ML080320562

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IR 05000528-07-012, 05000529-07-012, 05000530-07-012; 04/03/07 - 12/19/07; Palo Verde Nuclear Generating Station, Units 1, 2, and 3; Inspection Procedure 95003, Supplemental Inspection for Repetitive Degraded Cornerstones, Multiple Degraded
ML080320562
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 02/01/2008
From: Collins E
Region 4 Administrator
To: Edington R
Arizona Public Service Co
References
IR-07-012
Download: ML080320562 (162)


See also: IR 05000528/2007012

Text

UNITED STATES

NU CLEAR REGU LATOR Y C O M M I SSI O N

R E GI ON I V

611 R YAN PLAZA D R I V E, SU I TE 400

AR LIN GTON , TEXAS 76011-4005

February 1, 2008

Randall K. Edington,

Executive Vice President Nuclear

and Chief Nuclear Officer

Arizona Public Service Company

P.O. Box 52034

Phoenix, AZ 85072-2034

SUBJECT: PALO VERDE NUCLEAR GENERATING STATION - NRC SUPPLEMENTAL 95003

INSPECTION REPORT 05000528/2007012, 05000529/2007012, AND

05000530/2007012

Dear Mr. Edington:

On December 19, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at your Palo Verde Nuclear Generating Station (PVNGS), Units 1, 2, and 3, facility. The inspection

was conducted in accordance with the guidance contained in NRC Inspection Manual Chapter

(IMC) 0305, Operating Reactor Assessment Program and Inspection Procedure (IP) 95003,

"Supplemental Inspection for Repetitive Degraded Cornerstones, Multiple Degraded Cornerstones,

Multiple Yellow Inputs, or One Red Input," and was performed in response to your facility's

designation as having a Repetitive Degraded Cornerstone, as defined by the NRC's reactor

oversight process. The enclosed report documents the inspection findings, which were discussed

on December 19, 2007, with you and other members of your staff.

In our Annual Assessment Letter dated March 2, 2007, we informed you that PVNGS Unit 3 was

placed in the Multiple/Repetitive Degraded Cornerstone Column (Column IV) of the NRC's Action

Matrix. In accordance with IMC 0305, this decision was made on the basis of two separate safety

significant inspection findings (one Yellow and one White) in the Mitigating Systems cornerstone.

The Yellow finding, open since the fourth quarter 2004, involved a significant section of containment

sump safety injection piping that was void of water at all three PVNGS units. The White finding,

open since the fourth quarter 2006, involved two failures of the Unit 3, Train A emergency diesel

generator. This inspection evaluated the extent of condition of the performance issues, and the

adequacy of the safety culture at PVNGS.

The results of our inspection indicate that your facility is being operated safely. However, the team

identified numerous performance deficiencies that were additional examples of the organizational

and programmatic weaknesses that the NRC had previously identified. Despite previous attempts,

PVNGS had been unsuccessful in implementing changes that result in sustained improvement in

safety system reliability, human performance, problem identification and resolution, the quality of

engineering work products, and oversight of station activities by operations personnel. The

inspection and recent PVNGS safety culture self-assessment activities also identified degradations

in the safety culture of the facility. The team identified weaknesses in organizational characteristics

and attitudes associated with ten of the NRCs thirteen safety culture components. The

Arizona Public Service Company -2-

weaknesses were apparent across several functional groups at the site. This is of concern because

it indicates that, as an overriding priority, nuclear plant safety issues had not always received the

attention warranted by their significance.

The team validated that the root and contributing causes for the performance deficiencies at Palo

Verde included: (1) leaders did not establish, communicate, and enforce standards and

expectations for performance or hold individuals accountable to those standards; (2) the corrective

action program, operating experience, self assessments, and benchmarking did not drive individual

and station performance improvement; (3) responsibility, accountability, and authority for nuclear

safety were not well defined or understood; (4) individual behaviors that demonstrate nuclear safety

principles were not consistently applied; (5) management was not receptive to organizational issues

identified during investigations; (6) change management activities did not anticipate unintended

consequences and did not clearly define and communicate changes to station personnel; and (7)

oversight groups did not provide specific and meaningful interventions to correct declining

performance.

As stated in the June 21, 2007, Confirmatory Action Letter, and subsequently revised with NRC

approval by your letter dated November 28, 2007, you submitted an improvement plan to the NRC

on December 31, 2007. Following the NRCs review of the plan, we will issue a revised

Confirmatory Action Letter including the minimum actions believed necessary to improve

performance and sustain performance improvement. The NRC will also conduct periodic

performance improvement public meetings and inspections until PVNGS demonstrates sustained

performance improvement.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your licenses.

The team reviewed selected procedures and records, observed activities, and interviewed

personnel. A listing of the documents requested by the team for review during the inspection is

available electronically in the NRCs document system (ADAMS) as ML080250295.

The report documents numerous performance deficiencies resulting in 18 NRC identified findings.

The findings represent performance deficiencies in all 7 inspection cornerstones and 10 of the 13

safety culture components. Sixteen of these findings were evaluated under the significance

determination process as having very low safety significance (Green). One finding involving the

failure to update the Final Safety Analysis Report impacted the regulatory process and was

assessed in accordance with the NRC Enforcement Policy. Because of the very low safety

significance of these violations and because they were entered into your corrective action program,

the NRC is treating these findings as noncited violations consistent with Section VI.A of the NRC

Enforcement Policy. The significance of one finding (failure to implement corrective actions for a

risk significant planning standard in the emergency preparedness cornerstone) is being separately

evaluated by the NRC. Additionally, licensee-identified violations which were determined to be of

very low safety significance are listed in this report. If you contest these noncited violations, you

should provide a response within 30 days of the date of this inspection report, with the basis for

your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory

Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the

Arizona Public Service Company -3-

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington DC 20555-

0001; and the NRC Resident Inspector at the Palo Verde Nuclear Generating Station, Units 1, 2,

and 3, facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Elmo E. Collins

Regional Administrator

Dockets: 50-528

50-529

50-530

Licenses: NPF-41

NPF-51

NPF-74

Enclosure:

NRC Inspection Report 05000528/2007012, 05000529/2007012, and 05000530/2007012

w/Attachment: Supplemental Information

cc w/Enclosure:

Steve Olea

Arizona Corporation Commission

1200 W. Washington Street

Phoenix, AZ 85007

Douglas K. Porter, Senior Counsel

Southern California Edison Company

Law Department, Generation Resources

P.O. Box 800

Rosemead, CA 91770

Chairman

Maricopa County Board of Supervisors

301 W. Jefferson, 10th Floor

Phoenix, AZ 85003

Arizona Public Service Company -4-

Aubrey V. Godwin, Director

Arizona Radiation Regulatory Agency

4814 South 40 Street

Phoenix, AZ 85040

Scott Bauer, Director

Regulatory Affairs

Palo Verde Nuclear Generating Station

Mail Station 7636

P.O. Box 52034

Phoenix, AZ 85072-2034

Mr. Dwight C. Mims

Vice President, Regulatory Affairs and

Performance Improvement

Palo Verde Nuclear Generating Station

Mail Station 7636

P.O. Box 52034

Phoenix, AZ 85072-2034

Jeffrey T. Weikert

Assistant General Counsel

El Paso Electric Company

Mail Location 167

123 W. Mills

El Paso, TX 79901

Eric J. Tharp

Director of Generation

Los Angeles Department of Water & Power

Southern California Public Power Authority

P.O. Box 51111, Room 1255

Los Angeles, CA 90051-5700

John Taylor

Public Service Company of New Mexico

2401 Aztec NE, MS Z110

Albuquerque, NM 87107-4224

Geoffrey M. Cook

Southern California Edison Company

5000 Pacific Coast Hwy, Bldg. D21

San Clemente, CA 92672

Robert Henry

Salt River Project

6504 East Thomas Road

Scottsdale, AZ 85251

Arizona Public Service Company -5-

Brian Almon

Public Utility Commission

William B. Travis Building

P.O. Box 13326

1701 North Congress Avenue

Austin, TX 78701-3326

Karen O' Regan

Environmental Program Manager

City of Phoenix

Office of Environmental Programs

200 West Washington Street

Phoenix, AZ 85003

Matthew Benac

Assistant Vice President

Nuclear & Generation Services

El Paso Electric Company

340 East Palm Lane, Suite 310

Phoenix, AZ 85004

Chief, Radiological Emergency Preparedness Section

National Preparedness Directorate

Technological Hazards Division

Department of Homeland Security

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Arizona Public Service Company -6-

Electronic distribution by RIV:

Regional Administrator (EEC)

DRP Director (DDC)

DRS Director (RJC1)

DRS Deputy Director (ACC)

Senior Resident Inspector (GXW2)

Branch Chief, DRP/D (TWP)

Senior Project Engineer, DRP/D (GEW)

Team Leader, DRP/TSS (CJP)

RITS Coordinator (MSH3)

DRS STA (DAP)

V. Dricks, PAO (VLD)

D. Pelton, OEDO RIV Coordinator (DLP1)

ROPreports

PV Site Secretary (PRC)

SUNSI Review Completed: TWP ADAMS: X Yes No Initials: TWP

X Publicly Available Non-Publicly Available Sensitive X Non-Sensitive

R:\_REACTORS\_PV\2007\PV2007-012RP-TWP.doc

RI:SRA RIV:RI RIII:RE RI:SRI RII:SHP RIII:RI

CGCahill MPCatts BJose SMSchneider HJGepford RLSmith

E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/

12/26/07 12/19/07 12/20/07 12/19/07 01/03/08 12/20/07

RIII:RI RIV:SRI RIV:SRI RII:SRI RIII:PE RIV:RE

MAWilk JFDrake SDCochrum SAWalker ARBarker MRBloodgood

E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/

12/18/07 01/07/08 12/20/07 12/19/07 12/21/07 12/26/07

NRR:SHFA RI:OE NRR:HFS OE:ES NRR:SHFA RIV:SRI

VBarnes BCHaagensen MJKeefe JCai DRDesaulniers CCOsterholtz

E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/ E-TWP /RA/

12/24/07 12/27/07 12/20/07 12/20/07 01/04/08 12/24/07

RIV:EPI:DRS NSIR NSIR RIV:SPE:DRP/D RIV:C:DRP/D RIV:DD:DRP

PJElkmann REKahler KWilliams GEWerner TWPruett AVegel

E-TWP /RA/ E-TWP /RA/ T-TWP /RA/ E-TWP /RA/ /RA/ /RA/

01/09/08 01/09/08 01/09/08 12/26/07 01/25/08 01/26/08

RIV:D:DRP RIV:RA

DDChamberlain EECollins

/RA/ /RA/

01/25/08 02/01/08

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-528, 50-529, 50-530

Licenses: NPF-41, NPF-51, NPF-74

Report: 05000528/2007012, 05000529/2007012, 05000530/2007012

Licensee: Arizona Public Service Company

Facility: Palo Verde Nuclear Generating Station, Units 1, 2, and 3

Location: 5951 S. Wintersburg Road

Tonopah, Arizona

Dates: April 3 through December 19, 2007

Team Members: T. Pruett, IP 95003 Team Leader; Chief, Project Branch D

Division of Reactor Projects, Region IV

G. Werner, IP 95003 Assistant Team Leader; Senior Project Engineer,

Region IV

S. Gillum, Secretary, Region IV

Substantive Crosscutting Issues Group

M. Schneider, IP 95003 Group Leader; Senior Resident Inspector,

Region I

H. Gepford, Senior Health Physicist, Region II

M. Wilk, Resident Inspector, Region III

R. Smith, Resident Inspector, Region III

J. Drake, Senior Reactor Inspector, Region IV

R. Kahler, Team Leader, Office of Nuclear Security and Incident

Response

P. Elkmann, Emergency Preparedness Inspector, Region IV

Maintenance and Testing Group

S. Cochrum, IP 95003 Group Leader; Senior Resident Inspector,

Region IV

A. Barker, Project Engineer, Region III

S. Walker, Senior Reactor Inspector, Region II

M. Bloodgood, Reactor Engineer, Region IV

Engineering Group

C. Cahill, IP 95003 Group Leader; Senior Reactor Analyst, Region I

B. Jose, Reactor Engineer, Region III

M. Catts, Resident Inspector, Region IV

M. Villaran, Brookhaven National Laboratory, Contractor

-1- Enclosure

Safety Culture Group

V. Barnes, IP 95003 Group Leader; Senior Human Factors Analyst,

Office of Nuclear Regulatory Research

V. Mehrhoff, Secretary, Las Vegas Site Office

J. Cai, Enforcement Specialist, Office of Enforcement

M. Keefe, Human Factors Specialist, Office of New Reactors

C. Osterholtz, Senior Resident Inspector, Region IV

B. Haagensen, Operations Engineer, Region I

Accompanied By: D. Desaulniers, Senior Human Factors Specialist, Office of Nuclear

Reactor Regulation

K. Martin, Human Factors Engineer, Office of Nuclear Reactor

Regulation

M. Barrientos, Nuclear Safety Council, Spain

Approved By: Dwight Chamberlain, Director

Division of Reactor Projects

-2- Enclosure

CONTENTS

EXECUTIVE SUMMARY ............................................................................................................. 7

SUMMARY OF FINDINGS ......................................................................................................... 10

REPORT DETAILS ..................................................................................................................... 21

1 PERFORMANCE HISTORY ............................................................................................... 21

2 SITE INTEGRATED BUSINESS PLAN (SIBP) AND SITE INTEGRATED IMPROVEMENT

PLAN (SIIP) ........................................................................................................................ 23

3 COLLECTIVE SIGNIFICANCE REVIEW............................................................................. 29

4 NRC METHODOLOGY AND DIAGNOSTIC ASSESSMENT .............................................. 32

5 REACTOR SAFETY STRATEGIC PERFORMANCE ARENA ............................................ 34

5.1 Licensee Controls for Identifying, Assessing, and Correcting Performance

Deficiencies.............................................................................................................. 34

b.1 Failure to Implement Operability Determination Process for Bechtel

Nonconformance Reports

b.2 Failure to Implement Operability Determination Process for Action

Tracking System (ACT)

b.3 Failure to Implement Operability Determination Process for Spray

Pond Missile Hazards

b.4 Failure to Evaluate Abnormally High Lead Levels in Low Pressure

Safety Injection Pump Bearing Oil

b.5 Failure to Implement the Operability Determination Process on

Unit 2 Essential Cooling Water Heat Exchanger 'A' Sleeve Adhesive

b.6 Failure to Implement the Operability Determination Process on

the Unit 2 Essential Cooling Water Heat Exchanger A Tube Leak

b.7 Observations and Minor Noncited Violations Involving Licensee

Controls for Identifying, Assessing, and Correcting Performance

Deficiencies

b.7.1 Corrective Action Program Implementation

b.7.2 Problem Identification and Resolution Root Cause Report

b.7.3 Action Request Review Committee

b.7.4 Backlog Review

b.7.5 Self Assessments

5.2 Design52

b.1 Failure to Implement Adequate Design Controls for Condensate

Storage Tank Temperature

b.2 Inadequate Installation of Fire Sprinklers

b.3 Failure to Enter Environmental Qualification Self Assessment

Deficiencies into the Corrective Action Program

-3- Enclosure

b.4 Failure to Implement Corrective Actions for Operating Experience

Involving the Turbine Driven Auxiliary Feedwater Pump Trip and Throttle

Valve

b.5 Observations and Minor Noncited Violations Involving Design

b.5.1 High Pressure Safety Injection Pump Bearing Modification

5.3 Human Performance ................................................................................................ 61

b.1 Observations and Minor Noncited Violations Involving Human

Performance

b.1.1 Human Performance Root Cause Report

b.1.2 Main Control Room Observations

5.4 Procedure Quality .................................................................................................... 65

b.1 Observations and Minor Noncited Violations Involving Procedure Quality

b.1.1 Procedure Issues

5.5 Equipment Performance .......................................................................................... 66

b.1 Failure to Evaluate Performance Monitoring Criteria for Auxiliary

Feedwater System

b.2 Failure to Control Nonconforming Target Rock Reed Switches

b.3 Failure to Meet the Requirements of Technical Specifications

Surveillance Requirement 3.6.6.6

b.4 Failure to Meet the Requirements of Technical Specifications

Surveillance Requirement 3.0.3

b.5 Untimely Corrective Actions for Submerged Safety Related Cables

b.6 Failure to Properly Evaluate the Extent of Condition of 4160V and 480V

Motor Issues

b.7 Observations and Minor Noncited Violations Involving Equipment

Performance

b.7.1 Environmental Qualification Program

5.6 Configuration Control ............................................................................................... 80

5.6.1 Effectiveness of Corrective Actions ......................................................... 80

b.1 Failure to Implement Corrective Actions for Borg-Warner Check

Valves

5.6.2 Selected System Walkdown .................................................................... 83

b.1 Failure to Maintain Control of Transient Combustibles

b.2 Failure to Install Emergency Lighting in Containment

b.3 Incorrect Installation of Temporary Shielding

b.4 Observations and Minor Violations Involving Selected System

Walkdown

b.4.1 Inadequate Seismic Scaffolding Procedures

5.6.3 Work Control Process.............................................................................. 88

b.1 Failure to Adequately Manage Risk for Switchyard Activities

b.2 Observations and Minor Noncited Violations Involving Work

Control Process

b.2.1 Failure to Properly Document Temporary Modifications

b.2.2 Inadequate Shutdown Risk Assessments

-4- Enclosure

5.6.4 Control of Fission Barriers ....................................................................... 94

b.1 Incorrect Rigging for Personnel Air Lock Door

5.6.5 Review of Individual Plant Examination................................................... 96

5.6.6 Human Performance................................................................................ 96

b. Observations and Minor Noncited Violations Involving Human

Performance

b.1 Inadequate Procedure for Adjustment of Polar Crane Switch

5.6.7 Design .97

b.1 Failure to Maintain Configuration of Pressurizer Instrument

Condensing Pot Support Brackets

b.2 Observations and Minor Violations Involving Design

b.2.1 Lack of Design Control for Breaker Modification

5.6.8 Problem Identification and Resolution .................................................... .99

b.1 Failure to Evaluate Adverse Condition for the Emergency Diesel

Generators

b.2 Failure to Identify and Correct a Non-Conforming Condition

of Post Accident Monitoring Instrumentation Recorders

5.6.9 Equipment Performance ........................................................................ 104

b.1 Failure to Establish Maintenance Rule Goals for the Safety

Injection System

5.7 Emergency Response and Preparedness ............................................................ 105

b.1 Failure to Correct Weakness Associated with Risk Signifivant Planning

Standard 10 CFR 50.47(b)(4)

b.2 Inability to Implement Emergency Action Levels (EALs)

b.3 Observations and Minor Noncited Violations Involving Emergency

Response and Preparedness

b.3.1 Failure to Notify Offsite Agencies of Emergency Action Level

Changes

b.3.2 Failure to Train Emergency Planners

6 RADIATION SAFETY STRATEGIC PERFORMANCE ARENA ........................................ 114

6.1 Occupational Radiation Safety .......................................................................... 114

b.1 Inadequate Briefings on Radiological Conditions

b.2 Observations and Minor Violations Involving Occupational Radiation

Safety

b.2.1 Failure to Conduct Appropriate Radiological Surveys

6.2 Public Radiation Safety ..................................................................................... 116

b.1 Failure to Periodically Update the Final Safety Analysis Report

7 SAFEGUARDS STRATEGIC PERFORMANCE AREA..................................................... 118

-5- Enclosure

8 SAFETY CULTURE ........................................................................................................... 118

8.1 Evaluation of Licensees Independent Safety Culture Assessment .................. 118

8.2 NRC Independent Safety Culture Assessment ................................................. 124

b.1 Decision-Making

b.2 Organizational Change Management

b.3 Resources

b.4 Continuous Learning Environment

b.5 Accountability

b.6 Corrective Action Program

b.7 Work Practices

b.8 Work Control

b.9 Operating Experience

b.10 Self and Independent Assessments

b.11 Environment for Raising Concerns

b.12 Preventing, Detecting, and Mitigating Perceptions of Retaliation

b.13 Safety Policies

9 REVIEW OF YELLOW FINDING - CONTAINMENT SUMP VOIDING .............................. 147

10 REVIEW OF WHITE FINDING - DIESEL GENERATOR K-1 RELAY FAILURE ............... 148

11 LICENSEE-IDENTIFIED VIOLATIONS ............................................................................. 150

12 MANAGEMENT MEETINGS ............................................................................................. 151

ATTACHMENT: SUPPLEMENTAL INFORMATION................................................................ A-1

KEY POINTS OF CONTACT .................................................................................................... A-1

ITEMS OPENED AND CLOSED .............................................................................................. A-2

LIST OF ACRONYMS USED.................................................................................................... A-3

-6- Enclosure

Executive Summary

Palo Verde performance had declined since 2003. The team determined that Palo Verde is

safe for continued operation even though several longstanding performance concerns were

identified.

The root and contributing causes associated with declining performance included: (1) leaders

did not establish, communicate, and enforce standards and expectations for performance or

hold individuals accountable to those standards; (2) the corrective action program, operating

experience, self assessments, and benchmarking did not drive individual and station

performance improvement; (3) responsibility, accountability, and authority for nuclear safety

were not well defined or understood; (4) Individual behaviors that demonstrate nuclear safety

principles were not consistently applied; (5) management was not receptive to organizational

issues identified during investigations; (6) change management activities did not anticipate

unintended consequences and did not clearly define and communicate changes to station

personnel; and (7) oversight groups did not provide specific and meaningful interventions to

correct declining performance.

Multiple substantive crosscutting aspects associated with problem identification and resolution

have existed since 2004. Corrective actions continue to remain ineffective in sustaining

improving performance as noted by effectiveness reviews, external industry reviews, and NRC

inspections. The team determined that personnel often recognized appropriate problem

identification and resolution fundamentals and behaviors when interviewed; however, this

knowledge and understanding of expectations was not consistently demonstrated.

A number of weak or non-existent operability evaluations of degraded conditions affecting

safety-related equipment were identified. A lack of understanding of the need to assess

operability for some conditions adverse to quality and a lack of knowledge or skills necessary to

conduct an operability assessment were apparent. This is a continuing weakness at Palo Verde

and impacts nuclear safety margins. The inability to consistently perform operability

determinations formed part of the NRCs basis for leaving open the Yellow finding involving

voiding of the emergency core cooling suction piping in all three units.

Operating experience opportunities were missed, ignored or misapplied. A lack of technical

rigor was cited in component design basis reviews and self assessments with respect to the

application of operating experience. The station did not appear to have a sense of the

importance and benefits of a strong operating experience program. The failure to incorporate

operating experience into daily activities is an open issue from the Yellow finding. In addition,

the failure to effectively utilize operating experience contributed to several performance

deficiencies identified by the team.

Self-assessments performed by Palo Verde personnel lacked depth and did not always

effectively specify or implement corrective actions. As a result, the self-assessment program

seldom resulted in improved organizational performance. Self-assessment corrective actions

were not always tracked nor were corrective action documents always written to track the

expected actions. The team noted self-assessments conducted by a mix of Palo Verde and

industry personnel led to more meaningful results.

Multiple substantive crosscutting aspects associated with human performance have existed

since 2004. Corrective actions continue to remain ineffective in sustaining consistent

performance improvement as noted by effectiveness reviews, external industry reviews, and

-7- Enclosure

NRC inspections. Human performance concerns observed during this inspection included

weaknesses in implementing the operability determination program, failures to follow

procedures, failures to implement human error prevention tools, inadequate procedures, and

inconsistent implementation of fundamental control room behaviors. The licensees

effectiveness review for human performance concluded that corrective actions were not well

defined and there were no actions for implementation, monitoring, reinforcement, adjustment, or

transfer of human performance changes. Furthermore, the corrective actions were either not

fully implemented or not implemented as intended.

Knowledge gaps and a lack of an effective emergency response training program were

identified by the licensee and team. Because of ineffective corrective actions for emergency

preparedness deficiencies, emergency action levels could not be implemented for a Site Area

Emergency, an Alert, and a Notice of Unusual Event. In response to the emergency

preparedness deficiencies, the licensee instituted actions to augment the emergency response

organization by assigning six managers, specially trained on emergency action level

classification, to the shift rotation.

The licensees third-party safety culture assessment applied a multi-method approach to

conduct the safety culture assessment, including a survey, behavioral observations, interviews,

and document reviews. Two third-party teams performed their assessment activities in parallel,

but compared, contrasted, and reconciled their findings to ensure they provided integrated

assessment results to the licensee. The NRC did note that the multiple methods approach

provided a comprehensive understanding of the onsite safety culture, whereas a stand-alone

survey would not have provided sufficient information. The result of the NRC teams evaluation

of site safety culture was consistent with the third-party assessment.

Site personnel described past decision making as being governed by the goals of reducing

costs in preparation for deregulation and cost containment, unless the decisions involved

meeting regulatory requirements or ensuring continued operations. The sites reengineering

effort in the early 1990s, focused on streamlining work processes, reducing staff size, reducing

operating and maintenance costs, and allocating decision-making authority to those closest to

the work. These cumulative reductions contributed to the increase in equipment failures, plant

events, and other performance problems at the site.

Past efforts to reduce staff through attrition and the increasing rate of retirements in the aging

workforce have contributed to a reduction in the availability of qualified personnel at the site.

The reductions had the effect of requiring licensed personnel to routinely work overtime. The

team also observed that senior maintenance and engineering department personnel were

retiring at an accelerating rate. The licensees ability to replace senior personnel and ensure

knowledge transfer has been limited by past weaknesses in recruiting and hiring efforts and

reductions in the number of training staff. Replacement of senior staff with inexperienced

personnel has increased human error rates and hampered improvement efforts.

The team identified weaknesses in organizational characteristics and attitudes associated with

10 of the NRC's 13 safety culture components, as detailed in Section 06.07 of Inspection

Manual Chapter 0305 "Operating Reactor Assessment Program. The most significant

weaknesses were identified in the safety culture components of accountability, the licensee's

corrective action program, decision-making, and work practices. The team noted that these

-8- Enclosure

weaknesses were widespread among functional groups across the organization. Organizational

characteristics and attitudes were adequate in the safety culture components of safety policies;

the environment for raising concerns; and preventing, detecting, and mitigating perceptions of

retaliation.

-9- Enclosure

SUMMARY OF FINDINGS

IR 05000528/2007012, 05000529/2007012, 05000530/2007012; 04/03/07 - 12/19/07; Palo

Verde Nuclear Generating Station, Units 1, 2, and 3; Inspection Procedure 95003,

Supplemental Inspection for Repetitive Degraded Cornerstones, Multiple Degraded

Cornerstones, Multiple Yellow Inputs, or One Red Input.

This report covered a 9-month period of inspection by personnel in all four NRC Regional

Offices and from Headquarters, one contractor, and an observer from the Spanish Nuclear

Safety Council. The inspection identified numerous performance deficiencies that resulted in 15

noncited violations, 1 finding, 1 Severity Level IV violation, and 1 apparent violation with

significance to be determined. The significance of most findings is indicated by their color

(Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance

Determination Process." Findings for which the significance determination process does not

apply may be Green or be assigned a severity level after NRC management's review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

Initiating Events

failure of fire protection personnel to follow Procedure 14DP-0FP33, "Control of Transient

Combustibles," Revision 15. Specifically, the team identified that on the 70 elevation of the

Auxiliary Building (Radiation Protection Remote Monitoring Station) and in the Unit 3

containment, there were transient combustibles being stored without the proper evaluation

and required permits. This issue was entered into the corrective action program as Palo

Verde Action Request 3071785.

The finding is considered more than minor because storing unanalyzed material could result

in the potential to exceed combustible limits and is associated with an increase in the

likelihood of an initiating event. Using Inspection Manual Chapter 0609, Significance

Determination Process, Appendix F, Fire Protection Significance Determination Process,

this issue affected the Fire Prevention and Administrative Controls Category. In this case

the stored materials required a permit per the licensees procedure; however, the area was

attended, fire detection and suppression was available, and the amounts did not exceed the

loading calculation to the point of changing the loading classification. Therefore, this finding

is considered of Low Degradation and had very low safety significance. The cause of this

finding has crosscutting aspects associated with work practices in the human performance

area because: (1) the licensee failed to communicate human error prevention techniques

such that work activities were performed safely (H.4.(a)), and (2) the licensee did not

effectively communicate expectations regarding procedural compliance (H.4.(b)). The cause

of this finding is also related to the safety culture component of accountability in that fire

protection personnel failed to demonstrate a proper safety focus and reinforce safety

principles among their peers (O.1.(c)). (Section 5.6.2.b.1)

adequately assess the increase in risk and effectively implement risk mitigation actions for

maintenance activities in the switchyard. Specifically, the switchyard was not being

protected by controlling access and movement as required and the risk modeling did not

include all work being performed. The Unit 1 shift manager and the switchyard coordinator

- 10 - Enclosure

were unaware of the movement of multiple vehicles and pieces of equipment in or near

restricted areas and not all maintenance was included in the schedule provided to the

switchyard coordinator for risk review. This issue was entered into the licensees corrective

action program as Palo Verde Action Request 3078392.

This finding is greater than minor because the licensees risk assessment failed to consider

maintenance activities that could increase the likelihood of initiating events such as work in

the switchyard and failed to effectively manage compensatory measures. Inspection

Manual Chapter 0609, Significance Determination Process, Appendix K, Maintenance

Risk Assessment and Risk Management Significance Determination Process, was used to

assess the significance. Using data from the licensees probabilistic risk assessment, a

NRC Region IV senior reactor analyst calculated the risk deficit. Based on the magnitude of

the calculated risk deficit being less than 1E-6/year, this finding is determined to be of very

low safety significance. The cause of this finding has crosscutting aspects associated with

work control of the human performance area in that the licensee did not appropriately

coordinate switchyard activities incorporating risk insights (H.3.(a)) and did not communicate

with each other during activities in which coordination is necessary to assure plant and

human performance (H.3.(b)). (Section 5.6.3.b.1)

Mitigating Systems

"Instructions, Procedures, and Drawings," with eight examples for the failure of the licensee

to adequately evaluate degraded and unanalyzed conditions to support operability decision

making between May 2006 and October 26, 2007. The team noted a significant number of

weak or non-existent operability evaluations of degraded conditions affecting safety-related

equipment. There was a lack of understanding of the need to assess operability for some

conditions adverse to quality and a lack of knowledge or skills necessary to conduct quality

operability assessments. The examples of the violation involved two instances of conditions

adverse to quality documented in databases outside of the corrective action program,

missile hazards near the essential spray pond, two issues effecting essential cooling water

system heat exchangers, 480V and 4160V motor terminations, oil leaks on the emergency

diesel generators, and high lead content in a Unit 3 low pressure safety injection pump.

Each of the individual technical issues was entered into the licensees corrective action

program.

The examples associated with this finding are greater than minor because they were

associated with the mitigating systems cornerstone attribute of equipment performance and

affected the cornerstone objective of ensuring the availability and reliability of systems that

respond to initiating events to prevent undesirable consequences. Using the Inspection

Manual Chapter 0609, "Significance Determination Process," Phase 1 Worksheets, the

examples associated with this finding are determined to have very low safety significance

since they only affected the mitigating systems cornerstone and did not represent a loss of

system safety function. The causes of the examples of this finding have crosscutting

aspects associated with decision making of the human performance area in that operations

and engineering personnel: (1) did not make safety significant decisions using a systematic

process (H.1.(a)), and (2) failed to use conservative assumptions for operability decision-

making when evaluating degraded and nonconforming conditions (H.1.(b)). The causes of

the examples of this finding also have crosscutting aspects associated with evaluation and

corrective action of the problem identification and resolution area in that licensee personnel:

(1) did not assess conditions adverse to quality for impacts to the operability of safety-

- 11 - Enclosure

related equipment (P.1.(c), and (2) did not address safety issues in a timely manner P.1.(d)).

The causes of the examples of this finding also related to the safety culture component of

accountability in that workers and managers failed to demonstrate a proper safety focus and

reinforce safety principles (O.1.(b) and O.1.(c)). (Multiple Sections)

XVI, Corrective Action, with six examples for the failure of the licensee to identify, evaluate,

or correct conditions adverse to quality between 1988 and October 10, 2007. The corrective

actions implemented by the licensee to address the substantive human performance and

problem identification and resolution crosscutting issues were ineffective in sustaining

performance improvement as noted by licensee self assessments, external industry reviews,

and NRC inspections. The team also identified several examples of poor and inconsistent

implementation of corrective action program behaviors. The examples of the violation

involved not entering the use of unqualified tape in containment in the corrective action

process, evaluating the condition, or taking timely actions to remove the tape from all three

units; not identifying, evaluating, or implementing timely corrective actions associated with

operating experience applicable to the auxiliary feedwater pump trip and throttle valve; not

implementing timely corrective actions for water intrusion and flooding of underground

manholes and cable vaults; inadequate evaluation for nonconforming Target Rock reed

switches; not evaluating and correcting a degraded condition with post accident monitoring

instrument chart recorders, and not correcting a degraded/nonconforming condition

associated with 3 inch Borg-Warner check valves. Each of the individual technical issues

was entered into the licensees corrective action program.

The examples associated with this finding are greater than minor because they were

associated with the mitigating systems cornerstone attribute of equipment performance and

affected the cornerstone objective of ensuring the availability and reliability of systems that

respond to initiating events to prevent undesirable consequences. Using the Inspection

Manual Chapter 0609, "Significance Determination Process," Phase 1 Worksheets, the

examples associated with this finding are determined to have very low safety significance

since they only affected the mitigating systems cornerstone and did not represent a loss of

system safety function. The causes of the examples of this finding have crosscutting

aspects associated with decision making of the human performance area in that operations

and engineering personnel failed to use conservative assumptions for operability decision-

making when evaluating degraded and nonconforming conditions (H.1.(b)). The causes of

the examples of this finding have crosscutting aspects associated with: (1) corrective

actions of the problem identification and resolution area because the licensee failed to

evaluate previous issues such that resolutions addressed all conditions affecting operability

(P.1.(c)), (2) operating experience of the problem identification and resolution area in that

engineering personnel failed to ensure implementation and institutionalization of operating

experience through changes to station processes, procedures, equipment, and training

programs (P.2.(b)), and (3) self assessment of the problem identification and resolution area

in that the licensee did not follow their benchmarking and self assessment guide to ensure

findings were evaluated in their corrective action program (P.3.(c)). The causes of the

examples of this finding also related to the safety culture component of accountability in that

workforce and management personnel failed to demonstrate a proper safety focus and

reinforce safety principles (O.1.(b) and O.1.(c)). (Multiple Sections)

"Design Control," for the failure to translate design basis requirements into procedures to

ensure the plant is operated within its design basis. Specifically, between 1985 and

- 12 - Enclosure

October 2007, the maximum condensate storage tank temperature requirements did not

include the effect of recirculated hot condensate water from the main condenser. The issue

was entered into the corrective action program as Palo Verde Action Request 3073243.

This finding is greater than minor because it was associated with the mitigating systems

cornerstone attribute of equipment performance and affected the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding is determined to have very low

safety significance since it only affected the mitigating systems cornerstone and did not

represent a loss of system safety function. The cause of this finding has crosscutting

aspects associated with corrective action of the problem identification and resolution area in

that engineering personnel did not assess conditions adverse to quality for impacts to the

operability of safety related equipment (P.1.(c)). (Section 5.2.b.1)

  • Green. The team identified a noncited violation of License Condition 2.C(6) for the failure to

install sprinkler heads in accordance with the fire protection program. Specifically, on

October 2, 2007, the team identified several upright fire sprinkler heads in the auxiliary

building that were incorrectly installed in a downward orientation. This issue was entered

into the corrective action program as Palo Verde Action Request 3073824.

This finding is greater than minor because it was associated with the mitigating systems

cornerstone attribute of external factors and affected the cornerstone objective of ensuring

the availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding is determined to require additional

evaluation under Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance

Determination Process, because it was associated with the suppression element of

defense-in-depth. Since the installed configuration of the sprinkler heads represented a low

degradation of the fire suppression system, in accordance with Section 1.3.1, of Inspection

Manual Chapter 0609, Appendix F, the issue was determined to have very low safety

significance. (Section 5.2.b.2)

maintenance rule and engineering personnel to demonstrate that the performance or

condition of structures, systems, or components was being effectively controlled through

appropriate preventive maintenance to ensure systems or components remained capable of

performing their intended function. Specifically, between April and October 2007, an

inadequate evaluation of maintenance rule performance criteria was performed and, even

though the Unit 2 auxiliary feedwater Train A had exceeded its maintenance rule

10 CFR 50.65(a)(2) performance criteria, no goal setting and monitoring was performed as

required by 10 CFR 50.65(a)(1) of the maintenance rule. This issue was entered into the

corrective action program as Palo Verde Action Request 3075907.

This finding is greater than minor because it was associated with the mitigating systems

cornerstone attribute of equipment performance and affected the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding is determined to have very low

safety significance since it only affected the mitigating systems cornerstone and did not

represent a loss of system safety function. The cause of this finding has crosscutting

- 13 - Enclosure

aspects associated with self assessments of the problem identification and resolution area

in that maintenance rule and engineering personnel failed to perform self assessments that

were comprehensive, appropriately objective, and self-critical (P.3.(a)). The cause of this

finding has crosscutting aspects associated with decision-making of the human performance

area in that engineering personnel failed to make safety-significant or risk-significant

decisions using a systematic process (H.1.(a)). The cause of this finding is also related to

the safety culture component of accountability in that management did not reinforce safety

standards and display behaviors that reflected safety as an overriding priority (O.1.(b)).

(Section 5.5.b.1)

  • Green. The team identified a finding for the failure of maintenance personnel to install

emergency lighting in containment in support of the refueling outage per repetitive

maintenance work Order 2935399 and work Instruction WSL 24436. As a result, work

began in the Unit 3 containment with no emergency lighting installed and no egress

contingency plan for a loss of containment lighting. This issue was entered into the

corrective action program as Palo Verde Action Request 3070783.

This finding is considered more than minor because if left uncorrected, a failure to install

emergency lighting could hamper emergency response activities in the containment or

complicate emergency egress from the containment. Using the Inspection Manual Chapter

0609, "Significance Determination Process," Appendix M, Significance Determination

Process Using Qualitative Criteria, the finding is determined to be of very low safety

significance because emergency lighting was necessary for personnel safety and personnel

were expected to carry flashlights when responding to events. The cause of the finding has

crosscutting aspects associated with work control of the human performance area in that

maintenance personnel failed to properly plan the emergency lighting installation work by

incorporating contingencies in case the work was not completed in the appropriate

timeframe (H.3.(a)). The cause of this finding is also related to the safety culture component

of accountability in that management personnel failed to reinforce safety standards and

display behaviors that reflected safety as an overriding priority (O.1.(b)). (Section 5.6.2.b.2)

failure of radiation protection personnel to follow procedures for installing temporary

shielding at the 87 foot elevation of the auxiliary building west penetration room.

Specifically, temporary shielding (Package A-87-10) was installed in direct contact and

across the Train A low pressure safety injection pressure instrument sensing line. However,

a piping stress analysis was not performed as required by Procedure 75RP-9RP25,

Temporary Shielding, Revision 9. This issue was entered into the corrective action

program as Palo Verde Action Requests 3071468 and 3072224.

This finding is greater than minor because it was associated with the mitigating systems

cornerstone attribute of configuration control and affected the cornerstone objective to

ensure the availability and capability of systems to respond to initiating events. Using the

Inspection Manual Chapter 0609, "Significance Determination Process," Phase 1

Worksheets, this finding is determined to be of very low safety significance because the

condition did not result in an actual loss of safety function, and did not screen as risk

significant or contribute to external event initiated core damage sequences since it did not

involve a loss or degradation of equipment designed to mitigate a seismic event. This

finding has crosscutting aspects associated with the work practices component of the

human performance area because the licensee did not effectively use human error

- 14 - Enclosure

prevention techniques such as self checking and proper documentation of activities for the

shielding installation (H.4.(a)). (Section 5.6.2.b.3)

  • Green. The team identified a noncited violation of 10 CFR 50.65, for the failure of

engineering personnel to establish goals and monitor the performance of the safety injection

system. Specifically, on March 22, 2007, engineering personnel failed to establish goals to

properly monitor system performance, or provide a technical justification to demonstrate that

monitoring under 10 CFR 50.65(a)(1) was not required for the safety injection system

following the system changing status from 10 CFR 50.65(a)(2) to 10 CFR 50.65(a)(1). This

issue was entered into the corrective action program as Palo Verde Action Requests

3074255 and 3076699.

This finding is greater than minor because it was associated with the mitigating systems

cornerstone attribute of equipment performance and affected the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding is determined to have very low

safety significance since there was no loss of safety function. The cause of this finding has

crosscutting aspects associated with: (1) corrective actions of the problem identification and

resolution area in that engineering personnel failed to take appropriate actions to address

safety issues and adverse trends in a timely manner (P.1.(d)), and (2) self assessment of

the problem identification and resolution area in that engineering personnel did not perform

self assessments that were comprehensive, objective, and self critical (P.3.(a)).

(Section 5.6.9.b.1)

"Instructions, Procedures and Drawings," for the failure of maintenance and engineering

personnel to maintain proper configuration of the support brackets for the pressurizer

condensate pots in accordance with design drawings. Specifically, on October 2, 2007, the

team identified that the support bracket U-bolts were not tight against the condensate pot

piping, jam nuts were not installed on the U-bolts, and jacking bolts were not in full contact

with the pressurizer vessel. The support brackets minimize lateral motion during a seismic

event. This issue was entered into the corrective action program as Palo Verde Action

Requests PVAR 3070805 and 3075704.

This finding is greater than minor because it was associated with the mitigating systems

cornerstone attribute of equipment performance and affected the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding is determined to have very low

safety significance since it only affected the mitigating systems cornerstone and did not

represent a loss of system safety function. This finding has crosscutting aspects associated

with the work practices component of the human performance area because maintenance

personnel did not effectively use human error prevention techniques such as self checking

and proper documentation of activities for the installation of the support bracket (H.4.(a)).

(Section 5.6.7.b.1)

- 15 - Enclosure

Barrier Integrity

Instructions, Procedures, and Drawings, for the failure of maintenance personnel to

properly rig the Unit 3 100 foot elevation inner personnel airlock door in accordance with

engineering drawings. Specifically, the suspended rigging was completed with the

inappropriate placement of wire rope slings over two locking pins resulting in an unanalyzed

force being applied to the doors operating mechanism. This issue was entered into the

corrective action program as Palo Verde Action Request 3086057.

The finding is greater than minor because it could become a more significant safety concern

if left uncorrected in that the applied suspended force on the bronze bushing and the doors

operating mechanism, which were not designed for vertical loading, could degrade the

personnel airlock door sealing capability. This finding can not be evaluated by the

significance determination process because Inspection Manual Chapter 0609, "Significance

Determination Process," Appendix A, "Determining the Significance of Reactor Inspection

Findings for At-Power Situations," and Appendix G, "Shutdown Operations Significance

Determination Process," do not apply to the door for the plant conditions that existed during

the event. This finding affects the barrier integrity cornerstone and is determined to be of

very low safety significance by NRC management review using Inspection Manual Chapter

0609, Appendix M, "Significance Determination Process Using Qualitative Criteria," because

it was a deficiency that did not result in the actual breach of the containment barrier. The

cause of this finding has crosscutting aspects associated with the work practices aspect of

the human performance area in that maintenance personnel failed to provide adequate

oversight of work activities (H.4.(c)). (Section 5.6.4.b.1)

  • Green. The team identified a noncited violation of Technical Specification Surveillance

Requirement 3.6.6.6, for the failure to verify that each containment spray nozzle was

unobstructed. Specifically, the last completed surveillance test conducted on each unit,

identified that one nozzle in each unit was obstructed and that the nozzles were not retested

in accordance with the approved retest requirement. This issue was entered into the

corrective action program as Palo Verde Action Requests 3075026, 3075059, 3068647 and,

3048511.

