 November 1979 LER 79-049/01T-0:on 791101,four Seismic Supports Found W/Safety Factors of Less than Two.Caused by Engineering Design Deficiency.Redesign Performed.Corrective Action Implemented within Seven Days ML19249F0051979-09-27027 September 1979 LER 79-039/03L-0:on 790828,inadvertently Opened Drain Valve Caused Inoperability of Channel B of Main Steamline D High Flow Isolation Signal.Caused by Blow by Scaffolding Being Transported Through Area.Valve Closed ML19249E4491979-09-20020 September 1979 LER 79-042/01T-0:on 790906,seismic & Redundancy Design Deficiencies Re Electrical Feeds Were Found on Containment Atmosphere Dilution Sys Valves & Instrumentation.Caused by Inadequate Design by A/E.Control Cables Installed ML19249E1011979-09-18018 September 1979 LER 79-026/01T-0:on 790904,anchor 3-23-DDN-525 Identified as Failure.Caused by Improper Installation.Anchor Plates Attached to New Plates by Means of Fillet Welds ML19208A7681979-09-11011 September 1979 LER 79-037/03L-0:on 790812,A&B Control Room Intake Air Radiation Monitors a & B Failed Downscale.Caused by Transistor Circuit Failure within Monitors.Monitor a Replaced & Monitor B Repaired ML19207B8651979-08-29029 August 1979 LER 79-024/01T-0:on 790815,during Response Tests for IE Bulletin 79-02,three or Four Failed Anchor Bolts Were Found on Support to 3D RHR Pump Section Piping.Caused by Improper Installation.Bolts Replaced & Passed Insp ML19249A2731979-08-13013 August 1979 LER 79-022/03L-0 on 790719:annunciator Sys II Drywell Pressure Permits Containment Spray Alarmed During Routine Startup.Caused by Failure of Diaphragm on PS-3-10-119D. Switch Repaired,Tested & Returned to Svc within Five Days ML19225C8031979-07-26026 July 1979 LER 79-033/01T-0 on 790712:two shell-type Anchors Failed Torque Test.Caused by Improper Installation.Bolts Replaced & Successfully Tested ML19248C9921979-07-24024 July 1979 LER 79-016/03L-0 on 790628:while at Power,Routine Surveillance Test Revealed Setpoint of Switch 2 Was Below Tech Spec Min.Caused by Barton Model 288 Instrument Out of Calibr from Drift.Instrument Recalibr ML19247A0721979-07-20020 July 1979 LER 79-031/03L-0 on 790622:during Electrical Storm,Lost Main Stack Sampling Sys & Automatic Initiation Capability. Caused by Blown Fuses from lightning-induced Electrical Transient.Fuses Replaced ML19241A6941979-06-27027 June 1979 LER 79-013/01T-0 on 790613:main Steam Relief Valve RV3-2-71L Lifted,Causing Torus Water Vol to Exceed Tech Spec Limit by 2.6%.Reactor Manually Scrammed.Valve Replaced & Sent to Wiley Lab to Determine Cause for Failure ML19274F2251979-06-0808 June 1979 LER 79-026/01T-0 on 790524:during Startup,Offgas Stack Radiation Monitors Were Inoperable for 9-h,due to Failure of Operating Sample Pump.Caused by Broken Belt.Belt Replaced ML19270G4621979-06-0101 June 1979 LER 79-024/01T-0 on 790517:support for Control Rod Drive Line Return Line Outside Containment Does Not Meet Seismic Requirements.Seismically Qualified Pipe Support Designs Completed.Mods to Designs Scheduled to Begin 790601 ML19276F8831979-04-17017 April 1979 LER 79-014/03L-0 on 790327:trip Setpoint Drift of Drywell High Pressure Switch Was Beyond Tech Spec Limit.Caused by Static-O-Ring Model 12N-AA4 Being Out of Calibr Due to Setpoint Drift.It Was Recalibrated & Returned to Svc ML19282C1701979-03-14014 March 1979 LER 79-006/03L-1 on 790212:at Power & During Surveillance Test,Setpoint of B Core Spray Pump Start Timer Was Less than Tech Spec Min.Caused by Setpoint Drift on GE Model CR-2820 Time Delay Relay.Relay Readjusted & Tested ML19282C1531979-03-14014 March 1979 LER 79-007/03L-0 on 790212:during Surveillance,Setpoint of a Logic Automatic Depressurization Sys Time Delay Relay Was Greater than Tech Spec Limit.Caused by Setpoint Drift on GE Model CR-2820 Time Delay.Relay Readjusted & Tested ML19282C1591979-03-12012 March 1979 LER 