AO 50-219/74/35:on 740705,main Steam Line Low Pressure Switches RE23B,C & D Tripped at Pressure Less than Min Required Value of 860 Psig.Caused by Switch Repeatability. GE Requested to Investigate Feasibility of Tech Specs ModML19343C225 |
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Site: |
Oyster Creek |
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Issue date: |
07/15/1974 |
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From: |
JERSEY CENTRAL POWER & LIGHT CO. |
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To: |
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References |
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AO-50-219-74-35, NUDOCS 8103040504 |
Download: ML19343C225 (4) |
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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML19343C2181975-12-23023 December 1975 AO 50-219/75-33:on 751212,during 6-month Load Test on Station a batteries,125 Volt Dc Distribution Ctr de-energized.Caused by Personnel Error in Following Procedure.Distribution Ctr re-energized ML20090C9991975-12-12012 December 1975 AO 75-33:on 751212,125-volt Dc Distribution Ctr of Station a Battery Inadvertently de-energized.Caused by Failure to Establish Proper Breaker Lineup Preparation for Conducting Battery Load Test.Procedure changed.W/751219 Memo ML19343C2191975-12-11011 December 1975 AO 50-219/75-32:on 751203,during Testing,Emergency Diesel Generator 1 Failed to Start When Simulated Loss of Power Condition Applied to Fast Start Logic Circuit.Caused by Failure of Relay to Operate Due to Varnish on Armature ML20126E8281975-12-0303 December 1975 AO 50-219/75-31:on 751124,during Operability Test of Torus to Drywell Vacuum Breakers,Alarm Sys 2 Failed to Annunciate in Control Room When V-26-4 Opened.Caused by Failure of Relay Due to Contacts Being Detective.Relay Replaced ML20090D0071975-11-25025 November 1975 AO 75-31:on 751124,drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-4 Opened. Caused by Component Failure.Corrective Action Under Investigation ML20090D0161975-11-0707 November 1975 AO 75-30:on 751106,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17 a & C Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability.Pressure Switches Recalibr ML20090D0601975-11-0606 November 1975 AO 75-29:on 751027,torus Drywell Vacuum Breakers Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened. Caused by Sticking Microswitch ML20090D0761975-10-28028 October 1975 AO 75-29:on 751027,torus to Drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened.Caused by Component Failure.Corrective Action Under Investigation ML20090D0941975-10-24024 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil Replaced ML20090D1141975-10-17017 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1041975-10-16016 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil replaced.W/751016 ML20090D1341975-10-0808 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressures Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1501975-09-23023 September 1975 AO 75-26:on 750923,emergency Svc Water Pump 52C Failed to Start Automatically During Routine Surveillance Test of Containment Spray Sys Ii.Caused by Failure of Contact Switch in Time Delay Relay 16 K4B.Relay Replaced ML20090D2071975-09-0808 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML19291C2641975-09-0808 September 1975 AO 73-19:when Closing Signal Was Applied to Breaker S1A,loss of Power Occurred at 4160-volt Ac Bus 1A Causing Trip of Various Pumps.Caused by Incorrect Setting of Current Transformer Ratio Matching Taps.Taps Set Properly ML20090D1941975-09-0808 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2151975-09-0202 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML20090D2011975-09-0202 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2241975-08-21021 August 1975 AO 75-23:on 750817-20,stack Effluent for Iodine & Particulates Not Monitored.Caused by Personnel Error.Filter Installed in Operating Stack Gas Sampling Train ML20090D2261975-08-11011 August 1975 Preliminary AO-50-219/75-22:on 750810,stack Gas Sample Line Low Flow Alarm Received.Caused by Stack Gas Sample Pump a Not Running.Thermal Overload Protection Reset ML20090D2471975-08-0404 August 1975 Preliminary AO-50-219/75-21:on 750801,during Routine Surveillance on B Isolation Condensor Sys,Steam Line Valve V-14-32 Failed to Close on Simulation of Steam Line High Flow.Caused by Low Torque Switch Setting.Torque Increased ML20090D2521975-07-17017 July 1975 AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D, A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20090D2561975-07-0909 July 1975 Preliminary AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D,A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20084E1151975-07-0101 July 1975 RO 50-219/75-18:on 750623,two 8-1/2 Inch Handhole Covers in Standby Gas Treatment Filter Train Not in Place.Cause Unknown.Handhole Covers Repositioned & Secured