The finding is more than minor because it affected the configuration control attribute of the

barrier integrity cornerstone, and affected the associated cornerstone objective to provide

reasonable assurance that physical design barriers protect the public from radionuclide

releases caused by accidents or events. Using the Inspection Manual Chapter 0609,

"Significance Determination Process," Phase 1 Worksheets, the finding is determined to be

of very low safety significance because it did not involve an actual reduction in defense-in-

depth for the atmospheric pressure control function of the reactor containment.

(Section 5.5.b.3)

  • Green. The team identified a noncited violation of Technical Specification Surveillance

Requirement 3.0.3 for the failure of operations personnel to conduct an assessment and

manage the risk for a missed surveillance test. On September 27, 2007, the team identified

that the requirements for testing the containment spray nozzles in Units 1, 2, and, 3 did not

meet Technical Specifications Surveillance Requirement 3.6.6.6. Operations personnel did

not enter Technical Specification Surveillance Requirement 3.0.3 until prompted by the team

on October 30, 2007. This issue was entered into the corrective action program as Palo

Verde Action Request 3085708.

- 16 - Enclosure

The finding is determined to be more than minor because it affected the configuration

control attribute of the barrier integrity cornerstone, and affected the associated cornerstone

objective to provide reasonable assurance that physical design barriers protect the public

from radionuclide releases caused by accidents or events.

Using the Inspection Manual Chapter 0609, "Significance Determination Process," Phase 1

Worksheets, the finding is determined to have very low safety significance because it did not

involve an actual reduction in defense-in-depth for the atmospheric pressure control function

of the reactor containment. The cause of this finding has crosscutting aspects associated

with work practices of the human performance area in that operations personnel failed to

ensure supervisory and management oversight of work activities that resulted in a missed

Technical Specification surveillance requirement (H.4(c)). The cause of this finding is also

related to the safety culture component of accountability in that operations personnel failed

to demonstrate a proper safety focus and reinforce safety principles (O.1.(c)).

(Section 6.2.b.1)

Emergency Preparedness

Appendix E.IV.F.2.g, with the significance yet to be determined, for the licensees failure to

correct an identified risk significant planning standard weakness between May 2, 2007 and

October 28, 2007. Specifically, the licensee failed to implement adequate corrective actions

for identified weaknesses in the ability to correctly make a Site Area Emergency declaration

for a steam generator tube rupture event. This issue was entered into the licensees

correction action program as Palo Verde Action Request 3083911.

The team determined that the inability to consistently implement an Emergency Action Level

was a performance deficiency within the licensees control. This finding is more than minor

because it was associated with the Emergency Preparedness attribute of emergency

response organization performance and affected the cornerstone objective to implement

adequate measures to protect the health and safety of the public because the inability to

properly recognize and classify an emergency condition affects the licensees ability to

implement adequate protective measures. This finding was evaluated using the Emergency

Preparedness Significance Determination Process and was preliminarily determined to be of

low to moderate safety significance because it was a failure to comply with NRC

requirements; it was an issue associated with the requirements of Appendix E of

10 CFR Part 50; it was not an issue with a risk significant planning standard as described in

Manual Chapter 0609, Significance Determination Process, Appendix B, Emergency

Preparedness Significance Determination Process, Section 2.0; and it was a functional

failure of the requirements of Appendix E IV.F.2.g because the licensee failed to correct a

weakness associated with Risk Significant Planning Standard 10 CFR 50.47(b)(4). The

cause of this finding has crosscutting aspects associated with the corrective action aspect of

the problem identification and resolution area in that the licensee failed to thoroughly

evaluate problems such that resolutions ensured correcting problems (P.1.(c)). The cause

of this finding was also related to the safety culture component of accountability in that the

licensee failed to demonstrate a proper safety focus and reinforce safety principles (O.1.(c)).

(Section 5.7.b.1)

  • Green. The team identified a Green noncited violation of 10 CFR 50.54(q) and

§50.47(b)(4), for the failure of the licensee to be able to implement Emergency Action Levels

3-12 and 7-1. Specifically, area radiation Monitor RU-18 could not be utilized in the vicinity

- 17 - Enclosure

of the remote shutdown panels and therefore, the emergency classification associated with

Emergency Action Level 3-12 could not be declared at the Alert level as required in

Procedure EPIP-99, EPIP Standard Appendices. In addition, the licensee improperly

overclassified Emergency Action Level 7-1 as an Alert when presented conditions

warranting a classification of a Notification of Unusual Event. Specifically, the licensee did

not develop a procedure to enable personnel to differentiate between an aircraft and an

airliner and therefore, the proper emergency classifications could not be consistently

determined. This finding was entered into the licensees corrective action program as

Condition Report Disposition Requests 3071570, 3071572, and 3085175.

The team determined that the inability to implement Emergency Action Levels was a

performance deficiency. The finding was more than minor because it was associated with

the Emergency Preparedness attribute of procedure quality and could affect the cornerstone

objective associated with the licensees ability to correctly classify an emergency condition

which would affect the licensees ability to implement adequate measures to protect the

health and safety of the public. Using the Manual Chapter 0609, "Significance

Determination Process," Appendix B, Emergency Preparedness Significance Determination

Process, the finding was determined to have very low safety significance because the

licensee would be unable to declare one Emergency Action Level at the Alert and one

Emergency Action Level at the Notification of Unusual Event level. The cause of this finding

had crosscutting aspects associated with the corrective action of the problem identification

and resolution area in that the licensee had previous opportunities to identify the

deficiencies (P.1.(a)). (Section 5.7.b.2)

Occupational Radiation Safety

  • Green. The team identified a noncited violation of 10 CFR 19.12, Instructions to Workers,

for the failure of radiation protection personnel to provide adequate information regarding

radiological conditions and precautions to minimize exposure during pre-job briefs.

Specifically, on October 1 and 3, 2007, radiation protection personnel did not adequately

inform workers of radiological conditions and precautions to minimize exposure during

radiological briefings. This issue was entered into the corrective action program as Palo

Verde Action Request 3070507 and 3071940.

The finding is greater than minor because it is associated with the Occupational Radiation

Safety Cornerstone attribute of programs and process and affected the cornerstone

objective of ensuring the adequate protection of the workers health and safety from

exposure to radiation during routine operations. Using Inspection Manual Chapter 0609,

Significance Determination Process, Appendix C, Occupational Radiation Safety

Significance Determination Process, the finding was determined to be of very low safety

significance because it was not an as low as is reasonably achievable issue, there was not

an overexposure or substantial potential for an overexposure, and the ability to assess dose

was not compromised. The cause of this finding has crosscutting aspects associated with

decision making in the human performance area in that radiation protection personnel failed

to communicate decisions, and the basis for decisions, to personnel who had a need to

know the information (H.1.(c)). This finding also has a safety culture component aspect of

accountability in that radiation protection personnel did not demonstrate a proper safety

focus or reinforce safety principles among peers when conducting pre-job briefings (O.1.(c)).

(Section 6.1.b.1)

- 18 - Enclosure

Public Radiation Safety

failure of the licensee to periodically update the Final Safety Analysis Report (UFSAR) with

all changes made in the facility or procedures. Specifically, in 2002, radiation protection and

operations personnel changed the operation of the total dissolved solids holdup tanks from

that described in the Updated Final Safety Analysis Report (UFSAR) and did not submit an

update to the NRC. This issue was entered into the licensees corrective action program as

Palo Verde Action Request 3075089.

This issue is being treated as traditional enforcement because the failure to update the Final

Safety Analysis Report has the potential to impact the NRCs ability to perform its regulatory

function. The finding is characterized as a Severity Level IV violation because the

erroneous information was not used to make an unacceptable change to the facility or

procedures. The finding is of very low safety significance because the change in operation

of the total dissolved solids holdup tanks did not result in an increase in the likelihood of a

release of radioactive material. The cause of this finding has a crosscutting aspect

associated with resources in the human performance area in that the licensee failed to

ensure that personnel and equipment were available and adequate to maintain radiological

safety by minimization of long-standing equipment issues (H.2.(a)). (Section 6.2.b.1)

Physical Protection

  • N/A. The team identified a minor violation of the Palo Verde Physical Security Plan,

associated with the calculation of group work hours. This issue was entered into the

licensees corrective action program as Palo Verde Action Request 3078227. The details of

the finding can be found in Inspection Report 05000528; 05000529; 05000530/2007402.

Miscellaneous

  • N/A. The team noted that the licensee had not completed corrective actions and

effectiveness reviews associated with the root and contributing causes for the July 2004,

Yellow finding involving the voiding of emergency core cooling system piping in all three

units. The cause of the failure to implement effective corrective actions was related to the

safety culture component of organizational change management in that, licensee personnel

ceased to implement corrective actions and effectiveness reviews when the existing

management team members assumed that the activities would be integrated into other

station processes following the arrival of a new senior management team. (Section 9.0)

  • N/A. The team identified continuing human performance issues at Palo Verde consistent

with previously identified issues discussed in End-of-Cycle and Mid-cycle letters since 2005.

Specifically, human performance concerns observed during this inspection included

weaknesses in implementing the operability determination process, failures to follow

procedures, failures to implement human performance tools, and inadequate procedures. In

addition, a number of engineering issues reflected a lack of technical rigor in resolving

complex issues. The team noted a lack of adherence to basic radiological work practices

and inconsistent implementation of control room behaviors. The team also identified that

the licensees training department had been inconsistent in supporting site improvement.

Although a human performance root cause investigation had been conducted, corrective

actions were not effective in sustaining performance improvement. (Multiple Sections)

- 19 - Enclosure

  • N/A. Multiple substantive crosscutting aspects associated with problem identification and

resolution (PI&R) have existed since 2004. Corrective actions continue to remain ineffective

in sustaining improving performance as noted by effectiveness reviews, external industry

reviews, and NRC inspections. The licensees corrective action program was complicated

and cumbersome. Licensee personnel recognized the attributes of problem identification,

evaluation, and resolution when interviewed; however, the knowledge and understanding

was not consistently demonstrated to the NRC during the inspection. (Multiple Sections)

  • N/A. The team noted that the licensee's third-party safety culture assessment was

adequate to provide the licensee with the information necessary to develop

appropriate corrective actions for safety culture weaknesses. The results of the NRC's

independent safety culture assessment validated the results of the licensee's third-party

safety culture assessment.

The team identified weaknesses in organizational characteristics and attitudes associated

with 10 of the NRC's 13 safety culture components, as detailed in Section 06.07 of

Inspection Manual Chapter 0305 "Operating Reactor Assessment Program." The most

significant weaknesses were identified in the safety culture components of accountability,

the corrective action program, decision-making, resources, self assessments, and work

practices. The team noted that these weaknesses were widespread among functional

groups across the organization. Organizational characteristics and attitudes were adequate

in the safety culture components of safety policies; the environment for raising concerns;

and preventing, detecting, and mitigating perceptions of retaliation. (Sections 8.1 and 8.2)

Licensee-Identified Violations

Violations of very low safety significance which were identified by the licensee have been

reviewed by the team. Corrective actions taken or planned by the licensee have been entered

into the licensee's corrective action program. These violations and corrective actions are listed

in Section 11 of this report.

- 20 - Enclosure

REPORT DETAILS

1 PERFORMANCE HISTORY

On March 2, 2007, the NRC issued the Annual Assessment Letter, which documented the

results of the annual performance review for the Palo Verde Nuclear Generating Station

(PVNGS), including the decision to perform a supplemental inspection at PVNGS, using

Inspection Procedure (IP) 95003, Supplemental Inspection for Repetitive Degraded

Cornerstones, Multiple Degraded Cornerstones, Multiple Yellow Inputs, or One Red Input.

PVNGS Unit 3 was placed in the Multiple/Repetitive Degraded Cornerstone column

(Column 4) of the NRCs Action Matrix, effective in the fourth Quarter 2006. In accordance

with NRC Inspection Manual Chapter (IMC) 0305, Operating Reactor Assessment

Program, the decision to place Unit 3 in Column 4 was made on the basis of the definition

of a Repetitive Degraded Cornerstone in that there were two separate safety significant

inspection findings (one Yellow and one White) in the Mitigating Systems cornerstone and

the cornerstone had been degraded for more than four quarters.

Unit 3 was placed in Column 4 based on two findings: (1) a White finding (issued

February 21, 2007) for inadequate maintenance and corrective actions involving the K-1

electrical relay on a Unit 3 emergency diesel generator (EDG); and (2) a Yellow finding

(issued April 8, 2005) involving voiding in the suction line for the emergency core cooling

system (ECCS) pumps in all three units.

As a result of the Yellow finding, the NRC completed the IP 95002, Inspection For One

Degraded Cornerstone Or Any Three White Inputs In a Strategic Performance Area,

supplemental inspection in December 2005. The associated inspection report dated

January 27, 2006, closed the Severity Level III violation of 10 CFR 50.59 and kept the

Yellow finding open. The Yellow finding remained open because the licensees corrective

actions were not fully developed, were narrowly focused, and their implementation was not

effective. In August 2006, the NRC completed a second IP 95002 supplemental inspection.

The associated report dated November 11, 2006, documented that the Yellow finding could

not be closed because the corrective actions to address problems with questioning attitude,

technical rigor, and operability determinations (ODs) were not fully effective. In addition,

measures and metrics to monitor performance improvement had not been developed and

the licensee did not have an effective program for using operating experience (OE).

Throughout 2006, the licensee continued to have performance problems that challenged the

operation of all three units in the following areas: (1) equipment reliability; (2) human

performance; and (3) problem identification and resolution (PI&R). Two special inspections

were conducted in June and September of 2006. The June 2006 special inspection

reviewed concerns regarding spray pond chemistry control and a reduction in heat

exchanger performance for key safety systems. This inspection resulted in the issuance of

five noncited violations of very low risk significance (Green). The September 2006 special

inspection reviewed concerns with the failure of the K-1 electrical relay on the Unit 3 Train A

EDG. This inspection resulted in the issuance of a White finding. The causes for the

findings associated with both of these inspections were similar to the programmatic issues

associated with the 2005 Yellow finding and included: a lack of technical rigor in performing

evaluations and incomplete consideration of the extent of problems when they were

identified.

- 21 - Enclosure

The licensees performance also warranted the issuance of several substantive crosscutting

PI&R and human performance aspects in March 2005. The substantive crosscutting

aspects continue to remain open because of a failure to implement changes that would

result in sustainable performance improvement.

The licensee initiated an integrated performance improvement plan in the fourth quarter of

2005. Their improvement plan was ineffective and performance problems continued

throughout 2006 and into 2007. Factors associated with the lack of performance

improvement included:

  • Fixing symptoms and not addressing the root causes of problems,
  • Not performing a thorough review of issues,
  • Accepting incomplete answers and actions,
  • Failing to question the impact of actions,
  • Incomplete ODs, and
  • Inadequate corrective action program (CAP) implementation.

On June 21, 2007, the NRC issued Confirmatory Action Letter (CAL) 4-07-004, which

required PVNGS to perform additional actions to address their decline in performance.

Specifically, the licensee was required to:

1. Complete actions to address the root and contributing causes identified in evaluations

for the Yellow finding associated with the voided containment sump suction piping for all

three units, and the White finding associated with the Unit 3 Train A emergency diesel

generator electrical relay problems.

2. Complete corrective actions that will result in sustained improved performance in the

crosscutting areas of human performance and PI&R.

3. Complete an independent (third party) safety culture assessment by

September 15, 2007.

4. Incorporate the results of their in-depth evaluations and their safety culture assessment

described in Item 3 above into a modified improvement plan.

5. Submit the portions of the modified improvement plan that impact the Reactor Safety

strategic performance area, including safety culture improvement initiatives by

November 30, 2007.

On September 4, 2007, the licensee submitted a letter to the NRC indicating the

independent safety culture assessment had been completed. The NRCs review of the

safety culture assessment is documented in Section 8.1.

On November 28, 2007, the licensee submitted a letter to the NRC requesting an extension

to the submittal date of the modified improvement plan. The plan was being developed

during the IP 95003 inspection, and was therefore only partially reviewed in October 2007.

The licensee submitted the plan to the NRC on December 31, 2007.

- 22 - Enclosure

2 SITE INTEGRATED BUSINESS PLAN (SIBP) AND SITE INTEGRATED IMPROVEMENT

PLAN (SIIP)

Overview

Because the improvement plan was not complete at the time of the IP 95003 inspection, the

appropriateness, timeliness, and effectiveness of the corrective actions to address the root

and contributing causes, as well as other identified problems, could not be fully evaluated.

The team determined that additional NRC inspections of the modified improvement plan will

need to be conducted before an assessment can be completed.

a. Inspection Scope

The team performed a review of the SIBP and SIIP in accordance with IP 95003,

Sections 02.02.a - 02.02.e. This assessment of the improvement plan was

accomplished by reviewing numerous documents including, in part, root cause

evaluations, apparent cause evaluations, self assessments, condition report/disposition

requests (CRDRs), Palo Verde Action Requests (PVARs), condition report action items

(CRAIs), problem development statements (PDSs), fundamental overall problems

(FOPs), effectiveness reviews, the improvement plan database, and the Improved

Performance and Cultural Transformation (ImPACT) database. The team: (1) reviewed

the procedures for completing the ImPACT project and improvement plan; (2) assessed

the scope of the ImPACT project; (3) reviewed PVARs generated as a result of ImPACT

activities; (4) assessed the ability to cross reference data between the various

documents used to develop the improvement plan; (5) reviewed PDSs for adequacy and

for outstanding technical issues; (6) sampled completed improvement plan corrective

actions to determine timeliness, completion of actions, and measures of effectiveness;

(7) determined if corrective actions identified in ImPACT documents were included in the

improvement plan and the CAP at the appropriate priority level; (8) assessed the

resource loading of the improvement plan; (9) assessed the significance of overdue

action items; and (10) reviewed various background documents for areas that were not

included in the improvement plan.

b. Observations and Findings

Introduction. The team identified several observations associated with the development

of the improvement plan. Since the licensee did not submit the improvement plan to the

NRC before the IP 95003 inspection commenced, the team only reviewed a draft version

of the SIBP/SIIP.

Description. The SIBP and SIIP were developed and controlled by

Procedure 01DP-0AC06, Site Integrated Business Plan (SIBP)/Site Integrated

Improvement Plan (SIIP) Process, Revision 1. Revision 0 of this procedure was issued

in September 2007, which was well after the May 2007 start of the improvement plan

efforts. The SIBP plan is a database program that was developed using Microsoft

Access. This database was designed to track the implementation and completion of

actions contained within the SIBP. The actual corrective actions associated with the

improvement plan, which were CRAIs, were contained in the Site Work Management

System (SWMS) database that is used to track CAP documents. The SIBP included a

subset of corrective actions known as the SIIP. The SIIP contains corrective actions

associated with the ImPACT process, NRC CAL, PVNGS safety culture assessment, IP

- 23 - Enclosure

95001 issues (White finding for inadequate maintenance and corrective actions involving

the K-1 electrical relay on a Unit 3 EDG), IP 95002 issues (Yellow finding involving

voiding in the suction line for the ECCS pumps in all three units), and the substantive

crosscutting issues for human performance and PI&R. The SIIP is expected to be the

modified improvement plan described in Item 5 of the CAL.

The ImPACT process (see figure below) consisted of a series of assessment steps

including ImPACT procedures, checklist findings, PDSs, and FOPs. Checklists were

used to document the results of ImPACT assessments. PDSs were used to collate

related findings from individual assessment activities and then those findings were

grouped into FOPs. After developing the FOPs, the licensee used one or more of the

following tools to identify casual factors by conducting root cause evaluations, apparent

cause evaluations, self-assessments, or effectiveness reviews. Action plans were then

developed, analyzed, prioritized, and incorporated into the SIBP and SIIP. The team

concluded that the ImPACT process successfully identified the performance concerns at

Palo Verde in need of corrective actions.

95003 Inspection Topical Areas FOPs

Module and Selected Fundamental Overall Problems

MORE

RCA SA EFR

ImPACT Feedback Collective

Assessment Plan Evaluation

PVARs

Input CAs,

CHECKLISTS

Historical PDSs Data Base CAPRs &

- KART Effectiveness

Data - IA &CPD Multiple Fault Codes

Reviews

- Focused

Review Assessments

Site Integrated Improvement Plan

PVARs

Roll-Up

Process

- 24 - Enclosure

The ImPACT process reviewed the following seven areas:

  • Historical Data Review: reviewed and analyzed over 4000 documents since 2001

including, in part, significant internal and external assessments of performance at

PVNGS, NRC inspection reports, NRC assessment letters, licensee event reports

(LERs), maintenance rule functional failures, trends, various corrective action

documents, and unplanned downpowers.

and safety injection systems while focusing on the adequacy of programs and processes

for design, human performance, procedure quality, equipment performance,

configuration control, and emergency response organization readiness. The Key

Attribute Review also included the inspection attributes of NRC IP 95003.

  • Identifying, Assessing, and Correcting Performance Deficiencies Review: evaluated the

effectiveness of corrective actions associated with significant performance deficiencies,

audits and assessments, resource allocation, performance goals, employee concerns

program, technical resolution programs (e.g., differing professional opinions), and use of

industry information.

  • Focused Assessments Review: evaluated specific areas of known weaknesses and

significant change for the 1989 NRC Diagnostic Assessment, the licensees re-

engineering program, PI&R crosscutting assessment, human performance crosscutting

assessment, and performance improvement plan effectiveness assessment.

  • Safety Culture Assessment Review: utilized two independent third party teams that

reviewed the safety culture for the site. This item met the safety culture requirements of

NRC IP 95003 and the NRC Confirmatory Action Letter.

  • Recirculation Actuation System and K-1 Relay Review: assessed the root causes,

appropriateness of corrective actions, effectiveness of corrective actions, and

measurements of success.

  • Collective Evaluation and Action Plans Development: performed an evaluation of the

failures and deficiencies associated with the above six evaluations. This final process

was done to identify the causes for the performance problems and then develop

corrective actions necessary to improve performance.

As of October 1, 2007, the SIBP consisted of 20 building blocks with 5 building blocks that

were designed to always be included in the business plan. These five building blocks

include plant equipment, people, CAP, safety, and knowledge/training. The other 15

building blocks can change as progress and improvement is made on an individual block

and other issues arise which require improvement and corrective action. These blocks are

depicted in the above figure and include, in part, oversight, work management,

programs/processes, procedures, and emergency preparedness. Within each building block

there were one or more initiatives, with a total of 152 initiatives. Each initiative contained

numerous tasks. At the time of the inspection, there were 1609 tasks (each task had a

CRAI) in the SIBP, of which 357 were a part of the SIIP.

- 25 - Enclosure

As of November 1, 2007, there were 339 tasks (CRAIs) closed in SWMS, with only 12 tasks

having completed improvement plan closure packages. Procedure 01DP-0AC06, required

that each task be closed and that the closure review process use a graded approach based

on the category of the task or priority of the CRAI. The team observed a Closure Review

Board meeting on October 31, 2007, and reviewed the October 24, 2007, Closure Review

Board meeting minutes. During the October 31, 2007, meeting, only two tasks were

reviewed and both were rejected because objective evidence of the actions being completed

and sustainability of the actions were not demonstrated or included as part of the package.

The meeting minutes described seven tasks being reviewed for closure of which five were

closed, one was rejected, and one was tabled (supporting information was not included with

the closure package). The team determined that the closure review of the individual tasks

was in accordance with Procedure 01DP-0AC06. The team did note that the contractors

who attended the meeting were driving the Closure Review Board members to higher levels

of accountability and making sure the process was followed; however, the Closure Review

Board was still in the process of establishing repeatable standards.

The team identified the following observations associated with the development of the SIIP:

  • The root and contributing causes for each of the FOP root causes were attributed to a

lack of management oversight, leadership, and accountability. Many of the improvement

plan tasks contained little or no detail as to how the specific tasks were to be

implemented. No additional details were available on the criteria/goals that the tasks

should meet,the development schedule, or the resource needs. For example:

1. The root cause for CRDR 3048835, Operational Focus, attributed the problems to

senior management not establishing and enforcing expectations. The evaluation did

not investigate the operations department ability to lead and the appropriateness

and implementation of the current standards of conduct.

2. CRAI 3064362 was initiated to develop a leadership model that established a vision,

mission, values, and behaviors. This corrective action was the main action in

numerous root cause evaluations that was designed to prevent recurrence of various

performance problems that resulted in PVNGS being placed into Column 4 of the

NRC Action Matrix. The description contained in the improvement plan and SWMS

for CRAI 3064362 stated, Benchmark and develop a leadership/management model

that establishes the vision, mission, values and expected behaviors for each of the

problem areas identified by the ImPACT team and the additional areas noted above.

Additionally, the management model should address ownership, the Palo Verde core

fundamental areas (Plant Equipment, People, CAP, Safety, and

Knowledge/Training), a mechanism for continuous monitoring and improvement, and

metrics to measure effectiveness. This CRAI, with a due date of June 2008,

contained no further details as to how to achieve this corrective action.

3. CRAIs 3063852, 3075713, and 3075649, identified corrective actions that were not

specific or measurable as stated in Section 17 of Root Cause Investigation Manual

for Significant CRDRs. The three CRAIs discussed corrective actions to implement

a Management Review Meeting process, develop and implement a

leadership/management model, and establish a site-wide emphasis and alignment

on the core mission and on the core fundamental focus areas. However, the CRAIs

did not include specific details and/or measurable actions.

- 26 - Enclosure

  • The team determined that for most cases, actions were included in both the CAP and

the SIIP. However, two items were not found in the improvement plan: 1) CRAI

3076878, Develop, coordinate, and implement a campaign to establish and reinforce

the position that Engineering is the design authority of the site, was one of the

corrective actions to address CRDR 3048865, Design Control and Configuration

Management Weaknesses; and 2) from the independent safety culture assessment,

CRAI 3090979 was an action to include safety conscious work environment (SCWE)

expectations in the contracts for PVNGS contractors.

  • Most of the initiatives contained tasks to either develop or modify existing metrics in

order to measure progress. However, most of the new or modified metrics that the team

reviewed were not fully developed. As with corrective actions to address the root

causes, the actions to develop metrics were high level and contained few details. It was

unclear how CRAI 3064372, Develop and utilize metrics to ensure Palo Verde uses the

CAP, training, operating experience, self-assessments/benchmarking, and independent

oversight activities to establish a continuous learning environment, will address the

contributing cause of ineffective implementation of those programs to drive

improvements in individual and station performance as described in the CRDR 3048836,

Organizational Effectiveness root cause report.

  • Effectiveness review descriptions were broad, and the criteria provided ambiguous

information on acceptability. For example, CRAIs 3064491 and 3075832 stated that the

interim and final effectiveness reviews can be closed once the following are met: 1) site

performance indicators reflected acceptable performance or overall site improvement;

2) the independent assessment determined that actions were effective, specifically that

Palo Verde had established, communicated, and reinforced standards specific to each of

the focus areas in the leadership/management model and that accountability is

adequately addressed; and 3) overall responses from the safety culture survey indicated

an improving trend. The team did not identify specific criteria that will be used to

determine the effectiveness of the corrective actions (e.g., what constitutes overall site

improvement or an improving trend).

  • CRAIs 3063112, develop and implement a site-wide communication strategy, and

3063852, implement a Management Review Meeting process, were coded as Priority 3;

however, the improvement plan had the CRAIs listed as corrective actions to prevent

recurrence which should have been coded Priority 2 as specified by

Procedure 01DP-0AC06. Licensee personnel indicated that they were already aware of

these two examples and had documented these differences, as well as other differences

for CRAI due dates, priorities, and text descriptions on PVAR 3083805, dated

October 26, 2007. As of November 2, 2007, the licensee had identified 35 CRAIs whose

priority codes did not match the improvement plan classification.

  • As of November 2, 2007, the licensee had not resource loaded the SIBP/SIIP.

Nevertheless, over 1100 of the 1609 tasks (from November 2007 to December 2008)

were scheduled to be completed by December 31, 2008. This schedule did not appear

to be achievable based on the large number of tasks that have to be closed over the

next 12 months along with the large backlog of work activities that currently exist.

Numerous issues with corrective action due dates were identified by the team, including:

- 27 - Enclosure

1. CRAIs associated with CRDR 3048835, operational focus root cause, had out of

sequence due dates. CRAI 3065021, which was to develop a site indicator for

operational focus, had a due date of January 31, 2008. CRAIs 3062174, 3062184

and 3062188 were written to train leaders on the establishment and proper use of

performance indicators; however, this action had a due date of October 27, 2008,

well after the development of the operational focus indicator.

2. CRAI 3038014 was to conduct a site wide stand-down in order to communicate CAP

fundamentals to all PVNGS personnel. This corrective action item was initiated on

July 9, 2007, and had a due date of December 28, 2007. The team determined that

this action was untimely considering that the Unit 3 outage started

September 29, 2007, and the continuation of CAP weaknesses demonstrated at

PVNGS.

3. The PI&R root cause in CRAI 3037453 initiated on July 6, 2007, was to conduct a

self-assessment of the OD program by June 30, 2008. The team considered this

action untimely given the continued problems with the implementation of this

program for the past several years, as well as numerous OD issues identified during

this inspection.

4. The SIIP contained actions that had due dates significantly different from what was

initially specified for the root and contributing cause corrective actions. The team

was concerned that the corrective actions were untimely, especially for the

substantive crosscutting areas of human performance and PI&R, where performance

had not appreciably improved. After incorporation into the SIIP, all of the following

CRAIs had their due dates extended for more than a year from the originally

scheduled completion date: 1) CRAI 3015013, Facilitate implementation of

programmatic actions to improve procedure use and adherence, as well as improve

procedure quality, had the due date changed from October 1, 2007, to

October 1, 2008; 2) CRAI 2936516 was written to evaluate human performance

integration with key work processes. This CRAI was due to be completed December

31, 2007, but was changed to March 15, 2009; 3) CRAI 2941720 was written to

develop a process to add operating experience to work packages. This CRAI was

due to be completed by June 1, 2007, but was changed to December 31, 2008;

4) CRAI 2941718 was written to make operating experience search engines more

available and easier to use. This CRAI was due to be completed by June 1, 2007,

but was changed to December 28, 2008; and 5) CRAI 3038038 was a corrective

action to provide training for all advocates in their responsibilities for quality CAP

implementation with a due date of November 30, 2007. When the action was

incorporated into the SIBP as Task 3.3.3.d, the action was changed to Establish a

process to provide training for all Advocates with the same due date. Actual

training of the advocates is in Action 6.3.1.b (CRAI 3032702) with a due date of

March 15, 2009.

  • Limited reviews were completed by the licensee on past work products to look for

mistakes that could have a potential impact on plant equipment and a corresponding

reduction in safety. The team was concerned that a historical review of most

programs/processes work products, including the CAP, had not been conducted and

was not included as an action in the SIIP.

- 28 - Enclosure

  • Observations associated with the incorporation of safety culture insights into the

improvement plan are referenced in Section 8.1, under the heading titled, Licensee

Analysis and Corrective Actions. The observations included weaknesses in

resource/staffing levels, a lack of links between corrective actions associated with safety

culture and the SIIP, and ongoing incorporation of safety culture assessment findings

and recommendations into the SIIP.

3 COLLECTIVE SIGNIFICANCE REVIEW

Collective Review of Root and Contributing Causes

The team compared the results from the inspection to the root cause analyses performed by

the licensee and information docketed from previous NRC inspections. The team concluded

that the licensees root and contributing causes bounded the performance deficiencies

identified during the ImPACT review and the NRC IP 95003 inspection. The licensee

identified numerous root and contributing causes for the performance deficiencies. The

following is a summation of the key root and contributing causes applicable to most of the

licensees investigations: (1) leaders did not establish, communicate, and enforce standards

and expectations for performance or hold individuals accountable to those standards; (2) the

corrective action program, operating experience, self assessments, and benchmarking did

not drive individual and station performance improvement; (3) responsibility, accountability,

and authority for nuclear safety were not well defined or understood; (4) individual behaviors

that demonstrate nuclear safety principles were not consistently applied; (5) management

was not receptive to organizational issues identified during investigations; (6) change

management activities did not anticipate unintended consequences and did not clearly

define and communicate changes to station personnel; and (7) Oversight groups did not

provide specific and meaningful interventions to correct declining performance.

Collective Review of Risk

The team completed an assessment of the collective risk associated with the IP 95003

findings. The team was supported by senior reactor analysts from NRC Region IV and

headquarters during the risk assessment. Three methods were used: (1) an adjustment to

the human error probabilities in the Palo Verde Standardized Plant Analysis Risk (SPAR)

model, Revision 3.31, (2) assignment of risk results to each finding screened as having very

low safety significance, and (3) a qualitative assessment using the NRC IMC 0305,

Operating Reactor Assessment Program, criteria for determining if oversight of a licensee

should be performed under NRC Manual Chapter 0350, Oversight of Reactor Facilities in

Shutdown Condition due to Significant Performance and/or Operational Concerns. The

team concluded that Palo Verde was safe for continued operation even though a

degradation in safety performance had occurred and there were several longstanding

performance concerns.

Palo Verde SPAR Model

Palo Verde had documented substantive crosscutting issues in human performance and

PI&R since March 2005 NRC Annual Assessment Letter. Given the duration of the

substantive crosscutting issues, the analyst used approved significance determination tools

to estimate the effect that this condition had on the risk of operating the plant. The primary

source document used in this effort was the SPAR-H Human Reliability Analysis Method,

NUREG/CR-6883 (SPAR-H).

- 29 - Enclosure

The analyst used the Palo Verde SPAR model, Revision 3.31, dated June 18, 2007. The

model was updated to correct errors where the SPAR-H calculator did not account for

dependencies when three or more negative performance shaping factors (PSFs) were

judged to affect the human error probability (HEP) for a human action basic event. This had

the effect of lowering some of the HEPs in the base model.

The analyst assumed that the condition of poor work practices existed for at least one year,

consistent with the exposure time limits of the significance determination process, and that

the condition affected all of the human actions included in the SPAR model equally, with the

exception of offsite power recovery actions (which were deemed to be controlled mostly by

outside influences). Using the SPAR-H Worksheets for action steps at power, a PSF

penalty for poor work practices was assumed, which assigns a multiplier of 5.0 for the

likelihood of failure. For basic events where there were less than 3 negative PSFs, this

resulted in the HEP being increased by a factor of 5.0. For cases where three or more PSFs

existed, the factor of increase was less than 5.0. Although offsite power recovery actions

were left unchanged, the non-recovery probabilities for recovery of a diesel generator, which

use actuarial data in lieu of the SPAR-H method, were increased by a factor of 10 percent.

The base core damage frequency (CDF) was 8.989E-6/year. Application of the 5.0 PSF for

poor work practices resulted in a total CDF of 4.605E-5/year, or a delta-CDF of

3.706E-5/year.

This result accounts only for internal initiating events and does not consider the additional

risk associated with seismic, fire, or other external initiators, nor does it account for the risk

associated with shutdown conditions. Typically, external initiating events approximately

equal the risk associated with internal initiators. Using the above results, and assuming that

poor work practices would affect the recovery from external initiators to the same extent as

for internal initiators, the total baseline CDF would be 1.798E-5/year. The total CDF

associated with poor work practices would be 9.210E-5/year, and the delta-CDF would be

7.412E-5/year.

In accordance with IMC 0609, Appendix H, Containment Integrity Significance

Determination Process, for a large, dry containment, the large early release frequency

(LERF) is significant only with respect to steam generator tube ruptures and intersystem loss

of coolant accidents (ISLOCAs). Employing the same assumptions used in the CDF

calculation for the effect of poor work practices, the results for ISLOCAs and steam

generator tube ruptures are as follows:

Base CDF = 5.025E-7/year

Work Practices CDF = 5.371E-6/year

Delta CDF = 4.868E-6/year

The LERF fraction for both ISLOCAs and steam generator tube ruptures is 1.0. Therefore

the delta LERF is also equal to 4.868E-6/year. The significance bands for LERF are one

order of magnitude lower than those corresponding to CDF. Consequently, for the case of

poor work practices, the LERF significance is the same as the CDF significance.

The result is below the Regulatory Guide 1.174, An Approach to Using Probabilistic Risk

Assessment in Risk-Informed Decisions on Plant-Specific Changes to the Licensing Basis,

limitations for a maximum total plant CDF. Regulatory Guide 1.174 makes use of the NRCs

Safety Goal Policy Statement in evaluating increases in CDF and LERF. The safety goals

- 30 - Enclosure

define an acceptable level of risk that is a small fraction (0.1 percent) of the other risks to

which the public is exposed. Regulatory Guide 1.174 specified that, if there is an indication

that the total CDF may be considerably higher than 1E-4/year or 1E-5/year for LERF, the

focus should be on finding ways to decrease the risk. The team noted that the total

collective risk did not exceed the Regulatory Guide 1.174 upper limits.

Several defense in depth layers of protection are provided to protect the public and the

environment from potential events. These include the integrity of the physical structure of

the plant and its systems, the automatic initiation capabilities of the safety-related systems,

the proceduralized operator manual actions to start equipment and initiate systems, and the

ability of plant operators and technicians to restore, repair, or replace equipment as

necessary. Poor work practices can degrade any of these defense-in-depth layers of

protection, but would mostly cause a loss of efficiency and precision in the operators ability

to take important manual actions, as well as the ability of the plant staff to restore non-

functioning equipment. The team determined that there had been a reduction in defense in

depth features because of the degradation of the CAP and human performance safety

culture concerns; however, the reduction was not sufficient to result in an unsafe condition.

Collective Assessment of IP 95003 Findings

Inspection Manual Chapter 0609, Significance Determination Process, utilizes a counting

rule to assess the significance of a performance deficiency. Using the Phase 2 plant

specific worksheets, core damage sequences are assigned a range of numeric values.

Three sequences with the same numeric result are treated with the next lower value

(e.g., three sequences with an 8 would be treated as one 7). For the purpose of the

collective review, the team assigned a significance determination process result of 8 for all

findings screened as Green during the Phase 1 process. The counting rule was then used

to determine the collective risk. This result was combined with any numerical results

obtained as part of a Phase 3 SDP evaluation for an inspection finding. The emergency

preparedness finding was assigned a value of 3.3E-6. Fifteen examples of findings were

screened as Green during the Phase 1 SDP process (this included findings screened using

IMC 0609, Significant Determination Process, Appendix M, Significance Determination

Process using Qualitative Criteria). Using the counting rule, this equates to a result of one

5. The team applied a CDF value of 3.3E-5/year from the counting rule result. The results

from the Phase 3 SDP evaluation for the switchyard finding was 5.0E-7/year. The combined

result was a CDF of 3.68E-5/year.

If all of the significant findings since 2004 were included, the total result would be between a

range of 4.69E-5/year to 8.79E-5/year. This includes a range of 5.7E-6/year to 4.6E-5/year

for the Yellow finding and 10 CFR 50.59 Severity Level III violation, an assigned value of

3.3E-6/year for the Emergency Preparedness Plan Change Severity Level III violation, and a

range of 1.1E-6/year to 1.8E-6/year for the White finding. Both cases are below the

Regulatory Guide 1.174 limitations for a maximum total plant CDF.

Qualitative Assessment Using Manual Chapter 0305 Criteria

Manual Chapter 0305 uses three criteria to assess the applicability of Manual Chapter

0350. The teams assessment of the Manual Chapter 0305 criteria are as follows:

1. Multiple significant violations of the facilitys license, Technical Specifications,

regulations, or orders.

- 31 - Enclosure

Multiple significant violations (greater than green for SDP findings or greater than

Severity Level IV for non-SDP findings) have not recently occurred. Specifically, a

Severity Level III violation of 10 CFR 50.59 and a Yellow finding related to the

containment sump voiding issue occurred in 2004; a Severity Level III violation for the

failure to obtain prior NRC approval for an emergency plan change was issued in 2005;

and a White finding for the failure of an emergency diesel generator was issued in 2006.

In consideration of this attribute, the team reviewed significant violations identified since

2004, as well as the potentially significant emergency preparedness and overtime

findings identified during the IP 95003 inspection. The team concluded that while there

had been multiple significant findings dating back to 2004, the current assessment cycle

did not have any significant findings. If the emergency preparedness and overtime

findings are determined to be greater than Green (significant), they will be the only

significant items identified during 2007. As such, this criterion would still not be met.

2. Loss of confidence in the licensees ability to maintain and operate the facility in

accordance with the design basis (e.g., multiple safety significant examples where the

facility was determined to be outside of its design basis, either due to inappropriate

modifications, the unavailability of design basis information, inadequate configuration

management, or the demonstrated lack of an effective problem identification and

resolution program).

The team determined that while the licensees CAP is complicated and cumbersome, the

CAP contained the basic elements of an effective program. Licensee personnel

recognized the attributes of problem identification, evaluation, and resolution when

interviewed; however, the knowledge and understanding was not consistently

demonstrated to the NRC during the IP 95003 inspection. Nevertheless, multiple

significant examples of problems with the design basis have not been identified;

therefore, this criterion was not met.

3. A pattern of failure of licensee management controls to effectively address previous

significant concerns to prevent recurrence.

A substantial degradation of the CAP has occurred. There have been repetitive failures

in management controls to improve human performance and problem identification and

resolution. There have also been several repetitive occurrences of risk important

equipment failures (auxiliary feedwater Target Rock steam admission valves,

emergency diesel generator fuel and lube oil filters, safety injection system check

valves, and essential cooling water heat exchanger fouling). The licensee has not had a

recurrence of voided piping or emergency diesel generator K-1 relay failures following

the issuance of the Yellow and White findings. Because the repetitive occurrences were

determined to be of very low safety significance, this criterion was not met.

4 NRC METHODOLOGY AND DIAGNOSTIC ASSESSMENT

The intent of IP 95003 is to allow the NRC to obtain a comprehensive understanding of the

depth and breadth of safety, organizational, and performance issues at facilities where data

indicate the potential for serious performance degradation. The objectives of the IP 95003

inspection are to:

- 32 - Enclosure

(1) provide additional information to be used in deciding whether the continued operation of

the facility is acceptable and whether additional regulatory actions are necessary to

arrest declining performance;

(2) provide an independent assessment of the extent of risk significant issues to aid in the

NRCs current assessment that an acceptable margin of safety exists;

(3) independently evaluate the adequacy of facility programs and processes used to

identify, evaluate, and correct performance issues;

(4) independently evaluate the adequacy of programs and processes in the affected

strategic performance areas;

(5) provide insight into the overall root and contributing causes of identified performance

deficiencies;

(6) determine if the NRC oversight process provided sufficient warning of significant

reductions in safety; and

(7) independently assess the licensee safety culture and assess their evaluation of safety

culture.

A multi-disciplinary team conducted the inspection over the course of approximately nine

months, with a total of five weeks of onsite inspection effort. The inspection implemented

the applicable portions of IP 95003 necessary to assess the extent of performance problems

that led to the licensees entry into Column 4 of the NRCs Action Matrix, including the safety

culture contributions to the performance problems, as well as the licensees corrective action

plan. The team performed an independent diagnostic review of numerous programs and

processes with an emphasis on the reactor safety strategic performance areas. This

provided the NRC with a comprehensive understanding of the depth and breadth of safety,

organizational, and performance issues at PVNGS, in addition to the insights already gained

from the IP 95002 inspections conducted in 2005 and 2006.

The team selected the containment spray system and the turbine driven auxiliary feedwater

pump, high pressure safety injection pump, low pressure safety injection pump, and

essential spray pond pumps. The selection of these components was based on the impact

of component failure on large early release frequency and the completion of a detailed

design review being completed by the licensee as part of their component design basis

review. The team performed a review of the work performed on these components which

involved multiple licensee organizations, including operations, maintenance, engineering,

quality assurance, and management. With respect to these components, the team review

included, as applicable, permanent and temporary design modifications (including

implemented, planned, and cancelled modifications), procedure and drawing changes, ODs,

operator work arounds, configuration control, maintenance, root and apparent cause

evaluations, and various corrective action documents. Additionally, the team reviewed

PVNGS programs and processes associated with human performance and PI&R.