79-010/01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase ML19269D1301979-02-0909 February 1979 LER 79-001/03L-0 on 790111:discovered That Recorded hi-hi Trip Valve for Steam Line Radiation Monitor Was 50 man-rem/h Greater than Tech Spec Limit & No Corrective Action Taken. Caused by Procedural Deficiency ML19269B9441979-01-10010 January 1979 LER 78-049/03L-0 on 781218:surveillance Testing Revealed B Rod Block Monitor Set Points Had Shifted Upwards Approx 15%. Caused by Failure of Zener Diode in Flow Bias Circuitry Power Supply ML19289F1681978-09-22022 September 1978 LER 78-038/01T-0 on 780908:one Point on Piping Outboard MO-12-15 Had Stress During DBE Above Code Allowable. Restraint to Be Added to Code 1990-05-07
[Table view] Category:RO)
MONTHYEARML20042F9581990-05-0707 May 1990 LER 90-001-01:on 900124,shift Surveillance Log Did Not Meet Requirements of Tech Specs.Caused by Deficient Procedure. Surveillance Log Revised to Include Daily Instrument Check. W/900507 Ltr ML19332E7591989-11-27027 November 1989 LER 89-008-00:on 891027,primary Containment Isolation Sys Group II & III Isolations Occurred When Spurious Reactor Low Level Signal Sensed by Instruments.Possibly Caused by Air Bubble in Sensing Lines.Line backfilled.W/891127 Ltr ML20024A4251983-05-26026 May 1983 LER 83-010/03L-0:on 830427,sample Line Flow Meter Indicated No Flow & 3-way Selector Valve SV-2524 Found Stuck.Caused by Dirt Buildup Inside Solenoid Valve, (Asco Model S-36-734). Valve Tapped & Flow Returned ML20027E6441982-11-0505 November 1982 Revised LER 82-021/01P:on 821101,3A Reactor Bldg Vent Stack Radiation Monitor Found to Have Less than Desired Sensitivity.Caused by Drift in Channel Voltage Plateau. Monitor Calibr & Returned to Svc ML20027D9201982-10-28028 October 1982 LER 82-019/03L-0:on 820928,floor Cable Penetration Found W/ 1.5-square-inch Gap Due to Broken Marinite Barrier Board. Probably Caused by Impact to Kick Plate Encompassing Cable Tray Penetration.Board Repaired ML20027B1771982-09-0707 September 1982 LER 82-022/03L-0:on 820820,main Control Room Intake Air Radiation Monitor B Failed Downscale.Caused by Defective Geiger-Mueller tube,194X927GO11.Tube & Associated Electronics Replaced.Detector Recalibr ML20003C3281981-02-23023 February 1981 LER 81-008/03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 ML20003C3331981-02-23023 February 1981 LER 81-014/03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 ML19318D1051980-06-30030 June 1980 LER 80-031/03L-0:on 800605,during Surveillance Test,Pressure Switch Ps 3 5 12C Found 0.3 Psig Above Tech Spec Limit. Caused by Setpoint Drift.Switch Recalibr,Tested & Returned to Svc ML19331C7811980-06-19019 June 1980 LER 80-012/03L-0:on 800520,during Full Power Operation, Routine Testing Revealed Pressure Switch 5121B Setpoint at 700 Psi Above Tech Spec.Caused by Personnel Error.Setpoint Adjusted.Technician Instructed ML19323F2081980-05-21021 May 1980 LER 80-010/03L-0:on 800421,while Performing Surveillance Test,Lpci Injection valve,MO-3-10-25B,failed to Open.Caused by Lack of Guide Clearance Between Valve Disc & Valve Guide. Valve Was Repaired & Stroked Satisfactorily ML19305A9071980-03-0606 March 1980 LER 80-004/03L-0:on 800205 During Plant Startup,Reactor Water Conductivity Increased & Exceeded Tech Spec Limits. Caused by Resin Injection.Reactor Was Shut Down & Primary Coolant Chemistry Brought within Tech Spec Limits ML20008D6821979-12-21021 December 1979 LER 79-053/01T-0:on 791207,jumper,installed to Restore Manual Operation to Recirculation Sys Sample Isolation Valve That Failed to Open,Was Found to Inhibit Automatic Isolation.Caused by Technical Personnel Error ML19291B9611979-12-0505 December 1979 LER 79-051/01T-0:on 791121,fire Pump Controls Removed from Svc to Permit Mod on Fire Header.Diesel Pump Found to Be Inoperable.Caused by Dirty Relay Contacts in Regulator