05000278/LER-1979-024-01, /01T-0:on 790815,during Response Tests for IE Bulletin 79-02,three or Four Failed Anchor Bolts Were Found on Support to 3D RHR Pump Section Piping.Caused by Improper Installation.Bolts Replaced & Passed Insp

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/01T-0:on 790815,during Response Tests for IE Bulletin 79-02,three or Four Failed Anchor Bolts Were Found on Support to 3D RHR Pump Section Piping.Caused by Improper Installation.Bolts Replaced & Passed Insp
ML19207B865
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 08/29/1979
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19207B859 List:
References
LER-79-024-01T-01, LER-79-24-1T-1, NUDOCS 7909050443
Download: ML19207B865 (1)


LER-1979-024, /01T-0:on 790815,during Response Tests for IE Bulletin 79-02,three or Four Failed Anchor Bolts Were Found on Support to 3D RHR Pump Section Piping.Caused by Improper Installation.Bolts Replaced & Passed Insp
Event date:
Report date:
2781979024R01 - NRC Website

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.LE ASE PHINT OR TYPE ALL REQUIRED INFOnMATION)

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d 60 61 DOCKET NUMBER 6d bd EVENT 04Tt 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Inspection program performed in response to IE Bulletin 79-02 identified i

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1 3 of L test failed anchor bolts in one saport en the 3D RHR pump suct-l ion piping. During a seicnic event with the failed anchor support the

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piping system could possibly fail and caase ficoding in one of four RHR l

TT) I rocms. Because redundant RER pumps and backup Core Spray System are j

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40 41 42 43 44 41 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS o l The most probable cause of failure was improper installation. The three I

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