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5 REACTOR SAFETY STRATEGIC PERFORMANCE AREA

5.1 Licensee Controls for Identifying, Assessing, and Correcting Performance Deficiencies

The licensee had multiple substantive crosscutting aspects associated with human

performance and PI&R. Since 2004, the corrective actions implemented by the licensee

had yet to sustain performance improvement as noted by licensee self assessments,

external industry reviews, and NRC inspections. The team noted that licensee personnel

often recognized appropriate CAP fundamentals and expected behaviors when

interviewed; however, this knowledge and understanding of the program expectations was

not consistently demonstrated. The team noted several examples of poor and inconsistent

implementation of safety culture aspects associated with PI&R. Specifically:

  • Licensee personnel did not recognize the need to initiate a PVAR, the licensees

corrective action document form, when a degraded condition was identified by the

team. This particular behavior improved during the conduct of the inspection in

response to the teams repeated questioning of licensee personnel on whether a

PVAR was appropriate for NRC identified issues. The team noted that consistent re-

enforcement of expectations was needed to ensure PVARs would continue to be

initiated following the teams departure.

  • The team noted that a licensee component design basis review (CDBR) team

(consisting largely of contractor personnel) was documenting issues that challenged

the design basis at an appropriately low threshold. In contrast, Palo Verde

engineering personnel considered these issues below the PVAR threshold or that the

problems entered were not issues at all. This demonstrated a continuing lack of

understanding on the part of Palo Verde engineering personnel of the level at which

conditions adverse to quality should be documented in the CAP.

  • The team noted a significant number of weak or non-existent operability

determinations of degraded conditions affecting safety-related equipment, indicating

an apparent lack of understanding of the need to assess operability for conditions

adverse to quality and a lack of knowledge or skills necessary to conduct an operability

assessment. This is a continuing weakness in the implementation of the CAP at Palo

Verde and had a direct impact on maintaining nuclear safety margins. The inability to

consistently perform ODs formed part of the NRCs basis for leaving open the Yellow

finding involving voiding of the ECCS suction piping in all three units. Improvement in

the operations and engineering departments are required for Palo Verde to effectively

evaluate degraded conditions affecting safe plant operation.

  • The team noted that a significant backlog review was required due to the large number

of databases (at least 37) that existed outside of the corrective action process. The

team identified that at least two databases existing outside of the recognized CAP

contained conditions adverse to quality that had not been assessed for operability.

The Action Tracking System (ACT) database and the Bechtel non-conformance

reporting (NCR) database both contained conditions adverse to quality that were not

evaluated for operability impacts until prompted by the team. Licensee personnel

subsequently reviewed the databases and additional conditions adverse to quality that

required operability assessments were identified. The placement of conditions

adverse to quality in systems outside the CAP hindered the ability of operations

- 34 - Enclosure

personnel to assess challenges to the operability of structures, systems, and

components (SSCs).

evaluated within the CAP, the need to evaluate the extent of condition or impact to the

other units was not always recognized.

  • The team concluded that self-assessments completed by Palo Verde personnel lacked

depth and did not effectively specify or implement corrective actions. As a result, the

self-assessment program seldom resulted in improved organizational performance.

The team did note one training self-assessment that had been recently conducted

which had more depth and contained insightful observations. The team noted that this

self-assessment was conducted by a mix of Palo Verde and non-Palo Verde personnel

which may have led to the more meaningful self-assessment.

  • The teams evaluation of root cause analyses determined that the analyses of

problems did not consistently specify complete or adequate corrective actions, or

establish timely corrective actions for significant conditions adverse to quality.

  • The team identified that the licensee had difficulty determining the status or completion

of corrective actions taken in response to significant issues. This was most apparent

when licensee personnel could not effectively respond to a team request to

communicate the status of corrective actions related to the Yellow finding for voiding of

ECCS suction piping. The licensee could not effectively determine the completion

status of these corrective actions nor had the actions been effectively evaluated for

resolution of the issues. The licensees IP 95002 Readiness/Effectiveness Report

stated that the 95002 focus areas, Seem to have been administratively forgotten. In

addition, the team noted that an ImPACT Checklist intending to evaluate the status of

the Yellow finding, identified several problems; however, not all of the problems had

CAP actions written to address the identified issues.

  • Licensee personnel were assigned corrective actions for significant conditions adverse

to quality; however, processes were not consistently implemented to ensure corrective

actions were completed or that effectiveness reviews of these actions were completed.

The team identified that corrective actions taken in response to significant conditions

adverse to quality were sometimes closed prior to completion of the corrective action.

This sometimes occurred when a significant action was closed to another document,

which was subsequently closed prior to the completion of the action. In the past, the

licensee used an unsuccessful approach that relied on individual management team

members to verify significant corrective actions were complete and to evaluate their

effectiveness. More recently, the licensee instituted a Closure Review Board process

to assess completion of significant corrective actions and to assess their effectiveness.

The team acknowledged that a management team review could be more successful in

assuring the completion and effectiveness of corrective actions.

a. Inspection Scope

The team evaluated whether the licensees CAP was sufficient to prevent further

declines in safety that could result in unsafe operation. Specifically, the team

reviewed: (1) licensee investigations, evaluations, and corrective actions taken in

response to significant conditions adverse to quality; (2) audits and assessments

- 35 - Enclosure

conducted by the Nuclear Assurance Department, self-assessments by organizations,

and external evaluations and assessments; (3) the effectiveness of the licensees use

of operating experience and industry information for previously documented

performance issues; (4) historical and current resource allocations, as well as the

current backlog and existing operator work-arounds; (5) the business plan to

determine if licensee performance goals were congruent with corrective actions

needed to address performance issues; (6) the employee concerns program as well as

a significant number of focus group discussions with a cross-section of the licensees

workforce; and (7) the licensees programs and processes in place to support

improvement suggestions by employees and to provide employees feedback on issues

they had identified.

b. Findings and Observations

b.1 Failure to Implement Operability Determination Process for Bechtel

Nonconformance Reports

Introduction. The team identified an example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and

Drawings, for the failure of the licensee to follow procedures to evaluate

conditions adverse to quality for impacts on the operability of safety-related

equipment.

Description. On October 4, 2007, the team met with the licensee to discuss the

quality assurance program requirements agreed to between the licensee and

Bechtel for the conduct of the Unit 3 steam generator replacement outage, and

how Bechtel nonconformance reports (NCRs) generated during this activity were

reviewed by the licensee. The discussion was held in response to the teams

identification of a condition adverse to quality associated with the rigging of the

containment personnel airlock (PAL) door.

On October 6, 2007, the team questioned the CAP manager on how Bechtel

NCRs were reviewed by the licensee for potential impacts to the operability of

safety-related equipment. The team noted that a formal process to review NCRs

for immediate operability did not exist. As a result of the teams questioning, the

CAP manager initiated actions to review the NCR database. As a result, two

NCRs were identified which documented conditions adverse to quality that

affected safety-related equipment. Specifically, a piping support affecting

shutdown cooling heat exchanger Train A had been inadvertently removed by

Bechtel and an NCR was written to document the problem. No PVAR was

generated and as a result, no operability assessment of the degraded condition

was conducted. Shutdown cooling heat exchanger Train A was declared

inoperable until an engineering evaluation determined the missing support did

not affect operability. A second Bechtel NCR was then identified that

documented the inadvertent removal of steam generator weldment. This

condition was subsequently determined not to affect operability of safety-related

equipment.

On October 8, 2007, the licensee generated a night order that required all NCRs

generated by Bechtel to have PVARs written to assure operability assessments

of conditions adverse to quality were conducted.

- 36 - Enclosure

Analysis. The failure to implement the OD process for conditions adverse to

quality identified in the Bechtel NCR database was a performance deficiency.

The finding is greater than minor because it was associated with the equipment

performance attribute of the mitigating systems cornerstone and affected the

associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using the IMC 0609, Significance Determination Process,

Phase 1 Worksheets, the finding is determined to have very low safety

significance (Green) because it only affected the mitigating systems cornerstone,

and did not result in the loss of safety function. The cause of this finding had

crosscutting aspects associated with decision-making of the human performance

area in that licensee personnel did not make safety-significant or risk-significant

decisions using a systematic process (H.1.(a)). This finding also had a safety

culture component aspect in the area of accountability in that management did

not reinforce safety standards associated with the need to perform operability

assessments (O.1.(b)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, requires that activities affecting quality be prescribed

by instructions, procedures, or drawings, and be accomplished in accordance

with those instructions, procedures, and drawings. The assessment of

operability of safety-related equipment needed to mitigate accidents was an

activity affecting quality and was implemented by Procedure 40DP-9OP26,

Operability Determination and Functional Assessment, Revision 18. Procedure

40DP-9OP26, Step 3.1.1, stated the OD process was entered upon discovery of

circumstances where operability of any SSC described in the Technical

Specifications was called into question upon discovery of a degraded,

nonconforming, or credible unanalyzed condition. Contrary to the above,

between October 4 and 6, 2007, licensee personnel failed to enter the OD

process upon discovery of circumstances where the operability of a component

described in the Technical Specifications was called into question. Specifically,

the removal of a shutdown cooling heat exchanger support and the removal of

steam generator weldment were not evaluated for operability impacts to safety-

related equipment. Because this finding is of very low safety significance and

had been entered into the CAP as PVAR 3072732, this violation is being treated

as an NCV, consistent with Section VI.A of the Enforcement Policy: NCV

05000528, 05000529,05000530/2007012-01, eight examples of the Failure to

Implement Operability Determination Process. This was the first of eight

examples associated with the licensees failure to properly implement the OD

program.

b.2 Failure to Implement Operability Determination Process for ACTs

Introduction. The team identified a second example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and

Drawings, for the failure of licensee personnel to follow procedures to evaluate

conditions adverse to quality for degraded or non-conforming conditions that

required ODs or FAs.

Description. On June 22, 2007, the Palo Verde ImPACT team documented that

the ACT database contained conditions adverse to quality and that the, Entire

- 37 - Enclosure

ACT database needed to be scrubbed to identify all discrepancies. On

August 29, 2007, the team requested the status of the ACT database scrub, to

determine whether additional conditions adverse to quality were identified in the

ACT database since the June 22, 2007, roll-up, and whether these and the

previous conditions identified on June 22, 2007, had been evaluated by a

licensed senior reactor operator (SRO) for degraded or non-conforming

conditions that would require ODs or FAs. The ImPACT team determined that

additional conditions adverse to quality had been identified and that a PVAR had

been generated; however, neither the previously identified ACT issues nor the

more recently identified ACT issues had been assessed individually for OD or FA

requirements as discussed in Procedure 01DP-0AP12, Palo Verde Action

Request Processing, Revision 3. An SRO evaluated the initial PVAR

documenting the ACTs and determined that no impact to plant safety existed, but

did not complete a review of each individual ACT in question. Subsequent to the

teams questioning, an SRO reviewed each ACT that documented a condition

adverse to quality. The ImPACT team subsequently informed the NRC team on

September 4, 2007, that none of the conditions adverse to quality identified in the

ACT database required further evaluation.

Analysis. The failure to implement the PVAR process for conditions adverse to

quality identified in the ACT database was a performance deficiency. The finding

is greater than minor because it is associated with the equipment performance

attribute of the mitigating systems cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable circumstances.

Using the IMC 0609, Significance Determination Process, Phase 1 Worksheets,

the finding is determined to have very low safety significance (Green) because it

only affected the mitigating systems cornerstone and each of the ACT database

conditions adverse to quality were subsequently determined not to result in a loss

of safety function. The cause of this finding had crosscutting aspects associated

with decision-making of the human performance area in that licensee personnel

did not make safety-significant or risk-significant decisions using a systematic

process (H.1.(a)). The cause of the finding is also related to the safety culture

component of accountability in that management failed to reinforce safety

standards and display behavior that reflect safety as an overriding priority

(O.1.(b)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, requires that activities affecting quality be prescribed

by instructions, procedures, or drawings, and be accomplished in accordance

with those instructions, procedures, and drawings. The evaluation of the need to

forward degraded or non-conforming conditions documented in PVARs to the

control room for OD or FAs was an activity affecting quality implemented by

Procedure 01DP-0AP12. Procedure 01DP-0AP12 required that a SRO evaluate

PVAR issues to determine whether a degraded or non-conforming condition

exists in an SSC subject to the OD or FA process. Contrary to the above,

between June 22 and September 4, 2007, licensee personnel did not assess

individual conditions adverse to quality documented in ACTs and attached to a

PVAR for the need to conduct an OD or FA. This example is of very low safety

significance and had been entered into the CAP as PVAR 3057126 and CRDR

- 38 - Enclosure

3058751. This was the second of eight examples associated with the licensees

failure to properly implement the OD program.

b.3 Failure to Implement Operability Determination Process for Spray Pond Missile

Hazards

Introduction. The team identified a third example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, for the failure of licensee personnel to follow procedures to evaluate

conditions adverse to quality for impacts on the operability of safety-related

equipment.

Description. On August 29, 2007, the team conducted an external walkdown of

Unit 1 with licensee personnel and identified approximately 20 unsecured metal

bars (severe weather missile hazards) near the Unit 1 essential spray pond

(ESP). Following prompting by the team, the licensee generated PVAR 3057285

on August 30, 2007, to address this condition.

The ESPs function as the ultimate heat sink. Spray headers, located above the

surface of the ESPs, are used to maintain design temperature within safety

analysis assumptions. There are no missile hazard ESP design features to

protect the spray headers from airborne missiles and, as a result, they are

vulnerable to airborne missiles generated during a high wind event. Procedure

81DP-0ZY01, Control of Potential Tornado Borne Missiles in the Outside Areas,

Revision 2, Section 1.1 stated the purpose of the procedure was to establish

administrative controls for using and storing items in outside areas so the risk of

losing the ESPs was within acceptable limits. Procedure 81DP-0ZY01, Appendix

E, Tornado Missile Density Criteria (Zones 1-14), identified the average density

limit at four missiles per 10,000 square feet (sqft) within a defined area around

the ESP. The unsecured transient missiles identified by the team were within

this defined area.

On August 30, 2007, a civil engineer conducted a tour of the area. PVAR

3057285 stated that the engineer determined that there was no operational

impact on the spray pond headers because the condition did not exceed the

operability basis of 4 missiles/sqft. This PVAR incorrectly referenced the

guidance from Procedure 81DP-0ZY01, did not address the fact that there were

more than 4 missiles, and contained no operations shift manager assessment of

the impact to the Unit 1 ESPs.

Procedure 40DP-9OP26, Revision 18, Operability Determination and Functional

Assessment, Section 3.1.1 stated that the OD process was entered upon

discovery of circumstances where operability of any SSC described in the

Technical Specifications was called into question upon discovery of a degraded,

nonconforming, or credible unanalyzed condition. The team noted that the

licensee did not enter the OD process on August 29, 2007, upon discovery of an

unanalyzed condition (unsecured, transient missiles near the Unit 1 ESP).

Procedure 40DP-9OP26, Section 1.3 stated that the immediate OD was

performed based on the best information available to on-shift personnel within a

relatively short time, typically on the order of two hours. In this case, neither

- 39 - Enclosure

engineering nor operations personnel notified the control room of the condition

when PVAR 3057285 was generated. Instead a work control SRO reviewed

PVAR 3057285 on August 31, 2007, and determined that a degraded condition

no longer existed because PVAR 3057285 stated the 20 transient missiles were

being removed and an analysis was completed satisfactorily.

Procedure 40DP-9OP26, Section 2.1 stated that the shift manager (SM) was

responsible for the OD decision. In this case, the Unit 1 SM was not notified of

the condition. PVAR 3057285 noted that the Unit 1 shift technical advisor, a non-

licensed operator, was notified of the civil engineering evaluation completed on

August 30, 2007, and that the 20 unsecured transient missiles would be removed

by August 31, 2007. However, the shift manager was not informed and no

assessment of operability was conducted.

Analysis. The failure to implement the OD process to assess the impact of the

unsecured, transient missiles on the operability of the Unit 1 ESP was a

performance deficiency. The finding is greater than minor because it is

associated with the external factors attribute of the mitigating systems

cornerstone, and impacted the cornerstone objective of ensuring the availability,

reliability, and capability of the ultimate heat sink to respond to initiating events.

Using the IMC 0609, Significance Determination Process, Phase 1 Worksheets,

the finding is determined to have very low safety significance (Green) because

the finding did not involve the loss of a safety function due to a severe weather

initiating event. The cause of this finding had crosscutting aspects associated

with decision making in the human performance area in that operations and

engineering personnel failed to use conservative assumptions for operability

decision-making when evaluating degraded and nonconforming conditions

(H.1.(b)). This finding also had a safety culture component aspect associated

with accountability in that workforce did not demonstrate a proper safety focus

and reinforce safety principles among peers (O.1.(c)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, "Instructions,

Procedures, and Drawings, requires that activities affecting quality be prescribed

by instructions, procedures, or drawings, and be accomplished in accordance

with those instructions, procedures, or drawings. The assessment of operability

of the Unit 1 ESP was an activity affecting quality and implemented by Procedure

40DP-9OP26. Procedure 40DP-90P26, Step 3.1.1 stated the OD process was

entered upon discovery of circumstances where operability of any SSC described

in the Technical Specifications was called into question upon discovery of a

degraded, nonconforming, or credible unanalyzed condition. Contrary to the

above, between August 29 and 31, 2007, licensee personnel failed to enter the

OD process upon discovery of circumstances where the operability of a

component described in the Technical Specifications was called into question.

Specifically, operations personnel did not implement the OD process described in

Procedure 40DP-9OP26 during the period from discovery of the issue to the

removal of the missiles from the ESP area. This was the third of eight examples

of the NCV associated with the failure to implement the OD program. This

example was of very low safety significance (Green) and documented in the

licensees CAP as PVAR 3057285.

- 40 - Enclosure

b.4 Failure to Evaluate Abnormally High Lead Levels in Low Pressure Safety

Injection Pump Bearing Oil

Introduction. The team identified a fourth example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, for the failure of engineering personnel to determine the cause of an

abnormally high lead content in the Unit 3 low pressure safety injection (LPSI)

Pump Train B upper motor coupling bearing oil, to establish periodic monitoring

requirements, or to establish a lead content threshold upon which to take further

action on a degrading condition.

Description. On October 10, 2007, the team reviewed the OD associated with

the Unit 3 Train B LPSI Pump high lead levels (258 parts per million (ppm)),

which had existed in the upper motor coupling bearing oil since May 2006. This

coupling bearing was installed on all six LPSI pumps between 1995 and 2000.

The other five LPSI pumps at the site had not exhibited this condition and had oil

sample results of less than 1 ppm lead. The OD for this issue was documented

in CRDR 2896417.

During the initial investigation in May 2006, the Unit 3 Train B LPSI Pump

bearing oil was drained, flushed, and refilled with oil from a separate source. The

oil samples from the upper motor coupling bearing continued to show abnormally

high levels (242 ppm) of lead. The engineering evaluation concluded that there

should be no component materials in the pump assembly that contain lead.

Maintenance personnel determined that the parts used during the modification

were of the same type used for the other 5 LPSI pump modifications, whose

current oil samples showed lead levels to be less than 1 ppm. Oil chemistry

analysis determined that the lead particulates were relatively small and did not

detect any abnormal bearing wear metals. Also, the LPSI Pump Train B vibration

data remained within normal limits. On this basis, the licensee concluded the

Train B LPSI pump was operable and discontinued their investigation into the

cause of the high lead condition.

Engineering personnel determined that the expected lead content for the motor

coupling oil should be less than 1 ppm. The industry standard used in

determining precursor failure criteria assumed the oil environment contained less

than 10 ppm of lead content. The actual condition of the Unit 3 Train B LPSI

pump upper motor coupling bearing was approximately 242 ppm following the

drain, flush, and refill of the oil reservoir.

Procedure 40DP-9OP26, Revision 18, Section 1.3 stated that if a condition was

determined operable but degraded/nonconforming, then a PVAR will pursue the

appropriate corrective actions. The OD performed in May 2006 did not

determine a cause for this existing condition, did not develop a monitoring plan,

and did not develop a plan to take actions at predetermined thresholds in the

event of a further degradation in lead levels. In response to the teams

questions, the licensee initiated CRDR 3079670 on October 19, 2007, to

determine the source of the lead particles in the Unit 3 Train B LPSI upper motor

coupling bearing oil.

- 41 - Enclosure

Analysis. The failure to take measures to evaluate conditions adverse to quality,

to establish a monitoring program, or to establish a threshold of when to take

actions for a degrading condition was a performance deficiency. The finding is

greater than minor because it was associated with the equipment performance

attribute of the mitigating systems cornerstone, and impacted the cornerstone

objective of ensuring the availability, reliability, and capability of the LPSI system

to respond to initiating events to prevent undesirable consequences. Using the

IMC 0609, Significance Determination Process, Phase 1 Worksheets, the

finding is determined to have very low safety significance (Green) because the

finding did not result in an actual loss of Technical Specification equipment for

greater than the allowed outage time. The cause of this finding had crosscutting

aspects associated with corrective actions of the PI&R area because the licensee

failed to take appropriate corrective actions to address safety issues and adverse

trends in a timely manner (P.1.(d)). The cause of the finding was also related to

the safety culture component of accountability in that management failed to

reinforce safety standards and display behavior that reflected safety as an

overriding priority (O.1.(b)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, "Instructions,

Procedures, and Drawings, requires that activities affecting quality shall be

prescribed by instructions, procedures, or drawings, and shall be accomplished

in accordance with those instructions, procedures, and drawings. The

assessment of operability of safety-related equipment needed to mitigate

accidents was an activity affecting quality, and was implemented by

Procedure 40DP-9OP26. Section 1.3 stated that if a condition was determined

operable but degraded/nonconforming, then a PVAR will pursue the appropriate

corrective actions. Contrary to this, between May 2006 and October 19, 2007,

the licensee did not initiate a PVAR or CRDR to pursue the appropriate actions

for a high lead content in the Unit 3 train B LPSI pump. Specifically, the licensee

had not determined the cause of abnormally high lead levels in the Unit 3 Train B

LPSI motor coupling bearing oil, did not establish a monitoring plan, and did not

establish thresholds to take additional actions upon a degrading condition. This

was the fourth of eight examples associated with the NCV involving inadequate

implementation of the OD program. This example was of very low safety

significance (Green) and was documented in the licensees CAP as PVAR

3075442.

b.5 Failure to Implement the Operability Determination Process on Unit 2 Essential

Cooling Water Heat Exchanger A Sleeve Adhesive

Introduction. The team identified a fifth example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and

Drawings," for the failure of operations and engineering personnel to adequately

evaluate degraded and unanalyzed conditions to support operability decision

making associated with the Unit 2 essential cooling water (EW) Heat Exchanger

Train A epoxy sleeve adhesive degradation and leak. Specifically, on

October 23, 2007, operations and engineering personnel failed to consider all

relevant information to perform an adequate OD when evaluating Unit 2 EW Heat

Exchanger Train A sleeve adhesive under chemistry conditions associated with

the ESP system fouling identified in 2006.

- 42 - Enclosure

Description. The Unit 2 Train A EW Heat Exchanger developed a leak as noted

by elevated chlorides from the ESP into the EW system on June 27, 2007.

During a short notice outage on October 16, 2007, eddy current tests were

performed to determine and repair the source of the leak. Three tubes were

identified to be leaking, with location Row 2, Tube 26, found to have a leak

underneath the tube sleeve. After the source of the leak was identified,

operations and engineering personnel failed to validate the qualification of the

epoxy with respect to chemistry conditions associated with ESP fouling identified

in 2006. The epoxy was used to seal the EW heat exchanger tube sleeves into

the heat exchanger. All of the Unit 2 EW Heat Exchanger Train A tubes were

sleeved using the epoxy adhesive under limited design change package

2LM-EW-036. Unit 2 was the only unit to have sleeves inserted into the EW heat

exchanger tubes.

The leak was determined to be underneath the tube sleeve. The sleeve

adhesive was used to seal the sleeves to the heat exchanger tubes and to

prevent potentially corrosive water from causing leaks under the tube sleeves. In

response to the teams questions, the licensee initiated CRAI 3081800 on

October 23, 2007, to determine whether the sleeve adhesive was a potential leak

path under the Unit 2 EW Heat Exchanger Train A tube sleeves. However; no

OD of the condition was conducted.

The team reviewed Design Change Package 2LM-EW-036 and Combustion

Engineering Report TR-MCC-315, and determined the adhesive was tested

under design assumptions indicative of 1993 plant conditions. The adhesive was

not verified to perform under the chemistry conditions associated with the ESP

fouling concerns identified in 2006. ESP fouling came to the NRC's attention as

a result of unusual temperatures noted during a surveillance test of EDG 2B

conducted on May 17, 2006. The NRCs review was documented in NRC

Inspection Report 05000528, 05000529, 05000530/2006011. Significant

CRDR 2897810 documented changes made to ESP chemistry after the fouling

was identified, but no evaluation was documented on the potential effects of ESP

chemistry on the adhesive.

Procedure 40DP-9OP26, Step 3.1.1, stated that the OD process was entered

upon discovery of circumstances where operability of any SSCs described in

Technical Specifications was called into question upon discovery of a degraded,

nonconforming, or credible unanalyzed condition. Since a CRAI was written

without identification that a degraded or unanalyzed condition existed, the

adhesive concern did not receive an OD as required by Procedure 40DP-9OP26.

Per Procedure 01DP-0AP12, Palo Verde Action Request Processing, Revision

1, if additional work mechanisms changed the original degraded/non-conforming

evaluation, then the PVAR should be amended so that another degraded/non-

conforming evaluation can be performed.

After the team further questioned operations and engineering personnel,

PVAR 3083892 was initiated on October 26, 2007, and an immediate OD was

completed. The immediate OD evaluated the qualification of the adhesive used

to seal the U2 EW heat exchangers with respect to ESP fouling chemistry

conditions. Operations determined a reasonable expectation of operability of the

EW heat exchangers existed based on testing of the adhesive, no existing leaks

- 43 - Enclosure

under the remaining tube sleeves, and chemistry samples confirming no current

ESP leakage into the EW system.

Analysis. The performance deficiency associated with this finding was the failure

of operations and engineering personnel to adequately evaluate degraded and

unanalyzed conditions to support operability decision making associated with the

Unit 2 EW Heat Exchanger Train A epoxy sleeve adhesive degradation and leak.

This finding is greater than minor because it is associated with the mitigating

systems cornerstone attribute of equipment performance and affects the

cornerstone objective of ensuring the availability and reliability of systems that

respond to initiating events to prevent undesirable consequences. Using the

IMC 0609, "Significance Determination Process," Phase 1 Worksheets, the

finding is determined to have very low safety significance (Green) since it only

affected the mitigating systems cornerstone and did not represent a loss of

system safety function. The cause of this finding had crosscutting aspects

associated with decision making of the human performance area in that

operations and engineering personnel failed to use conservative assumptions for

operability decision-making when evaluating degraded and nonconforming

conditions (H.1.(b)). The cause of this finding was also related to the safety

culture component of accountability in that operations and engineering personnel

failed to demonstrate a proper safety focus and reinforce safety principles

(O.1.(c)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, "Instructions,

Procedures and Drawings," requires that activities affecting quality shall be

prescribed by instructions, procedures, or drawings, and shall be accomplished

in accordance with those instructions, procedures, and drawings. The

assessment of operability of safety-related equipment needed to mitigate

accidents was an activity affecting quality, and was implemented by

Procedure 40DP-9OP26. Procedure 40DP-9OP26, Step 3.1.1, stated the OD

process was entered upon discovery of circumstances where the operability of

any SSCs described in Technical Specifications was called into question upon

discovery of a degraded, nonconforming, or credible unanalyzed condition.

Contrary to the above, between October 23 and 26, 2007, operations and

engineering personnel failed to enter the OD process upon the discovery of

circumstances where the operability of a component described in Technical

Specifications was called into question. Specifically, operations and engineering

personnel failed to consider all relevant information to perform an adequate OD

when evaluating the Unit 2 EW Heat Exchanger Train A sleeve adhesive under

chemistry conditions associated with ESP fouling identified in 2006. This was the

fifth of eight examples of the NCV associated with inadequate OD program

implementation. This example was of very low safety significance and had been

entered into the CAP as PVAR 3083892.

b.6 Failure to Implement the Operability Determination Process on the Unit 2

Essential Cooling Water Heat Exchanger A Tube Leak

Introduction. The team identified a sixth example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and

Drawings," for the failure of operations and engineering personnel to adequately

evaluate degraded and nonconforming conditions associated with a Unit 2 EW

- 44 - Enclosure

Heat Exchanger Train A tube leak. Specifically, between June 27 and

October 4, 2007, operations and engineering personnel failed to consider all

relevant information to perform an adequate OD when evaluating the Unit 2 EW

Heat Exchanger Train A tube leak.

Description. Unit 2 EW Heat Exchanger Train A developed a leak as seen by

elevated chloride concentrations in the EW system from the ESP system.

PVAR 3033604 was initiated on June 27, 2007. A control room review was

performed and the Unit 2 EW Heat Exchanger Train A tube leak was determined

to be bounded for leak rate and chloride concentration by a similar condition that

occurred on the Unit 3 EW Heat Exchanger Train B on June 28, 2001, where

operations personnel determined the condition did not impact operability.

A prompt OD was performed on June 29, 2007, in PVAR 3033604. The prompt

OD determined there was no impact on operability based on the heat exchanger

having adequate structural integrity, thermal performance, and spray pond

inventory. Thermal performance was determined to not be impacted by the leak

since Calculation 13-MC-SP-0307, "SP/EW System Thermal Performance

Design Bases Analysis," Revision 8, assumed up to 257 of the 2575 tubes could

be plugged and only 30 tubes were currently plugged.

The team reviewed Calculation 13-MC-SP-0307 and determined that the

calculation assumed zero leakage of the heat exchanger tubes. Further, the

team determined the control room review and prompt OD only evaluated

chemistry concerns with respect to chloride concentrations. The team reviewed

Specification 74DP-9CY04, "Systems Chemistry Specifications," Revision 51,

and determined that other chemical constituents that are usually in the ESP

system were not evaluated for their effects on the EW system. These

constituents included dispersant, calcium hardness, and phosphate. The team

also noted that the prompt OD did not have acceptance criteria for when leakage

or chemistry parameters would render the Unit 2 EW Heat Exchanger Train A

inoperable.

The team determined operations personnel should have performed an immediate

OD on October 4, 2007, when the team questioned the validity of the initial OD.

Procedure 40DP-9OP26, Step 3.1.1, stated that the OD process was entered

upon discovery of circumstances where operability of any SSC described in the

Technical Specifications was called into question upon discovery of a degraded,

nonconforming, or credible unanalyzed condition.

After questioning by the team, PVAR 3033604 was redirected to the control room

for another immediate OD review on October 4, 2007. The immediate OD and

subsequent evaluation determined the current leak rate was 2.6 gallons per hour

and established a maximum acceptable leak rate of 3.3 gallons per hour, to

ensure chemistry parameters remained within specification in the EW system.

The evaluation also determined that the leak rate would not affect the structural

integrity or the heat removal design function based on the small size of the leak.

On October 16, 2007, the licensee plugged the leaking tubes.

Analysis. The performance deficiency associated with this finding was the failure

of operations and engineering personnel to adequately evaluate degraded and

- 45 - Enclosure

nonconforming conditions to support operability decision making associated with

the Unit 2 EW Heat Exchanger Train A tube leak. This finding is greater than

minor because it is associated with the mitigating systems cornerstone attribute

of equipment performance and affected the cornerstone objective of ensuring the

availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the IMC 0609, "Significance Determination

Process," Phase 1 Worksheets, the finding is determined to have very low safety

significance (Green) since it only affected the mitigating systems cornerstone and

did not represent a loss of system safety function. The cause of this finding had

crosscutting aspects associated with decision making in the human performance

area in that operations and engineering personnel failed to use conservative

assumptions for operability decision-making when evaluating degraded and

nonconforming conditions (H.1.(b)). The cause of this finding was also related to

the safety culture component of accountability in that operations and engineering

personnel failed to demonstrate a proper safety focus and reinforce safety

principles (O.1.(c)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, "Instructions,

Procedures and Drawings," requires that activities affecting quality be prescribed

by instructions, procedures, or drawings, and be accomplished in accordance

with those instructions, procedures, and drawings. The assessment of

operability of safety-related equipment needed to mitigate accidents was an

activity affecting quality, and was implemented by Procedure 40DP-9OP26,

Revision 18. Procedure 40DP-9OP26, Step 3.1.1, stated the OD process was

entered upon discovery of circumstances where operability of any SSC described

in the Technical Specifications was called into question upon discovery of a

degraded, nonconforming, or credible unanalyzed condition. Contrary to the

above, between June 27 and October 4, 2007, operations and engineering

personnel failed to enter the OD process upon discovery of circumstances where

the operability of a component described in the Technical Specifications was

called into question. Specifically, operations and engineering personnel failed to

consider all relevant information to perform an adequate OD when evaluating the

Unit 2 EW Heat Exchanger Train A tube leak. This was the sixth of eight

examples associated with the NCV involving inadequate implementation of the

OD program. This example was of very low safety significance and had been

entered into the CAP as PVAR 3033604.

b.7 Observations and Minor Noncited Violations Involving Licensee Controls for

Identifying, Assessing, and Correcting Performance Deficiencies

b.7.1 Corrective Action Program Implementation

Description: The team reviewed CAP implementation and identified the

following minor issues/observations:

During the week of October 2, 2007, the team noted that licensee

personnel consistently failed to recognize conditions under which a PVAR

would be required to document an adverse condition. Licensee

personnel believed they needed to ensure that a degraded condition was

a condition adverse to quality before they would consider initiating a

PVAR. Throughout the inspection, the team continued to prompt the

- 46 - Enclosure

licensee on initiating PVARs. The team noted improved performance by

licensee personnel late in the inspection. However, the team could not

conclude whether this was an artifact of the team being onsite or whether

this would result in sustained improvement.

The team noted that the CDBR team documented issues at an

appropriate threshold. However, the team also noted that engineering

personnel incorrectly considered that the CDBR team was entering issues

into the PVAR process that they considered below threshold or not worthy

of review.

The team reviewed the quality of ODs to evaluate the effect of degraded

conditions on safety-related equipment. The team also reviewed

degraded and nonconforming conditions for which the licensee had not

conducted any assessment of operability. In addition to the examples

discussed on ODs in this report, the team noted a generally poor

understanding of the insights necessary to conduct operability

assessments of degraded conditions and a failure to recognize the need

to conduct an operability evaluation. The team also noted failures to

recognize the need to conduct an extent of condition review for identified

degraded conditions. Poor operability assessments and program

implementation have been a longstanding concern at Palo Verde.

The team identified that corrective actions for conditions adverse to

quality were not always timely or were not completed. For example, the

team identified that corrective actions to train personnel on apparent

cause evaluations, which was a concern during the December 2006 NRC

PI&R inspection, were still not completed in November of 2007. The

licensee believed corrective actions to conduct 10 CFR 50.59 training for

chemistry personnel were completed in November of 2006. However, the

team determined that some chemistry personnel had not attended the

required training and even though CRAI 2942350 was closed.

On October 4 and 9, 2007, the team observed Corrective Action Review

Board (CARB) meetings and noted the following observations; the CARB

meeting was frequently interrupted, management personnel did not

appear prepared for or dedicated to the CARB meeting and frequently left

the meeting to answer cell phone and pager calls, the quorum was lost

when the minimum number of managers required was not maintained as

personnel left the meeting, and the meeting was cut short or cancelled

due to the number of distractions or due to other meetings considered to

have a higher priority. The team noted that the CARB members did not

challenge the disruptive behaviors and did not hold themselves

accountable for their participation in the meeting.

b.7.2 Problem Identification and Resolution Root Cause Report

Description: The team reviewed the PI&R Root Cause Report issued in

August 2007. The team noted the following weaknesses in the PI&R

report:

- 47 - Enclosure

On July 9, 2007, the licensee initiated CRAI 3038014, a corrective action

to prevent recurrence (CAPR), for the root cause of the failure to correct

continued poor accountability behaviors with implementation of the CAP.

As of November 2, 2007, CRAI 3038014 was not completed. The PI&R

root cause CAPR was to conduct a site wide stand-down in order to

communicate CAP fundamentals to station personnel, managers, and

supervisors. The PI&R root cause report CAPR defined the fundamentals

that needed to be communicated and specified the forum in which to

communicate the fundamentals (site wide stand-down); however, the

assigned CAPR completion date was December 28, 2007. The team

noted that this action was untimely considering that the Unit 3 refueling

outage was scheduled to start in October 2007. The team did note that

limited CAP discussions were conducted by site senior management

during weekly video presentations leading up to the Unit 3 refueling

outage; however, the discussions did not include all of the CAP

fundamentals described in the PI&R root cause.

The team noted that the PI&R root cause report discussed the lack of

Specific, Measurable, Achievable, Reasonable, and Timely (SMART)

corrective action criteria in CAP procedures and prior root cause reports.

The team recognized that the PI&R root cause report contained CRAI

3038040 to identify SMART criteria in the condition reporting procedure

and in the root cause evaluation manual. However, the teams review of

the corrective actions identified in the PI&R root cause report noted a

similar lack of SMART criteria (CRDR 3071645) in the PI&R root cause

report corrective actions. In general, the team noted that the PI&R root

cause report corrective actions (e.g., communication of CAP standards

and fundamentals) were not timely in consideration of the existing

weaknesses in the CAP. Also, the team noted that the continuing

problems identified with the OD process that have been identified by the

NRC over the last several years, and which continued to occur during this

inspection, were not discussed in any great detail in the PI&R root cause.

The only PI&R root cause report corrective action related to this program

was to conduct a self-assessment of the OD program by June 30, 2008.

The team did not consider this action timely given the problems identified

with the implementation of the OD process.

The team noted that the PI&R root cause report described the CAP as

comprising the PVAR, CRDR, corrective maintenance program,

engineering deficiency work process, OD and FA evaluations, and the

warehouse discrepancy notice program. However, the PI&R root cause

report did not recognize that the existence of this many tracking systems

had contributed to the complexity of the licensees CAP; thereby, creating

vulnerabilities to CAP implementation. This is consistent with the results

of interviews conducted during the inspection which identified that

licensee personnel did not see a difference between their multiple

database process and the more prevalent nuclear industry one form

process. In addition, the PI&R root cause did not recognize the existence

of other tracking systems (such as the ACT and Bechtel NCR databases)

which potentially included multiple unrecognized conditions adverse to

quality outside of the defined CAP.

- 48 - Enclosure

In March 2005, Palo Verde initiated significant CRDR 2780286 to perform

a root cause investigation of the substantive crosscutting issues in PI&R.

The identified root cause was management behaviors, in that they did not

hold themselves and others to high standards relative to the CAP. The

CAP substantive crosscutting area self assessment performed in

preparation for the ImPACT in 2007 determined that a new root cause

analysis did not need to be conducted, primarily because significant

CRDR 3015327 was already in progress to determine why the corrective

actions from CRDR 2780286 had not been effective. The identified root

cause in CRDR 3015327 was inadequate personnel and organizational

accountability. The evaluation determined that many of the CAPRs and

corrective actions implemented by CRDR 2780286 were conceptual,

poorly conceived, and did not follow the SMART model. Consequently,

they were not effectively implemented. Examples included CRAI

2828390 (revise the Palo Verde Business Plan to reflect the CAP as a

strategic focus area), CRAI 2828392 (develop improved CAP metrics),

and CRAI 2828404 (revise the Palo Verde expectations and standards

booklet to include the CAP). The team determined that the ineffective

corrective actions from CRDR 2780286 had not been incorporated into

the SIBP/SIIP. The team reviewed the SIBP/SIIP and determined that the

corrective actions for CRDR 3015327 had been incorporated. Because

the SIBP/SIIP was in draft form, and many of the proposed actions had

not yet been implemented, the team was unable to evaluate whether the

actions will be effective in correcting the PI&R issues the site is

experiencing.

The team reviewed a number of other root cause reports and noted

similar issues including; the failure to identify all contributing causes, the

failure to specify SMART corrective actions, a lack of timely corrective

actions, an inability to track the completion of or determine the status of

corrective actions taken in response to significant conditions adverse to

quality, and the closure of corrective actions taken in response to

significant conditions adverse to quality that had not been implemented or

completed.

b.7.3 Action Request Review Committee

Description: The team attended several Action Request Review

Committee (ARRC) meetings. The ARRC was established following the

implementation of the PVAR process to review and disposition each

PVAR to implement an effective CAP. The team noted the following

weaknesses in the conduct of the ARRC activities:

  • The team noted that the ARRC members frequently debated whether

a given condition documented in a PVAR was actually an adverse

condition. One ARRC member commented that if the subject

condition was considered adverse, Then we would have hundreds of

adverse conditions. The team noted that an adverse condition

should be judged as adverse based on its characteristics, not whether

it would subsequently result in a high number of adverse conditions

being documented.

- 49 - Enclosure

  • The team observed that ARRC members would call personnel in the

field to resolve a degraded condition and would then close the PVAR

to actions taken. The team noted that this had the appearance of the

ARRC acting as first line supervisors to correct conditions adverse to

quality rather than as a multi-discipline team to review and disposition

PVARs for corrective actions by responsible organizations.

  • ARRC members were observed to be rewriting PVARS rather than

returning them to the initiating organization. This prevented the

initiating organization from learning from the lack of a complete PVAR

description and precluded the originating organization (i.e., the

organization in the know) from providing the most accurate

information regarding the condition.

  • An ARRC member was observed to be overly biased against a PVAR

that he considered should not have been written and stated to the

group that he would handle this particular PVAR, and that he would

tell the originator that this was not a problem. It was apparent to the

team that the originator would receive negative feedback on the

generation of this PVAR from the ARRC member rather than allowing

the PVAR process to evaluate and resolve the condition. The team

also noted that the other ARRC members did not intercede, allowing

this negative behavior to continue.

  • The ARRC could determine no corrective actions were necessary by

designating a Review CRDR with no actions needed. The ARRC

also appeared to be conducting evaluations and specifying corrective

actions for PVAR issues. The team noted that this could put the

ARRC in the position of specifying corrective actions rather than

dispositioning PVARs to the responsible organization for review and

created a vulnerability to bypassing organizational processes for

evaluating conditions adverse to quality.

The team determined that the management oversight provided to the

ARRC, a relatively new review committee, was insufficient given the

number and depth of NRC observed concerns. The team discussed

these ARRC observations with the Performance Improvement and CAP

managers. In response to these concerns, the licensee initiated PVAR

3072299 and an ARRC improvement strategy was generated. The

ARRC Charter was revised, some ARRC members were reassigned, new

members were designated, and briefings were conducted with ARRC

members on the vision and expectations of the ARRC. The team noted

some improvement following these actions; however, the team also noted

some of the poor behaviors were repeated during subsequent ARRC

sessions.

- 50 - Enclosure

b.7.4 Backlog Review

Description: The team reviewed the licensees efforts in defining and

evaluating the existing backlog and had the following observations:

The team noted that there were over 250 OD backlog entries. The

characterization of this many ODs as part of a backlog could be confusing

since open ODs generally documented current degraded or

nonconforming equipment conditions that had been evaluated as not

affecting the ability of equipment to meet intended safety functions, but

that had not yet been corrected. At Palo Verde, ODs were kept open,

even if full qualification was restored, until all associated corrective

actions had been completed. The team noted that this approach may

dilute the significance of how issues documented under the OD process

were viewed and could confuse the organization and impact the ability to

effectively evaluate the aggregate impact of degraded and nonconforming

conditions on plant equipment.

The licensees backlog review team identified that items in the activity

tracking (AT) database had a low priority review need because ATs, did

not perform physical work. The team identified that some AT entries

appeared to perform physical work, such as AT work order (WO) 220774,

which required vibration readings to be taken on plant equipment.

Following the teams observations, the backlog review team reassessed

their decision not to review ATs. On October 31, 2007, the licensee

identified approximately 54 out of 3901 AT WOs that appeared to perform

physical work. The licensee determined that several of the items should

not have been entered into the AT database. No degraded or non-

conforming conditions were identified which would have affected safety-

related or other plant equipment. The team noted that the decision to not

review ATs assumed proper implementation of licensee programs and

processes and that prior decisions were valid. The apparent

unwillingness of licensee personnel to question decisions made during a

period of declining performance was a significant vulnerability for the

licensee. As noted during the SIBP/SIIP review, the licensee had not

developed any actions to evaluate the legitimacy of past decisions.