Circuit.Contacts Cleaned & Pump Returned to Svc ML19210D6251979-11-16016 November 1979 LER 79-049/01T-0:on 791101,four Seismic Supports Found W/Safety Factors of Less than Two.Caused by Engineering Design Deficiency.Redesign Performed.Corrective Action Implemented within Seven Days ML19249F0051979-09-27027 September 1979 LER 79-039/03L-0:on 790828,inadvertently Opened Drain Valve Caused Inoperability of Channel B of Main Steamline D High Flow Isolation Signal.Caused by Blow by Scaffolding Being Transported Through Area.Valve Closed ML19249E4491979-09-20020 September 1979 LER 79-042/01T-0:on 790906,seismic & Redundancy Design Deficiencies Re Electrical Feeds Were Found on Containment Atmosphere Dilution Sys Valves & Instrumentation.Caused by Inadequate Design by A/E.Control Cables Installed ML19249E1011979-09-18018 September 1979 LER 79-026/01T-0:on 790904,anchor 3-23-DDN-525 Identified as Failure.Caused by Improper Installation.Anchor Plates Attached to New Plates by Means of Fillet Welds ML19208A7681979-09-11011 September 1979 LER 79-037/03L-0:on 790812,A&B Control Room Intake Air Radiation Monitors a & B Failed Downscale.Caused by Transistor Circuit Failure within Monitors.Monitor a Replaced & Monitor B Repaired ML19207B8651979-08-29029 August 1979 LER 79-024/01T-0:on 790815,during Response Tests for IE Bulletin 79-02,three or Four Failed Anchor Bolts Were Found on Support to 3D RHR Pump Section Piping.Caused by Improper Installation.Bolts Replaced & Passed Insp ML19249A2731979-08-13013 August 1979 LER 79-022/03L-0 on 790719:annunciator Sys II Drywell Pressure Permits Containment Spray Alarmed During Routine Startup.Caused by Failure of Diaphragm on PS-3-10-119D. Switch Repaired,Tested & Returned to Svc within Five Days ML19225C8031979-07-26026 July 1979 LER 79-033/01T-0 on 790712:two shell-type Anchors Failed Torque Test.Caused by Improper Installation.Bolts Replaced & Successfully Tested ML19248C9921979-07-24024 July 1979 LER 79-016/03L-0 on 790628:while at Power,Routine Surveillance Test Revealed Setpoint of Switch 2 Was Below Tech Spec Min.Caused by Barton Model 288 Instrument Out of Calibr from Drift.Instrument Recalibr ML19247A0721979-07-20020 July 1979 LER 79-031/03L-0 on 790622:during Electrical Storm,Lost Main Stack Sampling Sys & Automatic Initiation Capability. Caused by Blown Fuses from lightning-induced Electrical Transient.Fuses Replaced ML19241A6941979-06-27027 June 1979 LER 79-013/01T-0 on 790613:main Steam Relief Valve RV3-2-71L Lifted,Causing Torus Water Vol to Exceed Tech Spec Limit by 2.6%.Reactor Manually Scrammed.Valve Replaced & Sent to Wiley Lab to Determine Cause for Failure ML19274F2251979-06-0808 June 1979 LER 79-026/01T-0 on 790524:during Startup,Offgas Stack Radiation Monitors Were Inoperable for 9-h,due to Failure of Operating Sample Pump.Caused by Broken Belt.Belt Replaced ML19270G4621979-06-0101 June 1979 LER 79-024/01T-0 on 790517:support for Control Rod Drive Line Return Line Outside Containment Does Not Meet Seismic Requirements.Seismically Qualified Pipe Support Designs Completed.Mods to Designs Scheduled to Begin 790601 ML19276F8831979-04-17017 April 1979 LER 79-014/03L-0 on 790327:trip Setpoint Drift of Drywell High Pressure Switch Was Beyond Tech Spec Limit.Caused by Static-O-Ring Model 12N-AA4 Being Out of Calibr Due to Setpoint Drift.It Was Recalibrated & Returned to Svc ML19282C1701979-03-14014 March 1979 LER 79-006/03L-1 on 790212:at Power & During Surveillance Test,Setpoint of B Core Spray Pump Start Timer Was Less than Tech Spec Min.Caused by Setpoint Drift on GE Model CR-2820 Time Delay Relay.Relay Readjusted & Tested ML19282C1531979-03-14014 March 1979 LER 79-007/03L-0 on 790212:during Surveillance,Setpoint of a Logic Automatic Depressurization Sys Time Delay Relay Was Greater than Tech Spec Limit.Caused by Setpoint Drift on GE Model CR-2820 Time Delay.Relay