ML20090D2741975-06-27027 June 1975 AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2661975-06-24024 June 1975 Preliminary AO 50-219/75-18:on 750623,handhole Covers in Standby Gas Treatment Filter Train 1-1 Not in Place.Cause Under Investigation.Covers Repositioned & Secured ML20090D2781975-06-24024 June 1975 AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83P & E Tripped at Pressures Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D2731975-06-19019 June 1975 Preliminary AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2901975-06-16016 June 1975 Preliminary AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83B & E Tripped at Pressure Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D6561975-06-0606 June 1975 AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned & Repaired ML20090D2971975-06-0606 June 1975 AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D2981975-06-0202 June 1975 Preliminary AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D6581975-05-30030 May 1975 Preliminary AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned ML20090D6611975-05-14014 May 1975 AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6641975-05-0707 May 1975 Preliminary AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6531975-05-0606 May 1975 AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17B & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatablilty.Switches Recalibr ML20090D6701975-04-28028 April 1975 Preliminary AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 178 & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatability.Switches Recalibr ML20090D6751975-04-18018 April 1975 AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7001975-04-14014 April 1975 AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure.Valves Adjusted &/Or Repaired ML20090D6811975-04-11011 April 1975 Preliminary AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7131975-04-0808 April 1975 AO-50-219/75-09:on 750329,breaker 1C Tripped Resulting in Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7061975-04-0707 April 1975 Preliminary AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure. Valves Adjusted &/Or Repaired ML20090D7271975-04-0303 April 1975 AO-50-219/75-08:on 750325,power Operation Continued W/ Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate.Caused by Failure to Properly Monitor Reactor Core.Rate Reduced ML20090D7211975-03-31031 March 1975 Preliminary AO-50-219/75-09:on 750329,breaker 1C Tripped Due to Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7651975-03-27027 March 1975 AO-50-219/75-07:on 750319,during Standby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Differential Relay Installed ML20090D7361975-03-26026 March 1975 Preliminary AO-50-219/75-08:on 750325,power Operation Continued W/Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate. Caused by Improper Reactor Core Monitoring.Rate Reduced ML20090D7761975-03-20020 March 1975 Preliminary AO-50-219/75-07:on 750319,during Stanby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Relay Installed ML20090D7801975-03-19019 March 1975 AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Continuously Monitor Stack Releases While Reactor in Unisolated Condition.Caused by Circuit Design.Request to Modify Circuit for Stack Gas Sample Pumps Submitted ML20090D7901975-03-13013 March 1975 AO-50-219/75-05:on 750306,during Monthly Surveillance Test, Containment Spray Pump 51A Failed to Start When Subjected to Simulated Signals.Caused by Breaker Trip Bar Failing to Reset After Previous Breaker Trip.Trip Bar Bushings Cleaned ML20090D7811975-03-11011 March 1975 Preliminary AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Monitor Stack Releases While Reactor in Unisolated Condition.Caused by faulty-circuit Design 1975-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000219/LER-1998-011, :on 980914,three Small Bore Pipe Lines Did Not Meet Design Bases for Seismic & Thermal Allowables.Caused by Inadequate Structural Piping Analysis.Two 1/2 Sdcs Lines Were Modified During 17R RFO & 3rd Was Modified During 19991999-09-30030 September 1999
- on 980914,three Small Bore Pipe Lines Did Not Meet Design Bases for Seismic & Thermal Allowables.Caused by Inadequate Structural Piping Analysis.Two 1/2 Sdcs Lines Were Modified During 17R RFO & 3rd Was Modified During 1999
ML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20216H5141999-09-24024 September 1999 Safety Evaluation Supporting Amend 209 to License DPR-16 ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With 05000219/LER-1999-001, :on 990208,prolonged Operation of TB with Condenser & Heater Bay Pressure Less than Design Was Noted. Caused by Lack of Clearly Documented Design Description. Placed Alternate Exhaust Fan in Service.With1999-07-29029 July 1999
- on 990208,prolonged Operation of TB with Condenser & Heater Bay Pressure Less than Design Was Noted. Caused by Lack of Clearly Documented Design Description. Placed Alternate Exhaust Fan in Service.With
ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1999-004, :on 990510,determined That Configurations of Two Pipe Supports in Spent Fuel Pool Cooling Sys Do Not Meet Design Requirements for Deadweight Loads.Caused by Inadequate Analysis.Pipes Upgraded.With1999-06-22022 June 1999
- on 990510,determined That Configurations of Two Pipe Supports in Spent Fuel Pool Cooling Sys Do Not Meet Design Requirements for Deadweight Loads.Caused by Inadequate Analysis.Pipes Upgraded.With
ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195C8141999-06-0202 June 1999 Safety Evaluation Supporting Amend 208 to License DPR-16 ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206U9511999-05-18018 May 1999 Safety Evaluation Supporting Amend 207 to License DPR-16 ML20206P0241999-05-13013 May 1999 Safety Evaluation Supporting Amend 206 to License DPR-16 ML20206P0881999-05-12012 May 1999 Safety Evaluation Supporting Amend 205 to License DPR-16 05000219/LER-1999-003, :on 990402,cable Trays Did Not Meet Separation Criteria.Caused by Inadequate Engineering Review.Fire Watch Was Stationed Immediately Upon Discovery.With1999-04-30030 April 1999
- on 990402,cable Trays Did Not Meet Separation Criteria.Caused by Inadequate Engineering Review.Fire Watch Was Stationed Immediately Upon Discovery.With
ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1999-002-01, :on 990330,fire Protection Deluge Sys Isolation Valve Was Found Out of Position.No Root Cause Determined. Technical Assessment Was Performed.With1999-04-29029 April 1999
- on 990330,fire Protection Deluge Sys Isolation Valve Was Found Out of Position.No Root Cause Determined. Technical Assessment Was Performed.With
ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20205A7451999-03-17017 March 1999 Safety Evaluation Supporting Amend 204 to License DPR-16 05000219/LER-1999-001-02, :on 990208,noted Prolonged Operation of TB with Condenser & Heater Bay Pressure.Caused by Loss of Integrity of Ventilation Envelope (Physical Boundaries).Alternate Exhaust Fan Was Placed in Service.With1999-03-0808 March 1999
- on 990208,noted Prolonged Operation of TB with Condenser & Heater Bay Pressure.Caused by Loss of Integrity of Ventilation Envelope (Physical Boundaries).Alternate Exhaust Fan Was Placed in Service.With
ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-016, :on 981028,single DG Start,Occurred.Caused by Loss of One Source of Offsite Power.Generator Relay Surveillance Revised to Eliminate Possibility of Inadvertent Procedural Breaker Trips.With1999-01-0505 January 1999
- on 981028,single DG Start,Occurred.Caused by Loss of One Source of Offsite Power.Generator Relay Surveillance Revised to Eliminate Possibility of Inadvertent Procedural Breaker Trips.With
ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-019, :on 981118,missed TS Required Surveillance Test.Caused by Inadequate Administrative Controls.Revised Related Surveillance Task Descriptions to Provide Improved Ref.With1998-12-18018 December 1998
- on 981118,missed TS Required Surveillance Test.Caused by Inadequate Administrative Controls.Revised Related Surveillance Task Descriptions to Provide Improved Ref.With
ML20196E2741998-11-30030 November 1998 Safety Evaluation Supporting Amend 203 to License DPR-16 ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-017, :on 981027,discovered That Station Battery Racks Did Not Comply with Seismic Design Basis.Caused by Inadequate Engineering Review.Restored Battery Rack Retainer Plates to Appropriate Configuration.With1998-11-25025 November 1998
- on 981027,discovered That Station Battery Racks Did Not Comply with Seismic Design Basis.Caused by Inadequate Engineering Review.Restored Battery Rack Retainer Plates to Appropriate Configuration.With
05000219/LER-1998-018, :on 981023,DG 2 Failed to Start from App R Local Shutdown Panel During Functional Test.Caused by Incorrectly Designed Wiring.Incorrect Wiring Was Modified & Demonstrated by Testing to Be Correct.With1998-11-23023 November 1998
- on 981023,DG 2 Failed to Start from App R Local Shutdown Panel During Functional Test.Caused by Incorrectly Designed Wiring.Incorrect Wiring Was Modified & Demonstrated by Testing to Be Correct.With
ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155G9311998-11-0404 November 1998 Safety Evaluation Supporting Amend 201 to License DPR-16 ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-014, :on 980928,noted Failure of Isolation Condenser Tube Bundles.Caused by Thermal Stresses/Tgscc Due to Leaky Valve.Replaced Failed Tubes Bundles & Repaired Condensate Return Valve.With1998-10-29029 October 1998
- on 980928,noted Failure of Isolation Condenser Tube Bundles.Caused by Thermal Stresses/Tgscc Due to Leaky Valve.Replaced Failed Tubes Bundles & Repaired Condensate Return Valve.With
05000219/LER-1998-015, :on 980929,SDC Isolation Occurred Due to Equipment Failure.Caused by Damaged Conduit That Appeared to Have Been Damaged by Personnel Error.Instrument Was Repaired & Bypass Was Removed.With1998-10-28028 October 1998