PVAR 3074083, CRDR 3079482, and CRAI 3079483 were generated to

document this issue.

The team discussed the status of the ACT database review with the

backlog review team. The backlog review team indicated that they were

nearing completion and that they were verifying whether the ACTs of

concern were in fact conditions adverse to quality. The team noted that

the backlog review team appeared to be spending an inordinate amount

of time verifying whether they considered a given ACT concern to be an

issue adverse to quality rather than initiating a PVAR and letting the CAP

determine the significance and required corrective actions.

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b.7.5 Self Assessments

Description: The team reviewed a number of self-assessments and had

the following observations:

A significant number of self-assessments conducted by Palo Verde

personnel lacked depth and did not challenge the assessed organization.

The recommendation for the November 2006 decision-making self-

assessment was vague because it only requested an Operational

Decision Making Instruction (ODMI) review and provided no further

details on current ODMI weaknesses. The only recommendation from the

December 2005 Operational Decision Making self-assessment was to

combine two procedures. The March 2007 work management self-

assessment concluded that the assessment needed to be re-performed

later in 2007 and provided no other insights. The self-assessment of the

maintenance rule program did not recognize that unavailability and

reliability performance criteria could not be validated and that numerous

systems had non-conservative performance criteria.

Self-assessment corrective actions were not always tracked nor did they

always have PVARs written to document the expected corrective actions.

The December 2006 leadership self-assessment recommended the

initiation of a mentoring program that was later postponed several

months. The decision was influenced by the upcoming change in senior

management. Deficiencies described in the assessment of the safety

injection system and environmental qualification assessments were not

entered into the CAP.

In one case, the team noted that a recent training assessment appeared

to be more probing and insightful. The team observed that the makeup of

the training self-assessment team included a mix of licensee and industry

personnel which may have led to the better assessment product when the

experiences of industry personnel were used.

5.2 Design

Weak engineering program and process implementation had been a continuing problem at

Palo Verde. The team noted numerous instances of design errors and omissions, and an

overall lack of technical rigor. Specifically:

  • The team noted that the CDBR effort was effective in identifying design issues. The

composition of the group included both site engineering and contractor support. The

success of this effort could be attributed to the broader perspective that the group had

due to the external contractor support. Although the CDBR effort had identified issues

at the appropriate threshold, the team noted instances in which issues entered into the

CAP were not appropriately addressed. The team also noted that a cumulative impact

review of all of the CDBR issues for a particular system or component could further

reduce the available margin.

  • The team noted several design documents had inadequate or unverified design

assumptions. For example, Calculation13-MC-SP-306, "MINET Hydraulic Analysis of

- 52 - Enclosure

SP System," Revision 4, stated values for essential spray pond net positive suction

head and submergence requirements to prevent vortexing, but the values were for

generic pump design and did not ensure operation under the specific PVNGS design

basis conditions, such as worst case ESP temperature.

  • The team noted that the engineering organization lacked a consistent questioning

attitude. Reviews and evaluations often addressed the simplest or primary causes

only. Extent of condition reviews, operability evaluations, and conditions dealing with

off-normal operations were frequently not well documented. When questioned by the

team, engineering personnel needed to perform further evaluation and documentation

to support the technical position.

a. Inspection Scope

The team reviewed licensing and design basis documents for safety injection, ESP,

and auxiliary feedwater (AF) systems, including the UFSAR, calculations, engineering

analyses, system descriptions, CDBR reports, and self assessments to determine the

functional requirements of the systems for normal, abnormal, and accident conditions.

The team reviewed a sample of risk-significant plant modifications for the selected

systems, including those that involved vendor supplied products and services to

determine whether the changes had an adverse impact on the ability of the systems to

perform their design basis functions and determine whether the changes would result

in an unexpected initiating event. During this review, the team evaluated the

effectiveness of the licensee in controlling design and licensing information, in

providing necessary calculations to support plant changes, and in developing and

implementing thorough post-modification testing procedures. The team assessed the

adequacy of the licenses engineering products in evaluating applicable system and

support system design attributes and regulatory requirements.

The team conducted general walkdowns of the selected systems and components.

Recent changes to plant maintenance and operating procedures were reviewed to

ensure that they did not result in inadvertent design changes to the systems. For

procedures that involved design changes, the team ensured that the change was

subjected to the appropriate design change processes, including a review in

accordance with 10 CFR 50.59, Changes, Tests, and Experiments. The team also

reviewed a sample of PVARs to assess the effectiveness of corrective actions for

deficiencies involving design activities. Additionally, the team reviewed a sample of

engineering training programs to verify that training programs were consistent with the

current design.

b. Findings and Observations

b.1 Failure to Implement Adequate Design Controls for Condensate Storage Tank

Temperature

Introduction. The team identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion III, "Design Control," for the failure of engineering personnel to translate

design basis maximum condensate storage tank (CST) temperature

requirements into procedures to ensure the plant is operated within its design

basis.

- 53 - Enclosure

Description. On October 4, 2007, the team questioned engineering personnel

with regards to the control of the maximum CST temperature. A CST maximum

temperature of 120°F was used in Calculation 13-MC-CT-0205, "Condensate

Storage Tank," Revision 4, Calculation 13-MC-CT-0307, "CST Minimum Level

Setpoint," Revision 4, and Calculation 13-MC-AF-0309, "AF Hydraulic

Calculation for Q-Trains," Revision 7, to ensure sufficient CST volume and net

positive suction head for the AF pumps during a design basis accident. Neither

operations nor maintenance and testing personnel took routine recordings of

CST temperature, the parameter was not monitored by Technical Specifications,

and no alarm existed for high CST temperature to ensure operation within the

design basis maximum temperature of 120°F.

The 120°F CST maximum temperature was based on summertime ambient

weather conditions affecting water temperature. The team noted that hotwell

condensate from the main condenser was rejected to the CST during startup,

shutdown, and on a high hotwell level. When the hotwell was rejected to the

CST, the potential existed to exceed the 120°F maximum temperature limit

because the condensate average temperature during July and August 2007 was

130°F.

Following the teams questions on control of CST temperature, engineering

personnel initiated PVAR 3073243. Operations personnel determined this

condition was not a degraded or nonconforming condition, and an immediate OD

was not performed due to current ambient temperatures being significantly lower

than the maximum tank temperature, and due to establishing compensatory

measures through a night order on October 11, 2007. The night order identified

the deficiencies in monitoring CST temperature and directed operations

personnel to take CST temperature readings once per shift, and contact system

engineering personnel if temperature exceeded a lower administrative limit of

110°F.

On November 13, 2006, PVAR 2949167 was written to evaluate how AF pump

heat load contributions were not considered in determining maximum CST

temperature. The team determined that the failure to consider other inputs that

could raise CST temperature during the licensees review of PVAR 2949167 was

a missed opportunity.

Analysis. The performance deficiency associated with this finding was the failure

of engineering personnel to adequately translate the design basis CST maximum

temperature requirements into applicable procedures. This finding is greater

than minor because it is associated with the mitigating systems cornerstone

attribute of equipment performance and affected the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events

to prevent undesirable consequences. Using the IMC 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding is determined to have

very low safety significance since it only affected the mitigating systems

cornerstone and did not represent a loss of system safety function. The cause of

this finding had crosscutting aspects associated with corrective action of the

PI&R area in that engineering personnel failed to thoroughly evaluate problems

such that resolutions ensured that the problems were resolved. (P.1.(c)).

- 54 - Enclosure

Enforcement. 10 CFR Part 50, Appendix B, Criterion III, Design Control,

requires, in part, that the design basis for SSCs be translated into specifications,

drawings, procedures, and instructions. Contrary to the above, since 1985,

engineering personnel failed to correctly translate design basis information into

specifications, drawings, procedures, and instructions. Specifically, engineering

personnel failed to translate design basis maximum CST temperature

requirements into procedures to ensure the plant is operated within its design

basis. This example was of very low safety significance and was entered into the

CAP as PVAR 3073243, this violation was treated as an NCV consistent with

Section VI.A of the Enforcement Policy: NCV 05000528, 05000529,5000530/2007012-02, Failure to Implement Adequate Design Controls.

b.2 Inadequate Installation of Fire Sprinklers

Introduction. The team identified a Green NCV of License Condition 2.C(6) for

the failure to install sprinkler heads in accordance with the FP program.

Specifically, on October 2, 2007, the team identified several upright fire sprinkler

heads in the auxiliary building that were incorrectly installed in a pendent or

downward orientation.

Description. During walkdowns of the Unit 3 auxiliary building high pressure

safety injection Train A pump room, the team identified that a FP sprinkler was

installed in the wrong orientation. The sprinkler was located in a drop line for

coverage below a heating ventilation and air conditioning unit and above cable

Tray 3EZACCATCBA. The sprinkler head was an upright style; however, the

sprinkler head was installed in a downward orientation. The team also identified

that the sprinkler head in an alcove area on the 40 foot elevation of the LPSI

pump room was installed in the incorrect orientation.

The team questioned engineering personnel on the orientation of these sprinkler

heads. License Condition 2.C(6), "Fire Protection Program," stated that the

licensee shall implement and maintain in effect all provisions of the approved FP

program as described in the UFSAR for the facility, as supplemented and

amended, and as approved in the Safety Evaluation Report (SER) through

Supplement 11, subject to the following provision: the licensee may make

changes to the approved FP program without prior approval of the Commission

only if those changes would not adversely affect the ability to achieve and

maintain safe shutdown in the event of a fire.

UFSAR Section 9.5.1.2.1.F stated that automatic preaction sprinklers,

hydraulically designed using National Fire Protection Association (NFPA)

Pamphlet No. 13 (1976) as guidance, are provided to protect the areas so

indicated in Table 9.5-1. Each automatic preaction system contains piping

supervised by service air and fusible link sprinkler heads arranged such that flow

densities meet the guidelines of the American Nuclear Insurer, and also NFPA

Pamphlet No. 13 (1976). NFPA Pamphlet No. 13 (1976) Section 3-15.2.2 stated

that the character of the discharge of sprinklers is such that it is necessary to use

two distinct designs, one approved for the upright and the other approved for the

pendent position.

- 55 - Enclosure

The team determined the three listed upright type sprinkler heads were found

installed in a downward position. In the installed configuration, there was no

testing to demonstrate that sprinklers would be capable of achieving the required

flow or densities. Engineering personnel initiated PVAR 3073824 to address

these issues.

Analysis. The performance deficiency associated with this finding was the failure

to install sprinkler heads in accordance with the FP program. This finding is

greater than minor because it was associated with the mitigating systems

cornerstone attribute of external factors and affected the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events

to prevent undesirable consequences. Using the IMC 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding was determined to

require additional evaluation under Manual Chapter 0609, Appendix F, "Fire

Protection Significant Determination Process," because it was associated with

the suppression element of defense-in-depth. Since the installation of the

sprinkler heads represented a low degradation of the fire suppression system, in

accordance with Section 1.3.1 of IMC 0609, Appendix F, the finding is

determined to have very low safety significance.

Enforcement. License Condition 2.C(6), Fire Protection Program, stated that

the licensee shall implement and maintain in effect all provisions of the approved

fire protection program as described in the Final Safety Analysis Report for the

facility, as supplemented and amended, and as approved in the safety evaluation

report through Supplement 11, subject to the following provision: the licensee

may make changes to the approved fire protection program without prior

approval of the Commission only if those changes would not adversely affect the

ability to achieve and maintain safe shutdown in the event of a fire. UFSAR

Section 9.5.1.2.1.F stated that automatic preaction sprinklers, hydraulically

designed using NFPA Pamphlet No. 13 (1976) as guidance, are provided to

protect the areas so indicated in Table 9.5-1. Each automatic preaction system

contains piping supervised by service air and fusible link sprinkler heads

arranged such that flow densities meet the guidelines of the American Nuclear

Insurer, and also NFPA Pamphlet No. 13 (1976). NFPA Pamphlet No. 13 (1976)

Section 3-15.2.2 stated that the character of the discharge of sprinklers is such

that it is necessary to use two distinct designs, one approved for the upright and

the other approved for the pendent position. Contrary to the above, as of

October 2, 2007, three listed upright type sprinkler heads were found in the

untested pendent position. Because the finding was of very low safety

significance and was entered into the CAP as PVAR 3072557, this violation was

treated as an NCV, consistent with Section VI.A of the Enforcement Policy:

NCV 05000530/2007012-03, "Inadequate Installation of Fire Sprinklers.

b.3 Failure to Enter Environmental Qualification (EQ) Self Assessment Deficiencies

into the Corrective Action Program

Introduction. The team identified an example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the failure of

engineering personnel to promptly identify and correct a significant condition

adverse to quality described in an environmental qualification self assessment

- 56 - Enclosure

report. Specifically, the licensee had not evaluated or removed unqualified tape

used to repair Anaconda conduit from the containment buildings.

Description. EQ Self Assessment No. 2957427, issued July 2, 2007, found that

Engineering Change Evaluation (ECE), ECE-ZZ-A143, Anaconda Degraded

Sealtite Repair Material, Scotch 33 Tape, Revision 1, was used as a basis for

the prompt OD for degraded Anaconda Sealtite flexible conduit (CRDRs

2940338, 2940354, and 2940359). The ECE did not address the worst-case in-

containment radiation dose. Under the worst case radiation levels, the tape was

calculated to be exposed to the combined normal, accident gamma, and accident

beta of over 300 Mrad. However, the ECE only evaluated the tape up to

radiation levels of 100 Mrad. Although the condition was identified in the self

assessment, it was not entered into the CAP and evaluated as a condition

adverse to quality. Based on concerns raised by the team, PVAR 3073528 was

written to evaluate why an adverse condition was not dispositioned properly in

the CAP and to evaluate the extent of condition for other issues in the EQ self

assessment.

The team was also concerned that the failure of the tape during an accident

could also result in the failure of the repaired flexible conduit. The additional

debris caused by this condition would contribute to containment sump loading. In

response, engineering personnel initiated PVAR 3071831, to evaluate the

potential impact of the additional tape and conduit sheathing loading on the

containment sump. Since Unit 3 was in a refueling outage at the time of

discovery and not impacted by the condition, engineering personnel evaluated

the impact of current operability on Units 1 and 2. Approximately six months

prior to the NRC team identifying the concern, Palo Verde replaced the Unit 1

sump strainers. The new Unit 1 strainers size was increased from 210 square

feet to 3142 square feet. Since Unit 2 was still configured with the smaller

strainers, engineering personnel evaluated this as the bounding condition. In

their evaluation, engineering personnel estimated that there would be

approximately 45 square feet of additional loading on the containment sump

strainers and concluded that there was still adequate margin for operation.

Subsequent to this evaluation, Unit 1 experienced a forced outage. On

October 26, 2007, as part of work Order 3034098, the licensee conducted a

containment walkdown to quantify and remove susceptible tape and flexible

conduit in containment. The licensee estimated that there was in excess of 600

square feet of combined tape and conduit that had not been accounted for in the

sump loading analysis and initiated PVAR 3083224, to evaluate the condition.

The licensee concluded that with the larger strainers, the additional loading

would have little impact.

The licensee conducted additional analyses to evaluate the past operability of the

strainers in the Unit 1 containment. The licensee evaluated the realistic radiation

dose that the 639 square feet of tape and conduit outside the bio-shield wall

would be exposed to and determined that it was substantially below the qualified

rating of 100 Mrads. Specifically, the realistic accident total integrated dose (TID)

within containment (wetted or dry but not submerged) during a loss-of-coolant-

accident was calculated to be approximately one-fifth of the TID values reported

in the bounding calculation of record 13-NC-ZC-105, Revision 9, or 58 Mrads.

- 57 - Enclosure

The 148 square feet of tape and flex conduit material found within the bio-shield

in Unit 1 also exceeded previous estimates. Generally, material within this zone

was more of a concern for containment sump strainer loading because it was

assumed that all material within the high energy break zone of influence would

be destroyed and potentially transported to the sump. Consistent with the

approach used for assessment of other potential debris source terms,

engineering personnel conducted a review of the tapes physical properties and

established that the specific gravity for the tape was approximately 1.3.

Therefore, the debris generated within the bio-shield wall may be transported out

of the steam generator compartment, but would have sufficient time to settle prior

to realignment of the ECCS pump suctions to the containment sump.

Additionally, most, if not all, of the material deposited outside the steam

generator compartment would remain submerged and in place since the

maximum flow velocities in and around this area were below the minimum

velocity required for incipient motion of the debris.

The team determined that since the actual TID was less than the qualification

rating for the tape outside the bio-shield wall, it would likely maintain its integrity

and not fail as a result of realistic radiation exposure. In addition, for conditions

in which the additional materials could be susceptible to high energy line break

effects, the specific characteristics of the material, transport velocities, and actual

location precluded any significant challenge to the containment sump loading

assumptions.

Analysis. The performance deficiency associated with this finding was the failure

to enter a condition adverse to quality into the CAP. This finding is greater than

minor because it is associated with the mitigating systems cornerstone attribute

of equipment performance and affected the cornerstone objective of ensuring the

availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the IMC 0609, "Significance Determination

Process," Phase 1 Worksheets, the finding is determined to have very low safety

significance (Green) since it only affected the mitigating systems cornerstone and

did not represent a loss of system safety function. The cause of this finding had

crosscutting aspects associated with self assessment of the PI&R area in that the

licensee did not follow their benchmarking and self assessment guide to ensure

findings were evaluated in the CAP (P.3(c)). The cause of the finding was also

related to the safety culture component of accountability in that management

failed to reinforce safety standards and display behavior that reflected safety as

an overriding priority (O.1.(b)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires that measures be established to assure that conditions adverse to

quality are promptly identified and corrected. Contrary to the above, between

July 2 and October 4, 2007, the licensee did not assure that conditions adverse

to quality were promptly identified and corrected. Specifically, conditions adverse

to quality identified in EQ Self Assessment No. 2957427 were not entered into

the CAP or corrected in a timely manner. Because the finding was of very low

safety significance and was entered into the CAP as PVARs 3073528, 3071831,

and 3083224, this violation was treated as an NCV, consistent with Section VI.A

of the Enforcement Policy: NCV: 05000528, 05000529,05000530/2007012-04,

Six Examples of the Failure to Implement Corrective Action Program

- 58 - Enclosure

Requirements. This was the first of six examples of the failure to implement the

corrective action program requirements.

b.4 Failure to Implement Corrective Actions for Operating Experience Involving the

Turbine Driven Auxiliary Feedwater Pump Trip and Throttle Valve

Introduction. The team identified a second example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for the failure of

engineering personnel to identify, evaluate, and correct degraded and

nonconforming conditions associated with OE applicable to the AF pump trip and

throttle valve (T&TV). Specifically, between February 8 and October 2, 2007,

engineering personnel did not enter applicable OE on the mechanical overspeed

trip mechanism for the AF turbine T&TV into the CAP.

Description. On February 8, 2007, system engineering reviewed industry OE

from South Texas (OE24167) and Saint Lucie (OE24002) in order to determine

the applicability to Palo Verde. The OE described failures of the turbine driven

AF pump T&TV's mechanical overspeed trip mechanism to trip on demand due

to rust forming on mating surfaces between the trip-hook and latch-up lever.

System engineering determined this OE was applicable to PVNGS and that

current preventative maintenance (PM) tests would not detect this failure.

On February 8, 2007, engineering personnel initiated ACT 3046427 to

incorporate force measurements needed to trip the T&TV into the existing

overspeed trip linkage PM tests. The OE review was documented in the January

to June 2007, AF system health report. The team determined engineering

personnel should have entered Procedure 65DP-0QQ01, "Industry Operating

Experience Review," Revision 13, which stated that ACTs can be used to track

industry OE when related actions are not corrective or adverse in nature. The

team questioned whether OE that was determined to be applicable to the site

and where current PMs could not detect the failure should be entered into the

CAP, not the ACT process. After further review by engineering personnel, the

licensee determined that a PVAR should have been written instead of an ACT,

and an OD should have been performed.

The assessment of operability of safety-related equipment needed to mitigate

accidents was an activity affecting quality, and was implemented by

Procedure 40DP-9OP26, "Operability Determination and Functional

Assessment," Revision 18. Procedure 40DP-9OP26, Step 3.1.1, stated that the

OD process is entered upon discovery of circumstances where operability of any

SSCs described in Technical Specifications is called into question upon

discovery of a degraded, nonconforming, or credible unanalyzed condition.

Since an ACT was written instead of a PVAR, the OE on the AF Pumps T&TVs

did not receive an OD as required by Procedure 40DP-9OP26.

In response to the teams observations, on October 2, 2007, engineering initiated

PVAR 3070597 to address the potential for the turbine driven AF pump T&TV's

mechanical overspeed trip mechanism to fail to trip on demand due to rust

forming on mating surfaces between the trip-hook and latch-up lever. Operations

personnel performed an immediate OD and noted that a reasonable expectation

of operability existed because the T&TVs were in a less harsh environment than

- 59 - Enclosure

Saint Lucie and South Texas and had not experienced the rust problems seen at

those facilities. The licensee changed ACT 3046427 to CRAI 3072364 to ensure

the item was entered into the CAP. CRAI 3072364 was initiated to include steps

in work order WSL245709 to ensure the T&TV trip levers trip at a value less than

25 pounds force, as specified in (EPRI) Manual, "Terry Turbine Maintenance

Guide AFW Application." Engineering management also provided additional

training to engineering personnel on the differences between when to initiate an

ACT and when to initiate a PVAR.

Analysis. The performance deficiency associated with this finding was the failure

of engineering personnel to adequately evaluate degraded and nonconforming

conditions to support operability decision making associated with OE applicable

to AF Pump T&TV. This finding is greater than minor because it is associated

with the mitigating systems cornerstone attribute of equipment performance and

affects the cornerstone objective of ensuring the availability and reliability of

systems that respond to initiating events to prevent undesirable consequences.

Using the Manual Chapter 0609, "Significance Determination Process," Phase 1

Worksheets, the finding is determined to have very low safety significance

(Green) since it only affected the mitigating systems cornerstone and did not

represent a loss of system safety function. The cause of this finding had

crosscutting aspects associated with OE of the PI&R area in that engineering

personnel failed to ensure implementation and institutionalization of OE through

changes to station processes, procedures, equipment, and training programs

(P.2.(b)). The cause of this finding was also related to the safety culture

component of accountability in that engineering personnel failed to demonstrate

a proper safety focus and reinforce safety principles (O.1.(c)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action,"

requires, in part, that measures be established to ensure that conditions adverse

to quality are promptly identified and corrected. Contrary to this, between

February 8 and October 2, 2007, engineering personnel failed to ensure that

conditions adverse to quality were promptly identified and corrected. Specifically,

engineering personnel failed to enter applicable OE on the mechanical

overspeed trip mechanism for the AF pump T&TV into the CAP. As a result,

testing to demonstrate the functionality of the overspeed trip mechanism was not

performed and an operability assessment of the degraded and nonconforming

condition was not completed. This was the second example of the NCV involving

failure to implement the CAP requirements. This finding was of very low safety

significance and was entered into the CAP as PVAR 3070597.

b.5 Observations and Minor Violations Involving Design

b.5.1 High Pressure Safety Injection Pump Bearing Modification

Description. The team identified an observation associated with a lack of

technical rigor during the development of a modification associated with

the high pressure safety injection (HPSI) pumps. Work Order (WO)

2972259 consisted of a temporary modification to lower the oiler height

on the Unit 3 HPSI pump bearings. As a result of this modification, the

pump bearing was no longer in a constant oil bath during long periods of

shutdown, when the residual oil in the bearing may drain away. WO

- 60 - Enclosure

2972259, HPSI Bubbler, Attachment 1, stated that for the new oil

configuration, "With the absence of the flooded condition and the

presence of the residual oil within the bearing, Flowserve did not

anticipate any significant bearing degradation resulting from idle periods

of up to and including three months." The team questioned how this

configuration constraint was incorporated into operating procedures. As a

result of the teams questioning, the licensee conducted a review of

procedures and found that they did not incorporate any guidance or

precautions dealing with the pumps being idle for up to three months.

The review for the temporary modification did not specify any concerns in

this area and did not resolve the concern of a pump being idle for more

than three months. The licensee entered this issue into their CAP as

PVAR 3069219.

5.3 Human Performance

The team identified continuing human performance issues at Palo Verde consistent with

previously identified issues discussed in End of Cycle and Mid-cycle letters since 2005.

Specifically, human performance concerns observed during this inspection included

weaknesses in implementing the OD process, failures to follow procedures, failures to

implement human performance tools, and inadequate procedures. In addition, a

significant number of engineering issues reflected a lack of technical rigor in resolving

complex issues. The team noted a lack of adherence to basic radiological work practices

and inconsistent implementation of control room behaviors. The team identified that the

licensees training department had been inconsistent in supporting site improvement.

Although a human performance root cause investigation had been conducted, corrective

actions to date had not been effective in improving human performance. These continuing

human performance deficiencies indicated that corrective actions to resolve the

substantive crosscutting issues had not been successful in sustaining performance

improvement.

a. Inspection Scope

The team evaluated the effectiveness of how Palo Verde personnel identified,

evaluated, and corrected deficiencies involving human performance. The team

evaluated training by reviewing instructional procedures and material, conducting

interviews with training department personnel, observing classes, and job performance

measure (JPM) evaluations, reviewing nuclear assurance department audits, and

reviewing training department self assessments. The team evaluated the work control

process by reviewing procedures, conducting interviews with work control personnel

and work control SROs, and observing outage control center and online work control

center activities. The team conducted a review of substantive human performance

crosscutting aspects and a review of the human performance crosscutting aspects

identified in the findings discussed in this report. Finally, the team conducted

emergency planning performance drills with a sampling of SRO, Technical Support

Center, and Emergency Operations Facility Emergency Directors to assess their ability

to implement the Emergency Plan (EP).

b. Findings and Observations

b.1 Observations and Minor Violations Involving Human Performance

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b.1.1 Human Performance Root Cause Report

Description: The team reviewed the human performance root cause

report issued in September 2005 and effectiveness reviews completed in

August 2007. The team noted the following weaknesses:

  • The September 2005 human performance root cause report identified

that the Palo Verde organization did not demonstrate ownership and

leadership of the human performance culture. The root cause report

stated, Palo Verde Management does not emphasize that excellence

in human performance will result in excellence in plant performance,

and Leaders sometimes model behaviors inconsistent with site

expectations. These statements indicated that the Palo Verde

management team may not have understood what behaviors

contributed to an excellent human performance culture. Also, the

August 2007 effectiveness review of CRAI 2830264 for decision

making stated, The evaluation concluded that there is a lack of an

organizational definition on what constitutes a decision making error

and the behaviors of questioning attitude and technical rigor are not

well defined or understood. The team noted that understanding and

defining the expected behaviors that contribute to an excellent human

performance culture were needed to achieve the desired culture

change.

  • In March 2005, the licensee initiated CRDR 2780273 to perform a root

cause investigation of the substantive crosscutting issues in human

performance. Although the August - September 2007 human

performance self-assessment performed in preparation for the

ImPACT review in 2007 determined that the root cause initiated in

CRDR 2780273 was ineffective in identifying the root cause, a

subsequent effectiveness review performed under CRAI 3033705 in

August 2007, determined that the root cause (i.e., the Palo Verde

organization does not demonstrate ownership and leadership of the

human performance culture) was correctly identified. The licensee

supported this conclusion based on subsequent CRDR evaluations

that used streaming analyses, fault tree analyses, common cause

analyses, and human performance models. The effectiveness review

also concluded that a new root cause determination was not

necessary because the root causes had been correctly identified, and

common cause analyses and/or streaming analyses had been

recently performed for industrial safety, clock reset events, and

decision making errors. Additionally, Building Block 6, Human

Performance/Continuous Learning, for the SIBP/SIIP had been

developed. The effectiveness review concluded that the corrective

actions for CRDR 2780273 were not well-defined and there were no

actions for implementation, monitoring, reinforcement, adjustment, or

transfer of human performance ownership change. Furthermore, the

corrective actions were either not fully implemented or not

implemented as intended. During review of the SIBP/SIIP, the team

noted that none of these corrective actions for CRDR 2780273 had

been incorporated into Building Block 6.

- 62 - Enclosure

  • The team reviewed apparent cause and root cause evaluations

addressing human performance issues to determine whether the

licensees conclusion that the root cause analysis for CRDR 2780273

was correct. These included CRDR 2994589 (Human Performance

Department Clock Reset Events ACE Report), CRDR 2994593

(Continuous and Reference Procedure Use and Adherence

Department Clock Resets ACE Report), CRDR 2936096 (2006 Site

Clock Reset and Significant Event Stream Analysis), CRDR 3011305

(Industrial Safety Events Common Cause Analysis), CRDR 3008308

(Decision Making Errors from 1/1/06-3/30/07 ACE Report), CRDR

3031159 (2007 Human Performance Site clock Reset Events ACE

Report), and Significant CRDR 3048800 (Industrial Safety

Performance Weakness). The identified causes for CRDRs 2994589,

2994593, and 3031159 were the same; failures in human

performance tool use, leadership oversight, knowledge/skills, and

procedure quality. Of these causes, only leadership oversight and

procedure quality were addressed by CRDR 2780273. Because the

identified contributing causes in CRDR 2780273 included

management not setting/reinforcing clear standards and expectations,

the team concluded that the workforce was unfamiliar with the use of,

and expectation to use, human performance tools such as stopping

when unsure. Discussions with licensee personnel involved in the

apparent cause analyses of department clock resets revealed that it

was common for workers to not be aware of an expectation to stop

before proceeding when procedure quality problems were

encountered. The team verified that corrective actions from these

additionally reviewed CRDRs related to human performance had been

incorporated into the SIBP/SIIP. The team also reviewed CRDR

2928806 which was initiated to track actions in the human

performance crosscutting issue closure plan. CRDR 2928806

contained 75 actions which were included in Building Block 6 of the

SIBP/SIIP. Because the SIBP/SIIP was still in draft form, and many of

the proposed actions had not yet been implemented, the team was

unable to evaluate whether the actions will be effective in correcting

the human performance issues the site was experiencing.

b.1.2 Main Control Room Observations

Description: The team conducted control room observations in all three

units. The team observed Unit 3 for 28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> (October 4 and 5), Unit 1

for 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> (October 9), and Unit 2 for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> (October 11). During

these observations the team observed turnovers between crews, control

room briefs, response to control room alarms, and performance of

control room duties. The team noted the following weaknesses in

control room behaviors:

  • On October 4, 2007, the team observed the off going and oncoming

shift managers (SMs) conducting turnover in the Unit 3 Control

Room. The oncoming SM did not use the SM turnover sheet and

there was no discussion between the two SMs of a new night order

- 63 - Enclosure

concerning an Emergency Action Level clarification issued the

previous evening. The team waited until completion of the turnover

to inquire if there were any new night orders. At that point, the off

going SM provided a turnover of the new night order.

  • Operations personnel were inconsistent in the use of 3-way

communications. The third part of the 3-way communications was

either not performed or was conducted by body language. Certain

crews demonstrated a higher standard than others. This

demonstrated inconsistency across the operations organization in

the use of 3-way communications.

  • Control room personnel did not demonstrate a consistent manner in

declaring expected alarms. Site procedures allowed expected

alarms not to be declared if it is agreed to prior to the test/evolution.

When this methodology was agreed upon, it was not followed

consistently by the control room operators.

  • The team noted that there was no methodology in place to identify

who was assigned as the Control Room Supervisor (CRS). On

October 4, 2007, during a turnover brief, the CRS was announced,

but during other briefs this was not done. The team also noted the

lack of a formal announcement by the CRS when leaving the at the

controls (ATC) area and the lack of a formal turnover to another on

shift SRO for control room oversight. On October 9, 2007, the team

observed that while the SM was out of the control room, the CRS

stepped out of the ATC area and the CRS did not inform the control

room of his whereabouts. The team noted this was in compliance

with Procedure 40DP-9OP02, Conduct of Shift Operations,

requirements which defined the control room as the entire 140 level

of the auxiliary building. During this time, there was no command

SRO in the ATC area. This did not provide effective SRO oversight

of control room activities and did not promote a high standard for

control room oversight.

  • Crew briefs were not consistently announced by the briefer, nor did

all attendees respond by stating, Ready, as described by site

procedure. Some briefs were interrupted by plant manipulation

requests and in one case a medical emergency. During these

interruptions, the briefs continued while a reactor operator and the

CRS responded to the requests.

  • In reviewing control room logs for October 4 and 5, 2007, the team

noted that the Unit 3 shutdown cooling (SDC) Train A inoperability

issue was in two different control room logs used by the SM and the

CRS. One log was used for Limiting Condition for Operations

entries and the other for ODs. The Unit 3 SDC Train A inoperability

times contained in each log were different, which made it difficult to

recover the event timeline.

- 64 - Enclosure

  • During the Unit 1 observation on October 11, 2007, the team

determined that the control room was unaware that utility vehicles

were conducting work within the onsite Salt River Project (SRP)

switchyard. The licensee did not track switchyard work in the

respective control room nor did they routinely apply risk

management features to their risk profile.

  • Peer checking was inconsistent. On October 4, 2007, the team

noted that a peer checker was not paying attention (eyes diverted in

another direction) as he was providing a peer check to an operator

performing system manipulations. In another example, the peer

checker did not respond verbally about equipment being started.

  • The licensee used jumpers to achieve a black board status (a state

in which there are no lighted false or non-impacting alarms on the

control room panels). The licensee had approximately eight

jumpers installed between all 3 units for greater than a year that had

been used to achieve black board status.

5.4 Procedure Quality

Poor procedure quality has been a continuing problem at Palo Verde. The root cause

analysis for the substantive crosscutting issues in human performance documented in

CRDR 2780273 identified that non-conservative decisions were made because of

inadequate procedural guidance and/or poor anticipation of system and human interaction

during procedure and document development. The root cause report also identified that

cognitive decisions were made to not follow procedures because personnel were not able

to follow the procedure as written. During this inspection, the team noted continuing

examples of poor procedure quality indicating that prior corrective actions had not been

completely effective.

a. Inspection Scope

The team reviewed a sampling of procedures to determine whether inadequate

procedures contribute to initiating events, improper mitigating system operation, poor

maintenance or testing, or inadequate emergency and abnormal operations response.

Specifically, the team assessed the effectiveness of corrective actions taken for

procedure quality issues, evaluated the adequacy of the procedure development and

revision processes, and reviewed a sampling of Emergency Planning Implementing

Procedure (EPIP) changes to determine if the EPIP change process was adequate to

correct EPIP related deficiencies and maintain EP commitments.

b. Findings and Observations

b.1 Observations and Minor Violations Involving Procedure Quality

b.1.1 Procedure Issues

Description: The team noted examples of poor procedure quality during

this inspection, including:

- 65 - Enclosure

  • Emergency Operating Procedures (EOPs) written for the operation of

AF allowed operation outside of the design basis. For example, the

procedure for using AF for cold shutdown allowed a cooldown rate of

100°F per hour; however, the design basis for AF limits the cooldown

rate to 70°F per hour.

  • The team noted that a procedure used to set the limit switch on the

polar crane was based on handwritten engineering notes that did not

have a second verification performed. Furthermore, the notes were

not attached to the procedure. Since the WO was incorrectly

annotated as a non-quality package, it was not maintained and all the

information, including the engineering notes, were discarded after

completion of the work. The licensee subsequently requested copies

of the documents from the team to recreate the record.

  • The team noted that the head lift procedure included handwritten

calculations and email communications, but did not include references

to the drawings used to verify proper heights and that no tolerances

were specified for the height measurements. In addition, a sign-off

step involving a cautionary statement was located two steps after the

caution was applicable.

  • The team noted numerous weaknesses in EPIPs. For example,

EPIP-03, Technical Support Center Actions, did not provide direction

on appropriate actions to implement when radiation Monitor RU-13A

was out of service. This radiation monitor was used to evaluate the

habitability of the Technical Support Center. Other examples of

emergency preparedness procedure weaknesses are discussed in

Section 5.7 of this report.

5.5 Equipment Performance

Long standing equipment performance issues have challenged the site. Engineering

programs and processes required to reliably track and trend systems important to safety

and reliable operations were often weak. Specifically:

  • The team noted that system engineers generally did not understand the implementing

requirements of the maintenance rule (MR) program. Specifically, system trending

was not consistent, establishment and maintenance of performance criteria was not

well understood, and the training of system engineers was not sufficient to ensure that

the program was consistently implemented.

The team noted weaknesses in the evaluation of operating experience relied upon to

maintain adequate plant performance. For example, since 1988, engineering

personnel had not adequately evaluated and inspected pre-1983 Target Rock reed

switches in response to OE. Consequently, the licensee was unaware of a pre-1983

reed switch, that did not conform to requirements, had been installed in Unit 2 safety-

related solenoid operated valve (SOV) 2JRCEHV0403 (Reactor Vessel Seal Drain

Valve to Reactor Drain Tank).

- 66 - Enclosure

  • The team identified on September 27, 2007, that the requirements for testing the CS

nozzles in Units 1, 2, and, 3 did not meet TSSR 3.6.6.6. Operations personnel did not

enter TSSR 3.0.3 until prompted by the team on October 30, 2007.

  • The team noted that several long standing degraded conditions were not aggressively

pursued by the licensee. Noteworthy examples include cable vault flooding, ESP

material condition, AF system performance, and safety injection system performance.

a. Inspection Scope

The team reviewed various engineering related issues for the selected systems

(containment spray, turbine driven AF pump, ESP pumps, HPSI pumps, and LPSI

pumps) to evaluate the licensees effectiveness in identifying the causes and extent of

equipment problems, as well as developing and implementing corrective actions.

Additionally, a review of the implementation of the EQ program was conducted. The

team reviewed equipment performance related documents, observed inspection

activities, and conducted plant tours to assess the effectiveness of the licensee in

entering equipment performance issues into the CAP. The team also reviewed open

PVARs and corrective maintenance WOs for the selected systems to assess their

potential impact on operability.

The team reviewed surveillance and post-maintenance tests to assess the

effectiveness of the licensee in specifying appropriate acceptance criteria and to

determine whether the licensees controls to restore equipment to operation following

testing and maintenance were effective. For example, the team reviewed the

licensees program and procedures used to test containment sump butterfly valves to

ensure that the ECCS piping was filled with water as required by Technical

Specifications.

The team reviewed selected EQ preventive maintenance activities for the selected

systems to assess program adequacy and to determine whether the design document,

vendor manual, and generic communication information were appropriately

incorporated into the maintenance program.

The team conducted interviews with licensee personnel, including engineering and

procurement personnel, who had an input into maintenance-related activities, to

determine how the system was operated, whether that operation conflicted with the

intended safety function, and whether engineering input was at an appropriate level to

ensure safe and reliable plant operation.

The team evaluated line organization, quality assurance, external audits, and

assessments to determine whether the licensee had demonstrated the capability to

identify performance issues before they resulted in actual events of undesired

consequence. The team reviewed the licensees management support to the audit

and assessment process, as evidenced by staffing of the quality assurance

organization, responsiveness to audit and assessment findings, and contributions of

the quality organization to improvements in licensee activities.

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b. Observations and Findings

b.1 Failure to Evaluate Performance Monitoring Criteria for Auxiliary Feedwater

System

Introduction. The team identified a Green NCV of 10 CFR 50.65, "Requirements

for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," for the

failure of MR and engineering personnel to demonstrate that the performance or

condition of SSCs was being effectively controlled through the performance of

appropriate preventive maintenance to ensure the SSCs remain capable of

performing their intended function. Specifically, between April and October 2007,

an inadequate evaluation of MR performance criteria (PC) was performed. As a

result, Unit 2 AF Train A exceeded the 10 CFR 50.65(a)(2) PC, and goal setting,

and monitoring was not performed as required by 10 CFR 50.65(a)(1).

Description. The team reviewed the MR PC for the AF system to verify that the

performance and condition of SSCs was being controlled through the

performance of appropriate preventive maintenance to ensure the AF system

was capable of performing its intended function.

The team questioned MR and engineering personnel on the establishment and

evaluation of MR unavailability and reliability PC for the AF system. Maintenance

Rule and engineering personnel discussed the AF system health report for

January 1, 2007 through June 30, 2007, which provided unavailability and

reliability PC for the AF system. During interviews with MR and system

engineering personnel, the team was unable to identify the roles and

responsibilities, as well as the ownership of establishing and maintaining PC for

the AF, CS, and ESP systems. Further, no documentation existed to validate

that unavailability and reliability were appropriately balanced through the

establishment of accurate PC.

The team reviewed Procedure 70DP-0MR01, "Maintenance Rule," Revision 16.

Step 3.3.2.4 stated that, "Performance criteria will be established such that there

would not be an unacceptable increase in plant risk as measured by Core

Damage Frequency (CDF) when SSC performance is at or near the performance

criteria limit." The team questioned MR personnel to determine what an

acceptable increase in plant risk would be to establish PC. MR personnel

determined an increase in CDF of 1E-6 per year from the baseline CDF, as

described in Study 13-NS-C025R004, "Risk-Informed Performance Criteria,"

Revision 4, would be appropriate for establishing PC. However, Step 3.3.2.4 did

not provide explicit direction to consider this CDF criterion.

The team requested PC data for unavailability and reliability of the AF system

considering the change in CDF criteria from Study 13-NS-C025R004. The

allowed unavailability PC used in the AF system health report for

January 1, 2007, through June 30, 2007, was 1.60 percent while the change in

CDF criteria from Study 13-NS-C025R004 would have only allowed an

unavailability PC of 1.16 percent.

The team questioned MR personnel as to the validity of the PC in the AF system

health report. On October 12, 2007, MR personnel initiated PVAR 3075907 to

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evaluate the AF system unavailability and reliability PC. PVAR 3075907 created

an action plan to reconstitute the PC for any system where the PC was greater

than the value documented in Study 13-NS-C025R004. Maintenance Rule

personnel reevaluated the PC in a white paper attached to PVAR 3075907 and

determined that 22 systems had non-conservative PC for either unavailability or

reliability or both.

Procedure 70DP-0MR01, Step 3.5.2.3, also stated that if goal setting is

determined to be necessary, then the SSC will be moved from

10 CFR 50.65(a)(2) to 10 CFR 50.65(a)(1), PC will be monitored, goal setting will

be established, and management attention will be focused on the poorly

performing SSC. Maintenance Rule and engineering personnel failed to move

Unit 2 AF Train A from 10 CFR 50.65(a)(2) to 10 CFR 50.65(a)(1) status in

April 2007, to ensure heightened monitoring and goal setting for the system. In

accordance with the new PC, Unit 2 AF Train A should have been moved from

10 CFR 50.65(a)(2) status to 10 CFR 50.65(a)(1) status due to exceeding

unavailability criteria. The MR expert panel met on October 12, 2007, and

determined Unit 2 AF Train A should have been placed in 10 CFR 50.65(a)(1)

status in April 2007 when unavailability exceeded 1.16 percent.

On October 10, 2007, MR personnel initiated PVAR 3074255 to evaluate the

adequacy of Procedure 70DP-0MR01 with regard to determining PC.

Maintenance Rule personnel also initiated PVAR 3076699 on October 15, 2007,

to reiterate an understanding of the ownership and responsibilities of system

engineers with respect to managing the MR PC.

The team reviewed the Palo Verde "Periodic Assessment of Maintenance Rule

Program," July 2005 through December 2006, assessment. Maintenance Rule

personnel reviewed system engineering inputs to the periodic assessments

including a review of 10 CFR 50.65(a)(2) systems performance criteria. This

periodic assessment did not identify any problems with PC exceeding the values

documented in Study 13-NS-C025R004. The team determined that the annual

assessment was a missed opportunity to identify the non-conservative

performance criteria.