Readjusted & Tested ML19282C1591979-03-12012 March 1979 LER 79-010/01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase ML19269D1301979-02-0909 February 1979 LER 79-001/03L-0 on 790111:discovered That Recorded hi-hi Trip Valve for Steam Line Radiation Monitor Was 50 man-rem/h Greater than Tech Spec Limit & No Corrective Action Taken. Caused by Procedural Deficiency ML19269B9441979-01-10010 January 1979 LER 78-049/03L-0 on 781218:surveillance Testing Revealed B Rod Block Monitor Set Points Had Shifted Upwards Approx 15%. Caused by Failure of Zener Diode in Flow Bias Circuitry Power Supply ML19289F1681978-09-22022 September 1978 LER 78-038/01T-0 on 780908:one Point on Piping Outboard MO-12-15 Had Stress During DBE Above Code Allowable. Restraint to Be Added to Code 1990-05-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000278/LER-1999-005-03, :on 990920,uplanned Esfas During Planned Mod Activitives in Main CR Were Noted.Caused by Inattention to Detail by Individuals Performing Work.All CR Mods Were Ceased to Allow Review of Mod Work Packages.With1999-10-20020 October 1999
- on 990920,uplanned Esfas During Planned Mod Activitives in Main CR Were Noted.Caused by Inattention to Detail by Individuals Performing Work.All CR Mods Were Ceased to Allow Review of Mod Work Packages.With
ML20217K9931999-10-14014 October 1999 Safety Evaluation Supporting Amend 234 to License DPR-56 ML20217B4331999-10-0505 October 1999 Safety Evaluation Supporting Amend 233 to License DPR-56 05000278/LER-1999-004-03, :on 990901,3A RPS Bus Was Inadvertently Deenergized,During Planned Mod Activities on Main CR Panel. Caused by Electrician Failing to Self Check Work.All CR Work Was Ceased Immediately & Shutdown Meeting Held1999-10-0101 October 1999
- on 990901,3A RPS Bus Was Inadvertently Deenergized,During Planned Mod Activities on Main CR Panel. Caused by Electrician Failing to Self Check Work.All CR Work Was Ceased Immediately & Shutdown Meeting Held
ML20217G3541999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbaps,Units 2 & 3. with ML20216H7091999-09-24024 September 1999 Safety Evaluation Supporting Amends 229 & 232 to Licenses DPR-44 & DPR-56,respectively ML20212D1281999-09-17017 September 1999 Safety Evaluation Supporting Proposed Alternatives CRR-03, 05,08,09,10 & 11 05000278/LER-1999-003-03, :on 990814,HPCIS Was Declared Inoperable Due to Erratic Behavior Resulting in Loss of Single High Train Safety Sys.Caused by Weakness in Procedural Guidance. Readjusted Hydraulic Governor Needle Valve.With1999-09-13013 September 1999
- on 990814,HPCIS Was Declared Inoperable Due to Erratic Behavior Resulting in Loss of Single High Train Safety Sys.Caused by Weakness in Procedural Guidance. Readjusted Hydraulic Governor Needle Valve.With
ML20212A5871999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Peach Bottom,Units 2 & 3.With ML20211D5501999-08-23023 August 1999 Safety Evaluation Supporting Amends 228 & 231 to Licenses DPR-44 & DPR-56,respectively ML20212H6311999-08-19019 August 1999 Rev 2 to PECO-COLR-P2C13, COLR for Pbaps,Unit 2,Reload 12 Cycle 13 ML20210N7641999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for PBAPS Units 2 & 3. with 05000277/LER-1999-005-01, :on 990616,failure to Maintain Provisions of FP Program Occurred.Caused by Less than Adequate Engineering Rigor in Both Development & Review Analysis.Fire Watch Immediately Established.With1999-07-16016 July 1999
- on 990616,failure to Maintain Provisions of FP Program Occurred.Caused by Less than Adequate Engineering Rigor in Both Development & Review Analysis.Fire Watch Immediately Established.With
ML20209H1121999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbaps,Units 2 & 3. with ML20195H8841999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbaps,Units 2 & 3. with 05000278/LER-1999-002-02, :on 990406,safeguard Sys to Unrelated Door Was Inadvertently Disabled by Security Alarm Station Operator. Caused by Noncompliance with Procedures & Less than Adequate Shift Turnover.Briefed Personnel on Event.With1999-05-0606 May 1999
