05000277/LER-1979-010-01, /01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase

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/01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase
ML19282C159
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 03/12/1979
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19282C157 List:
References
LER-79-010-01T, LER-79-10-1T, NUDOCS 7903210114
Download: ML19282C159 (1)


LER-1979-010, /01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase
Event date:
Report date:
2771979010R01 - NRC Website

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