Analysis. The performance deficiency associated with this finding was the failure

of MR and engineering personnel to demonstrate that the performance or

condition of SSCs was being effectively controlled through the performance of

appropriate preventive maintenance for Unit 2 AF Train A. This finding is greater

than minor because it is associated with the mitigating systems cornerstone

attribute of equipment performance and affects the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events

to prevent undesirable consequences. Using the Manual Chapter 0609,

"Significance Determination Process," Phase 1 Worksheets, the finding is

determined to have very low safety significance (Green) since it only affected the

mitigating systems cornerstone and did not represent a loss of system safety

function. The cause of this finding had crosscutting aspects associated with self

assessments of the PI&R area in that MR and engineering personnel failed to

perform self assessments that were comprehensive, appropriately objective, and

self-critical (P.3.(a)). The cause of this finding had crosscutting aspects

associated with decision-making of the human performance area in that

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engineering personnel failed to make safety-significant or risk-significant

decisions using a systematic process (H.1.(a)). The cause of the finding was

also related to the safety culture component of accountability in that management

failed to reinforce safety standards and display behavior that reflected safety as

an overriding priority (O.1.(b)).

Enforcement. 10 CFR 50.65(a)(1) requires, in part, that the licensee monitor the

performance or condition of SSCs against licensee-established goals, in a

manner sufficient to provide reasonable assurance that such SSCs are capable

of fulfilling their intended functions. 10 CFR 50.65(a)(2) requires, that monitoring

as specified in 10 CFR 50.65(a)(1) is not required where it has been

demonstrated that the performance or condition of a SSC is being effectively

controlled through the performance of appropriate preventive maintenance, such

that the SSC remains capable of performing its intended function. Contrary to

the above, from April to October 2007, MR and engineering personnel failed to

demonstrate that performance of Unit 2 AF Train A was being effectively

controlled through appropriate scheduled maintenance. Specifically, an

inadequate evaluation of MR performance criteria was performed and, as a

result, Unit 2 AF Train A exceeded its 10 CFR 50.65(a)(2) PC and goal setting

and monitoring was not performed as required by 10 CFR 50.65(a)(1). Because

the finding was of very low safety significance and was entered into the CAP as

PVAR 3075907, this violation was treated as a NCV, consistent with Section VI.A

of the Enforcement Policy: NCV 05000529/2007012-05, "Failure to Implement

Maintenance Rule Requirements for Auxiliary Feedwater.

b.2 Failure to Control Nonconforming Target Rock Reed Switches

Introduction. The team identified a third example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for the failure of

engineering personnel to evaluate and correct the installation of nonconforming

Target Rock reed switches. Between 1988 and October 10, 2007, engineering

personnel had not adequately evaluated and inspected pre-1983 Target Rock

reed switches in response to OE. Consequently, the licensee was unaware that

a pre-1983 reed switch, that did not conform to requirements, had been installed

in Unit 2 safety-related solenoid operated valve (SOV) 2JRCEHV0403 (reactor

vessel seal drain valve to reactor drain tank).

Description. Operating Experience (OE) on Target Rock reed switches,

manufactured before 1983 with Part Number 100967-1, was originally reviewed

at PVNGS in 1988 to determine if any of these reed switches were installed in

the plant. The reed switches had deterioration of the lead wire insulation, that

cracked when the wires were flexed during maintenance or handling. Some of

the cracks occurred at the terminal blocks while tensioning the terminal block

fasteners. This degradation can cause a short to ground of the exposed wires

resulting in dual position indication, blown fuses, or inadvertent opening of the

valves.

The original disposition closed the OE to the PVNGS Generic Letter 91-15,

"Operating Experience Feedback Report, Solenoid-Operated Valve Problems at

U.S. Reactors, SOV Program. During a review by the CDBR, the licensee

determined that a formal SOV program did not exist, and the OE had been

- 70 - Enclosure

closed without a thorough evaluation. The CDBR team wrote PVAR 2959880 on

January 12, 2007, and determined no degraded or non-conforming condition

existed without performing a review to determine if any of these reed switches

were installed in the plant.

CRAI 2960705 was initiated on January 19, 2007, to evaluate the availability and

current use of the reed switches. The CRAI determined no pre-1983 Target

Rock reed switches were available or in use in the plant and no further action on

the OE was required. However, CRAI 2960705 also determined that six reed

switches were installed in the plant that had not been inspected, reworked, or

replaced. Three of the six were located inside containment, with one being

safety related and two being quality augmented. The other three were located in

the auxiliary building.

The team questioned engineering personnel about the conclusion of the CRAI

that no pre-1983 reed switches were installed in the plant and that no further

action was required. The team also questioned the CRAI 2960705 conclusion

that none of these reed switches were installed in the plant since the CDBR

evaluation stated one safety related reed switch had not been inspected,

reworked, or replaced. After further review by the licensee, it was determined

that one Target Rock reed switch, made before 1983, was installed in safety-

related Valve SOV 2JRCEHV0403. Valve SOV 2JRCEHV0403 provides

isolation for the reactor vessel o-ring to maintain a boundary to fission product

release.

On October 10, 2007, PVAR 2959880 was redirected to the control room for an

immediate OD/FA. Operations personnel determined that all other pre-1983

Target Rock reed switches had been inspected or had no design basis safety

function. Engineering personnel determined Valve SOV 2JRCEHV0403

remained functional because the length of time in service with no failures

indicated Valve SOV 2JRCEHV0403 was not susceptible to cracking and that no

cracking had occurred. In addition, Valve SOV 2JRCEHV0403 had no history of

being reworked, replaced, or inspected, so the integrity of the reed switch had

not been challenged. A corrective maintenance WO was generated per

PVAR 2959880 to inspect Valve SOV 2JRCEHV0403.

Analysis. The performance deficiency associated with this finding was the failure

of engineering personnel to evaluate and correct a condition adverse to quality

involving the installation of nonconforming Target Rock reed switches. The

finding is greater than minor because it is associated with the equipment

performance cornerstone attribute of the initiating event cornerstone and affects

the associated cornerstone objective to limit the likelihood of those events that

upset plant stability and challenge critical safety functions during shutdown as

well as power operations. Using the IMC 0609, "Significance Determination

Process," Phase 1 Worksheets, the finding is determined to have very low safety

significance (Green) because assuming the worst case degradation, the finding

would not result in exceeding the Technical Specification limit for reactor coolant

system leakage because a redundant valve existed in series with

SOV 2JRCEHV0403. The cause of this finding had crosscutting aspects

associated with OE of the PI&R area in that operations and engineering

personnel failed to ensure implementation and institutionalization of OE through

- 71 - Enclosure

changes to station processes, procedures, equipment, and training programs

(P.2.(b)). The cause of this finding was also related to the safety culture

component of accountability in that operations and engineering personnel failed

to demonstrate a proper safety focus and reinforce safety principles (O.1.(c)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires, in part, that measures be established to assure that conditions adverse

to quality are promptly identified and corrected. Contrary to the above, between

1988 and October 10, 2007, engineering personnel failed to ensure that

conditions adverse to quality were promptly identified and corrected. Specifically,

in response to OE issued in 1988, the licensee did not identify and correct the

installation of a pre-1983 Target Rock reed switch in Unit 2 safety-related

SOV 2JRCEHV0403. This was the third example of the NCV involving the failure

to implement CAP requirements. This finding was of very low safety significance

and was entered into the CAP as PVAR 2959880.

b.3 Failure to Meet the Requirements of Technical Specifications Surveillance

Requirement 3.6.6.6

Introduction. The team identified a Green NCV of Technical Specification

Surveillance Requirement (TSSR) 3.6.6.6 for the failure of operations personnel

to verify that each containment spray (CS) nozzle was unobstructed.

Specifically, the last completed surveillance test conducted on each unit

identified that one nozzle in each unit was obstructed and that the nozzles were

not tested in accordance with the approved retest requirement.

Description. The team reviewed Procedure 73ST-9SI02, Containment Spray

Nozzle Air Test, Revision 5, completed on Unit 3 in April 27, 2000, to verify that

the CS nozzles were not obstructed. The surveillance test aligns warmed

compressed air to the spray headers and then verifies that the nozzles are

unobstructed either through use of an infrared camera to observe the nozzles or

by visually observing movement of streamers attached to the nozzle. If a nozzle

is determined to be obstructed, Section 10.1 of 73ST-9SI02, stated that

corrective actions must be taken and the nozzle retested to verify flow prior to

entry into Mode 4. During the test on Unit 3, Nozzle 3PSIAL429 was found to be

obstructed. CRDR 117284 was initiated to evaluate the condition and clear the

blockage. The surveillance test log indicates that the blockage was cleared;

however, there was no evidence to indicate that the nozzle was retested in

accordance with the surveillance test requirement.

As a follow-up to the extent of condition, the team also reviewed the surveillance

test results for Units 1 and 2. Procedure 73ST-9SI02, Revision 5, was partially

completed for Unit 1 on July 12, 2001. During that test, Nozzle 1PSIAL433 was

plugged. Work Order 2380383 was initiated to clear the blockage. Upon review

of the test results the licensee determined that two additional nozzles were not

tested. These two nozzles were later retested on October 21, 2002. However,

there is no evidence to indicate that blocked Nozzle 1PSIAL433 was retested in

accordance with the surveillance test requirement. Procedure 73ST-9SI02,

Revision 6, was completed for Unit 2 on April 12, 2002. The test discovered that

Nozzle 2PSIBL419 was obstructed. Work Order 2797713 was initiated to clean

- 72 - Enclosure

and replace the nozzle. Again, there was no evidence to indicate that the

blocked nozzle was retested in accordance with the surveillance test

requirement.

Following the teams questioning, PVARs 3075026, 3075059 and 3068647 were

initiated to document that during performance of Procedure 73ST-9SI02 in Units

1, 2 and 3 respectively, corrective maintenance was performed to clean a nozzle

that was observed to be obstructed. In each case, a WO was written to inspect

and clean the nozzle. Based on this the licensee concluded that there was no

immediate impact on operability.

Analysis. The performance deficiency associated with this finding was the failure

to meet the requirements of TSSR 3.6.6.6. The finding is determined to be more

than minor because it affected the configuration control attribute of the barrier

integrity cornerstone, and affected the associated cornerstone objective to

provide reasonable assurance that physical design barriers protect the public

from radionuclide releases caused by accidents or events. Using the IMC 0609,

"Significance Determination Process," Phase 1 Worksheets, the finding is

determined to have very low safety significance (Green) because it did not

involve an actual reduction in defense-in-depth for the atmospheric pressure

control function of the reactor containment.

Enforcement. TSSR 3.6.6.6 required that the CS nozzles be verified free of

obstructions. Contrary to the above, as of April 11, 2000, for Unit 3,

March 22, 2002, for Unit 2, and April 13, 2001, for Unit 1, the licensee did not

verify CS nozzles were free of obstructions through the conduct of surveillance

testing. Specifically, Units 1, 2, and 3 each had a blocked CS nozzle during the

performance of Procedure 73ST-9SI02; however, retests were not conducted

following corrective maintenance. Because of the very low safety significance of

the issue and because the issue was entered into the licensees CAP as PVARs

3075026, 3075059, 3068647, and 3048511, the issue was treated as an NCV

consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000528,

05000529,05000530/2007012-06, Failure to Meet the Requirements of

Technical Specification Surveillance Requirement 3.6.6.6.

b.4 Failure to Meet the Requirements of Technical Specifications Surveillance

Requirement 3.0.3

Introduction. The team identified a Green NCV of TSSR 3.0.3 for the failure of

operations personnel to conduct an assessment and manage the risk for a

missed surveillance test. Specifically, on September 27, 2007, the team

identified that the requirements for testing the CS nozzles in Units 1, 2, and, 3 did

not meet TSSR 3.6.6.6. Operations personnel did not enter TSSR 3.0.3 until

prompted by the team on October 30, 2007.

Description. On September 27, 2007, the team identified that the requirements

for testing the CS nozzles (described above) in Units 1, 2, and, 3 did not meet

TSSR 3.6.6.6. The licensee initially entered the condition into their CAP as

PVAR 3068647. On October 18, 2007, the licensee was pursuing approval from

the Plant Review Committee to credit the work orders that removed the blockage

from the nozzles as equivalent to the retest specified Procedure 73ST-9SI02,

- 73 - Enclosure

"Containment Spray Nozzle Air Test," Revision 5, Section 10.1. Although the

Plant Review Committee did not act on this request, they had the opportunity to

recognize that the surveillance requirements had not been met and the

requirement for a missed surveillance test had not been invoked.

Upon further prompting by the team, the licensee entered TSSR 3.0.3 for Units 1

and 2 on October 30, 2007. Since Unit 3 was shutdown, the requirements of

TSSR 3.6.6.6 were not applicable and therefore TSSR 3.0.3 was not required to

be entered. Engineering personnel initiated PVAR 3085708 to address these

issues.

Analysis. The performance deficiency associated with this finding was the failure

of operations personnel to conduct an assessment and manage the risk for a

missed surveillance test in accordance with TSSR 3.0.3. The finding is

determined to be more than minor because it affected the configuration control

attribute of the barrier integrity cornerstone, and affected the associated

cornerstone objective to provide reasonable assurance that physical design

barriers protect the public from radionuclide releases caused by accidents or

events. Using the IMC 0609, "Significance Determination Process," Phase 1

Worksheets, the finding is determined to have very low safety significance

because it did not involve an actual reduction in defense-in-depth for the

atmospheric pressure control function of the reactor containment. The cause of

this finding had crosscutting aspects associated with work practices of the human

performance area in that operations personnel failed to ensure supervisory and

management oversight of work activities that resulted in a missed TSSR

(H.4.(c)). The cause of this finding was also related to the safety culture

component of accountability in that operations personnel failed to demonstrate a

proper safety focus and reinforce safety principles (O.1.(c)).

Enforcement. TSSR 3.0.3, requires that a risk evaluation be performed for any

surveillance delayed greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and the risk impact be managed.

Contrary to the above, between September 27, 2007, and October 30, 2007,

operations personnel failed to perform a risk evaluation and manage the impact

of risk for a delayed surveillance test. Specifically, the team identified that the

requirements for testing the CS nozzles in Units 1, 2, and, 3 did not meet TSSR

3.6.6.6. Operations personnel did not enter TSSR 3.0.3 for Units 1 and 2 until

prompted by the team on October 30, 2007. Because of the very low safety

significance of the issue and because the issue was entered into the CAP as

PVAR 3085708, the issue was treated as an NCV, consistent with Section VI.A

of the Enforcement Policy: NCV 05000528,05000529/2007012-07, Failure to

Meet the Requirements of Technical Specifications Surveillance Requirement

3.0.3.

b.5 Untimely Corrective Actions for Submerged Safety Related Cables

Introduction. The team identified a fourth example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the failure of

operations and engineering personnel to take timely corrective actions for

conditions adverse to quality involving water intrusion and flooding of

underground manholes and cable vaults. Specifically, since 1996, water

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intrusion and flooding of underground manholes and cable vaults had been a

recurrent problem affecting electric cables and cable splices for safety-related,

non-safety-related, and security systems.

Description. Since 1996, water intrusion and flooding of underground manholes

and cable vaults had been a recurrent problem affecting electric cables and cable

splices for safety-related, non-safety-related, and security systems. Operations

and engineering personnel initiated CRDR 2407009, CRDR 2784074, and CRAI

2800511 to address these issues.

In October 2007, the team observed the pump-out and inspection of non-safety

related manhole (KMA07) that contained a faulted power cable affecting security

equipment. The cable had been submerged when it failed. Approximately 15

feet of water was pumped from the manhole in order to allow access to the

damaged cable. The team noted that duct banks connecting to adjacent

manholes were approximately 6 feet from the bottom of the manhole vault and

could have served as a potential conduit for the water intrusion. The team

observed water dripping from the ends of a splice on another cable in the

manhole that had been repaired from a previous failure. The team noted that

neither safety related nor non-safety related electric cables and cable splices, in

these underground cable runs, were qualified for continuous submergence.

The team reviewed repeated efforts to address the extent and cause of water

intrusion into underground vaults described in CRAI 2425879, CRAI 2429470,

CRDR 2882166, and CRAI 2919409. The team also reviewed the root cause

investigation, documented in CRDR 2784074, for the Unit 1 spray pond

degraded cable splice failure on March 23, 2005. The team determined that the

root cause analyses failed to address that power cables, not just cable splices,

are susceptible to degradation and failure when submerged for extended periods.

The team also determined that past corrective actions have not been effective in

eliminating underground manhole and cable vault flooding, or cable failures due

to submergence.

The team reviewed a standing order that required the inspection of manholes

that are susceptible to water intrusion following a rainfall of greater than 0.3

inches within a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period. The team determined there were no formal

administrative controls in place to initiate this inspection. The inspection was not

incorporated into station procedures to assure that the process was reviewed,

documented, approved and, administratively controlled.

The team also determined that the OD for Unit 1 Spray Pond Pump 1MSPB01,

documented in CRDR 2784074, relied on inspection of manhole

1EZV06BKEM04 after a rainfall of greater than 0.3 inches to ensure that the

power cable splice stayed dry. The 0.3 inch rainfall number was arbitrarily

chosen by examining rainfall history at the site and selecting a value that would

result in about 4 to 5 rainfall-based inspections per year. The team determined

that there was no technical data or root cause analysis that indicated excessive

rainfall was the primary cause of the flooding problem in the electrical manholes

and underground cable systems, and not water from another source.

- 75 - Enclosure

The team noted that, in addition to site specific experiences, a substantial

amount of external OE had been provided to the station. The licensee's

evaluation of Generic Letter (GL) 2007-01, "Inaccessible or Underground Power

Cable Failures that Disable Accident Mitigation Systems or Cause Plant

Transients," was not technically rigorous nor comprehensive since it did not

address failures associated with cable splices. Additionally Information Notice

2002-12, "Submerged Safety-Related Electrical Cables," was closed on March

29, 2002, by reference to CRDR 2407009. CRDR 2407009 evaluated cables in

manholes in response to a 2001 manhole flooding and cable submergence event

and established a long term plan to deal with water intrusion. CRDR 2407009

remained open and had not been effective in addressing the root causes of the

manhole water intrusion problem nor in implementing effective corrective action

as evidenced by the U1 Spray Pond B degraded cable splice failure on

March 23, 2005, and the non-safety manhole flooding and 12.5kV cable failure

observed during this inspection.

Analysis. The performance deficiency associated with this finding was the failure

of operations and engineering personnel to take timely corrective action for

conditions adverse to quality involving water intrusion and flooding of

underground manholes and cable vaults. This finding is greater than minor

because it is associated with the mitigating systems cornerstone attribute of

equipment performance and affects the cornerstone objective of ensuring the

availability and reliability of systems that respond to initiating events to prevent

undesirable consequences. Using the IMC 0609, "Significance Determination

Process," Phase 1 Worksheets, the finding is determined to have very low safety

significance since it only affected the mitigating systems cornerstone and did not

represent a loss of system safety function. The cause of this finding had

crosscutting aspects associated with decision making of the human performance

area in that operations and engineering personnel failed to use conservative

assumptions for operability decision-making when evaluating degraded and

nonconforming conditions (H.1.(b)). The cause of the finding was also related to

the safety culture component of accountability in that management failed to

reinforce safety standards and display behavior that reflected safety as an

overriding priority (O.1.(b)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires in part, that measures shall be established to ensure that conditions

adverse to quality are promptly identified and corrected. Contrary to the above,

since 1996, operations and engineering personnel failed to take timely corrective

actions for conditions adverse to quality involving water intrusion and flooding of

underground manholes and cable vaults. Specifically, water intrusion and

flooding of underground manholes and cable vaults had been a recurrent

problem affecting electric cables and cable splices for safety-related, non-safety-

related, and security systems. This was the fourth example involving the failure

to implement the CAP. This example was of very low safety significance and

was entered into the CAP as PVAR 3072557.

- 76 - Enclosure

b.6 Failure to Properly Evaluate the Extent of Condition of 4160 V and 480 V Motor

Issues

Introduction. The team identified a seventh example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and

Drawings," for the failure of operations and engineering personnel to adequately

evaluate degraded and unanalyzed conditions to support ODs associated with

CS and LPSI motor lug issues. Specifically, since April 2005, CRDR 2841653

noted that the extent of condition review required by CRDR 2790388, was

complete for the CS and LPSI motor issues, but identified that the condition may

be transportable to other 4160V and 480V motors. However, no evaluation of

additional 4160V and 480V motors was conducted.

Description. Between April and October 2005, there were several CRDRs

documenting loose lugs, improper crimping, and broken motor lead strands on

the CS and LPSI pumps on all three units. The licensee performed technical and

operability evaluations associated with these conditions in CRDR 2968639. On

February 8, 2007, the licensee initiated CRDR 2973072 to address several

process issues associated with the disposition of the CS and LPSI motor lug

issue.

On October 25, 2005, the licensee initiated CRDR 2841653, which identified that

loose lugs, improper crimping, and broken motor lead strands may be

transportable to other 4160V and 480V motors. The evaluation in CRDR

2973072, stated that although the originator of the CRDR believed the issues

were transportable to other 4160V and 480V motors, it was impractical to open

the terminations on each and every 4160V and 480V motors. Engineering and

operations personnel decided to address the rest of the stations motor

terminations as they were removed and re-terminated as part of regularly

scheduled maintenance. No specific corrective action or work-tracking

mechanism was specified to ensure that the inspections were performed.

The team determined operations should have entered Procedure 40DP-9OP26,

"Operability Determinations and Functional Assessment," Revision 18.

Procedure 40DP-9OP26, Step 3.3.5 stated that if other plant conditions or

disassembly is required, then the extent of condition should be addressed by the

CAP, where work mechanisms can be developed and scheduled as appropriate

based on the safety significance. Operations personnel failed to schedule work

mechanisms to ensure the extent of condition on other 4160V and 480V motors

was addressed. On October 24, 2007, engineering personnel initiated

PVAR 3082645 to address this issue.

Analysis. The performance deficiency associated with this finding was the failure

of operations and engineering personnel to adequately evaluate degraded and

unanalyzed conditions to support operability decision making associated with CS

and LPSI motor issues. This finding is greater than minor because it is

associated with the mitigating systems cornerstone attribute of equipment

performance and affects the cornerstone objective of ensuring the availability and

reliability of systems that respond to initiating events to prevent undesirable

consequences. Using the IMC 0609, "Significance Determination Process,"

Phase 1 Worksheets, the finding is determined to have very low safety

- 77 - Enclosure

significance (Green) since it only affected the mitigating systems cornerstone and

did not represent a loss of system safety function. The cause of this finding had

crosscutting aspects associated with corrective actions of the PI&R area in that

operations and engineering personnel failed to take corrective actions to address

safety issues and adverse conditions in a timely manner (P.1.(d)). The cause of

the finding was also related to the safety culture component of accountability in

that management failed to reinforce safety standards and display behavior that

reflected safety as an overriding priority (O.1.(b)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, Instructions,

Procedures and Drawings, requires that activities affecting quality be prescribed

by instructions, procedures, or drawings, and be accomplished in accordance

with those instructions, procedures, and drawings. The assessment of

operability of safety-related equipment needed to mitigate accidents was an

activity affecting quality and was implemented by Procedure 40DP-9OP26,

Operability Determination and Functional Assessment, Revision 18. Step 3.3.5

stated that if other plant conditions or disassembly is required, then the extent of

condition should be addressed by the CAP, where work mechanisms can be

developed and scheduled as appropriate based on the safety significance.

Contrary to the above, since April 2005, engineering personnel failed to ensure

work mechanisms were developed and scheduled to determine the extent of

condition of motor termination degradations. Specifically, operations and

engineering personnel failed to adequately evaluate the extent of condition for

4160 V and 480 V motor lug issues, including loose lugs, improper crimping, and

broken motor lead strands. This is the seventh of 8 examples associated with

the NCV involving failure to implement the OD program. This example was of

very low safety significance and was entered into the CAP as PVAR 3082645.

b.7 Observations and Minor Violations Involving Equipment Performance

b.7.1 Environmental Qualification Program

Description. The existing EQ group responsibility is focused on the EQ

requirements of 10 CFR 50.49 for electrical equipment important to safety

in harsh environments and seismic qualification. Responsibility for EQ

requirements outside of these areas falls upon procurement engineering,

the warehouse and supply chain group, maintenance engineering, and

design engineering. When interviewed, these groups stated several of

their members had previous EQ experience, but that their personnel did

not receive any formal EQ training. Consequently, there was no single

group with overall responsibility for the full range of environmental and

seismic qualification requirements.

The formal mechanical EQ program was deleted from the EQ program

based on a position paper entitled, The Elimination Of The Mechanical

EQ Program, prepared by Tenera in 1994. This study stated that

continued compliance with 10 CFR Part 50, Appendix A, Criterion 4,

Environmental and Dynamic Effects Design Basis, will be maintained by

the procurement program, that had in place detailed and sophisticated

controls of all materials in mechanical equipment to confirm the ability of

equipment and components to perform their required functions in harsh

- 78 - Enclosure

environments; and the maintenance program, that will monitor, trend, and

correct equipment aging for mechanical equipment. However, as

mentioned previously, these groups stated that although several of their

members had previous EQ experience, their personnel do not receive any

formal EQ training.

The fragmented approach to the various aspects of EQ requirements

relied heavily on the EQ awareness and knowledge of the persons in the

groups responsible for implementing the EQ requirements of

10 CFR 50.49 and 10 CFR Part 50, Appendix A, Criterion 4. Examples of

how this EQ program approach and the lack of formal training in groups

required to implement EQ requirements led to problems in the EQ area

included the following:

  • During a Unit 3 plant walkdown the team identified minor

discrepancies in the installation configuration of ASCO solenoid

valves on the Unit 3 atmospheric dump valves. The configuration

discrepancy had no impact on the function of the components. In

their investigation of the discrepancies, the licensee identified that

there was no existing design control in place for mechanical

components requiring EQ (PVAR 3079739).

  • During a July 1, 2005, review of preventive maintenance for charging

pump motors, the licensee noted that EQ-required lubrication

activities had been stopped in 1998. The condition was documented

in CRDR 2811528 on June 27, 2005, and the activities were re-

verified. Although the condition did not impact the ability of the

equipment to function, this illustrated a lack of communication and

coordination between various site organizations and the EQ program.

  • During a Unit 3 containment walkdown, the team observed that the

outer polymer sheath covering for flexible conduit connectors in

numerous equipment locations was cracked, split, and separating

away from the underlying flexible metal conduit. Three different types

of repairs were performed on several degraded flexible conduit

sheaths: wrapping with black electrical tape, application of room

temperature vulcanization sealant at the ends of the sheath that

remained on the flex conduit after other sections had broken away,

and wrapping with a fiberglass tape. As a result of this observation,

the licensee initiated PVAR 3079739 to evaluate this deficiency in the

design control process.

  • Water intrusion and flooding of underground manholes and cable

vaults had been a recurrent problem affecting electric cables and

cable splices for safety-related, non-safety-related, and security

systems. Electric cables and cable splices in these underground

cable runs were not qualified for continuous submergence.

  • During an October 26, 2006, review of the routine tasks associated

with the EQ requirements for the GL 89-10, "Safety Related Motor

- 79 - Enclosure

Operated Valve Testing and Surveillance," motor operated valves, the

licensee identified that repetitive tasks did not reflect the correct

frequency and initiated CRDR 2936445. Specifically, the work

descriptions for the maintenance activities did not adequately note the

EQ requirements.

The team reviewed the results of Self Assessment No. 2957427,

Equipment Qualification Program, and CRDR 3048870, Engineering

Programs, Appendix B, Equipment EQ Program Review, and found that

the reviews generally identified performance issues at the appropriate

level. However, the team found that lax procedural ties to other plant

organizations were symptomatic of the fragmentation and organizational

weakness in the treatment of the full range of EQ issues.

In summary, EQ program weaknesses were attributed to: insufficient

staffing; a fragmented approach to the EQ program implementation with

no single group with overall responsibility for the full range of

environmental and seismic qualification requirements; and no formal EQ

training for groups responsible for implementing the EQ requirements of

10 CFR 50.49 and NRC general design criteria.

5.6 Configuration Control

5.6.1 Effectiveness of Corrective Actions

The team concluded that corrective actions to address adverse conditions regarding

configuration control were generally effective. The team reviewed a sample of planned and

installed modifications, as well as unapproved and cancelled modifications, to ensure that

changes to equipment were effectively controlled and implemented. The team noted the

licensees program was adequate in implementing corrective actions related to changes in

the plant. However, there were some weaknesses identified with modifications that were

tracked in the licensees database. The potential existed for scheduled modifications to

inadvertently appear on the cancelled or unapproved list. This caused confusion in

determining the status of a specific modification. The team also identified weaknesses in

the thoroughness of performing evaluations regarding changes, or modifications to the

plant that may be outside of the licensing and design bases.

a. Inspection Scope

The team assessed whether corrective actions which affected configuration control

were effective because the loss of configuration control of risk-significant systems or

equipment could lead to the initiation of a reactor transient and/or compromise

mitigation capability. The team reviewed several corrective action documents, WOs,

system health reports, assessments, and audits, as well as conducted interviews of

licensee personnel, in order to adequately assess the effectiveness of corrective

actions for deficiencies involving configuration control. The team reviewed selected

ODs and modifications to verify if a loss of configuration control of risk-significant

systems or equipment which led, or potentially led, to the initiation of a reactor

transient and/or compromised the systems mitigation capability.

- 80 - Enclosure

b. Observations and Findings

b.1 Failure to Implement Corrective Actions for Borg-Warner Check Valves

Introduction. The team identified a fifth example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for the failure of

maintenance and engineering personnel to promptly correct a

degraded/nonconforming condition associated with a Part 21 notification related

to 3 inch Borg-Warner check valves. Specifically, the licensee did not perform a

disassembly and inspection of Valve 1PSIEV123, HPSI header containment

penetration check valve, during the Unit 1 R13 refueling outage for a 2001 Part

21 corrective action. The failure to perform the maintenance resulted in the

failure of 1PSIEV123 in July 2007, and the continued degradation of additional

safety injection system check valves.

Description. On August 23, 2001, the licensee received Part 21 2001-27-0 on

Borg-Warner Flowserve check valves which expanded the scope of the original

Part 21 notification issued in 1993 to include all 3 and 4 inch Borg-Warner swing

check valves of any pressure class. The condition described in the original Part

21 report was a potential failure of Borg-Warner valves to go fully closed due to

the valve disk becoming lodged under the lip of the valves seat. The licensee

assumed that CRDR 2332280 initiated on October 23, 2000, already performed

the required evaluations for this issue and thus no action was taken.

On January 26, 2007, mechanical engineering determined that not all Borg-

Warner check valves had been evaluated by CRDR 2332280 and generated

PVAR 2963565, coded as degraded/nonconforming, to address the 2001 Borg-

Warner Part 21 notification. This PVAR identified valves that were more critical

due to the potential for having a nonconformance issue, and the last reassembly

being implemented before Procedure 31MT-9ZZ17, "Borg-Warner Check Valve

Disassembly and Assembly, was developed. This list included Valve

1PSIEV123. On February 2, 2007, the ARRC initiated CRDR 2965988 to

complete the necessary action for the 2001 Part 21 notification. CRDR 2965988

was closed after addressing the 2001 Part 21 evaluation without any action taken

to address the degraded/nonconforming conditions of the check valves.

On May 2, 2007, Significant CRDR 2930774, "Failure of LPSI Injection Check

Valve 1PSIEV134," was issued following the failure of another Borg-Warner

check valve. The valve failed because of excessive friction in the disc to seat

landing zone, spherical bearing and swing arm bore, and the spherical bearing

and disc/stud raised weld. This corrective action document was issued to

change the extent of cause to apply to the weld size, gap measurements and

stiffness issues to all Borg-Warner valves, including the 3 and 4 inch valves, and

revise Procedure 31MT-9ZZ17, "Borg-Warner Check Valve Disassembly and

Assembly," to incorporate new Borg-Warner assembly information and

clearances.

On May 19, 2007, the licensee did not perform Procedure 73ST-9SI05, "Leak

Test of HPSI/LPSI Containment Isolation Check Valves," Section 8.2, Revision

21, on 1PSIEV123. Procedure 73ST-9SI05, Section 7.6, stated, in part, that a

typical refueling outage involves performance of Sections 8.1 through 8.4 during

- 81 - Enclosure

plant shutdown, and then retest of individual valves during the startup if work was

performed on any valve during the outage. However, during the Unit 1 R13

refueling outage the licensee did not perform the leak tests during the plant

shutdown. This was further affected by the maintenance on Valve 1PSIEV123

being removed from the outage schedule on June 24, 2007, because of a

perceived parts issue by supply chain services. The parts required for the

maintenance were actually staged on May 24, 2007. The licensee failed to

properly code the WO as degraded/nonconforming which allowed for the

maintenance to be cancelled without an OD or FA. Completion of the scheduled

maintenance would have provided another chance to identify the

degraded/nonconforming condition.

On July 5, 2007, Valve 1PSIEV123 failed during performance of Procedure

73ST-9SI05, "Leak Test of HPSI/LPSI Containment Isolation Check Valves,"

Revision 21, and was declared inoperable. The valve failure was because of

binding in the spherical bearing due to excessive wear between the hinge arm

and spherical bearing. The valve also exhibited excessive washer to hinge arm

gap and indications of disc to stud weld interference.

Analysis. The performance deficiency associated with this finding was the failure

of maintenance and engineering personnel to promptly correct a

degraded/nonconforming condition associated with a Part 21 notification related

to 3 inch Borg-Warner check valves. The finding is more than minor because it is

associated with the equipment performance attribute of the mitigating systems

cornerstone and affected the associated cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences. Using the Manual Chapter 0609,

"Significance Determination Process," Phase 1 Worksheets, the finding is

determined to have very low safety significance (Green) because the condition

only affected the mitigating systems cornerstone and did not result in the actual

loss of safety function to any component, train, or system. The cause of this

finding had crosscutting aspects associated with OE of the PI&R area in that

maintenance and engineering personnel failed to ensure implementation and

institutionalization of OE through changes to station processes, procedures,

equipment, and training programs (P.2.(b)). The cause of the finding was also

related to the safety culture component of accountability in that management

failed to reinforce safety standards and display behavior that reflected safety as

an overriding priority (O.1.(b)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action,"

states, in part, that measure shall be established to assure that conditions

adverse to quality are promptly identified and corrected. Contrary to the above,

the licensee failed to promptly correct a degraded/nonconforming condition

associated with a Part 21 notification related to 3 inch Borg-Warner check valves

and site specific OE, resulting in the failure of Valve 1PSIEV123 while in Mode 3

on July 5, 2007. This was the fifth example of the NCV involving the failure to

implement the CAP. This example is of very low safety significance and was

entered into the CAP as CRDR 3038601.

- 82 - Enclosure

5.6.2 Selected System Walkdown

The team determined that the LPSI and CS systems were in good material condition, and

system components were found in the expected positions. Equipment labels, hangers and

supports, and environmental conditions were adequately maintained. There were no

observed system leakage points that would degrade the system function. General

housekeeping practices were found to be adequate; however, the team did identify several

issues regarding a lack of control of transient combustibles. No significant deficiencies

with regards to configuration control for the selected systems were identified. The team

did identify several examples that demonstrated a weakness with the licensee maintaining

an adequate condition of less risk significant systems, incorrectly installed scaffolding,

equipment tagging, and fire protection features.

a. Inspection Scope

The team performed a walkdown of general plant areas, and accessible portions of the

LPSI and the CS systems for Units 1 and 2, in order to verify the licensee maintained

adequate configuration control of risk significant systems. The team reviewed design

documents, plant drawings, and system procedures to verify actual plant conditions

were consistent with as-built requirements. In addition, the team reviewed applicable

temporary modifications to ensure proper installation in accordance with the design

information. The team also performed observations of components and surrounding

plant areas for the selected systems to identify additional equipment conditions and

items that might degrade system performance.

b. Observations and Findings

b.1 Failure to Maintain Control of Transient Combustibles

Introduction. The team identified two examples of a Green NCV of Technical

Specification 5.4.1.d for the failure of Fire Protection (FP) personnel to follow

procedures for the control of transient combustibles. Specifically, the team

identified that on the 70 foot elevation of the auxiliary building (radiation

protection (RP) remote monitoring station) and in the Unit 3 containment building,

there were transient combustibles being stored without a proper evaluation or the

required permits.

Description. During a walkdown of auxiliary building 70 foot elevation (RP

remote monitoring station) on October 1, 2007, the team noted a large amount of

transient combustibles (rolls of large plastic bags, large rolls of paper, etc)

being stored in the area. The team requested the transient combustible control

permit (TCCP) for the stored materials. Upon further inspection, the team

determined that the licensee did not evaluate the mass quantities of material that

were being stored in the area per Procedure 14DP-0FP33, "Control of Transient

Combustibles," Revision 15, and that the licensee did not have a TCCP for the

additional combustibles. The team noted that the excess combustible material

should have been identified during fire watch walkdowns when verifying the

requirements for the RP remote monitoring station TCCP were being met.

During a walkdown of the Unit 3 containment building on October 2, 2007, the

team noted a large amount of transient combustibles being stored in the area.

- 83 - Enclosure

The team requested the TCCP for the stored materials. During interviews with

the program owners, the team was informed that containment was exempt from

the TCCP program. The team was provided a licensee evaluation that stated

issuing permits during the refueling outage for the containment would, Create a

bottleneck and impact work scheduling. Upon further review of the TCCP

program, the team identified that licensee procedures did not exempt

containment from the TCCP program. Specifically, Procedure 14DP-0FP33,

"Control of Transient Combustibles," Revision 15, stated that all levels and all

areas of the containment building required permits for transient materials,

including treated wood scaffolding.

Analysis. The failure to control transient combustibles in accordance with the FP

program requirements was a performance deficiency. The finding is more than

minor because storing unanalyzed combustibles results in the potential to exceed

combustible limits and may increase in the likelihood of an initiating event.

Additionally, this finding represented degradation in the FP defense-in-depth

strategy in that the licensee did not recognize that bulk materials were being

stored in the area in support of the outage. Without proper evaluation, this

storage increased the likelihood of a transient fire. Using the Manual Chapter

0609, "Significance Determination Process," Appendix F, "Fire Protection

Significance Determination Process," this issue affected the Fire Prevention and

Administrative Controls Category. The stored materials required a permit per the

licensees procedure; however, the area was attended, fire detection and

suppression was available, and the amounts did not exceed the loading

calculation to the point of changing loading classification. Therefore, this finding

is considered of low degradation and is determined to have very low safety

significance (Green). The cause of this finding had crosscutting aspects

associated with work practices of the human performance area in that the

licensee failed to communicate human error prevention techniques such that

work activities were performed safely (H.4.(a)). The cause of this finding had

crosscutting aspects associated with work practices of the human performance

area in that the licensee did not effectively communicate expectations regarding

procedural compliance (H.4(b)). The cause of this finding was also related to the

safety culture component of accountability in that FP personnel failed to

demonstrate a proper safety focus and reinforce safety principles among their

peers (O.1.(c)).

Enforcement. Technical Specification 5.4.1.d, states, in part, that written

procedures shall be established, implemented, and maintained for FP program

implementation. Procedure 14DP-0FP33, "Control of Transient Combustibles,"

Revision 15, stated in part that transient combustibles being stored in the

Auxiliary Building and Containment Building in support of maintenance (outage)

activities are required to have a permit. Contrary to the above, between

August 23, 2007, and October 5, 2007, the licensee failed to have a proper

permit for all of the stored materials in the RP remote monitoring station.

Specifically, Fire Area 37A had transient combustibles stored with no associated

permit. Additionally, between September 29, 2007, and October 10, 2007, the

licensee failed to have a proper permit for all of the stored transient materials in

the containment building. Specifically, Fire Areas 63, 66, and 67 had transient

combustibles stored with no associated permit. Because this finding was of very

low safety significance and was entered into the CAP as PVARs 3071785,

- 84 - Enclosure

3072224, and 3072260, this violation was treated as a NCV, consistent with

section VI.A of the NRC Enforcement Policy: NCV 05000530/2007012-08, "Two

Examples of a Failure to Maintain Control of Transient Combustibles."

b.2 Failure to Install Emergency Lighting in Containment

Introduction. The team identified a Green finding for the failure of maintenance

personnel to install emergency lighting in containment in support of the Unit 3

refueling outage per repetitive maintenance WO 2935399 and work instruction

WSL 24436. As a result, work began in the Unit 3 containment with no

emergency lighting installed and no egress contingency plan for a loss of

containment lighting.

Description. During a walkdown of the Unit 3 containment on October 2, 2007,

the team identified that emergency lighting units did not have the batteries

installed. Upon further research, the team found the licensee removed

emergency lighting batteries in containment while at power to preserve the

availability and reliability of the batteries. The batteries were to be reinstalled for

outage support; however, the licensees work instructions did not prescribe when

the batteries needed to be re-installed (prior to commencing work). As a result of

the inadequate procedural guidance, work commenced in the Unit 3 containment

building on September 29, 2007, without having completed the emergency

lighting battery installation. Additionally, the licensee did not have a contingency

plan for personnel in the event normal power to containment lighting was lost.

Analysis. The performance deficiency associated with this finding was the failure

of maintenance personnel to have an adequate procedure for installing

emergency lighting in containment and not including appropriate acceptance

criteria for determining that the activity had been satisfactorily accomplished.

This finding is considered more than minor because it is associated with the

Mitigating Systems Cornerstone attribute of procedural quality and if left

uncorrected, a failure to install emergency lighting could hamper emergency

response activities in the containment or complicate emergency egress from the

containment. Using the IMC 0609, "Significance Determination Process,"

Appendix M, Significance Determination Process Using Qualitative Criteria, the

finding is determined to have very low safety significance because emergency

lighting was necessary for personnel safety and personnel were expected to

carry flashlights when responding to events. The cause of the finding has

crosscutting aspects associated with work control of the human performance

area in that maintenance personnel failed to properly plan the emergency lighting

installation work by incorporating contingencies in case the work was not

completed in the appropriate timeframe (H.3.(a)). The cause of this finding was

also related to the safety culture component of accountability in that management

personnel failed to reinforce safety standards and display behavior that reflected

safety as an overriding priority (O.1.(b)).

Enforcement. No violation of regulatory requirements occurred. The team

determined that the finding did not represent a noncompliance, because the

failure to install the emergency lighting or adequately evaluate the condition

occurred on a non-safety-related system. The finding was of very low safety

significance and the issue was entered into the CAP under PVAR 3070783.

- 85 - Enclosure

FIN: 05000530/2007012-09, Failure to Install Emergency Lighting in

Containment Prior to Work Commencement.

b.3 Incorrect Installation of Temporary Shielding

Introduction. The team identified a Green NCV of TS 5.4.1a for the failure of RP

personnel to follow procedures for installing temporary shielding in the 87 foot

auxiliary building west penetration room.

Description. During a walkdown of the auxiliary building 87 foot elevation on

October 3, 2007, the team observed temporary shielding Package A-87-10

installed near Train A LPSI piping. Upon further inspection, it was noted that the

shielding was in direct contact and installed across the Train A LPSI instrument

sensing line. The shielding had been erected per WO 2955341on

September 5, 2007, to reduce dose during the Unit 3 refueling outage.

Procedure 75RP-9RP25, Temporary Shielding, Revision 9, stated, in part, that

if shielding is to be installed on piping systems which are declared operable, a

piping stress analysis must be performed and cited in Specification 13-CN-0211,

Installation Specification for Temporary Shielding for the Palo Verde Nuclear

Generation Station Units 1, 2, & 3, Revision 9. Temporary shielding Evaluation

07-017 and installation Specification 13-CN-0211 had evaluated the shielding

installation near large bore LPSI piping with no evaluations or operability

concerns noted. WO 2955341 stated that the shielding was installed per

specification requirements. However, neither the temporary shielding evaluation,

the temporary shielding package, nor the installation specification addressed or

evaluated the shielding installed in contact with and over the LPSI instrument

sensing line.

After reviewing the procedures for temporary shielding installation, the team

contacted RP personnel and questioned the seismic qualification of the LPSI

pressure instrument sensing line. The licensee immediately rearranged the

shielding blankets to eliminate the contact with the instrument line. Engineering

concluded that the condition could have caused the line to fail during a

postulated design basis seismic event. No loss of safety function occurred since

the other LPSI train was not affected.