- on 990406,safeguard Sys to Unrelated Door Was Inadvertently Disabled by Security Alarm Station Operator. Caused by Noncompliance with Procedures & Less than Adequate Shift Turnover.Briefed Personnel on Event.With
ML20206N1661999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pbaps,Units 2 & 3. with ML20206A2921999-04-20020 April 1999 Safety Evaluation Concluding That Proposed Changes to EALs for PBAPS Are Consistent with Guidance in NUMARC/NESP-007 & Identified Deviations Meet Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 05000278/LER-1999-001-03, :on 990312,ESF Actuation of Rcics Occurred Due to High Steam Flow Signal During Sys Restoration.Temporary Change to Restoration Procedure Was Initiated to Open RCIC Outboard Steam Isolation Valve in Smaller Increments1999-04-0808 April 1999
- on 990312,ESF Actuation of Rcics Occurred Due to High Steam Flow Signal During Sys Restoration.Temporary Change to Restoration Procedure Was Initiated to Open RCIC Outboard Steam Isolation Valve in Smaller Increments
ML20205K7411999-04-0707 April 1999 Safety Evaluation Supporting Amends 227 & 230 to Licenses DPR-44 & DPR-56,respectively ML20205P5851999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Peach Bottom Units 2 & 3.With ML20207G9971999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Peach Bottom Units 2 & 3.With 05000278/LER-1998-009-01, :on 981227,unplanned Esfa Were Noted.Caused by Transformer Insulator Failure.Replaced Failed Insulator. with1999-01-20020 January 1999
- on 981227,unplanned Esfa Were Noted.Caused by Transformer Insulator Failure.Replaced Failed Insulator. with
ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199E3471998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Peach Bottom,Units 1 & 2.With ML20206D3591998-12-31031 December 1998 1998 PBAPS Annual 10CFR72.48 Rept. with ML20206D3651998-12-31031 December 1998 1998 PBAPS Annual 10CFR50.59 & Commitment Rev Rept. with ML20206P1651998-12-31031 December 1998 Fire Protection for Operating Nuclear Power Plants, Section Iii.F, Automatic Fire Detection 05000277/LER-1998-008-01, :on 981130,circuit Breaker SU-25 Tripped.Caused by Less than Adequate Procedural Guidance.Operators Verified Sys Integrity & Successfully Returned Sys to Svc.With1998-12-30030 December 1998
- on 981130,circuit Breaker SU-25 Tripped.Caused by Less than Adequate Procedural Guidance.Operators Verified Sys Integrity & Successfully Returned Sys to Svc.With
05000277/LER-1998-007-02, :on 981107,failure to Meet TS & Associated LCO Requirments of Absolute Difference in APRM & Calculated Power of Less than 2% Was Noted.Caused by Substitute Valves Being Used.Removed Substitute Valves.With1998-12-0404 December 1998
- on 981107,failure to Meet TS & Associated LCO Requirments of Absolute Difference in APRM & Calculated Power of Less than 2% Was Noted.Caused by Substitute Valves Being Used.Removed Substitute Valves.With
ML20196G7021998-12-0202 December 1998 SER Authorizing Proposed Alternative to Delay Exam of Reactor Pressure Vessel Shell Circumferential Welds by Two Operating Cycles ML20196E8261998-11-30030 November 1998 Response to NRC RAI Re Reactor Pressure Vessel Structural Integrity at Peach Bottom Units 2 & 3 ML20198B8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pbaps,Units 2 & 3. with 05000278/LER-1998-005-03, :on 981025,inadvertent Unit 3 Electrical Bus E33 Trip (Esfa) During Performance of Unit 2 Electrical Bus E32 Surveillance Test Was Noted.Caused by Personnel Error. Sp S12M-54-E32-XXF4 Was Completed.With1998-11-20020 November 1998
- on 981025,inadvertent Unit 3 Electrical Bus E33 Trip (Esfa) During Performance of Unit 2 Electrical Bus E32 Surveillance Test Was Noted.Caused by Personnel Error. Sp S12M-54-E32-XXF4 Was Completed.With