- on 980929,SDC Isolation Occurred Due to Equipment Failure.Caused by Damaged Conduit That Appeared to Have Been Damaged by Personnel Error.Instrument Was Repaired & Bypass Was Removed.With
05000219/LER-1998-013-01, :on 980926,LLRT Results Indicated That MSIV NS03B Exceeded TS Leak Rate Limit.Caused by Component Wear. Maint Was Performed on Subject Valve to Restore Seat Integrity & as-left LLRT Was Acceptable.With1998-10-26026 October 1998
- on 980926,LLRT Results Indicated That MSIV NS03B Exceeded TS Leak Rate Limit.Caused by Component Wear. Maint Was Performed on Subject Valve to Restore Seat Integrity & as-left LLRT Was Acceptable.With
ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R 05000219/LER-1998-012-01, :on 980916,unplanned Actuation of Esfs Occurred.Caused by Written Communication.Procedure Revised to Include Signature Verifications to Install & Subsequently Remove Ohmmeter1998-10-16016 October 1998
- on 980916,unplanned Actuation of Esfs Occurred.Caused by Written Communication.Procedure Revised to Include Signature Verifications to Install & Subsequently Remove Ohmmeter
ML20154M6311998-10-15015 October 1998 Safety Evaluation Supporting Amend 200 to License DPR-16 05000219/LER-1998-011-01, :on 980914,discovered That Three Small Bore Piping Lines Did Not Meet Design Basis Seismic &/Or Thermal Allowables.Caused by Design Deficiency.Subject Lines Will Be Modified During Present Refueling Outage.With1998-10-15015 October 1998
- on 980914,discovered That Three Small Bore Piping Lines Did Not Meet Design Basis Seismic &/Or Thermal Allowables.Caused by Design Deficiency.Subject Lines Will Be Modified During Present Refueling Outage.With
ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification 05000219/LER-1998-010, :on 980724,DG Switchgear Was Found Beyond Design Bases.Caused by Inadequate Installation During Original Construction.Evaluated Temporary Mod to Determine If It Should Be Reclassified as Permanent Mod1998-08-24024 August 1998
- on 980724,DG Switchgear Was Found Beyond Design Bases.Caused by Inadequate Installation During Original Construction.Evaluated Temporary Mod to Determine If It Should Be Reclassified as Permanent Mod
ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B7331998-08-13013 August 1998 Safety Evaluation Supporting Amend 196 to License DPR-16 ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station 05000219/LER-1997-013, Has Been Canceled1998-06-30030 June 1998 Has Been Canceled 1999-09-30
[Table view] |
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Jersey Central Power & Light Companyf %d MADISON AVENUE AT PUNCH BOWL ROAD
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OYSTER CREEK NUCLEAR GENERATING STATION FORKED RIVER, NEW JERSEY 08731 Abnormal Occurrence Report No. 50-219/74/35 Nr JM'o "
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July 5, 1974 Identification of Occurrence Violation of the Technical Specifications, paragraph 2.3.7, main steam line low pressure switches RE23B, C, and D were found to trip at pressures less than the minimum required value of 860 psig. This event is considered to be an abnormal occurrence as defined in the Technical Specifications, paragraph 1.15A.
Conditions Prior to Occurrence The plant was in a routine startup.
The major plant parameters at the time of the event were:
Power: Reactor, 1200 FMt Electric, 399 FMe Flow: Recirculation, 8.6 x 104 gpm Feedwater, 4.5 x 10 6 lb/hr Reactor Pressure: 1020 psig Description of Occurrence On Friday, July 5, 1974, at 1540, while performing a routine surveillance test on the four main steam line low pressure switches, it was discovered that switches RE23B, C, and D tripped at 845, 857, and 854 psig, respectively. These
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2 Abnormal Occurrence No. 50-219/74/35 Page 2 values are below the minimum required trip point of 860 psig which is derived by adding to the Technical Specification limit of 850 psig a 10 psig head correction factor.
Th "as found" and "as left" switch settings were:
"As Found" Settings "As Left" Settings RE23A 864 psig 864 psig RE23B 845 psig 862 psig RE23C 857 psig 863 psig RE23D 854 psig 862 psig Apparent Cause of Occurrence Design is considered to be a major factor contributing to this event. Switch repeatability is a recognized problem and work is in progress to formulate a final solution.
Analysis of Occurrence As indicated in the bases of the Technical Specifications, "The low pressure isolation of the Main Steam Lines at 850 psig was provided to give protection against fast reactor depressurization and the resultant rapid cooldown of the vessel. Advantage was taken of the scram feature which occurs when the Main Steam Isolation Valves are closed to provide the reactor shutdown so that high power operation at low reactor pressure does not occur, thus providing protection for the fuel cladding integrity safety limit."