Analysis. The team determined that the licensees failure to correctly install

temporary shielding was a performance deficiency. This finding is greater than

minor because it is associated with the mitigating systems cornerstone attribute

of configuration control and affected the cornerstone objective to ensure

availability and capability of systems to respond to initiating events. Using the

IMC 0609, "Significance Determination Process," Phase 1 Worksheets, this

finding is determined to have very low safety significance (Green) because the

condition did not result in an actual loss of safety function and did not screen as

risk significant or contribute to external event initiated core damage sequences

since it did not involve a loss or degradation of equipment designed to mitigate a

seismic event. The cause of this finding had a crosscutting aspect associated

with work practices of the human performance area in that the licensee did not

effectively use human error prevention techniques such as self checking and

proper documentation of activities for the shielding installation (H.4.(a)).

- 86 - Enclosure

Enforcement. Technical Specification 5.4.1.a requires that written procedures be

established, implemented, and maintained covering the activities specified in

Appendix A, "Typical Procedures for Pressurized Water Reactors and Boiling

Water Reactors," of Regulatory Guide 1.33, "Quality Assurance Program

Requirements (Operations)," dated February 1978. Regulatory Guide 1.33,

Appendix A, Section 9a, requires maintenance that can affect safety-related

equipment be properly preplanned and performed in accordance with written

instructions appropriate to the circumstances. Procedure 75RP-9RP25,

Temporary Shielding, Revision 9, stated in part, that if shielding is to be

installed on piping systems which are declared operable, a piping stress analysis

must be performed and cited in Specification 13-CN-0211, Installation

Specification for Temporary Shielding for the Palo Verde Nuclear Generation

Station Units 1, 2, & 3. Contrary to this, between September 5, 2007, and

October 3, 2007, the licensee installed temporary shielding in contact with the

Train A LPSI instrument sensing line, and a piping stress analysis was not

performed. Because the finding was of very low safety significance and was

entered into the CAP as PVARs 3071468 and 3072224, this violation was treated

as an NCV, consistent with Section VI.A of the Enforcement Policy: NCV

05000530/2007012-10, "Failure to Follow Procedures for Temporary Shielding

Installation."

b.4 Observations and Minor Violations Involving Selected System Walkdown

b.4.1 Inadequate Seismic Scaffolding Procedures

Technical Specification 5.4.1.a requires that written procedures be

established, implemented, and maintained covering the activities

specified in Appendix A, "Typical Procedures for Pressurized Water

Reactors and Boiling Water Reactors" of Regulatory Guide 1.33, "Quality

Assurance Program Requirements (Operations)," dated February 1978.

Regulatory Guide 1.33, Appendix A, Section 9a, requires maintenance

that can affect safety-related equipment be properly preplanned and

performed in accordance with written instructions appropriate to the

circumstances. Contrary to this, as of October 8, 2007, the licensee did

not have adequate procedures or written instructions for maintenance that

affects safety related equipment. Specifically, Procedure 30DP-9WP11,

"Scaffolding Instructions," Revision 18, did not specify clearance

requirements for scaffolding installed near risk important non-safety

components that have a potential to impact safety related equipment.

Scaffolding was erected with an approximately one half inch clearance

between the CS pump room Train A flooding level switch. A failure of the

level switch could impact the operability of the CS system during a room

flooding event. The finding is determined to be minor because the

inadequate procedure did not have any actual safety significance. The

finding was of very low safety significance and was entered into the CAP

as PVARs 3073777 and 3071468. This performance deficiency is being

documented because of the insights associated with inadequate

procedures and recurring scaffolding concerns.

- 87 - Enclosure

5.6.3 Work Control Process

The team identified several weaknesses involving the licensees work control process,

including the following areas: adequate risk management of maintenance activities,

effective control of main control room deficiencies, prioritization of work with consideration

to environmental qualification, adherence to and effectiveness of controls for transient

combustibles and hot work, and thoroughness of pre-job briefings. Specifically:

  • The team observed several control room and work control activities to verify the

licensees controls for independent verification were adequate, including the EDG

standby readiness testing and an EW system tagout. No significant discrepancies

were observed during these activities. The team did note an event on

October 26, 2007, when an incorrect breaker was manipulated because the workers

were at the wrong unit. The individuals recognized the mistake and returned the

breaker to the as-found position; however, did not immediately notify the control room.

Once the control room became aware of the event, all site wide maintenance work was

stopped to reinforce independent verification practices and expectations.

  • The team identified several examples of inadequate risk management regarding

shutdown activities and switchyard activities. The team identified a lack of effective

communication between the switchyard owners, Salt River Project, and the licensee.

Maintenance activities in the switchyard, which could increase the risk of an initiating

event, were not thoroughly scheduled and integrated with on-site work activities. In

response to the team's findings, the licensee implemented immediate and long term

corrective actions to address risk management of switchyard maintenance activities.

The team also observed two minor examples of inadequate shutdown risk

assessments performed by the licensee which further demonstrated a weakness with

the licensees understanding of risk management.

  • The team noted there were several means of tracking control room deficiencies

including: control room deficiency log, jumpered alarm log, lit annunciator log, and

multiple operator workaround logs. The team identified that the pens were removed

on some strip charts required for post accident monitoring instrumentation. The charts

were tagged as being degraded and requiring maintenance; however, it was not

recognized by the control room operators that this rendered the instrumentation

inoperable.

  • The team inspected the prioritization of maintenance activities as it relates to EQ to

verify if equipment was being effectively maintained and not subject to environmental

degradation. The team identified an inability of the licensee to maintain the cable

vaults void of water and the use of unqualified tape in containment.

  • There were several incidents during the Unit 3 refueling outage involving hot work.

The licensee conducted two stand-downs in response to multiple small fires caused by

hot work activities. None of the fires were significant enough to warrant an emergency

declaration; however, the incidents supported the team's assessment that there

appeared to be lack of effective control and communication of expectations regarding

administrative controls for hot work and the control of transient combustibles. The

licensee did not consistently adhere to the procedures in place for controlling and

evaluating temporary and long term storage of transient combustibles throughout the

- 88 - Enclosure

plant. Ownership and accountability responsibilities for the control of transient

materials was fragmented between FP engineers, operations, and the site fire

department.

a. Inspection Scope

The team conducted a review of the backlog of corrective and preventive maintenance

activities to determine if the work control process used risk-insights during planning

and scheduling of maintenance and surveillance testing activities and the control of

emergent work. The team conducted interviews of licensee personnel, reviewed work

packages, and work control and maintenance procedures in order to assess the

adequacy of the licensee's efforts to integrate maintenance to minimize equipment

unavailability, establish effective communication and coordination, and address plant

performance deficiencies. The team reviewed the licensees policies to assess if the

licensee adequately considered the need for planned contingencies, compensatory

actions, and abort criteria when scheduling and executing work. The team reviewed

the performance history for selected systems and components and compared it to the

design basis to verify the licensee made conservative assumptions when scheduling

and performing work. The team also reviewed the following: long-term (typically

greater than six months) tagouts, caution and danger tags, disabled control room

annunciators and instruments, control room deficiencies, operator work-arounds and

other equipment deficiency tracking systems, to assess the significance of these

conditions.

b. Observations and Findings

b.1 Failure to Adequately Manage Risk for Switchyard Activities

Introduction. The team identified a Green NCV of 10 CFR 50.65(a)(4) for the

failure to adequately assess the increase in risk and effectively implement risk

mitigation actions for maintenance activities in the switchyard (SWYD).

Description. On October 11, 2007, the team observed several personnel and

pieces of equipment moving about the switchyard and noticed postings that

stated, in part, to contact the Unit 1 shift manager (SM) for entry into the SWYD.

While the activities appeared to be positioning of materials and equipment, the

team was unable to determine if any work was being conducted. The team

contacted the Unit 1 SM who stated that he was not aware of work in the SWYD

and that no one had contacted him for entry into the SWYD. The team then

contacted the SWYD coordinator and was informed that work on PL-942 and

PL-928 525kV breakers was being performed but he had failed to inform the Unit

1 SM. The team reviewed the risk assessment for the SWYD work and noted it

was revised to include the breaker work being performed. During discussions

with the licensees risk analyst and SWYD coordinator about the control and

modeling of work in the SWYD, it was noted that the risk model only accounts for

certain breakers and relays, and does not independently model equipment or

personnel traffic in the SWYD since that was considered in the modeling of the

work. It was also noted that routine relay planned maintenance (PM) and

equipment movement is not included on the schedule provided to the coordinator

and may not be included in the risk assessment. The SWYD coordinator stated

that equipment traffic was communicated to him and that the risk was managed

- 89 - Enclosure

by scheduling the work, controlling access to the SWYD via the Unit 1 SM, and

restricting equipment to designated lanes and areas in the SWYD.

On October 24, 2007, the team, accompanied by the SWYD coordinator and a

Transmission/Generation Operations (TGO) SWYD foreman, performed a

walkdown of the SWYD to observe breaker work. The team noticed multiple

trucks, pieces of equipment, and personnel moving around the SWYD that were

not involved with the breaker work. The team asked the TGO SWYD foreman

about the additional traffic, he stated that this was considered normal and that his

crew of 3-10 personnel works almost every day in the SWYD performing

maintenance. Procedure 40DP-9OP34, Switchyard Administrative Control,

Revision 16, Step 2.7 stated, in part, that all personnel entering the switchyard

shall notify the Unit 1 Shift Manager. When asked about contacting the Unit 1

SM prior to entering the SWYD, he stated that his supervisor coordinated any

work with the SWYD coordinator but was not aware of the need to contact the

Unit 1 SM for access to the SWYD. During the walkdown, the team also

observed a truck outside the designated traffic lanes and noted multiple tire

tracks and a man lift inside a restricted access area were no work was being

performed. The SWYD coordinator stated he was unaware of all of the

equipment traffic occurring in the SWYD.

The team noted that the SWYD was not being protected by controlling access

and movement as required and that the risk modeling did not include all work

being performed. The Unit 1 SM and SWYD coordinator were unaware of the

movement of multiple vehicles and pieces of equipment in or near restricted

areas nor is this included in the risk model. Additionally, routine relay PMs and

maintenance was not included on the schedule provided to the SWYD

coordinator for risk review.

The team noted that OE existed related to switchyard work, including vehicles in

the switchyard, potential impact of switchyard work on offsite power, and taking

into consideration all switchyard work when calculating risk in accordance with

10 CFR 50.65. Based on the amount of OE and the importance of offsite power

in relation to risk, the licensee should have incorporated more controls to

manage work in the switchyard and factored that work into the risk assessment

process. In particular:

Coolant System Heat-up, described an event that occurred when a truck

backed into a support column for a feeder line in the switchyard resulting in a

loss of power to the vital buses.

Plant Risk and the Operability of Offsite Power, describes calculating risk

associated with 10 CFR 50.65(a)(4), including the impact of switchyard

maintenance on the operability of offsite power sources.

  • Temporary Instructions 2515/156, Offsite Power System Operational

Readiness, and 2515/163, Operational Readiness of Offsite Power, both

described the potential impact of switchyard maintenance on offsite power

sources.

- 90 - Enclosure

Operability of Offsite Power, describes the need for effective coordination of

switchyard maintenance and the need to assess risk for switchyard activities.

Analysis. The failure to integrate all SWYD work into the risk assessment and

implement effective risk management actions to assess and manage the risk was

a performance deficiency. This finding is greater than minor because the

licensees risk assessment failed to consider maintenance activities that could

increase the likelihood of initiating events such as work in the SWYD and failed

to effectively manage compensatory measures. Inspection Manual Chapter

0609, Appendix K, Maintenance Risk Assessment and Risk Management

Significance Determination Process, was used to assess the significance. The

senior risk analyst made the following assumptions:

1. In accordance with IMC 0609, Appendix K, the significance of this finding was

numerically equal to the incremental core damage probability deficit (ICDPD),

or the difference between the ICCDP calculated by the licensee and the

ICCDP that would have been calculated had the SWYD work been properly

incorporated within the on-line risk monitor.

2. The exposure period for the finding was one year. The finding included both

at-power and shutdown conditions.

3. Three initiating events were postulated to be caused by human error

associated with general work in the SWYD: loss of offsite power (LOOP),

partial loss of offsite power, and turbine trip/reactor trip.

4. There was insufficient data at Palo Verde to estimate the frequency of

switchyard-centered LOOPs (none have occurred in the 20 years of

operation). Therefore, industry data were used to estimate this value.

5. The frequency of LOOP events caused by SWYD human error events was

derived from NUREG/CR6890, Reevaluation of Station Blackout Risk at

Nuclear Power Stations, Analysis of Loss of Offsite Power Events:

1986-2004.

A bounding assumption was made that the baseline LOOP and transient initiating

event frequencies in the licensees risk monitor do not include consideration of

data related to human error in the SWYD. Although this was not the actual

situation, it simplified the analysis and produces a result that can be used to

define an upper bound to the significance (which could be refined later if

necessary). Therefore, based on this assumption, the baseline was zero and the

risk deficit was equal to the expected rate of events caused by SWYD work

multiplied by the conditional core damage probability (CCDP) of the event as

quantified in the Palo Verde SPAR model, Revision 3.31. The CCDP of a LOOP

event was determined to be 4.332E-5. Using industry data, LOOP event

frequencies caused by SWYD work were determined to be 0.0016/year for at-

power and 0.0042/year for shutdown conditions during a typical calendar year.

The at-power frequency was doubled to account for an increased presence of

workers in the Palo Verde SWYD. The average CCDP for a shutdown LOOP

was determined by doubling the at-power CCDP. The resulting delta-CDF was

- 91 - Enclosure

5.0E-7/year. The risk effect of partial LOOPs and transients caused by SWYD

work was determined to be insignificant for this analysis. Neither external events

nor large early release contributed to the risk of the finding. Based on the

magnitude of the calculated risk being less than 1E-6/year, this finding is

determined to have very low safety significance (Green). The cause of this

finding had crosscutting aspects associated with work control of the human

performance area in that the licensee failed to plan work activities incorporating

risk insights (H.3.(a)). The cause of this finding had crosscutting aspects

associated with work control of the human performance area in that the licensee

failed to appropriately communicate work activities (H.3.(b)).

Enforcement. 10 CFR Part 50.65(a)(4), states in part, that before performing

maintenance activities (including but not limited to surveillance, post-

maintenance testing, and corrective and preventive maintenance), the licensee

shall assess and manage the increase in risk that may result from the proposed

maintenance activities. Contrary to this, between October 11 and 24, 2007, the

licensee failed to adequately assess and manage the increase in risk.

Specifically, the licensee failed to include all work being performed in the risk

assessment and fully implement risk management actions to protect the SWYD.

Because the finding was of very low safety significance and was entered into the

CAP as PVAR 3078392, this violation was treated as an NCV, consistent with

Section VI.A of the Enforcement Policy: NCV 05000528, 05000529,05000530/2007012-11, Inadequate Implementation of Risk Management

Actions and Risk Assessment for the Switchyard.

b.2 Observations and Minor Violations Involving Work Control Processes

b.2.1 Failure to Properly Document Temporary Modifications

The team identified a minor violation of Technical Specification 5.4.1.a for

the failure of operations and maintenance personnel to follow Procedure

81DP-0DC17, "Temporary Modification Control," Revision 20. Procedure

81DP-0DC17 required, in part, that: 1) upon completion of the

installation, a copy of the temporary modification procedure/work order

pages shall be given to the control room, and 2) upon receiving a copy of

the procedure/work order, the SM, control room supervisor, or authorized

designee shall log the temporary modification into a temporary

modification book or computer spread sheet. Contrary to this, on

October 15, 2007, the team identified that temporary modifications

installed to support the Class 1E Bus E-PBA-S03 and Non Class 1E Bus

NAN-S02 outages on Unit 3, were not accounted for in the temporary

modification book and the procedures/work orders were not being given

to the control room in accordance with procedural guidance. This finding

was entered into the licensee's CAP as PVAR 3076979. Using IMC

0612, Appendix E, "Examples of Minor Issues," this finding was

determined to be minor because this was an insignificant procedural error

and there were no safety consequences. This performance deficiency is

being documented because of insights associated with procedure

compliance and conduct of operations.

- 92 - Enclosure

b.2.2 Inadequate Shutdown Risk Assessments

The team identified two minor examples of improperly performed

shutdown risk assessments for Units 2 and 3 performed by the shift

technical advisors (STAs).

  • At 6:58 p.m. on October 4, 2007, the site entered a severe thunder

storm warning. The STA was called back to the Unit 3 control room to

re-evaluate the risk assessment due to this emergent condition. The

STA used the control room posted risk assessment as a tool to

determine if the risk to the current plant conditions had changed due

to the severe weather. The STA incorrectly determined that part two

of the shutdown risk assessment identified severe weather as a high

risk to electrical resources and inventory control. The STA then

marked the two identified areas as increased risk to yellow from

green. When questioned by the team as to why inventory control risk

had increased as well as electrical resources, the STA acknowledged

he had made an error and inventory control should not have been

increased to yellow risk. The STA corrected the error for inventory

control and downgraded the risk to green. The licensee generated

PVAR 3072733 to document this issue.

  • The Unit 2 SM declared the Train A EDG available at 5:58 a.m. on

October 11, 2007. The team noted that the shutdown risk

assessment did not include the availability of the Train A EDG in the

shutdown risk assessment. The shutdown risk assessment was

evaluated as the EDG being unavailable placing the unit in the

incorrect yellow risk category for electrical resources. When the team

questioned the STA about the Train A EDG status; the STA was not

aware the SM had declared the EDG available. Procedure

70DP-0RA01, Shutdown Risk Assessment, Section 3.1 required the

STA to provide actual plant conditions for determining the plant

shutdown risk profile. Contrary to this, the STA failed to correctly

evaluate risk for the electrical resources and placed the Unit in a

yellow risk status when it should have been in a green risk status. A

contributing cause to this incorrect shutdown risk assessment was the

lack of timely information being made available to all control room

staff members in reference to the status of the Train A EDG.

Using IMC 0612, Appendix E, "Examples of Minor Issues," these

examples were determined to be minor because they were an

insignificant procedural error and there were no safety consequences.

The performance deficiencies are being documented because of insights

associated with control room behaviors and maintenance rule

implementation.

- 93 - Enclosure

5.6.4 Control of Fission Barriers

The team determined that the programs outlining configuration control of components and

equipment related to fission product barriers were adequate. During a walkdown of

containment, the team noted discrepancies with rigging of the personnel air lock (PAL)

door that had the potential to impact the functionality of the PAL door.

a. Inspection Scope

The team observed a selected portion of the containment isolation lineup to

independently verify whether valves, dampers, and airlock doors were being properly

controlled in accordance with the licensing and design bases. The team reviewed

plant drawings and system procedures to verify that selected components were in their

required positions. The team conducted interviews and reviewed the licensees

policies to assess whether the programs and controls (tracking systems) in place for

maintaining knowledge of the configuration of the fission product barriers including:

containment leakage monitoring and tracking, containment isolation device operability

(valves, blank flanges), and reactor coolant leak-rate calculation and monitoring were

adequate. The team also observed selected containment isolation tests to

independently verify whether the valves were being properly controlled in accordance

with 10 CFR Part 50, Appendix J, "Primary Reactor Containment Leakage Testing for

Water-Cooled Power Reactors," and local leak rate testing programs.

b. Observation and Findings

b.1 Incorrect Rigging for Personnel Air Lock Door

Introduction. The team identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion V, "Instructions, Procedures, and Drawings," for the failure of

maintenance personnel to follow procedures to rig the Unit 3 100 foot elevation

inner PAL door. Specifically, the suspended rigging was completed with the

inappropriate placement of the wire rope slings over two of the locking pins

resulting in an unanalyzed force being applied to the doors operating

mechanism.

Description. On October 2, 2007, during a walk down of the Unit 3 containment,

an inappropriate rigging configuration of the Unit 3 100 foot elevation inner PAL

door was identified. The team questioned the Bechtel rigging engineer on the

placement of the wire rope slings over the locking pins of the door. The Bechtel

rigging engineer explained the tension forces developed for the basket rigging

configuration of the door, but did not provide any additional supporting

information to address the teams questions. On October 2, 2007, Bechtel

generated NCR 25030-U3-035 to document that the rigging configuration was

not completed in accordance with Bechtel Drawing U3-FSK-C-022. Specifically,

the shackles shown on drawing Section D-D, Item 9, were installed inverted and

the slings shown on drawing Section D-D, Item 11, were installed over the

existing door closure pin instead of behind the pin. The licensee generated

PVAR 3070843 to document that the PAL door rigging installation was in error.

The teams review of Procedure VTD-T966-0001,Section XIII, Maintenance, on

lubrication, identified that the door latch pin guides each have bronze bushings.

- 94 - Enclosure

The bronze bushing in the door latch pin guide was not a fixed support. The

identification of a bushing that was not designed for vertical loading invalidated

the Bechtel engineering evaluation bounding assumption that the configuration

was in cantilever loading. The licensee generated PVAR 3086057 to document

that the PVAR 3070843 and NCR 25030-U3-035 responses were not adequate,

and that there was potential bushing damage.

Analysis. The performance deficiency associated with this finding was the failure

of maintenance personnel to rig the Unit 3 100 foot elevation inner PAL door in

accordance with WO 2688885, and the subsequent failure to adequately

evaluate any potential impacts from the unanalyzed rigging configuration. The

finding is greater than minor because it would become a more significant safety

concern if left uncorrected in that the applied suspended force on the bronze

bushing and the doors operating mechanism, which were not designed for

vertical loading, could degrade the PAL door sealing capability. This finding

could not be evaluated by the significance determination process because

IMC 0609, "Significance Determination Process," Appendix A, "Determining the

Significance of Reactor Inspection Findings for At-Power Situations," and

Appendix G, "Shutdown Operations Significance Determination Process," did not

apply to the PAL door for the plant conditions that existed during the event. This

finding affects the barrier integrity cornerstone and is determined to have very

low safety significance (Green) by NRC management review using the IMC 0609,

"Significance Determination Process," Appendix M, "Significance Determination

Process Using Qualitative Criteria," because it is a deficiency that did not result in

the actual breach of the containment barrier. The cause of this finding had

crosscutting aspects associated with work practices of the human performance

area in that maintenance personnel failed to provide adequate oversight of work

activities, including contractors, such that nuclear safety was supported (H.4.(c)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, "Instructions,

Procedures and Drawings," requires, in part, that activities affecting quality shall

be accomplished in accordance with prescribed instructions, procedures, and

drawings. Contrary to the above, Bechtel construction workers failed to rig the

Unit 3 100 foot elevation inner personnel air lock door per Bechtel Drawing

U3-FSK-C-022 and Work Order 2688885. Specifically, the suspended rigging

was completed with the inappropriate placement of the wire rope slings over two

of the locking pins resulting in an unanalyzed force being applied to the doors

operating mechanism. The slings were required to be placed under the locking

pins, not over. Because this violation was of very low safety significance and

was entered into the corrective action program as PVAR 3086057, the issue was

treated as a NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

NCV 05000530/2007012-12, Incorrect Rigging for Personnel Air Lock Door.

- 95 - Enclosure

5.6.5 Review of Individual Plant Examination

a. Inspection Scope

The inspection team reviewed the results of the plant specific Individual Plant

Examination relative to selected systems to determine if the Individual Plant

Examination is being maintained to reflect actual system conditions regarding system

capability and reliability.

b. Observations and Findings

No findings or observations were identified.

5.6.6 Human Performance

a. Inspection Scope

The team observed several maintenance related work activities to determine if Palo

Verde personnel effectively identified, evaluated, and corrected deficiencies involving

human performance. The team observed pre-job briefings, clearance order activities,

and work performance.

b. Findings and Observations

b.1 Observations and Minor Violations Involving Human Performance

b.1.1 Inadequate Procedure for Adjustment of Polar Crane Limit Switch

Technical Specification 5.4.1.a, requires, in part, that written procedures

be established, implemented, and maintained covering the activities

specified in Appendix A, "Typical Procedures for Pressurized Water

Reactors and Boiling Water Reactors," of Regulatory Guide 1.33, "Quality

Assurance Program Requirements (Operations)," dated February 1978.

Regulatory Guide 1.33, Appendix A, Section 9a, requires maintenance

that can affect safety-related equipment be properly preplanned and

performed in accordance with written instructions, documented

instructions and drawings appropriate to the circumstances. Contrary to

this, on October 9, 2007, the licensee performed maintenance without the

appropriate instructions and drawings resulting in a failure to retain quality

related documents and an incorrect evaluation of maintenance results.

Specifically, on October 10, 2007, the team identified that WO 3068693

did not contain appropriate direction for the setting of the 18 foot

maximum limit switch position for the Unit 3 polar crane main hoist

resulting in the electrical technicians documenting a height of 18 foot

0.375 inches when the actual height was 17 foot 6.375 inches. Using

IMC 0612, Appendix E, "Examples of Minor Issues," this finding was

determined to be minor because this was an insignificant procedural error

and there were no safety consequences. This finding was of very low

safety significance and was entered into the CAP as PVARs 3073911,

3074132 and 3086770. This performance deficiency is being

documented because of insights associated with inadequate procedures.

- 96 - Enclosure

5.6.7 Design

a. Inspection Scope

The team conducted general walkdowns of the containment and auxiliary buildings

and reviewed current component configuration, material condition, and equipment

status. The team also reviewed a sample of PVARs and CRDRs to assess the

effectiveness of corrective actions for deficiencies involving design activities. During

the walkdown and review the team noted discrepancies with pressurizer instrument

brackets and breaker modifications.

b. Observations and Findings

b.1 Failure to Maintain Configuration Control of Pressurizer Instrument Condensing

Pot Support Brackets

Introduction. The team identified a NCV of 10 CFR Part 50, Appendix B,

Criterion V, "Instructions, Procedures and Drawings," for the failure of

maintenance and engineering personnel to maintain proper configuration of the

support brackets for the pressurizer condensate pots in accordance with design

drawings. Specifically, on October 2, 2007, the team identified that the support

bracket U-bolts were not tight against the condensate pot piping, jam nuts were

not installed on the U-bolts, and jacking bolts were not in full contact with the

pressurizer vessel. The support brackets minimize lateral motion during a

seismic event.

Description. On October 11, 2007, the team conducted a containment walkdown

and observed that the support brackets for Valves 3PRCCV204 and

3PRCAV206, (pressurizer instrumentation root valves), had different

configurations. The licensee evaluated the brackets and determined that they

were not configured in accordance with design Drawings 13-J-ZZS-0080,

"Condensing Pot Support Details," and 13-J-ZZS-0081, "Condensing Pot Support

Details Pressurizer. The design drawings stated to field tighten the jacking bolt

stud to the pressurizer vessel hand tight, then add jam nuts; and the U-bolts to

be field tightened to obtain zero clearance around the pipe, then secured with a

jam nut. The bracket for Valve 3PRCCV204 had both U-bolts in full contact with

the pipe and 3 of the 4 jack bolt studs in contact with the pressurizer vessel. The

bracket for Valve 3PRCAV206 had 1 of 2 U-bolts in full contact with the pipe and

3 of the 4 jack bolt studs in contact with the pressurizer vessel. The licensee

entered the issue into the CAP as PVAR 3075704 and generated CRDR

3078397 and corrective maintenance WO 3076022 to resolve the deficiency.

On October 13, 2007, the licensee performed an OD which determined that

based on Calculation 13-MC-ZZ-0037, "Evaluation of Double U-Bolts Used as an

Anchor Restraint," only 1 of 2 U-bolts was required to maintain the design

function of the support; and Calculation 13-MC-RC-501, "RCS - Pressurizer

Surge Line," indicated that there was margin in the design to transfer the load to

the remaining jack bolt studs. Civil engineering determined that the incorrect

support configuration was acceptable without an adverse effect on the subject

pipe stresses and pipe support design. PVAR 3075704 identified a need to

- 97 - Enclosure

review the potential transportability to the other units and similar valves around

the pressurizer using this hanger design.

On October 30, 2007, the team visually inspected the support brackets for

Pressurizer Instrument Root Valves 3PRCDV205 and 3PRCBV207. The team

identified that 2 of 4 jack bolts on Valves 3PRCDV205 and 3PRCBV207 were not

in contact with the pressurizer vessel in accordance with design Drawings

13-J-ZZS-0080 and 13-J-ZZS-0081. The team noted that the original immediate

OD stated that there was a margin in the design to transfer the load to the

remaining 3 of 4 jack bolts still in contact with the pressurizer vessel, not when 2

of 4 jack bolts were not in contact. Civil engineering personnel evaluated the

effect of 2 jack bolts not being in contact with the pressurizer vessel and

determined that this condition was acceptable without an adverse affect to the

subject pipe stresses and pipe support design/evaluation.

On November 5, 2007, the licensee completed WO 3076022 to correct the

deficiencies identified in the support brackets associated with Valves

3PRCCV204, 3PRCDV205, 3PRCAV206, and 3PRCBV207, restoring the

support brackets in accordance with design drawings.

On November 6, 2007, the team visually inspected the support brackets for Valve

3PRCDV205 and 3PRCBV207 and identified that the bracket for Valve

3PRCDV205 was missing the jam nuts for the U-bolt farthest from the

pressurizer vessel. WO 3076022 indicated that the bracket U-bolts were

restored to the appropriate configuration and verified by civil engineering on

November 3, 2007. This issue was entered into the CAP as PVAR 3089364.

Analysis. The performance deficiency associated with this finding was the failure

of maintenance and engineering personnel to maintain proper configuration of

the support brackets on Valves 3PRCCV204, 3PRCDV205, 3PRCAV206, and

3PRCBV207 in accordance with the design drawings. This finding is greater

than minor because it is associated with the mitigating systems cornerstone

attribute of equipment performance and affected the cornerstone objective of

ensuring the availability and reliability of systems that respond to initiating events

to prevent undesirable consequences. Using the Manual Chapter 0609,

"Significance Determination Process," Phase 1 Worksheets, the finding is

determined to have very low safety significance (Green) since it only affected the

mitigating systems cornerstone and did not represent a loss of system safety

function. This finding had crosscutting aspects associated with the work

practices component of the human performance area because maintenance

personnel did not effectively use human error prevention techniques such as self

checking and proper documentation of activities for the installation of the support

bracket (H.4.(a)).

Enforcement. 10 CFR Part 50, Criterion V, "Instructions, Procedures and

Drawings," requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings and shall be accomplished in

accordance with these instructions, procedures, or drawings. Contrary to this,

since 2003, maintenance personnel did not ensure that Unit 3's support brackets

for Valves 3PRCCV204, 3PRCDV205, 3PRCAV206 and 3PRCBV207 were

configured and maintained in accordance with design drawings 13-J-ZZS-080

- 98 - Enclosure

and 13-J-ZZS-081. Specifically, the support bracket U-bolts were not tight

against the pipe, jam nuts were not installed on the U-bolts, and jacking bolts

were not in full contact with the pressurizer vessel. Because the finding was of

very low safety significance and was entered into the CAP as PVAR 3070805

and 3075704, this violation was treated as an NCV consistent with Section VI.A

of the Enforcement Policy: NCV 05000530/2007012-13, "Failure to Maintain

Configuration Control of Pressurizer Instrument Condensing Pot Support

Brackets."

b.2 Observations and Minor Violations Involving Design

b.2.1 Lack of Design Control for Breaker Modification

The team identified a minor finding for the failure of engineering

personnel to maintain design control measures for a temporary electrical

power modification per Procedure 01DP-0CC01, "Configuration Control,"

Revision 0. The team identified that a modification to install 70 amp

breakers in place of 60 amp breakers for temporary power used during

the outage to power instrument air and breathing air was placed on the

cancelled modifications list. After questioning engineering personnel, the

team determined the modification was cancelled before full

implementation. Plant drawings were updated for Unit 3 to reflect a 70

amp breaker installation. No changes to drawings were made for Units 1

and 2. During a plant walkdown, the team discovered all 60 amp

breakers were installed in each of the three units. The licensee was

unaware the modification was on the cancelled modifications list and

records indicated the modification had been completed in October 1993.

This finding was determined to be of very low safety significance because

the cancelled modification was for temporary power for instrument air and

breathing air and did not affect any safety related equipment. The

licensee placed the issue into their CAP as PVAR 3068451.

5.6.8 Problem Identification & Resolution

a. Inspection Scope

The team conducted general walkdowns of the containment and auxiliary buildings.

The team reviewed current component configuration, material condition, and

equipment status. The team also reviewed a sample of PVARs and CRDRs to assess

the effectiveness of corrective actions for degraded and unanalyzed conditions. The

team ensured that licensee evaluations of, and corrective actions to, significant

performance deficiencies have been sufficient to correct the deficiencies and prevent

recurrence.

b. Observations and Findings

b.1 Failure to Evaluate Adverse Condition for the Emergency Diesel Generators

Introduction. The team identified an eighth example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and

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Drawings," for the failure of operations and engineering personnel to adequately

evaluate degraded and unanalyzed conditions to support operability decision

making associated with EDG leaks.

Description. On October 2, 2007, the team conducted a walk down of the Unit 3

EDGs. During the walk down, several puddles of oil and surfaces wet with fluids

were identified. The observations were shared with the licensee who stated that

CRDR 2914886 initiated August 1, 2006, addressed the issue of lube oil leaks.

In response to the teams observations, maintenance personnel conducted

additional walk downs of the Unit 3 EDGs to make an assessment of any new

leaks.

The team reviewed the evaluation for CRDR 2914886 which stated that,

"Engineering, operations, and maintenance were aware of the several small oil

leaks but no program existed to quantify the leakage, nor had an evaluation of

the aggregate impact been performed." The team also reviewed CRAI 2979205

completed on June 6, 2007, that contained an engineering evaluation of the

maximum allowable leak rate for diesel lube oil of 0.5 gallons per hour (gph) was

acceptable. This was based on the lube oil burn rate of 1.0 gph such that a total

net lube oil consumption rate of 1.5 gph for seven days would not exceed the

Technical Specification bases. Additionally, the team reviewed engineering white

paper, "EDG Fluid Leakage and Operability," issued December 1, 2006. The

white paper listed several areas that were known to leak and gave some general

guidance on leak locations that would be of operational concern. The guidance

also listed several leak locations that were considered nuisance leaks and that

minor drips or weeps were not an operability concern. However, no definition of

what quantity of leakage would be considered minor or nuisance was provided.

The team reviewed the EDG fluid leakage database used to track leaks that are

being monitored. The database listed the source, WOs written, and internal

engineering severity rankings. Engineering classified all of the identified leaks as

minor with varying severity rankings. The licensee concluded that none of the

individual leaks would challenge the operability of the EDGs. Concerned that the

total aggregate of all of the leaks may exceed the allowed leak rate, the team

questioned operability based on the number and location of leaks.

Procedure 40DP-9OP26, "Operability Determination and Functional

Assessment," Revision 18, Step 3.1.1, stated, in part, that the OD process is

entered upon discovery of circumstances where operability of any SSCs

described in Technical Specifications is called into question upon discovery of a

degraded, nonconforming, or credible unanalyzed condition. However,

engineering personnel stated that only individual leaks greater than 0.5 gph

would be of concern for operability and performing a quantitative evaluation or

aggregating all the oil leaks would be too difficult. Engineering personnel

acknowledged that it would be beneficial to determine if the total oil leak rate

exceeded 0.5 gph.

The team performed walkdowns to determine if additional leaks existed. Based

on transportability of oil and poor EDG housekeeping, the team was unable to

determine if leaks, other than the leaks listed in the EDG fluid leakage database,

existed. While none of the individual leaks identified were determined to

challenge the operability of the EDGs (each was less than 0.5 gph), the team

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expressed their concern about the adequacy of the licensee's program to identify

individual leak rates and track the aggregate leak rates of the EDGs to ensure

that material condition issues would not create a challenge to operability.

Analysis. The performance deficiency associated with this finding was the failure

of operations and engineering personnel to adequately evaluate degraded and

unanalyzed conditions to support operability decision making. This finding is

greater than minor because it would become a more significant safety concern if

left uncorrected in that unanalyzed conditions could challenge the operability of

the EDGs. The finding affected the mitigating systems cornerstone. Using the

IMC 0609, "Significance Determination Process," Phase 1 Worksheets, the

finding is determined to have very low safety significance (Green) because the

finding did not result in the actual loss of safety function. The cause of this

finding had a crosscutting aspect associated with corrective action of the PI&R

area in that the licensee did not thoroughly evaluate previous EDG leaks such

that the resolutions addressed all conditions affecting operability (P.1.(c)).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, "Instructions,

Procedures and Drawings," requires that activities affecting quality shall be

prescribed by instructions, procedures, or drawings, and shall be accomplished

in accordance with those instructions, procedures, and drawings. The

assessment of operability of safety-related equipment needed to mitigate

accidents was an activity affecting quality, and was implemented by

Procedure 40DP-9OP26, "Operability Determination and Functional

Assessment," Revision 18. Procedure 40DP-9OP26, Step 3.1.1, stated, in part,

that the OD process is entered upon discovery of circumstances where

operability of any SSC described in the Technical Specifications is called into

question upon discovery of a degraded, nonconforming, or credible unanalyzed

condition. Contrary to the above, between August 1, 2006 and October 2, 2007,

operations and engineering personnel failed to enter the OD process upon

discovery of circumstances where the operability of a component was called into

question. Specifically, operations and engineering personnel failed to consider

all relevant information to perform an adequate OD when evaluating aggregate

EDG lube oil leaks. This was the eighth example of the NCV involving the failure

to implement the OD program. This example was of very low safety significance

and was entered into the licensees CAP as PVAR 3073559.

b.2 Failure to Identify and Correct a Non-Conforming Condition of Post-Accident

Monitoring Instrumentation Recorders

Introduction. The team identified a sixth example of the Green NCV of

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to

promptly correct a nonconforming condition that resulted in the inoperability of

several post accident monitoring (PAM) chart recorders.

Description. On October 10, 2007, the team conducted a Unit 3 control room

walk down and observed that several PAM chart recorders had significant ink

bleeding on the paper roll and that pens had been removed from several

instruments. Operations personnel stated that this was normal due to the design

of the pens, that the bleeding rendered the affected chart recorders unusable for

historical trending, and that if the bleeding was severe enough they would pull

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the pen from the chart recorder. The team questioned the operability of the PAM

chart recorders if the trend plots were unusable or if the pens were pulled. The

team was referred to CRDR 2629437, initiated on August 8, 2003, that indicated

there were no immediate operability concerns, even with the trend data not

usable, because the paper scales of the chart recorders were not calibrated.

During the review of CRDR 2629437, the team noted that the evaluation stated

that no cause could be determined and that the only corrective action was to

track the cause determination and solution implementation. No corrective

actions were identified for removing the pens from the PAM chart recorders.

Based on this cause evaluation, the licensee initiated CRAI 2637936 on

September 28, 2003, to replace the instruments.

On March 9, 2005, during procurement engineerings review of the issue, an

engineer questioned the original operability determination contained in CRDR

2629437, stating that UFSAR Table 1.8-1, "PVNGS Compliance with Regulatory

Guide 1.97 (Revision 2) Requirements," listed chart recorders that are required

for compliance with Regulatory Guide 1.97, Instrumentation for Light-Water-

Cooled Nuclear Power Plants to Assess Plant and Environs Conditions During

and Following an Accident, Revision 2. Regulatory Guide 1.97 states, in part,

where direct and immediate trend or transient information is essential for

operator information or action, recording should be continuously available on

dedicated recorders. CRAI 2790230 was issued to perform another operability

evaluation of the chart recorders. However, this action was not taken until

April 11, 2005, approximately 21 months after the initial concern and over a

month after procurement engineering questioned the original operability

evaluation. Again, this second operability evaluation determined that no

immediate operability concerns existed since there were no surveillance

requirements for the recorders and the Technical Specification basis did not

specifically address the recorder as part of a required PAM channel. The team

noted that both operability evaluations failed to address the UFSAR requirements

for compliance with Regulatory Guide 1.97.

On October 24, 2007, the team conducted additional walk downs of the Units 1

and 2 control rooms. The Unit 1 control room had several recorders with

moderate chart bleeding and two with pens removed. The team noted that the

Unit 2 control room had two recorders with moderate ink bleeding. The team

again questioned the licensee about PAM instrument operability based on the

UFSAR Table 1.8-1 listing of chart recorders that are required for compliance

with Regulatory Guide 1.97. Operations again provided the basis contained in

CRAI 2790230 for continued operability of the chart recorders.

On October 29, 2007, after additional discussions about operability with PVNGS

senior management, the licensee recognized that two chart recorders in the

Unit 1 control room had pens removed. Senior management immediately

directed operations personnel to install the pens and made operations aware of

the requirements to maintain pens in the recorders. During the Unit 2 walk down,

senior management discovered that operations personnel had minimized the ink

bleeding on the chart recorders by removing about half of the ink from the pens.

This interim corrective action was not shared with the other units or documented

in the CAP.

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On October 29, 2007, the licensee initiated PVAR 3086251. PVAR 3086251

indicated that the recorders were required for trending and recording. All the

recorders were verified to have pens installed and a night order was written to

alert operations personnel about this condition. The night order required

operations personnel to declare the PAM instrument channel inoperable if the

recording function was not available for any reason (including blotching or

bleeding).

The inspectors concluded that the licensee had failed to review the licensing

basis for the PAM chart recorders and failed to implement corrective actions to

maintain the functionality of the instruments. This condition involved multiple

safety and non-safety related recorders that were in a non-conforming condition

for an unspecified period with no controls or compensatory actions in place.

Analysis. The performance deficiency associated with this finding involved the

failure to identify an inadequate operability evaluation and the failure to promptly

correct a non-conforming condition that resulted in the inoperability of PAM chart

recorders. The finding is greater than minor because it would become a more

significant safety concern if left uncorrected in that safety-related equipment that

was not maintained in a qualified condition may not be available to perform its

safety function under certain accident conditions. The finding affected the

mitigating systems cornerstone. Using the IMC 0609, "Significance

Determination Process," Phase 1 Worksheets, the finding is determined to have

very low safety significance because it did not result in a complete loss of system

safety function. The cause of this finding had crosscutting aspects associated

with corrective actions of the PI&R area in that the licensee did not thoroughly

evaluate previous issues such that the resolutions addressed all conditions

affecting operability (P.1.(c)). The cause of the finding was also related to the

safety culture component of accountability in that management failed to reinforce

safety standards and display behavior that reflected safety as an overriding

priority (O.1.(b)).

Enforcement. 10 CFR Part 50, Criterion XVI, "Corrective Action," requires, in

part, that measures shall be established to assure that conditions adverse to

quality, such as failures, malfunctions, deficiencies, deviations, defective material

and equipment, and nonconformance, are promptly identified and corrected.

Contrary to this, from August 8, 2003, to October 29, 2007, operations personnel

did not promptly identify and correct conditions adverse to quality. Specifically,

licensee personnel unknowingly rendered chart recorders for PAM

instrumentation inoperable by removing the ink pens and failed to take prompt

corrective actions to restore operability of PAM instrument chart recorders. This

was the sixth example of the failure to implement the CAP. This example was of

very low safety significance and was entered into the CAP as CRDR 3088033.

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5.6.9 Equipment Performance

a. Inspection Scope

The team reviewed the operational performance of selected safety systems to verify

their capability of performing the intended safety functions. The team assessed the

effectiveness of corrective actions for deficiencies involving equipment performance,

including equipment designated for increased monitoring via implementation of the

Maintenance Rule. The team also ensured that the licensee has effectively

implemented programs for control and evaluation of surveillance testing, calibration,

and post-maintenance testing.

b. Observations and Findings

b.1 Failure to Establish Maintenance Rule Goals for the Safety Injection System

Introduction. The team identified a Green NCV of 10 CFR 50.65 for the failure of

engineering personnel to establish goals and monitor the performance of the

safety injection system. Specifically, as of March 22, 2007, engineering

personnel failed to establish goals to properly monitor system performance, or

provide a technical justification to demonstrate that monitoring under

10 CFR 50.65(a)(1) was not required for the safety injection system following the

system changing status from 10 CFR 50.65(a)(2) to 10 CFR 50.65(a)(1).