ML20206R2571998-11-17017 November 1998 PBAPS Graded Exercise Scenario Manual (Sections 1.0 - 5.0) Emergency Preparedness 981117 Scenario P84 ML20198C6751998-11-0505 November 1998 Rev 3 to COLR for PBAPS Unit 3,Reload 11,Cycle 12 ML20195E5341998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pbaps,Units 2 & 3. with ML20155C6071998-10-26026 October 1998 Safety Evaluation Supporting Amend 226 to License DPR-44 ML20155C1681998-10-22022 October 1998 Safety Evaluation Accepting Proposed Alternative Plan for Exam of Reactor Pressure Vessel Shell Longitudinal Welds ML20155H7721998-10-12012 October 1998 Rev 1 to COLR for Peach Bottom Atomic Power Station Unit 2, Reload 12,Cycle 13 05000277/LER-1998-006-02, :on 980915,automatic RWCU Isolation Occurred While Placing RWCU Sys in Svc.Caused by Unexpected Surge of Water.Procedure Change Was Initiated to Open MO-2-12-74 & RWCU Sys Was Successfully Returned to Svc.With1998-10-0909 October 1998
- on 980915,automatic RWCU Isolation Occurred While Placing RWCU Sys in Svc.Caused by Unexpected Surge of Water.Procedure Change Was Initiated to Open MO-2-12-74 & RWCU Sys Was Successfully Returned to Svc.With
ML20154J2401998-10-0505 October 1998 Safety Evaluation Supporting Amends 224 & 228 to Licenses DPR-44 & DPR-56,respectively ML20154H4771998-10-0505 October 1998 Safety Evaluation Supporting Amends 225 & 229 to Licenses DPR-44 & DPR-56,respectively ML20154G6631998-10-0101 October 1998 Safety Evaluation Supporting Amends 223 & 227 to Licenses DPR-44 & DPR-56,respectively ML20154G6821998-10-0101 October 1998 SER Related to Request for Relief 01A-VRR-1 Re Inservice Testing of Automatic Depressurization Sys Safety Relief Valves at Peach Bottom Atomic Power Station,Units 2 & 3 ML20154H5541998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Pbaps,Units 2 & 3. with 05000278/LER-1998-004-03, :on 980820,automatic RWCU Isolation Occurred While Placing B RWCU Sys Demineralizer in Svc.Caused by less-than-adequate Control of Equipment.Isolated B Demineralizer & Returned RWCU Sys to Svc1998-09-18018 September 1998
- on 980820,automatic RWCU Isolation Occurred While Placing B RWCU Sys Demineralizer in Svc.Caused by less-than-adequate Control of Equipment.Isolated B Demineralizer & Returned RWCU Sys to Svc
05000277/LER-1998-005-02, :on 980824,noted Failure to Meet TS Actions for Suppression chamber-to-drywell Vacuum Breaker Not Being Fully Seated.Caused by Personnel Failing to Take All TS Required Actions.Temporary Procedure Changes Were Made1998-09-18018 September 1998
- on 980824,noted Failure to Meet TS Actions for Suppression chamber-to-drywell Vacuum Breaker Not Being Fully Seated.Caused by Personnel Failing to Take All TS Required Actions.Temporary Procedure Changes Were Made
ML20153B9651998-09-14014 September 1998 Safety Evaluation Supporting Amend 9 to License DPR-12 ML20151Y2901998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbaps,Units 2 & 3. with 1999-09-30
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nach morum-nir xman on txcruanct (717)456-7014-- '[
- D. M. Smith Vice President - i 4
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November 22, 1989
. Docket No. 50-278
- ' Document Control Desk :
U.!S. Nuclear Regulatory Commission l Washington, DC 20555-
SUBJECT:
Licensee Event Report (LER)
Peach Bottom Atomic Power Station - Unit 3 i This LER concerns an unplanned Engineered Safety Feature (Reactor Protection System) actuation.
Reference:
Docket No. 50-278
. Report Number: 3-89-006 l Revision Number: 00 Event-Date: 10/23/89 Report Date: 11/22/89 Facility: Peach Bottom Atomic Power Station RD 1, Box 208, Delta, PA 17314
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i l This LER is being submitted pursuant to the requirements of 10 CFR 50.73(a)(2)(iv).