The adverse consequences of reactor isolation occurring at reactor pressure approximately 15 psig below the specified minimum value of 860 psig is limited to those effects attendant to a greater than normal reactor cooldown rate. The fuel cladding integrity safety limit only comes into effect for power operation at recctor pressures less than 600 psig or for power operation greater than 354 FMt with less than 10's recirculation flow. Therefore, the consequences of a 15 psig lower than normal reactor isolation and scram setpoint has no threatening effect whatsoever on the fuel cladding integrity.
The effects of a too rapid cooldown due to the lower isolation pressure are incensequential since there is less than 2*F difference between the saturation temperature for 850 psig and 835 psig.
Corrective Action The corrective actions being taken at this time are:
- 1. Formal correspondence was initiated with General Electric Company on March 26, 1974 following numerous attempts at informal resolution of this problem. Since then, additional follow up conversation and correspond-ence, as recent as June 4, 1974, has ensued. General Electric has been
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Abnormal Occurrence No. 50-219/74/35 Page 3 requested to investigate the feasibility of a change to the Technical Specifications which would allow for tolerances or deviations on all instrumentation connected with safety systems and proteccive functions.
If this approach cannot be technically justified, General Electric has been requested to develop a basis for a Technical Specification change to reduce the main steam low pressure setpoint considerably lower than the present 850 psig but with an acceptable margin to the 600 psig fuel cladding integrity limit for power operation. The above actions, if taken, will resolve the problem of the main steam line low pressure deviations.
Unfortunately, the approach and response by General Electric has not been entirely satisfactory and has caused delay in our resolution of the matter.
- 2. He Ashcroft switch that was reported in Abnormal Occurrence Nos. 50-219/74/10, 50-219/74/12, and 50-219/74/22 to have been undergoing tests, has been found to give excellent repeatability under contr611ed conditions. However, under conditions similar to that presently found during the surveillance of the Barksdale switches, the repeatability of the Ashcroft switches vary within their design limitations (+ 1% of full scale). hhereas they may be somewhat superior to the Barksdale switches, they still are unsatisfactory for the Technical Specification limiting safety system settings.
Testing is continuing. Consequently, the above stated results are still considered to be preliminary in nature.
- 3. He General Office Review Board has been involved in every instance of instrument setpoint repeatability and has assigned to the General Public Utilities Service Corporation's Electrics 1 Engineering Department the task of problem investigation. He item has been pursued in various Genera?
Office Review Board meetings when appropriate abnormal occurrences have been discussed, and the General Office Review Board, as well as the Plant Operations Review Co=mittee, is committed to following the problem to a final solution. To date, a total of thirteen abnormal occurrences have 3
been identified this year to be the result of instru=entation repeatability I problems. Most, if not all of the setpoint inaccuracies, however, fall within the manufacturer stated tolerances for the instrument involved. This implies that repeatability as such is not in question. Consequently, the preferred action identified in "1" above would appear, at this time, to be l
the only reasonable solution for this condition. Six of the thirteen reports have been generated as a result of " repeatability" of the cain steam l
line low pressure switches. In this case, the alternate action in "1" above will be pursued in the event that the preferred action is not feasible.
l Additionally, the General Public Utilities Service Corporation's Electrical l
Engineering Department has identified other means of monitoring this i parameter and has made recommendations to correct the problem, all of which l involve redesign of the monitoring network from either a techanical and/or electrical standpoint. The Jersey Central Power 6 Light Cocpany Generation Engineering Department is currently investigating with General Electric Co=pany the feasibility of several of these alternate plans recoc= ended by both General Public Ut'lities Service Corporation and the plant staff.
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I Abnormal Occurrence No. 50-219/74/35 Page 4 Manufacturer data pertinent to these switches are. as follows:
Meletron Corporation (subsidiary of Barksdale)
Los Angeles, California Pressure Actuated Switch Model 372 Catalog #372-6SS49A-293 Range 20-1400 psig Proof psi 1750 G Previous abnormal occurrence reports involving these switches are:
- 1. Letter to Mr. A. Giambusso from Mr. D. A. Ross, dated December 24, 1973.
- 2. Abnormal Occurrence Report No. 50-219/74/1
- 3. Abnormal Occurrence Report No. 50-219/74/9
- 4. Abnormal Occurrence Report No. 50-219/74/10
- 5. Abnormal Occurrence Report No. 50-219/74/12
- 6. Abnormal Occurrence Report No. 50-219/74/22 b
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