Description. On October 25, 2007, following the teams request

for 10 CFR 50.65(a)(1) action plans for several risk significant systems, it was

discovered that the licensee had reclassified the safety injection system from 10

CFR 50.65(a)(2) status to 10 CFR 50.65(a)(1) status because of unacceptable

unavailability. Specifically, the HPSI pumps had experienced unavailability

issues and sporadic reliability issues for the last three years. However,

engineering personnel did not establish goals to properly monitor system

performance, or provide a technical justification to demonstrate that monitoring

under 10 CFR 50.65(a)(1) was not required. As a result of the team's questions,

the licensee initiated actions to establish goals and monitoring for the safety

injection system. The team noted that this concern was not identified during the

licensees annual maintenance rule program assessment.

Analysis. The performance deficiency associated with this finding was the failure

of engineering personnel to properly establish goals and monitor system

performance; and provide technical justification for not establishing goals for the

safety injection system. This finding is greater than minor because it was

associated with the mitigating systems cornerstone attribute of equipment

performance and affected the cornerstone objective of ensuring the availability

and reliability of systems that respond to initiating events to prevent undesirable

consequences. Using the IMC 0609, "Significance Determination Process,"

Phase 1 Worksheets, the team concluded the finding is of very low safety

significance (Green) because there was no design deficiency, and the finding did

not represent an actual loss of a safety function. The cause of this finding had

crosscutting aspects associated with corrective action of PI&R area in that

engineering personnel failed to take appropriate actions to address safety issues

and adverse trends in a timely manner (P.1.(d)). The cause of this finding had

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crosscutting aspects associated with self assessments of the PI&R area in that

engineering personnel failed to perform self assessments that were

comprehensive, appropriately objective, and self-critical (P.3.(a)).

Enforcement. 10 CFR 50.65(a)(1) states, in part, that the performance or

condition of systems shall be monitored against established goals, to provide

reasonable assurance that the systems are capable of performing their intended

functions. 10 CFR 50.65(a)(2) requires, in part, that monitoring as specified in

paragraph 10 CFR 50.65(a)(1) is not required where it had been demonstrated

that the performance or condition of a system was being effectively controlled

through the performance of appropriate preventive maintenance such that the

system remained capable of performing its intended function. Contrary to the

above, Between March 22 and October 25, 2007, the licensee failed to establish

goals and monitor the performance of the safety injection system to provide

reasonable assurance that the system was capable of performing its intended

function. Specifically, the licensee determined that the performance of the safety

injection system was such that it was necessary to monitor system performance

against established goals under 10 CFR 50.65(a)(1), yet failed to establish goals

and/or monitor the performance of the system against such goals. Because this

finding is of very low safety significance and had been entered into the CAP as

PVARs 3074255 and 3076699, this violation is being treated as an NCV,

consistent with Section V1.A of the Enforcement Policy: NCV 05000528;

05000529;05000530/2007012-14, Failure to Implement Maintenance Rule

Requirements for the High Pressure Safety Injection System.

5.7 Emergency Preparedness and Response

The team had not originally planned an in-depth review of the Emergency Response

Strategic Performance Area. However, between October 1 and 12, 2007, the team

identified significant issues with the licensees ability to correctly classify an emergency

condition and/or determine a Protective Action Recommendation (PAR). Between

October 29 and November 2, 2007, emergency planning specialists from both NRC

Region IV and Headquarters were added to the team to conduct a more detailed

emergency response assessment. Further review by the team noted significant

knowledge gaps associated with emergency classifications and PARs, and a failure to

correct identified weaknesses. On October 28, 2007, in response to the problems

identified by the team, the licensee instituted corrective actions to augment the emergency

response organization (ERO) by assigning 6 managers, specially trained on EAL

classification, to the shift rotation until additional training could be provided to the

remaining ERO members. The team determined that this interim measure should be

effective in improving EAL implementation. Nevertheless, significant improvement in

emergency response program knowledge, and correction of emergency plan weaknesses

was warranted.

a. Inspection Scope

The team conducted a limited assessment of the ability of licensee personnel to

activate the ERO augmentation of on-shift personnel. The team assessed the

effectiveness of prior corrective actions involving ERO deficiencies. Although, no ERO

drills were conducted or reviewed during this evaluation, the team reviewed

emergency response facilities, planned on-shift emergency response, and augmented

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emergency response staffing. The team selected 10 members of the ERO and tested

their ability to implement EAL event classifications. Since the Emergency

Preparedness Cornerstone was not degraded, IP Attachment 95003.01, Emergency

Preparedness, was not conducted.

b. Observations and Findings

b.1 Failure to Correct a Risk Significant Planning Standard

Introduction: The team identified an apparent violation with the significance to be

determined for the licensees failure to correct an identified risk significant

planning standard weakness from May 2, 2007, through October 28, 2007. The

finding had a potential safety significance of White.

Description: 10 CFR Part 50, Appendix E.IV.F.2.g., requires, in part, that any

deficiencies identified as a result of training, exercises, or drills be corrected.

Between May 2 and October 28, 2007, the licensee failed to implement adequate

corrective actions for identified deficiencies which impacted a risk significant

planning standard associated with the ability to make EAL declarations.

Background:

For a steam generator tube rupture (SGTR), with a 200 gpm primary/secondary

leak, valid reactor vessel level monitoring system (RVLMS) level < 21 percent

plenum level, and the use of automatic depressurization valves (ADVs) with the

secondary plant stabilized, EPIP-99, EPIP Standard Appendices, Table 1,

Fission Product Barrier Reference (Modes 1-4), specified the following EAL

classification.

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FUEL CLAD RCS BARRIER CONTAINMENT

BARRIER BARRIER

POTENTIAL POTENTIAL LOSS LOSS

LOSS LOSS

Valid RVLMS SGTR > 44 SGTR >132 gpm Release of

currently or gpm with a prolonged contaminated

previously < 21 (EAL 1-7) release of secondary side to

percent plenum contaminated atmosphere (i.e., S/G

(EAL 1-2) secondary coolant safety or ADV) with

occurring from the S/G primary to

ruptured S/G to the secondary leakage >

environment (See Technical Specification

Limitations in allowable limits

Section 1) (EAL 1-14)

(EAL 1-7)

APPLY THE CRITERIA ABOVE TO THE CONDITIONS BELOW

UNUSUAL ALERT SITE AREA GENERAL

EVENT EMERGENCY EMERGENCY

Any loss OR Any loss OR Loss of both fuel Loss of any two

any potential any potential clad and RCS barriers

loss of loss of either Or And

containment fuel clad or Potential loss of Potential loss of a third

reactor coolant both fuel clad and barrier

system (RCS) RCS

Or

Potential loss of

either fuel clad or

RCS and loss of

any additional

barrier

EPIP-99, Section 1, Precautions and Limitations, Step 1.7, stated, Used in the

context of a steam generator tube rupture as stated in the Fission Product Barrier

EAL [1-7], a "prolonged release of contaminated secondary coolant"

encompasses a main steam line break, feedwater line break, stuck open steam

generator safety and/or atmospheric dump valve(s), and plant cooldown (i.e., to

Mode 5) while steaming the affected steam generator to atmosphere. The team

noted that for the associated EAL JPMs, the licensee was using the ADVs to

stabilize the secondary plant (a plant cooldown was not in progress). The correct

emergency classification was a Site Area Emergency based on the following

conditions: SGTR >44 gpm resulting in a potential loss of the RCS barrier;

RVLMS <21 percent resulting in a potential loss of the fuel clad barrier; and a

release of contaminated secondary side to atmosphere through the ADVs with

primary to secondary leakage exceeding Technical Specification limits resulting

in a loss of containment barrier.

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Training Requirement:

Licensed Operator Continuing Training (LOCT) Program Description,

Revision 31, required SROs responsible to fill ERO positions to maintain

emergency preparedness proficiency by receiving annual training to meet EP

training requirements as specified in Section 8.1.1.2, Specialized Training for

Key Emergency Organization Personnel, of EPIP-59, Emergency Planning

Training Program Description. EPIP 59 further defined the necessary training to

maintain emergency preparedness proficiency for onshift emergency

coordinators, which included all of the control room supervisors and SMs.

PVNGS Emergency Plan, Revision 36, Section 3.0 stated, in part, that, the

Emergency Plan was based upon NRC and Federal Emergency Management

Agency (FEMA) guidance as contained in NUREG-0654 (FEMA-REP-1), Criteria

for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1. NUREG-0654,

Section N, stated, in part, that, periodic drills will be conducted to develop and

maintain key skills, and deficiencies identified as a result of drills will be

corrected. NUREG-0654 further defined a drill as a supervised instruction period

aimed at testing, developing, and maintaining skills.

Operator Licensing Requalification Program EP Classification Failures:

As part of LOCT Cycle 3 (April 3 - May 4, 2007), the licensee included

JPM EP009-CR-002, "Direct the Emergency Response as the Emergency

Coordinator," as part of their training to maintain emergency preparedness

readiness. This JPM consisted of a SGTR event with the following conditions:

200 gpm primary/secondary leakage, valid RVLMS level < 21 percent plenum

level, and the use of automatic depressurization valves to control steam

generator pressure. The evaluation standard (expected trainee response), which

was incorrect for this event, was a General Emergency based on, Loss of any

two barriers AND Potential Loss of a third barrier. The incorrect classification

resulted from the misapplication of EPIP-99, Section 1, Precautions and

Limitations, Step 1.7. JPM EP009-CR-002 identified the EAL classification as a

General Emergency because of an incorrect assumption that under the

described conditions a prolonged release was occurring, when the definition of

prolonged release did not apply (see above description).

From April 4 through May 2, 2007, 10 SROs were given this JPM and were

asked to identify the EAL classification. Nine of 10 SROs classified a General

Emergency, while one classified a Site Area Emergency. On May 2, the SRO

who classified the event as a Site Area Emergency identified that the evaluation

standard was incorrect because under the presented conditions only one barrier

was lost (Containment, use of automatic depressurization valves) and two

potentially lost barriers (RVLMS level < 21 percent plenum, SGTR > 44 gpm).

Under these conditions the correct classification was a Site Area Emergency

(see above table). After discussing this with the emergency planning personnel,

the instructors determined that this event should have been classified as a Site

Area Emergency and the 9 SROs that classified the event as a General

Emergency were given immediate remedial training (per the Training

Supervisor). However, the licensee failed to enter the incorrect evaluation

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standard into either the CAP or the training deficiency program and no additional

training was given to the other ERO personnel responsible for classifying events.

The licensee did not remove JPM EP009-CR-002 from the training bank or make

any corrections to the JPM.

Initial Exam EP Classification Failures:

JPM SA-5 (identical to JPM-EP009-CR-002) was administered during an initial

license examination on July 27, 2007. The evaluation criteria incorrectly

specified the classification as a General Emergency. Two of the five SRO

candidates classified the event as a Site Area Emergency, while the other three

classified the event as a General Emergency. An evaluation of the JPM was

conducted that day by training personnel. An EPIP training instructor recognized

that the misclassification issue involved the same concern from the JPM that was

given in LOCT Cycle 3. On July 27, 2007, the licensee entered the

misclassification issue into the CAP as CRDR 3046233, Incorrect Interpretation

of Event Conditions During the Creation of and Administration of an NRC Exam

JPM, and conducted an apparent cause evaluation. The apparent cause

evaluation was completed on August 31, 2007. As of October 5, 2007, no

training had been conducted on what constituted a prolonged release and the

proper classification for SGTR events. The team noted that training on this

particular SGTR event was not scheduled to be completed until

November 30, 2007.

The licensee identified three apparent causes of the performance deficiency:

(1) a lack of knowledge/understanding on the specific conditions of EAL 1-7;

(2) insufficient use of the Limitations in Section 1 referenced in the EAL 1-7

description box in Table 1 of EPIP-99; and (3) insufficient use of the technical

bases in Appendix P of EPIP-99. The team determined these apparent causes

stemmed from inadequate training, in that SROs were given generalized initial

and continuing training on EALs and were not provided systematic training on the

entry conditions and basis for individual EALs to ensure their understanding of

entry conditions.

IP 95003 Emergency Plan (EP) Classification Failures:

As a result of the incorrect EAL classifications during the operator licensing initial

exam in July 2007, the team selected JPM EP009-CR-002 to test the ability of

ERO personnel to properly classify a SGTR event and to verify that the licensee

had taken actions to correct the knowledge deficiencies associated with the

SGTR EAL classification. The team was unaware of the additional failures

associated with this JPM during LOCT Cycle 3 training. The team administered

JPM EP009-CR-002, to one SRO. The JPM contained the exact same

conditions as described above: 200 gpm primary/secondary leak, valid RVLMS

level < 21 percent plenum level, and the use of ADVs to control steam generator

pressure. The SRO incorrectly classified the event as a General Emergency

verses a Site Area Emergency.

Due to this additional failure, the licensee implemented immediate corrective

actions to provide intensive training to six managers and assigned them to shift

rotations, beginning on October 28, 2007, to assist ERO personnel in making

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EAL declarations. These six managers were to remain on-shift until the licensee

completed their review of the other EALs and provided training to the remainder

of the applicable ERO positions. Between October 9 and November 16, 2007,

the licensee did provide specific training on EAL 1-7 to the applicable ERO

positions.

Analysis: The team determined that the failure to correct an identified risk

significant planning standard weakness was a performance deficiency. This

finding was more than minor because it was associated with the Emergency

Preparedness attribute of response organization performance and could affect

the cornerstone objective to implement adequate measures to protect the health

and safety of the public because of the licensees inability to properly classify an

emergency condition. This finding was evaluated using the Emergency

Preparedness SDP and was preliminarily determined to be of low to moderate

safety significance because it was a failure to comply with NRC requirements; it

was an issue associated with the requirements of Appendix E of 10 CFR Part 50;

it was not an issue with a risk significant planning standard as described in

Manual Chapter 0609, Appendix B, Section 2.0; and it was a functional failure of

the requirements of Appendix E IV.F.2.g because the licensee failed to correct a

weakness associated with Risk Significant Planning Standard

10 CFR 50.47(b)(4). The cause of this finding had crosscutting aspects

associated with corrective action of the PI&R area in that the licensee failed to

thoroughly evaluate problems such that resolutions ensured that the problems

were resolved (P.1.(c)). The cause of this finding was also related to the safety

culture component of accountability in that the licensee failed to demonstrate a

proper safety focus and reinforce safety principles (O.1.(c)).

Enforcement: 10 CFR 50.54(q) states in part, that, a licensee authorized to

possess and operate a nuclear power reactor shall follow and maintain in effect

emergency plans which meet the standards in §50.47(b) and the requirements in

10 CFR Part 50, Appendix E. 10 CFR Part 50, Appendix E, Section IV.F.2.g,

states, in part, that all training shall provide formal critiques in order to identify

deficient areas. Any deficiencies that are identified shall be corrected.

Contrary to the above, between May 2, 2007, and October 28, 2007, the licensee

failed to correct identified deficiencies pertaining to the ability to correctly

implement EALs for one Site Area Emergency classification associated with a

SGTR event. Specifically, the deficiency involved licensee personnel being

unable to consistently implement EAL 1-7 associated with a SGTR which

resulted in an over classification of a Site Area Emergency as a General

Emergency. The issue associated with EAL implementation was entered into the

licensees correction action program as PVAR 3083911. Pending determination

of the findings final safety significance, this finding was identified as Apparent

Violation (AV) 05000528, 05000529,0500030/2007012-15, Failure to Correct a

Risk Significant Planning Standard.

b.2 Inability to Implement Emergency Action Levels (EALs)

Introduction: The team identified a Green NCV for the failure to correctly

implement two EALs as required by 10 CFR 50.54(q) and 10 CFR 50.47(b)(4).

Specifically, between January 2006 and October 2007 the licensee was not able

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to implement one EAL at the Alert level and over-classified one Notification of

Unusual Event EAL at the Alert level.

Description: The team identified a performance deficiency related to the

licensees inability to ensure implementation of EALs associated with an

aircraft/airliner attack threat and remote shutdown panel area high radiation

levels.

Aircraft/Airliner Threat

In January 2006 the licensee added EAL 7-1 in response to NRC Bulletin 2005-002, dated July 18, 2005. The EAL was associated with an aircraft and

airliner attack threat. The EAL action was defined as follows:

  • EAL 7-1 required declaration of an Unusual Event when the NRC notified

PVNGS of an aircraft threat greater than 30 minutes away.

On October 4 and 5, 2007, the team administered one JPM associated with the

aircraft and airliner attack threat, EAL 7-1, to two licensee ECs. The first EC

classified the postulated conditions as an Alert, when the correct classification for

the JPM condition was a Notification of Unusual Event. Licensee management

informed the NRC staff that they would not evaluate the EC for the application of

EAL 7-1 when the JPM was administered to the second EC because they

recognized that they were unable to implement the EAL with existing procedures

and guidance available to the ECs. The team determined that the licensee would

be unable to properly classify this EAL during an actual threat because the

licensee failed to develop implementing procedures for classifying an

aircraft/airliner attack threat.

Procedure EPIP-99, EPIP Standard Appendices, Appendix P, Emergency

Action Level Technical Bases, Revision 15, stated in part, that an airliner was

based on the size of aircraft as defined in the site-specific procedure developed

for response to airborne threats. The team noted that EPIP-99, Revision 15, did

not define an airliner. In response to the teams observation, the licensee issued

EPIP-99, Appendix P, Revision 16, on October 11, 2007, to include the definition

of an airliner as a large aircraft with the potential for causing significant damage

to the plant. The licensee documented the aircraft/airliner EAL classification

findings in PVAR 3070849.

Remote Shutdown Panels

Procedure EPIP-99, EPIP Standard Appendices, Revision 15, EAL 3-12

required an Alert to be declared when radiation levels at the remote shutdown

panels exceeded 5000 mrem/hr as indicated on area radiation Monitor RU-18.

The purpose of this EAL was to identify conditions that could impede the

operation of systems required to establish and/or maintain cold shutdown plant

conditions. The team determined that area radiation Monitor RU-18 was located

inside the control room envelope, on the 140 foot elevation, while the remote

shutdown panels are located one level below, on the 100 foot elevation. The

team determined that area radiation monitors were not installed in the vicinity of

the remote shutdown panels and that area radiation Monitor RU-18 could not be

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monitored from and did not represent the radiological conditions at the remote

shutdown panels. Therefore, the licensee could not determine the radiation

levels at the remote shutdown panels with radiation Monitor RU-18 and could not

properly classify an Alert condition based on high radiation levels in the area. On

July 13, 1994, this EAL was modified to meet guidance contained within

NUMARC/NESP-007, Methodology for Development of Emergency Action

Levels, Revision 2, and at that time, EAL 3-12 was added to include radiation

readings at the remote shutdown panel. The licensee documented the inability to

declare an Alert based on EAL 3-12 in PVAR 3073229.

Analysis: The team determined that the inability to implement EALs was a

performance deficiency within the licensees ability to foresee and control. The

finding was more than minor because it was associated with the Emergency

Preparedness attribute of procedure quality, and could affect the cornerstone

objective of implementing adequate measures to protect the health and safety of

the public, if the licensee cannot promptly recognize an emergency condition.

Using the IMC 0609, "Significance Determination Process," Appendix B,

Emergency Preparedness Significance Determination Process, the finding was

determined to have a very low safety significance (Green) because the licensee

could be unable to declare one EAL at the Alert and one EAL at the Notification

of Unusual Event level. The cause of this finding had crosscutting aspects

associated with the corrective action of the PI&R area in that the licensee had

previous opportunities to identify the deficiencies (P.1.(a)).

Enforcement: 10 CFR 50.54(q) states, in part, that a licensee authorized to

possess and operate a nuclear power reactor shall follow and maintain in effect

emergency plans which meet the standards in §50.47(b) and the requirements in

10 CFR Part 50, Appendix E. Risk Significant Planning Standard §50.47(b)(4),

states, in part, that a standard emergency classification and action level scheme

shall be used. 10 CFR Part 50, Appendix E, IV(B), states, in part, that the means

for determining the magnitude of and assessing the impact of the release of

radioactive materials shall be described and the EALs shall be based on in-plant

conditions and instrumentation. Contrary to the above, from July 1994 until

October 2007, the licensee failed to have the ability to implement EAL 3-12 at the

Alert level. Specifically, area radiation Monitor RU-18 could not be monitored

from the remote shutdown panels and therefore, the emergency classification

could not be declared as required in Procedure EPIP-99. In addition, from

January 2006 until October 2007, the licensee failed to have the ability to

implement EAL 7-1 resulting in the over-classification of a Notification of Unusual

Event. Specifically, the licensee did not develop a procedure to enable

personnel to define an airliner and therefore, the proper emergency

classifications could not be declared. Because this finding was of very low safety

significance and was entered into the CAP as PVARs 3073229 and 3070849,

this violation was treated as an NCV, consistent with Section VI.A of the

Enforcement Policy: NCV 05000528, 05000529,0500030/2007012-16, Inability

to Implement Emergency Action Levels.

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b.3 Observations and Minor Violations Involving Emergency Response and

Preparedness

b.3.1 Failure to Notify Offsite Agencies of Emergency Action Level (EAL)

Changes

The team identified a minor violation of 10 CFR 50.54(q) which requires in

part, that, licensees follow and maintain emergency plans which meet the

standards in §50.47(b) and Appendix E. Palo Verdes Emergency Plan,

Section 5.1, Revision 37, stated in part, that, EAL changes would be

discussed and agreed upon with state and county governmental

authorities. Contrary to the above, between January 2005 and

October 2007, the licensee made changes to the EALs without discussing

and obtaining the prior approval of state and county governmental

authorities. The team determined that following a change to

10 CFR Part 50, Appendix E, IV(B), which permitted a licensee to

discontinue the practice of obtaining the prior approval of offsite agencies

for EAL changes under the authority of 10 CFR 50.54(q), the licensee

implemented the change, without changing the requirements of the

Emergency Plan. Using IMC 0612, Appendix E, Examples of Minor

Issues, this finding was determined to be minor because it was similar to

Example 2.d. in that there was no regulatory requirement requiring

approval of EAL changes from offsite agencies and there was no impact

on public health and safety. The performance deficiency was entered into

the licensees corrective action system as PVAR 3085397. This

performance deficiency is being documented because of insights

associated with emergency preparedness concerns.

b.3.2 Failure to Train Emergency Planners

10 CFR 50.54(q) states, in part, that a licensee authorized to possess and

operate a nuclear power reactor shall follow and maintain in effect

emergency plans which meet the standards in §50.47(b).

10 CFR 50.47(b)(16) states in part, that, responsibilities for plan

development and review and for distribution of emergency plans be

established, and planners are properly trained. EPIP-59, Emergency

Planning Training Program Description, Section 1.7.1, stated, Training

for PVNGS Emergency Planning staff is conducted via the completion of

a required reading list and/or other training and includes participation in

industry sponsored emergency planning symposia and workshops.

Contrary to the above, prior to October 2007, not all emergency planners

participated in industry symposia and workshops. Specifically, for one

emergency planner, the licensee was unable to provide documentation or

determine that the individual had ever attended symposia or workshops.

Using IMC 0612, Appendix E, Examples of Minor Issues, this

performance deficiency was determined to be minor since it was similar to

the Example 4.h. in that there were other planners whose qualifications

were current. The performance deficiency was entered into the licensees

corrective action system as PVAR 3086481. This performance deficiency

is being documented because of insights associated with emergency

preparedness concerns.

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6 RADIATION SAFETY STRATEGIC PERFORMANCE AREA

6.1 Occupational Radiation Safety

A review of radiological work practices was conducted in conjunction with other site

activities that were reviewed in more detail. A number of observations were noted which

identified failures to implement radiological worker expectations and failures to follow

radiological procedures. Areas of note included: the failure to conduct personal

contamination monitoring by radiological workers in the presence of posted signs,

out-of-date surveys, using out-of-date survey information to conduct briefings, and

incomplete radiological briefings. Though this was not a significant focus of the teams

activities, the number of adverse observations indicate improvement is warranted in

implementation of the occupational radiation safety program at Palo Verde.

a. Inspection Scope:

The team did not conduct an in-depth review of the occupational radiation safety

program; however, observations relevant to this Radiation Safety Strategic

Performance Area were collected and assessed to provide insights into Palo Verdes

performance. Work site observations and the results of plant tours, including

radiologically controlled areas, were evaluated to determine if applicable radiological

program procedures were adequately implemented, including worker radiation

exposure controls, radiation work permits, implementation of as low as reasonably

achievable (ALARA) concepts, and effectiveness of work planning, coordination,

implementation, and lessons learned. In addition, the team reviewed a sample of

radiological facilities, equipment, and radiation monitoring instrumentation. Information

relevant to this area was collected during tours of shutdown and operating units

including tours of radiologically controlled areas, the Unit 3 containment, and other

plant areas that contained radioactive material storage areas. Interviews with

radiological protection managers, supervisors, and workers were conducted to provide

additional insights into this performance area. Finally, the contribution of radiological

worker human performance issues identified over the course of this inspection were

assessed to determine if these issues were adequately investigated, evaluated, and

resolved.

b. Observations and Findings:

b.1 Inadequate Briefings on Radiological Conditions

Introduction. The team identified a Green NCV of 10 CFR 19.12 for the failure of

RP personnel to provide adequate information regarding radiological conditions

and precautions to minimize exposure during pre-job briefs.

Description. During select pre-job briefs performed between October 1 and

October 3, 2007, RP personnel failed to provide accurate information regarding

the radiological conditions commensurate with the hazard. For a Unit 3

containment entry briefing that did not involve entry into high radiation areas on

October 1, 2007, dose rate information was communicated by RP personnel

using elevation drawings and pointing to different locations and verbally stating

Aless than 2 mrem/hr, elevated (with no actual dose rates specified), or AHRA

[high radiation area], which your REP [radiation exposure permit] does not allow.@

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The elevation drawings used for the briefing were not radiological surveys and

contained no dose rate data. In addition, the expected contamination levels were

not reviewed and the RP person giving the briefing did not know if the 80 foot

elevation had been released. Furthermore, although it was the first entry for the

radiological workers, the expected response to dose and dose rate alarms was

not discussed, the expectation to check the electronic dosimeter every 15

minutes was not mentioned, and the electronic dosimeter setpoints were not

reviewed.

During a briefing at the RP control point on the 70 foot elevation of the Unit 3

auxiliary building on October 1, 2007, it was stated there were no high radiation

areas in the Train A CS room, based on information contained in the posted

radiation survey. While performing a walkdown of the room, the team identified a

posted and barricaded high radiation area. Subsequently, the team noted that a

number of the radiation survey maps at the 70 foot RP control point used for the

briefing were out of date, including the survey for the Train A CS room. The

licensee initiated PVAR 3070507 with the action to replace the survey maps with

the most recent version. However, the posted survey maps at the RP control

point for the Train A charging pump room and the 140 foot hot lab were out of

date when used for a briefing on October 3, 2007.

Analysis. The failure of RP personnel to adequately inform workers of the

radiological conditions in the Unit 3 containment and auxiliary building was

determined to be a performance deficiency. This finding is greater than minor

because it is associated with the Occupational Radiation Safety Cornerstone

attribute of program and process and affected the cornerstone objective of

ensuring the adequate protection of the worker health and safety from exposure

to radiation during routine operations. The finding was determined to be of very

low safety significance (Green) because it was not an ALARA issue, there was

not an overexposure or substantial potential for an overexposure, and the ability

to assess dose was not compromised. The cause of the finding had crosscutting

aspects associated with decision making of the human performance area in that

RP personnel performing briefings failed to communicate decisions, and the

basis for decisions, to personnel who had need to know the information to

perform work safely (H.1.(c)). The cause of this finding was also related to the

safety culture component of accountability in that RP personnel failed to

demonstrate a proper safety focus and reinforce safety principles (O.1.(c)).

Enforcement. 10 CFR 19.12 requires, in part, that all individuals who in the

course of employment are likely to receive in a year an occupational dose in

excess of 100 mrem be kept informed of the transfer or use of radioactive

material and in precautions to minimize exposure. Contrary to these

requirements, on October 1 and 3, 2007, RP personnel did not adequately inform

workers of radiological conditions and precautions to minimize exposure during

radiological briefings. Specifically, RP personnel failed to adequately inform

workers of the radiological conditions and precautions/procedures to minimize

exposure in the Unit 3 containment and auxiliary building so that the workers

could take the necessary precautions to minimize exposure. Because the finding

was of very low safety significance and had been entered into the licensee's CAP

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as PVARs 3070507 and 3071940, this violation was treated as an NCV

consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000530/2007012-17, Inadequate Briefings on Radiological Conditions.

b.2 Observations and Minor Violations Involving Occupational Radiation Safety

b.2.1 Failure to Conduct Appropriate Radiological Surveys

The team identified a minor violation of 10 CFR 20.1501(a) which

requires, in part, that each licensee make or cause to be made surveys

that may be necessary to comply with regulations in this part, and are

reasonable under the circumstances to evaluate the magnitude and

extent of radiation levels, concentration/quantities of radioactive material,

and the potential radiological hazards. Contrary to the above, on October

1 and 2, 2007, licensee personnel failed to make or cause to be made

surveys to ensure compliance with 10 CFR 20.1201. Specifically, the

team observed radiological workers failing to complete personnel

contamination monitoring surveys in Unit 3 and the 70 foot auxiliary

building and 140 foot fuel building, as specified by signs posted adjacent

to the respective monitoring stations. Using IMC 0612, Appendix B,

Issue Screening, this finding was minor because the survey was an

administrative requirement and there was no unexpected contamination.

The performance deficiency was entered into the CAP as PVARs

3070009 and 3072066. This performance deficiency is being

documented because of insights associated with implementation of RP

program and accountability of management personnel.

6.2 Public Radiation Safety

Selected aspects of the public radiation safety program were reviewed including; (1) a

sampling of plant facilities, equipment, and instrumentation for radioactive effluent

monitoring, (2) a sampling of procedures affecting the processing, control and discharge of

radioactive effluents, and (3) a sampling of training and qualifications of personnel

involved in radioactive waste and effluent processing. Performance issues identified in

this area related to failures to operate liquid radiological waste tanks in accordance with

station procedures and the UFSAR.

a. Inspection Scope

The team did not conduct an in-depth review of the Public Radiation Safety program;

however, a sampling of program effluent monitoring equipment and radioactive

material controls was evaluated. Unit 3 radiological waste systems were walked down

and valve alignments were compared to system drawing requirements; observations

during site tours and radiological work activities were evaluated against program

requirements. Interviews with managers, supervisors, engineers, and radiological

workers were conducted. Radiological waste system procedures, applicable sections

of the UFSAR, the Offsite Dose Calculation Manual, the Radiological Environmental

Monitoring Report, the 2006 Annual Radioactive Effluent Release Report, radiation

protection self-assessments, and CAP documents were reviewed. In addition, the

Units 1, 2, and 3 radiological waste tank farms were walked down and the operation of

radiological waste systems (total dissolved solids and recycle monitor tanks) were

- 116 - Enclosure

evaluated. The above activities provided insight into the assessment of plant facilities,

equipment, and radiological instrumentation intended for public radiation safety. In

addition, the team used feedback from these activities to evaluate the implementation

of public radiation safety programs and processes, and to evaluate how any observed

human performance issues affected the public radiation safety area.

b. Observations and Findings

b.1 Failure to Periodically Update the Final Safety Analysis Report

Introduction: The team identified a Severity Level IV NCV of 10 CFR 50.71(e) for

the failure of the licensee to periodically update the UFSAR with all changes

made in the facility or procedures.

Description: While conducting a review of the Unit 2 liquid radiological waste

system, the team found that the system was not being operated in accordance

with the description provided in the UFSAR. Specifically, evaporator concentrate

was being pumped to one of the high total dissolved solids (TDS) holdup tanks

rather than the concentrate monitor tanks as specified in Section 11.2.2 of the

UFSAR.

The licensee stated that the Unit 2 concentrate monitor system had been out of

service since 2002. The teams review of corrective action documents related to

the system determined that the concentrate monitor tanks were not being used

because of equipment/maintenance issues with the concentrate monitor system.

The UFSAR stated in Section 11.2.2.4.1.2, that flow from the high TDS holdup

tank can be terminated or diverted to an alternate path by operator action based

on evaporator or holdup pump malfunction, high-pressure drop across the

adsorption bed or ion exchangers, an exhausted resin bed, or when the

radiological waste section leader determines it is necessary. The UFSAR did not

specify the alternate flow path nor the allowed duration. The team concluded

that operating outside of the UFSAR design basis for approximately 5 years was

not the intent of UFSAR Section 11.2.2.4.1.2.

Analysis: The team determined that the failure to update the UFSAR to reflect

changes made to the facility was a performance deficiency. This issue was

subject to traditional enforcement because it had the potential for impacting the

NRCs ability to perform its regulatory function. The finding is characterized as a

Severity Level IV violation because the erroneous information in the UFSAR was

not used to make an unacceptable change to the facility or procedures. The

cause of this finding had a crosscutting aspect associated with resources of the

human performance area in that the licensee failed to ensure that personnel and

equipment were available and adequate to maintain radiological safety by

minimization of long-standing equipment issues (H.2.(a)).

Enforcement: 10 CFR 50.71(e) requires that the licensee periodically update the

USFAR with all changes made in the facility or procedures. Contrary to the

above, in 2002 the licensee made a change to the facility and procedures as

described in the UFSAR and failed to update the UFSAR. Specifically, the

licensee began operating the Unit 2 liquid radiological waste system in a manner

different than that specified by UFSAR when they commenced pumping

- 117 - Enclosure

evaporator concentrate to the high TDS holdup tanks rather than the concentrate

monitor tanks as specified in UFSAR Section 11.2.2. The failure to update the

UFSAR was characterized as a Severity Level IV violation. The finding was of

very low safety significance because the change in operation of the total

dissolved solids holdup tanks did not result in an increase in the likelihood of a

release of radioactive material. This issue was entered in the licensees CAP as

PVAR 3075089. This violation was treated as an NCV, consistent with Section

VI.A.1 of the NRC Enforcement Policy: NCV 05000529/2007012-18, Failure to

Periodically Update the Updated Final Safety Analysis Report.

7 SAFEGUARDS STRATEGIC PERFORMANCE AREA

7.1 Safeguards Strategic Performance Area

The team did not conduct an in-depth review of the Safeguards Strategic Performance

Area; however, the team conducted tours of site physical protection areas and evaluated

their attributes and performed spot checks of security equipment. In addition, the team

interviewed security personnel to determine if latent organizational or security equipment

issues exist at Palo Verde. The team also observed the owner controlled area and

protected area access control process. One finding associated with the calculation of

group work hours was identified. The finding is discussed in NRC Inspection Report

05000528, 05000529, 05000530/2007402.

8 SAFETY CULTURE

8.1 Evaluation of the Licensees Independent Safety Culture Assessment

The team determined that the licensees third-party safety culture assessment was

adequate to provide the licensee with the information necessary to develop appropriate

corrective actions for safety culture weaknesses, although limitations in the interpretability

of the survey tool decreased its usefulness to the licensee. Without the many write-in

comments provided by the survey participants, the licensee may not have been able to

use the survey results to develop specific corrective action plans. The results of the

NRCs independent safety culture assessment validated the results of the licensees third-

party safety culture assessment.

a. Inspection Scope

Consistent with inspection requirements in Section 02.07 of IP 95003, the team

evaluated the licensees safety culture assessment to determine whether: (1) the

assessment was comprehensive, (2) the assessment team members were

independent and qualified, (3) the assessment was methodologically sound, (4) the

data collected supported the conclusions derived from the assessment, and (5) the

licensees corrective actions in response to the assessment findings were likely to be

effective.

The team met with licensee representatives and one of the licensees safety culture

assessment contractors (Synergy) at NRC Headquarters in Rockville, Maryland, on

March 14, 2007, to discuss the independent safety culture assessment. The team also

reviewed the licensees plans for conducting the safety culture assessment, the

resumes of the personnel who conducted the assessment and analyzed the data, and

- 118 - Enclosure

the survey instrument and interview guides. Team members and the NRC resident

inspectors observed the administration of the survey on six different occasions

between April 15 - 25, 2007, to verify that the instructions provided to survey

participants were consistent and did not introduce the potential for response biases.

During the week of June 18-21, 2007, the team completed an onsite review of the

preliminary results from the safety culture assessment and conducted interviews with

licensee personnel and members of the assessment team to better understand their

methods to aid in interpreting the preliminary results. In addition, conference calls with

the licensee and Synergy were held on June 27, 2007, and July 26, 2007, to discuss

the measurement properties of the survey instrument and the statistical analyses of

the survey data. During the weeks of October 1-12, 2007, and October 29-

November 2, 2007, the team solicited feedback on the safety culture assessment

during individual and group interviews with site personnel and evaluated the licensees

corrective action plans for addressing identified safety culture weaknesses.

b. Observations

Comprehensiveness

The team concluded that the safety culture assessment provided the licensee with the

information necessary to: (1) develop appropriate corrective actions for the identified

safety culture weaknesses and (2) take actions to maintain the sites safety culture

strengths.

Two teams with different areas of emphasis, using complementary methods,

conducted the assessment. One team, the Independent Safety Culture Performance

Evaluation Team (ISCPET), focused on the effectiveness of the sites policies,

programs, processes, and procedures in establishing that nuclear plant safety issues

receive the attention warranted by their significance. This team conducted interviews,

document reviews, and behavioral observations to obtain information. A second team

focused on the site workforces attitudes and perceptions related to the extent to which

nuclear plant safety issues receive attention. This team, Synergy, collected

information for the assessment by administering a site-wide safety culture survey

augmented by follow-up interviews with site personnel. The combined activities of the

assessment teams addressed all levels of site and corporate management, obtained

safety culture survey responses from approximately 80 percent of the Palo Verde

workforce including contractors, and sampled organizational characteristics and

attitudes related to each of the 13 safety culture components identified in Section

06.07 of NRC IMC 0305, Operating Reactor Assessment Program.

Independence and Qualifications

The team concluded that the licensees safety culture assessment was conducted

independently and that the assessment teams members were qualified. Although

licensee personnel administered the safety culture survey, the NRC teams

observations of survey administration and focus group interviews with Palo Verde staff

indicated that the independence of the effort was not compromised. Licensee

personnel administering the survey followed the instructions provided by the

assessment team and implemented adequate methods for collecting completed

surveys to ensure participants believed their responses would remain anonymous and

confidential.

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The NRC team verified that the licensees safety culture assessment teams had

unrestricted access to information and opportunities to interview the individuals

necessary to complete the assessment.

The NRC team verified that the assessment teams were composed of individuals with

a knowledge of nuclear safety culture and the topics they were assigned to assess.

The licensee ensured that Synergy subcontracted with an independent professional

survey research firm, Westat, to assist in analyzing the statistical properties of the

survey instrument and the survey results. The additional analyses performed by

Westat enhanced the interpretability of the survey portion of the safety culture

assessment.

Assessment Methods

The team concluded that the methods used to perform the assessment were

appropriate, although some weaknesses in the safety culture survey were identified.

Multi-method approach. The NRC team verified that the assessment teams applied a

multi-method approach to conduct the safety culture assessment, including a survey,

behavioral observations, interviews, and document reviews. Sample sizes for applying

each method obtained representative information, and the teams behavioral

observation and interview guides did not bias the assessment results. The teams

performed their assessment activities in parallel, but compared, contrasted, and

reconciled their findings to ensure they provided integrated assessment results to the

licensee. The NRC teams review of the preliminary results from the teams confirmed

that the large majority of their results were consistent and required little additional data

gathering to reconcile contrasting results.

Survey tool. The team concluded that the safety culture survey appropriately screened

for workforce attitudes and that the most useful information was contained in the write-

in comments provided by the participants. Over half of those participating in the

survey provided write-in comments. The write-in comments provided more detailed

information related to safety culture strengths and weaknesses at the site, and

enhanced the overall usefulness of the results. The NRC team verified that Synergy

had appropriately grouped the write-in comments to identify the recurring safety culture

themes.

Site personnel who participated in the survey and were interviewed by the NRC team

believed that the anonymity of their responses had been maintained and that the

survey gave them an opportunity to express their views on important issues at the site.

None of the participants interviewed reported feeling any pressure to respond to the

survey questions.

Survey participants interviewed by the NRC expressed reservations about the length

of the survey (i.e., they perceived it to be too long and repetitive) and indicated that the

construction of some survey items made it difficult to respond. For example, some

items asked participants to respond with respect to both their managers and

supervisors. Interviewees stated they had difficulty in responding to these items

because their perceptions of their supervisors differed from perceptions of their

managers. The team identified additional examples of survey items that addressed

multiple topics within a single item, which is inconsistent with standard survey design

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techniques described in IP 95003, Enclosure F, Guidance for Evaluating Safety

Culture Surveys. Licensee personnel who were developing improvement plans also

reported similar interpretation difficulties. Synergy indicated that they did not pilot-test

the safety culture survey on a representative sample of Palo Verde survey participants

before the survey was administered. The team concluded that the licensee may have

been able to make better use of the results had these items been addressed before

administering the survey.

The team noted a low response rate from security personnel on the survey

(approximately 40 percent participated), compared to other functional groups at the

site. Synergy indicated that this response rate is characteristic of security groups at

other sites and results from (1) a perception among security personnel that the survey

items are less relevant to their jobs than to other jobs at nuclear facilities and

(2) typical difficulties in arranging to administer the survey to security personnel

because of shift schedules. The team noted that shift scheduling issues did not

adversely affect response rates from other functional groups, such as operations, and

verified that all security personnel had an opportunity to participate. During focus

groups, the NRC verified that security personnel who took the survey believed the

items were more relevant to the crafts, consistent with Synergys experience at other

sites. Interviews indicated that security personnel believed the effort of taking the

survey would not be worthwhile because it would not result in positive changes related

to staffing and overtime. The team determined that the failure to include items directly

relevant to the security function or adjust existing items to be more clearly relevant to

the security function was a weakness in the survey tool. The team noted that Synergy

and licensee personnel followed-up on the low response rate with individual interviews

to more clearly understand the security groups safety culture concerns.

Survey analyses. Based on the NRC teams review of the statistical analyses of the

survey data performed by Westat, the team concluded that the survey results were of

limited effectiveness in differentiating between functional groups at the site that may

have localized safety culture issues. Statistically significant differences were found

only between the functional group with the most positive responses on the survey and

the group with the most negative results. Therefore, Synergy relied more heavily on

the write-in comments and interview results to discriminate among functional groups.

Based on their review, Synergy identified 12 priority groups in need of particular

attention. The NRC team determined that the recommendation to focus on these 12

groups may be narrowly focused given the similarities in the safety culture issues

raised in the write-in comments from all of the groups.

The NRC team reviewed the survey data analyses performed by Westat and

determined that the survey met standard survey design requirements for internal

consistency. The write-in comments, the results of Synergys and the licensees

follow-up interviews, the ISCPET review, and the NRCs independent safety culture

assessment indicated that the survey tool provided adequate information related to

safety culture attitudes at Palo Verde.

Third-party assessment conclusions

The team concluded that the results and conclusions of the assessment were

consistent with the data collected. The team also noted that the themes identified from

the assessment were very similar to the results of licensee safety culture assessments

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performed in 2004 and 2005. Responses to the 2007 survey items were more

negative than responses to the 2005 survey, and write-in comments on the 2007

survey were both more extensive and more negative in tone than the write-in

comments from 2005. The issues raised by site personnel in each of these

assessments were consistent and were discussed by site personnel in progressively

stronger terms. This trend suggests that corrective actions were not effective in

sustaining improvement following the 2004 and 2005 safety culture assessments.

Licensee analysis and corrective actions

The team concluded that individual findings and recommendations from the safety

culture assessment were appropriately reviewed by the licensee to identify corrective

actions. The licensee had not finished developing corrective actions at the time of the

inspection; therefore, the team could not evaluate the completeness and effectiveness

of the planned corrective actions.

The licensee addressed the results of the safety culture assessment using several

methods. These methods included Employee Concerns Program (ECP) actions to

respond to some write-in comments, establishment of a Safety Culture Team (SCT),

development of safety culture improvement plans for the 12 functional groups

identified by Synergy, and efforts to develop site-wide safety culture improvement

plans.