Sincerely, 1
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- J. J. Lyash, USNRC Senior Resident inspector
- W. T. Russell, USNRC, Region I jfh20gggj$$ c s
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- . ' APPROvtD OMB NO 310..t.4 LICENSEE EVENT REPORT (LER) ' """' 8 3 0 "
i I I F ACILITY NAME (H DOCE ST NUMStR (21 PAGI (34 'J
' Peach Bottom Atomic Power Station'- Unit 3 o is t o l o l o l 217 l 8 1 loFl014 ,
"' Reactor High Pressure Scram During Reactor Temperature Adjustment Due To Improper-Planning and' Coordination of Multiple Evolutions IVINT DAf t (SI LIR NUM84R (el REPORT DATI 17 OTMth F ACILITits INVOLVED ten MONTH DAY YEAR YEAR 0$$ g' h"' [*f,*,$ MONTH DAY Y E Ar; f actLe t hAuts DOCetti NUMBtHISI O15101010 1 1l
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NAug TE LEPHONE NUM86H Atti A CODE T. E..Cribbe, Regulatory Engineer 71 117 41516 l -l 7101114 COMPLEf t ONE LINE FOR EACM COMPONENT F AILURE DESCRISED IN TMiB REPORT 1131 R ORTA d "" #C CAUSE SYSTEM COMPONENT 'gAC. o qpq g CAU50 systtY COMPONENT "fD NPR I I I I I I i l i l I l l I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED H46 MONTH DAY VIAR SUBMIS$40N VES tir en.
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On October 23, 1989 at 0900 while performing a Hydrostatic test of the Reactor Pressure Vessel (RPV), RPV pressure and temperature were required to be maintained around 1000 psig and greater than 175 degrees Fahrenheit (F). RPV pressure and l' temperature were being maintained by adjusting the Reactor Water Cleanup (RWCU) discharge to radwaste flow (192 degree.F water) to match the Control Rod Drive flow entering the vessel (65 degree F water). RWCU discharge to radwaste was reduced to l maintain RPV drain temperatures above 175 degrees F. During this evolution, RPV pressure indication on the process computer display remained unchanged leading the l
Reactor Operator to believe RPV pressure was under control. The process computer,
-however, had stalled'and was not providing updates, in actuality, RPV pmssure had l' begun a 6 psi per minute increase. At 0939, reactor pressure reached 1056 psig and L .the reactor scrammed on high pressure. The root cause of this event was inadequate planning and coordination of the multiple work activities being performed resulting in the RPV narrow range pressure recorder being out of service and the RPV high pressure alarm (1040 psig) being inoperable. As corrective actions: (1) a Unit Coordinator will be established to coordinate numerous work activities, (2) this ,
event will be reviewed by appropriate Licensed Operators, and (3) the RPV Pressure Surveillance and Hydrostatic Tests will be revised to ensure the RPV narrow range pressure recorder is operable.
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DOCML) NUMBER (21 LER NUM8(R (0) - PA06 (3)
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-Requirements'for the' Report
lThis report is required per 10 CFR 50.73(a)(2)(iv) because of an unplanned Engineered 1 L Safety Feature (Reactor-Protection System (RPS) (EIIS:JC)) Actuation. -)
1 0 Unit Status at-Time of the Event Unit 3 Reactor Mode Switch (EIIS:HS) was in the Refuel position. Reactor Pressure Vessel (RPV):(EIIS:RPV) Hydrostatic (Hydro) testing was in progress.. ]
Unit'3 process computer-(EIIS:ID) had stalled -failing to update the most recent 'l displayed plant parameter process variables. '
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- The RPV narrow range pressure recorder (EIIS:PR) was out of service.
' Unit 3 RPV high pressure alarm (1040 psig) was inoperable.
Description of the Event On October 23, 1989 while performing the RPV Hydro test procedure, RPV pressure and-temperature were required to be maintained around 1000 psig and greater than 175 degrees-Fahrenheit (F), respectively. RPV pressure was being maintained around 1000 psig to simulate normal operating pressure during the performance of Excess Flow Check Valve:(EFCV) (EIIS:V)_ testing per Surveillance Test (ST) 13.8-2 and Control Rod
. Drive (CRD) (EIIS:AA) scram insertion time testing per ST 10.13. At 0930, the RPV drain (EIIS:DRN) temperature was-logged as required by ST 9.12-1 " Reactor Vessel ,
Temperatures" as decreasing to 179.7 degrees F. In' order to increase the RPV drain r temperature, the Unit 3 Reactor _ Operator (RO) (Utility, Licensed) bumped open MO ~12-68-_" Unit 3~ Reactor Water Cleanup (RWCU) (EIIS:CE) Outlet Isolation Valve" increasing the RWCU recirculation flow of 192 degree F water back to the RPV which resulted in a decrease of_RWCU discharge to radwaste flow. The purpose of this action is to minimize the. amount of 192 degree F water being discharged from the RPV >
to offset the 65 degree F CRD water being supplied to the RPV. In a Hydrostatic condition a change in the mass flow rate of water either entering or being-discharged from the RPV will affect RPV pressure. During this evolution RPV pressure indication displayed on the process computer remained unchanged leading the R0 to believe RPV .
. pressure was under control and therefore, it was not necessary to reduce CRD flow .
entering the vessel. The R0 did not realize the process computer was stalled, not ,
updating the displayed plant parameter process variables. In actuality, RPV
-pressure had begun a 6 psi per minute increase. At 0939, reactor pressure reached 1055 psig and the reactor scrammed on high pressure. At the time of the scram the Control Rods were fully inserted. Seconds after the scram the RPV high pressure condition cleared. At 1122, the scram was reset.
-Cause of the Event The root cause of this event was inadequate planning and coordination of the multiple work activities being performed resulting in the narrow range pressure recorder being out of service and the RPV high pressure alarm (1040 psig) being inoperable. A contributing cause associated with this event was the process computer stalling (not updating the displayed plant parameter process variables),
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION - mtovio ove No maiom i
' _ '~ (XPtRES: 8/31/WI -
F ACILBTY NAME (1) Docetti NUE.R (2) LtR NUMSER (6) PA0613)
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fEXT (# mo,e space e soviewed, ese emanans/ MC Form JlsEA sf (In Inadequate planning and coordination ~1ead to multiple Control Room activities which ,
distracted the RO from monitoring other available RPV pressure indications. On going '
concurrent activities that the R0 was involved with during his shift included: (a)
. Control Rod Drive Stroking (performed by a second licensed RO), (b) troubleshooting L
- RPV high' pressure alarm (1040 psig), (c) swapping CRD discharge filters (EIIS:FLT),
(d)troubleshootingM0-14-26B"CoreSprayFullFlowTest. Valve,"(e)EFCVtesting, (f)_RPV parameter readings every 15 minutes in accordance with (IAW) Technical Specifications (IS), (g) RPV parameter readings required every hour IAW TS, and (h)
Local Leak Rate Testing.
The RPV: narrow range pressure recorder and RPV high pressure alarm (1040 psig) were not operable at the time of'the event. Had the narrow range pressure recorc'er been available, it would ha'se been used to~ monitor RPV pressure. Because the narrow range-pressure recorder was out or service the R0 was using the process computer to monitor RPV pressure. During this event, however, the process computer was in a stalled condition (not updating the displayed plant parameter process variables) indicating a
. pressure value corresponding to_the one at the time of the stall. There was no indication that the process computer had stalled, thus the R0 was unaware that the
' computer was not functioning.
I Additionally..had the RPV high pressure alarm (1040 psig) been operable the Operator would.have been alerted to a high RPV pressure condition and the scram may have been prevented. .The annunciator was inoperable because of incomplete maintenance activities.
Analysis of the Event No safety consequences occurred as a result of this event.
At the time'of the event, the Control Rods wcre fully inserted. The RPS initiated the scram signal and its logic functioned properly. Therefore, there were no adverse consequences.
The Main Steam Relief Valves (Ells:RV) were operable and could have functioned to terminate.the pressure rise.
This event would not have occurred at power because the initial conditions, in which the RPV is in a hydrostatic test condition maintaining pressure and temperature using the RWCU and CRD systems, would not be duplicated during power operations.
Corrective Actions The. role of Unit Coordinator will'be established and implemented. The responsibilities of the Unit Coordinator will be to coordinate numerous work e activities to minimize their impact on the operation's shifts.
This avent will be reviewed by Appropriate Licensed Operators.
, The Unit 2 and Unit 3 RPV Prer, ure Test STs (Check Off List (COL) ST 25.1-2 and COL 93T 25.1-3 "RPV Pressure Test Instrumentation") and the Unit 2 and Unit 3 RPV Hydro Test.STs (COL ST 25.2-2 and COL ST 25.2-3 "RPV Hydrostatic Test Instrumentation")
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PACILITY 8sAME (1), DOCKl1 NUMBER G) LER NUMetR (Si PAOL (3)
Peach Bottom Atomic Power Station "'" "UW ' YEO Unit-3' o l5 j o l0 l 0 l 217 l 8 819 -
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will be revised to ensure the RPV narrow range pressure recorder is operable prior to '
the commencement of a RPV Hydro test.
Previous Similar Events One previous'LER 2-85-02 was identified in which a high pressure scram occurred
' during.a RPV Hydro test and EFCV testing. The corrective actions in LER 2-85-02 r
would not have prevented this event because its cause was poor communications. The Control Room R0 increased CRD flow responding'to a pressure decrease caused-by a leaking EFCV. The Test Engineers stopped the EFCV leak without notifying the Control i
' Room and.the subsequent rapid pressure rise resulted in a RPV scram .
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