ECP actions. ECP staff reviewed the write-in comments from the survey for any

instances in which a comment implied or reported perceptions of retaliation for raising

concerns. Using information collected from the survey, the ECP identified the work

groups of approximately 9 cases, but made no attempt to identify individuals who had

submitted the comments in order to maintain their anonymity and confidentiality. The

ECP manager provided an overview to the team of how each case was investigated

and dispositioned. The team concluded that the handling of the comments was

appropriate.

SCT actions. The licensee established the SCT to facilitate the development,

communication, and implementation of actions to improve safety culture. The SCT

tasked the managers of the 12 functional groups to develop improvement plans. The

SCT provided the managers their groups survey scores, write-in comments, and other

relevant information from the assessment, and directed the managers to communicate

the survey results and develop improvement plans. The SCT worked with the

managers to plan their communications with their groups, provided individual and

organizational consulting to the managers in developing their improvement plans, and

were responsible for tracking implementation and effectiveness of the plans. Senior

management met with each manager to review the improvement plans. The NRC

team also reviewed the improvement plans, observed meetings between senior

management and the managers, and conducted individual interviews with the

managers to obtain their views of the process. The team concluded that the safety

culture improvement plans for the 12 groups were appropriate.

The SCT also provided safety culture assessment results to other managers at the site

in September 2007, with a request for the managers to meet with staff to discuss the

results, and develop any necessary improvement plans. In addition, the SCT

requested the managers review the results for their work groups and determine

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whether any immediate improvement actions were necessary before the start of the

Unit 3 steam generator replacement outage. The SCT requested the managers

complete their meetings by the end of October 2007, but did not require that any

improvement plans be entered into the CAP for tracking to completion. At the time of

the inspection, the SCT did not plan to monitor implementation of the managers

dissemination of the assessment results or development of improvement plans.

This approach for non-priority groups was consistent with the licensees process for

responding to the results from the 2005 safety culture assessment. About half of the

frontline participants in the NRCs focus groups had not yet met with managers to

receive detailed information about the assessment results or participate in developing

improvement plans. The team noted that a failure to communicate specific results

from a survey and develop improvement plans may discourage personnel from

participating in future surveys. In addition, because the statistical differences between

functional groups on the survey responses were not significant, this approach may not

ensure improvement in other groups that could have safety culture issues.

Site-wide actions. The SCT informed the team that they intended to address safety

culture weaknesses identified through the assessment with site-wide improvement

actions. The SCT performed streaming analyses on: (1) the areas for improvement

identified by the Synergy survey and follow-up interviews; (2) the summary of the

write-in comments from the survey; and (3) the areas for improvement identified by the

ISCPET. The analyses identified drivers and contributing causes for each of the

areas, which were then consolidated into a set of overall key drivers. These key

drivers were: (1) individual accountability and ownership; (2) clarity and

communication of overall priorities and strategies; (3) quality of leadership and

management; (4) receptivity to employee input; (5) change management, and (6) site

programs and processes. The NRC team determined that the key drivers captured the

issues from the licensees safety culture assessment.

The licensees corrective actions to address the safety culture drivers were primarily

high-level actions referenced from several ImPACT Root Cause Evaluations. For

example, to address individual accountability and ownership, the SCT corrective

actions referenced actions being taken under the Organizational Effectiveness Root

Cause Evaluation, including developing an accountability model (CRAI 3075803),

implementing a management review meeting process (CRAI 3063852), developing a

leadership/management model (CRAI 3082328), and developing a site-wide

communication strategy (CRAI 3063112). The corrective actions from the ImPACT

Root Cause Evaluations were either recorded in the Site Integrated Business Plan

(SIBP) or were in the process of being added at the time of the inspection. The SCT

also described plans to establish mechanisms for tracking, measuring, and assessing

the effectiveness of the corrective actions to address the key drivers. Based on the

level of detail available, the NRC team was unable to assess the effectiveness of the

corrective actions or the SCTs plans.

Verification of completeness. The SCT performed a detailed review of the findings,

recommendations, and write-in comments from the safety culture assessment teams

and compared them with SIBP tasks and existing CAP items. For issues that were not

in the SIBP or CAP, the SCT initiated additional actions. For example, one of the

findings from the ISCPET and Fundamental Overall Problem 9, Organizational

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Effectiveness, was a need to establish safety conscious work environment (SCWE)

expectations for contractors and incorporate them into their contracts. The SCT

initiated CRAI 3090979 on November 9, 2007, to address this action.

In addition, for actions that were described at a general level in the SIBP or CAP, the

SCT issued or planned to take additional actions to ensure findings and

recommendations from the safety culture assessment were addressed. For example,

the SCT initiated CRAI 3082328 to verify that the communication strategy being

developed under CRAI 3063112 (related CRDR 3048836, Organizational

Effectiveness root cause) included actions to motivate site personnel to understand

and take responsibility for improving current levels of performance. Another example

was CRAI 3082469, which was to verify that the formal process for change

management being developed under CRAI 3064376 (related CRDR 3048836),

required solicitation of employee input in appropriate cases. The SCT identified

several issues from the licensees safety culture assessment that were not addressed

by existing actions, and planned to enter those into the CAP.

The NRC team noted that the actions that were referenced in the CRAIs owned by the

SCT did not have a link back to the safety culture improvement efforts. For example,

CRAI 3082469 to develop the process for change management, which was in the

SIBP, did not have a link back to CRAI 3082469 to ensure the change management

process solicits input from employees as appropriate. With this structure, the SCT had

the responsibility to communicate with the action owner, initiate involvement, and

ensure the products met the specifics stated. The action owner, however, did not have

any responsibility to ensure the product addressed specific findings from the safety

culture assessment. This one-way linkage created the potential for the action owners

to not fully consider the safety culture assessment findings when developing and

implementing corrective actions.

8.2 NRC Independent Safety Culture Assessment

The team identified weaknesses in organizational characteristics and attitudes associated

with 10 of the NRCs 13 safety culture components, as detailed in Section 06.07

of Inspection Manual Chapter (IMC) 0305, Operating Reactor Assessment Program.

The most notable weaknesses were identified in the safety culture components related to

decision-making, organizational change management, resources, the licensees corrective

action program, accountability, operational experience, self assessments, and work

practices. The observed weaknesses were widespread among functional groups across

the organization, involving operations, engineering, maintenance, radiation protection, and

corrective action program personnel. Organizational characteristics and attitudes were

acceptable in the safety culture components of safety policies; the environment for raising

concerns; and preventing, detecting, and mitigating perceptions of retaliation. The team

concluded that although the safety culture has degraded at the site, Palo Verdes existing

safety culture supports continued safe operation.

a. Inspection Scope

Consistent with the inspection requirements in Sections 02.08 and 02.09 of IP 95003,

the team conducted an independent assessment of the licensees safety culture. The

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purposes of this assessment were to (1) inform the NRCs assessment of the

contributors to degraded performance in the affected Strategic Performance Areas and

(2) validate the licensees third-party safety culture assessment.

The team relied on document reviews, individual and group interviews, and behavioral

observations to conduct the assessment. The team assessed safety culture attitudes

by conducting 125 individual interviews and 34 focus groups with an average of 8

participants in each group, for an approximate total of 400 safety culture-specific

interviews over the course of the inspection. These interviews involved personnel from

the majority of functional groups at the site and at each management level affecting

the organization, including Arizona Public Service (APS) corporate and owner

personnel, former senior site managers, and an Arizona Corporate Commission (ACC)

staff member. The team also assessed safety culture-related behaviors during plant

tours, system walkdowns, control room and outage control center observations, and

observations of site meetings and pre-job briefings. The team assessed the licensees

organizational characteristics with respect to each safety culture component using at

least two data-collection methods. The data-collection methods were implemented by

at least two inspectors. The team also integrated the safety culture insights from the

inspection findings into the overall assessment of the safety culture at Palo Verde.

b. Observations and Findings

b.1 Decision-making

The team identified past decisions that continue to adversely affect site

performance as well as ongoing weaknesses in some site decision-making

processes. Results of the NRCs safety culture assessment indicated that the

majority of Palo Verde personnel interviewed perceived that cost reduction efforts

inadvertently created an environment in which nuclear safety was degraded.

Most of the site personnel interviewed described decision-making as being

primarily governed by the goals of reducing costs in preparation for deregulation

and cost containment, unless the decisions involved meeting new regulatory

requirements or ensuring continued production (e.g., steam generator

replacements). Site personnel provided numerous examples of decisions related

to the erosion of nuclear and industrial safety margins; failures to maintain

adequate levels of qualified staff to implement programs, processes and

procedures; failures to replace or upgrade out-dated or degrading equipment; a

lack of preventative maintenance; and untimely repairs.

Impact of Deregulation. During the early 1990s, the ACC determined that APS

should deregulate its generation assets, including Palo Verde, and separate

these assets to enter into a commercially competitive retail electricity market. In

anticipation of a deregulated retail market, APS implemented cost reductions with

a goal of decreasing retail rates by approximately 30 percent. The cost

reductions were implemented by reducing staffing levels through reductions in

force and an extended hiring freeze, and by cutting operations and maintenance

(O&M) budgets by 10 percent per year across the board. Senior management

believed that this reduction could be completed without degrading nuclear safety

by eliminating the inefficiencies in processes and workflow. By 1998, total

expenditures (O&M + capital) at Palo Verde had been cut by 35 percent from

1992 levels.

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The consequences of the cost reductions combined with the effects of plant

aging, contributed to an increase in unplanned outage time and equipment

failures. In 2000, after nine consecutive years of across-the-board O&M cost

reductions, O&M expenditures began increasing. By 2006, O&M costs had

increased by 64 percent from their low point in 2000 and were 21 percent higher

than 1992 baseline levels.

Palo Verde replaced steam generators and initiated plans to replace the reactor

vessel pressure heads in all three units. This caused capital expenditures to

increase by a factor of 5 from 1996 to 2005. The increase in combined O&M and

capital expenditures between 1998 and 2005 was 85 percent and was

attributable to both capital expenditures on major improvement projects as well

as increased O&M costs associated with declining performance.

Interviews with site personnel and document reviews indicated that during the

period of 2000 to 2007, cost-containment pressure increased. Licensee

personnel stated high priority modifications were cancelled or deferred, the

backlog of preventive maintenance deferrals increased, aging equipment was not

replaced, tools and equipment needed to perform simple tasks were not repaired

or replaced, training staff was reduced, training materials were not updated,

benchmarking efforts and external training opportunities were curtailed, and

procedures were not updated or maintained. These cumulative reductions

contributed to the increase in equipment failures, plant events, and other

performance problems at the site.

The licensee continued to lose qualified staff in the line organizations

(e.g., operations, engineering, maintenance) during this period as Palo Verdes

workforce began to retire or personnel took other jobs. Further, experienced

people were shifted to support large capital projects, such as the main turbine

and steam generator replacements, or the improvement projects necessitated by

Palo Verdes declining performance. These personnel were not replaced in the

line organizations, which exacerbated the lack of support for operations,

maintenance, engineering work, and improvement projects at the station.

During interviews, corporate personnel stated that they had lost touch with site

operations over the five years preceding Palo Verdes entrance into Column 4 of

the NRCs action matrix, and were unaware that cost-containment efforts were

adversely affecting performance. A complicating factor was that corporate

management allowed multiple lines of communication with the site to be closed

off. Virtually all significant non-financial assessments of site performance flowed

to the corporate organization through a single communication channel at the site.

From the corporate perspective, APS was appropriately investing a steadily

increasing amount of resources to protect the Palo Verde asset. Senior onsite

management believed that the site had to become more efficient and more

productive in order to establish competitive rates and maintain safety. The site

leadership was determined to avoid problems with cyclic performance by

maintaining sustainable budgets while addressing latent problems.

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In 2005, the ACC reversed the original decision to deregulate. In April 2007, the

ACC approved the first APS base rate increase in 14 years and implemented a

process whereby APS was reimbursed for increased fuel costs.

Licensee response. Management at the most senior corporate levels has taken

steps to enhance decision-making processes affecting nuclear safety at Palo

Verde. For example, to ensure that Board and owner decision-making is more

fully informed, the composition of Palo Verdes off-site safety review committee

has been changed and the committee has an avenue to report directly to the

Board of APS rather than to the site vice president/chief nuclear officer

(SVP/CNO). Additionally, the Nuclear Oversight Committee provides a second

source of information by directly reporting to the Board and APS corporate

executives. At the time of the inspection, Board members were making more

frequent visits to the site to meet with frontline and other personnel, and owner

representatives were regularly observing site decision-making meetings.

During the first quarter of 2007, APS hired a new SVP/CNO who has a clear

focus on nuclear safety and is knowledgeable of current industry practices and

standards. The new SVP/CNO assembled a team of similarly knowledgeable

and experienced managers in key senior management positions to improve site

decision-making and performance. During NRC safety culture interviews, station

personnel cited examples of visible decisions made by the new senior

management team within the past few months that they perceived as initial

indications of an increased emphasis on nuclear safety. These decisions

included the development and scheduling of departmental top 10 lists of

equipment repairs, extending a refueling outage to correct some longstanding

equipment deficiencies, and authorization to hire new staff or contractors.

APS has increased the current O&M budget to address the backlog of issues.

Corporate and site management indicated that the resources needed to sustain

improvement at Palo Verde will be provided.

Continuing challenges. With the exception of operations personnel and some

mid-level managers who have been interacting with members of the new senior

management team, most site personnel interviewed by the NRC reported that

they had yet to see or experience a significant change in the decision-making

patterns that affected their individual work groups.

Consistent with this perception were the NRC teams observations that decision-

making at lower levels in the organization had not yet become fully aligned with

station managements expectations. Although corrective actions have been

formulated and some were beginning to be implemented to enhance station

decision-making, the licensee did not consistently make safety-significant or risk-

significant decisions using a systematic process that ensured safety is

maintained. For example, as previously discussed, the licensees process for

making operability determinations has not ensured that (1) all degraded

equipment conditions that may require an operability determination are identified,

(2) SROs are provided the technical information necessary to make timely

operability determinations, and (3) the technical information that is provided is

sufficiently rigorous to support decisions that ensure safety is maintained.

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Licensee safety culture assessment. The team determined that the licensees

third-party safety culture assessment had adequately captured these issues.

b.2 Organizational Change Management

Results of the NRCs safety culture assessment indicated that (1) the licensee

was continuing to experience adverse consequences from previous poorly

managed change efforts and (2) organizational change management continues

to be a significant challenge.

A key organizational change that impacted Palo Verdes performance was the

sites reengineering effort in the early 1990s, which focused on streamlining

work processes, reducing staff to reduce O&M costs, and allocating decision-

making authority to those closest to the work (Checklist #FA-4, Reengineering

Checklist). Palo Verde management undertook the reengineering effort to

position the organization for the anticipated deregulation. Reengineering was a

popular and successful management approach undertaken by other companies

during this time period. This effort was based on a best-selling book by Hammer

and Champy entitled Reengineering the Corporation published in 1993.

Fundamental to this approach was the premise that productivity gains will

naturally follow as processes are streamlined and wasteful steps are eliminated.

The productivity gains should translate directly to cost reductions. However,

budget and staff reductions first require a commensurate increase in worker

productivity in order to match the estimated resource supply and demand.

The actions taken to reduce staff and costs from 1992 to 1998 enhanced cost

competitiveness in response to the pending deregulation. However, the

reengineering effort did not sustain the desired productivity and performance

improvements. The goal to achieve sustained cost reductions was not met

because of several factors, including flaws in how the reengineering effort was

implemented, failures to recognize unanticipated consequences, and failures to

make adjustments when unintended consequences occurred.

Productivity methods and tools. The licensee focused on cost reductions without

a commensurate effort to provide the workforce with productivity-enhancing

methods and tools. Interviewees perceived that past senior management did not

want to invest current resources to save future resources. Interviewees believed

that past senior management approached the productivity problem by first cutting

staff and budgets, and then demanding that middle management find new and

creative ways of enhancing productivity. This approach did not include investing

in the processes or technology that might have enabled the desired productivity

improvements.

For example, the CAP was structured around SWMS, a commercial software

database. Palo Verde procured this software application but did not also

purchase the optional interfacing application package that was more intuitive and

would have more readily facilitated linking of CRDRs, CRAIs and other related

CAP documents. As a result, gaining proficiency with the SWMS database

required extensive training and effort to master the software. The consensus

from interviews and focus groups was that many of the workers had not spent the

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time to become proficient because SWMS was too complex. As a result,

personnel continued using multiple problem identification and corrective action

tracking databases they had developed before SWMS was implemented and that

were tailored to their unique needs. The team noted that there were at least 37

separate problem identification and action tracking databases in use at the site at

the time of the inspection. Fragmenting the action tracking systems into separate

databases that were not linked prevented site management from being able to

monitor problems effectively and trend the status of corrective actions. This

fragmentation masked the true extent of the backlogs and made cross-

department prioritization of corrective actions difficult and time consuming.

Palo Verde financial management processes also did not support productivity

improvements, such as effective planning to fund emergent work. A consistent

theme from interviews with mid-management personnel was that department

budgets were considered to be inviolate (i.e., department budgets could not be

overrun and unbudgeted emergent work generally had to be funded from existing

line items). Specifically, when important equipment failed, middle management

was required to find the funds to repair the equipment from within their own

departmental budgets. These unplanned repairs often required that other key

department projects had to be deferred, reduced in scope, or cancelled in order

to fund the emergent repairs. Important projects in one department would be

delayed due to emergent work while other less important projects in other

departments were executed because they were funded under a different

department or group budget.

This weakness in financial management processes contributed to the increase in

the stations backlog. The lack of integration of budget priorities allowed some

low priority projects to be executed while higher priority projects were cancelled

or deferred. Some managers reportedly resorted to padding their budgets to

fund emergent work while others attempted to accurately estimate each budget

line item. Those who padded their budgets had the funds to support both

planned and emergent work, while those who attempted to comply with the spirit

of the formal budgeting process ran short of funds to complete planned work by

the end of the year.

Streamlining. The effort to streamline processes and procedures at the site was

initially effective, as indicated by the decade during which Palo Verde received

favorable NRC and industry assessments. Interviewees described many

examples of efficiencies that were achieved from reducing the number of

management levels in different functional groups and empowering individuals

and teams at lower levels of the organization to solve problems.

The streamlining effort also resulted in the elimination of clear lines of authority,

roles, and responsibilities for programs and processes, which were replaced by

informal, and typically undocumented or poorly documented, methods of

decision-making. Interviewees described the streamlined processes as relying

on expert power. They believed they were effective because of the knowledge

and skills of the staff, many of whom had joined the organization during

construction and start-up. When technical knowledge was required to make a

decision or solve a problem, personnel knew who on the staff had the necessary

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expertise and could access it with a phone call. One interviewee described the

resulting methods of accomplishing work as management by friendship.

The sites streamlined processes began to falter as qualified personnel left the

site or were moved into other positions. Experienced personnel who left a work

group took their knowledge with them. Their expertise was not systematically

captured in site documentation or training programs with the result that overall

organizational effectiveness was reduced.

Staff reductions and reassignments. Middle management and frontline

personnel interviewed by the team consistently reported that the loss or

reassignment of qualified staff from the line organizations (e.g., operations,

engineering, and maintenance) contributed to the sites declining safety

performance. Attrition actually reduced staff to approximately 2000 full-time

licensee personnel by 2001. An internal licensee staffing study in 2002

recommended increased hiring of operations and engineering personnel. The

study showed that this action was necessary because of projected workforce

attrition from retirements, job migration, and the length of time required for new

hires to become fully qualified. The study recommended that the effort to hire

and train new personnel should begin no later than 2004 to preclude significant

shortages of qualified staff. The licensee initiated the Legacy Engineer

program to recruit and train recently graduated engineering personnel, but did

not otherwise implement the recommended aggressive hiring strategy.

Reductions in standards and technical rigor. Interviewees indicated that the

reduced availability of qualified personnel in the line organizations, the loss of

organizational formality and expert knowledge, and increased cost-containment

pressure, as both the workload and annual expenditures (both O&M and capital)

began to increase combined to influence site personnel to reduce standards and

the technical rigor of their work. Interviewees reported finding new ways to meet

management expectations to expedite or defer work in order to contain costs.

However, when it was not possible to find ways to complete necessary work

more productively, interviewees reported that they sometimes resorted to cutting

corners, reducing technical rigor, and reducing the total effort spent on jobs.

Consequently, technical standards in some groups began to slip and quality

suffered. Interviewees also indicated that management accepted less technical

rigor or a lack of product quality as a necessary compromise to meet deadlines

or keep equipment operating. According to site personnel, the sites

streamlined processes were inadequate barriers to prevent such compromises

and over time, the organizations standards degraded as compromises became

more common.

Licensee response. The team concluded that the new senior management

understands the extent of the changes required to reverse the adverse effects of

the past reengineering and cost-containment efforts and has appropriately

prioritized the necessary changes. The team noted that the licensee was

revising the sites financial planning processes; planned to enhance the SWMS

interface; had published and disseminated standards to clarify expectations for

technical rigor and quality work to the line organizations; had begun to implement

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a program for funding and expediting minor modifications and repairs at the time

of the inspection; and was taking steps to recruit new staff and enhance training

programs to qualify the new hires.

Continuing challenges. The team observed that managements efforts to engage

the workforce in implementing the needed changes were not yet fully effective.

Frontline personnel interviewed by the team were not aware of many of the

changes that management was planning or had made, which, over time, would

resolve some of the staffs more significant concerns, particularly with respect to

hiring and training new personnel.

In addition, the large majority of interviewees stated that they were willing to

make changes to improve performance, but, other than being encouraged to

write PVARs, were seeking direction and information about how they, as

individuals, could play a part in turning the site around. After their early

successes with empowerment under the reengineering initiative, this mature

workforce perceived themselves as an untapped resource for improving

performance in their work groups that management has ignored over the past

five years. Only the interviewees from the operations department were clear

about the new managements expectations for their role as the sites leaders.

In other cases, interviewees were experiencing changes but did not fully

understand or accept the bases for the changes. For example, some specialty

maintenance personnel interviewed were recently reassigned to begin cross-

training in other disciplines. These staff recalled a similar effort in the early

1990s that was undertaken as part of the reengineering initiative, then later

cancelled because it caused the specialty staffs primary skills to degrade, and

reduced rather than enhanced staff competence overall. It was unclear to these

interviewees why management was again pursuing a cross-training effort.

The team observed that the licensee had identified the communication

challenges associated with change management at the site, including: the need

to enhance two-way communication between the frontline and management to

ensure that changes are implemented as intended, do not have unintended

consequences, and minimize resistance to change. The team noted that the

licensee was initiating the development of departmental communication plans to

include effectiveness measures during the inspection.

Licensee safety culture assessment. The team determined that the licensees

third-party safety culture assessment had adequately captured these issues.

b.3 Resources

The results of the NRCs independent safety culture assessment indicated that

past resource allocation decisions have challenged nuclear safety at Palo Verde.

Cost-containment efforts caused or contributed to a reduction in the availability of

qualified personnel, procedures that have not been upgraded or maintained, and

degraded facilities and equipment.

Staffing, qualifications, and work hours. The licensee reduced staffing at the site

through reductions in force and attrition over the past 15 years. The team

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concluded that the availability of qualified staff in key departments was reduced

to levels that impacted the licensees ability to simultaneously: (1) respond to the

high amounts of emergent work and unplanned outages, (2) plan for and execute

2 refueling outages each year, (3) reduce growing backlogs, (4) train and qualify

new hires, and (5) complete implementation of multiple programs and processes

to improve site performance. The team noted that improving the staffing issues

and performance issues are challenged by: (1) the relatively long periods

required to fully qualify new staff in key disciplines (ranging from 2 to 6 years);

(2) challenges in recruiting personnel; (3) limited training resources; and (4) the

increasing rate of attrition from retirements.

Operations

Introduction: The team identified an unresolved item (URI) associated with

Technical Specification 5.2.2.d. for the routine use of heavy amounts of overtime

for operations personnel.

Description: Interviews with frontline personnel and managers in operations

indicated that shortages of licensed operators and operator training personnel

were perceived to be the most significant issue facing the operations

organization. Interviewees reported that the licensed operator training pipeline

was interrupted several times after 2000 with a resulting net loss of 20 licensed

operators by 2007 (see chart below). This loss occurred concurrently with a

reduction from 6 operator shifts to 5 self-relieving shifts (i.e., shift crews that

have sufficient numbers of personnel to ensure that regulatory and administrative

control room staffing requirements can be met without overtime or assigning a

member of another shift crew to cover for an individuals absence). The

continued loss of operators reduced shift staffing to a point where 13 of 15 shifts

were not self-relieving. This meant that most control room shifts did not have a

sufficient number of operators to make up for a temporary absence or permanent

loss of either a reactor operator (RO) or SRO. The reductions had the effect of

requiring personnel to work additional overtime and limited most licensed

operators activities to standing watch in the control room. Interviewees indicated

that career advancement opportunities for licensed operators were limited

because of pressures to maintain shift crews; thereby, limiting the ability of

licensed operators to integrate an operations perspective into other site activities.

The team reviewed operations payroll data that summarized the cumulative

regular and overtime hours for each operations department position and

calculated the annual overtime rate for select positions. Since 2003, overtime, as

a percent of regular hours worked, has increased steadily and substantively for

control room and auxiliary operators. The team noted that the increase in

overtime rates for operations department positions appeared to be largely the

result of a decrease in staffing, rather than the result of an increase in the total

number of person-hours expended.

Specifically, from 2003 through 2006, the total number of hours worked annually

by personnel in the control room supervisor (CRS), SRO, RO, and auxiliary

operator (AO) positions remained relatively constant, or decreased, while the

percentage of those total hours that were worked as overtime increased. As a

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result, the payroll data indicated that the licensee increasingly relied on the use

of overtime to provide the person-hours necessary to operate the three units.

Technical Specification 5.2.2.d requires administrative procedures to be

developed and implemented to limit the working hours of unit staff that perform

safety-related functions (e.g., licensed SROs, licensed ROs, radiation protection

technicians, auxiliary operators and key maintenance personnel). The Technical

Specifications further requires that the controls shall include guidelines on

working hours that ensure adequate shift coverage shall be maintained without

routine heavy use of overtime. Pending the completion of a review of the actual

work hours by operations personnel, this issue is identified as URI 05000528,

05000529,05000530/2007012-19, Routine Heavy Use of Overtime.

Maintenance. Interviews with maintenance personnel did not indicate that

overtime was a particular concern. Staffing and qualifications were consistent

areas of concern among those interviewed. Some individuals described the

staffing issue as huge, adding that with low staffing the attitude has become, I

will do it however I can. Many of the comments were focused on the increasing

loss of experienced and qualified personnel. They indicated that although an

apprentice or other new hire represents a pair of hands, so that it may appear

that staffing levels are adequate, their knowledge and skills do not replace those

of a senior technician who has retired. They also stated that training and

supervising new hires, many of whom have not worked in an industrial

environment before, also increased their workload.

The team reviewed maintenance department staffing levels since 2003 and

found that the total number of maintenance staff has remained relatively stable

during this period. However, consistent with the interviewees perceptions of the

loss of senior staff, the team also noted that 125 maintenance personnel (about

23 percent of the departments staff) have retired or left the site since 2000, 48 of

whom left in the 18-month period preceding the inspection. Overtime levels also

increased markedly from their levels during the 2003 through 2004 time period as

workload from emergent work has increased.

Maintenance Department Overtime

Annual Averages for Years 2003 through 2007

Year 2003 2004 2005 2006 2007

Total

546 546 542 545 524

Staff*

Overtime 10.4% 10.1% 15.8% 18.5% 17.9%**

  • Estimate based on total department staff during September of year shown.
    • Estimate based on monthly overtime rates for January through September 2007.

The teams review of an Apparent Cause Evaluation (ACE) Report, Analysis of

Maintenance Organization Performance 2003 Present, Event Date:

March 1, 2007, (CRDR 3039642), indicated that the increase in maintenance

organization overtime was related to an increase in the maintenance organization

human performance error rate. The report states, The current materiel issues of

the plant require more and more frequent overtime, which has shifted the

performance of the maintenance organization in a negative direction. The

organization generally performs at an error occurrence rate of 4/10000 hours or

- 133 - Enclosure

less when overtime worked is 5000 hours0.0579 days <br />1.389 hours <br />0.00827 weeks <br />0.0019 months <br /> or less. When overtime worked

exceeds 5000 hours0.0579 days <br />1.389 hours <br />0.00827 weeks <br />0.0019 months <br /> the error-occurrence rate changes to 5.5/10000 hours or

worse. Second, after overtime begins to escalate and longer periods of overtime

are experienced a cumulative effect on error-occurrences becomes apparent.

These two observations may be indications of overload and fatigue.

In addition to describing an association between overtime and maintenance

human performance, the report provided some additional validation of the

concerns expressed by maintenance personnel regarding the experience level of

the staff. Specifically, the report described an analysis of human performance,

overtime, and worker experience levels in the electrical maintenance shop and

states, The Electrical Maintenance shop is not the only work group showing

evidence of this condition, but the indications are more pronounced and easier to

illustrate What is evident is that the increased error occurrence rate caused by

overtime demand is exacerbated by the decreasing level of station experience

within the organization.

Engineering. Interviews with personnel in the engineering organization indicated

that overtime was not generally perceived as excessive or a particular area of

concern. Staffing and qualifications were significant concerns for the engineering

personnel interviewed, and were described by some as the biggest issue facing

the engineering organization. Although many interviewees acknowledged that

Palo Verde had made significant efforts to hire additional engineering staff, they

were concerned that given the extended time period required to train engineers,

the effort to hire and train new personnel (i.e., the Legacy Program) was not

started soon enough to effectively support transfer of the expert knowledge held

by the many senior engineers who will soon be eligible for retirement.

The team reviewed a summary of engineering organization payroll data from

January 2003 through September 2007. The review indicated that staffing

numbers had remained stable from 2003 through 2005 and then began

increasing substantively beginning in June 2006. However, consistent with the

interviewees perceptions of the loss of senior staff, the team also noted that 102

engineering personnel (or about one-third of the departments staff) have retired

or left the site since 2000, 46 (or about half) of whom left in the 18-month period

preceding the inspection. Recorded overtime rates during this period peaked in

2006 at 8.4 percent, although the team noted that the majority of engineering

personnel are classified as exempt and do not record overtime hours.

Engineering Department Staff and Overtime

for Years 2003 through 2007

Year 2003 2004 2005 2006 2007

Total

331 337 335 366 410

Staff*

Overtime 4.5% 4.0% 6.3% 8.4% 5.9%**

  • Estimate based on total department staff during September of year shown.
    • Estimate based upon monthly overtime rates for January through September 2007.

Other groups and interactive effects. Interviewees from other functional groups

at frontline and mid-management levels also consistently reported inadequate

levels of qualified staff to support the current workload, including the procedures

- 134 - Enclosure

and standards group, work management, radiation protection, chemistry,

business operations, performance improvement, quality assurance, and the

training and human resources groups.

Because little hiring outside of APS occurred between 1993 and 2004, the

human resources workload associated with recruiting and hiring was negligible

and human resources staff did not develop recruiting skills. Interviewees stated

that any active recruiting for open positions was carried out by line managers and

supervisors, typically by friendship when possible. Interviewees reported that

when friendship was insufficient, positions would sometimes remain open for

years. If an individual was identified to be hired, competing demands on human

resources staff often delayed completing the hiring process. The result for the

line organizations was that the workload associated with the unfilled positions

became the responsibility of the remaining staff for extended periods of time, or

was simply not addressed.

The licensee also permitted the number of qualified training personnel to decline.

When an individual left a training position, the position either was eliminated or

was difficult to fill because the line organizations could not afford to move

personnel into the training positions. As a result, when new staff or contractors

were hired and needed training to become fully qualified for their positions, the

training resources were not available to qualify them in a timely manner.

Interviewees reported numerous examples of staff in chemistry, radiation

protection, security, maintenance, and engineering that could not perform all of

the tasks required for their positions without supervision, over extended periods

of time, because there were insufficient training personnel to provide the required

training.

The procedures and standards group was created in late October 2006, to

centralize responsibility for maintenance and operations procedures, in response

to procedure-related site performance problems. The original staffing plan for the

group had eight vacancies, three of which were to be filled by hiring people

external to APS. In addition, the group hired nine contractors for a project to

enhance maintenance procedures. Because of difficulties in filling the open

positions and a growing backlog of procedure change requests, the maintenance

procedure improvement project was deferred and the contractors were assigned

to address the backlog. This action met the groups need for procedure writers

who were knowledgeable of maintenance practices. However, because of the

staffing limitations in the operations department discussed above, the group was

unable to recruit Palo Verde operations personnel to fill the in-house positions

and was seeking to hire experienced operators from other sites.

Licensee response to staffing and qualifications issues. The team noted that the

new senior managers have implemented an aggressive plan to recruit, hire, and

train new staff to overcome the current shortages and prepare for staff

retirements. In November 2007, the licensee had 226 open positions and was

actively seeking staff from outside of APS with the requisite skills and knowledge

of current industry standards and practices. Personnel to fill 50 of those open

positions had been identified and were expected to begin work at the site in

December 2007. In addition, the licensee had approximately doubled the

number of Legacy Program engineers, maintenance apprentices, and junior

- 135 - Enclosure

staff in other disciplines. Positions for new instructors have been authorized.

The licensee is also augmenting many staff capabilities with additional skilled

contractor personnel.

Since arriving at Palo Verde, senior managements highest priority has been to

recruit and train large numbers of operator candidates, including candidates for

non-licensed operator positions and instant SROs. The human resources

department recently hired an experienced nuclear recruiter to assist in the hiring

of personnel. In addition, the licensee hired four new operations training

instructors and was considering alternative approaches to increase training

instructors. During the inspection, senior management elected to advance the

schedule for a class for non-licensed operator candidates by five months. The

licensee also increased authorized staffing levels for the operations department

to 333 positions.

To maintain a more stable level of staffing within the security department, the

licensee was increasing the frequency of the security training academy to twice

per year and posting a continuously open vacancy announcement to establish a

training pipeline for security officers. The licensee was also considering

alternative methods to improve the retention of security personnel.

The licensee was taking steps to reduce barriers to recruiting, hiring, and

retaining staff. For example, APS had previously implemented a policy to

achieve compensation parity between engineers at Palo Verde and in the non-

nuclear business units of APS. This change caused several Palo Verde

engineers to take other, non-nuclear positions within APS to reduce stress or

shorten their commutes. Senior management worked with corporate decision-

makers to revise the policy and reduce the attrition of skilled engineers from the

site. The licensee has also authorized hiring and retention bonuses for targeted

skill sets and is offering reimbursement for relocation costs to some new hires.

Procedures and documentation. Interviewees uniformly indicated that station

procedures, work instructions, drawings, and other documentation necessary to

perform work were: (1) difficult to follow, (2) unnecessarily complicated, and

(3) sometimes inaccurate, incomplete, or inconsistent with regulatory and other

applicable requirements. Many procedures have become outdated over time.

Although these documentation deficiencies have been identified by the NRC and

the licensee as important contributing causes for Palo Verdes performance

decline, the team noted that licensee actions to correct this problem had been

ineffective in sustaining performance improvement.

The team observed that the licensees processes for managing procedures and

other critical documentation continued to be fragmented among various

organizations across the site. At the time of the inspection, the licensee had

identified the need for, but had not yet developed a comprehensive, integrated

approach to address the full scope of site-wide documentation deficiencies

(CRDR 3079100 - Programmatic Weaknesses in PV Programs, procedures, and

processes - ImPACT FOP 11 and safety culture, Apparent Cause Evaluation

Report, October 2007).

- 136 - Enclosure

The licensee had not determined whether to initiate a wholesale upgrade to its

existing maintenance and operating procedures to bring them up to current

industry standards or continue to address individual procedural deficiencies. As

previously discussed, the procedures and standards group initiated a project to

enhance maintenance procedures by ensuring the procedures incorporated

human factors good practices. However, the project was stopped and the

resources diverted when the backlog of procedure change requests began

increasing in 2007 as a result of management efforts to reinforce procedure use

and adherence expectations. Interviewees indicated that preliminary results of

the enhancement project were less than satisfactory to the procedure users, who

had been hoping for complete procedure rewrites. The team noted that the

availability of qualified staff in the maintenance and operations organizations may

not have supported the technical reviews and procedure validation activities that

a wholesale upgrade project would require.

Interviews also indicated that licensee personnel were aware of the implications

of the changing workforce at the site (i.e., increasing numbers of less

experienced staff) on the level of detail and usability of the sites documentation,

but have not developed a plan to address the issue. The deficiencies in current

procedures and work instructions were described as particularly problematic by

the less experienced personnel interviewed. These interviewees commented

that procedures and other documentation were not helpful as training tools, were

not written in plain language that could be understood without step-by-step

translation from a senior staff person, and that the level of detail in the

procedures was frequently inadequate for them to understand how to perform the

task. Because procedures and documentation were of limited usefulness to the

less experienced interviewees, these individuals were particularly concerned

about the loss of expert knowledge and guidance they rely on when senior

members of their work groups retire.

Facilities and equipment. Examples of longstanding degraded equipment

conditions identified by the team include, in part, Borg Warner check valves, post

accident monitoring chart recorders, radioactive waste systems, Target Rock

solenoid valves, and cable vault flooding. In addition, interviewees provided

numerous examples of degraded or inadequate facilities and equipment that they

described as challenging their ability to perform work effectively. Examples

included work spaces that were not air conditioned, being denied heat protection

when working outside during the summer, bird droppings in work spaces, frayed

and decaying safety harnesses, outdated and unreliable software, instruments

and test equipment that cannot be repaired because parts are no longer

available, security personnel being required to use personal vehicles to patrol

because there were an inadequate number of site vehicles, temporary power

and ventilation systems in workspaces that have been in-place for years, training

spaces too small to accommodate class sizes, inadequate access to desks,

computers and telephones, and inadequacies in the availability of simple items,

such as chairs, stools, shop cabinets, hand tools, or lockers for storing personal

belongings. Interviewees reported that they had raised these needs to their

supervisors, documented them in the CAP, but had been unsuccessful in

resolving the issues over long periods of time. The team concluded that the

staffs longstanding inability to resolve such issues contributed to the apparent

tolerance for degraded conditions the team has observed. The team also noted

- 137 - Enclosure

that new management was taking steps to address some of these concerns with

mechanisms such as the departmental Top 10 lists and the safety culture

improvement plans for some work groups.

Continuing challenges. Corporate and senior site management personnel have

repeatedly affirmed that the resources are available to address these issues.

The team noted that the licensees ability to make a rapid improvement in overall

site performance may be hampered by limitations in the availability of qualified

staff and that previous performance improvement efforts were partly ineffective

for similar reasons. Although senior management is taking aggressive steps to

augment staff capabilities, the productivity of inexperienced personnel will likely

be challenged until the improvement is made in programs, processes, and

procedures.

Licensee safety culture assessment. The team determined that the licensees

third-party safety culture assessment adequately captured these issues.

b.4 Continuous Learning Environment

The team determined that Palo Verde has not established a continuous learning

environment. Results of the licensees self-assessments, the licensees third-

party safety culture assessments, and the results of the NRCs safety culture

assessment concurred that the site had become insular over the past 15 years.

As a result of cost-containment efforts, the licensee curtailed benchmarking and

external training opportunities, the few new personnel who were hired between

1994 and 2003 were drawn from inside of APS, and internal training resources

were cut. Palo Verde personnel had little exposure to new practices and rising

standards in the nuclear industry.

Palo Verdes success in the 1990s created an attitude of arrogance, according

to many interviews. Interviewees reported this as another reason they stopped

sending people to other utilities on benchmarking trips or for training

opportunities. They saw themselves as a world-class nuclear plant that did not

need to learn from others. Interviewees indicated that this attitude had hampered

previous improvement efforts and led staff to dismiss information about current

industry practices and standards from new hires and contractors with broader

knowledge.

At the time of the inspection, the team did not identify any evidence that

personnel were resistant to new ideas or feedback on means to improve

individual and site performance. Interviewees were aware of planned

benchmarking activities and perceived that benchmarking was necessary to fully

understand and be able to implement new expectations and standards. As one

operator stated, I dont know what an operations-led organization looks like.

However, because of high workload levels, some interviewees predicted that

many of the planned benchmarking activities would be cancelled or curtailed.

Based on past experiences, some believed that lessons learned from

benchmarking activities would not result in improvements at the site because

they would be judged by management to be unnecessary enhancements that

would just add to the work groups workload, when workload was already

excessive.

- 138 - Enclosure

Many interviewees also expressed the desire for more technical training. This

was particularly true of the engineering groups. Focus group participants and

individual interviewees were generally dissatisfied with the technical training they

received because it had become solely focused on maintaining qualifications

rather than enhancing knowledge and skills. Interviewees attributed the

perceived training deficiencies to staffing shortages in the training function and

restricted resources allocated to training. Some newer employees reported that

they had elected to supplement the training they received from the organization

by using personal funds to travel to conferences, attend seminars, or take

classes because management would not pay for these activities.

Frontline and supervisory personnel and most middle managers interviewed

believed that knowledge transfer was one of the more important challenges

facing the site. Frontline and supervisory staff perceived that: (1) site

procedures are particularly difficult for new hires to understand and follow and

they were not aware of any plans to revise the procedures to make them more

usable by new employees; (2) there have been limitations in the quality of

training materials and the training provided to new employees that did not

adequately prepare them for work in the field; (3) hiring plans within their work

groups did not appear to take into account the length of time required for new

employees to become fully qualified and effective in their jobs; and (4) the hiring

plans did not take into account the additional workload that mentoring new staff

imposes on the senior staff. The interviewees indicated that the consequences

they experienced from the perceived inadequacies in ensuring knowledge

transfer have included an increase in human errors in job performance and on-

the-job injuries from inexperienced employees who are unfamiliar with an

industrial environment, as well as increased difficulty in managing current

workloads. The interviewees perceived that these problems have further

contributed to the sites backlogs.

Licensee response. In addition to accelerating the hiring of new staff and training

personnel, the licensee was beginning to address the knowledge transfer

challenges. The human resources department had developed a tool to aid

managers in planning for the upcoming retirements in their work groups. Human

resources had also developed and recently pilot-tested a knowledge

management assessment tool to aid managers in understanding the scope of

knowledge those personnel who were retiring would take with them. The tool

could be used to identify new-employee training needs. The licensee has also

retrained line managers in the systematic approach to training to improve their

ability to ensure that training programs are effective. Senior management has

also established the expectation with middle management that they, rather than

the training department, own and are therefore responsible for the quality of

training provided to their work groups.

Continuing challenges. The overhead costs associated with transitioning to an

effective continuous learning organization are formidable. Adding and training a

large number of new personnel, while at the same time increasing the work

output from the existing workforce, will require personnel to do more than just

work harder. Substantial productivity increases will be necessary to sustain this

environment in the long-term. Site productivity will also be challenged by the

expected loss of experienced personnel.

- 139 - Enclosure

Licensee safety culture assessment. The team determined that the licensees

third-party safety culture assessment adequately captured these issues, but did

not fully explore their implications.

b.5 Accountability

The team observed that a positive consequence of the sites reengineering effort

was to create a strong sense of empowerment, individual responsibility for site

performance, and pride in the site within the workforce. This sense of ownership

was evident in: (1) the number of individuals who provided detailed write-in

comments on the licensees safety culture surveys in 2005 and 2007 (over half of

the respondents on the latter); (2) the personnel who called the NRCs

confidential hotline established for the inspection to request an interview simply

to ensure that the team had their insights regarding the reasons for the

performance decline at Palo Verde and what is needed to improve; (3) the many

statements by focus group participants that they had been raising concerns

about degrading site performance and offering improvement suggestions to

management as early as 2001/2002, as documented in CRDRs, white papers, or

PVARs provided to the team; and (4) the demonstrated willingness of personnel

during the inspection to challenge ARRC decisions and submit repeat PVARs to

attempt to ensure that their concerns were fully understood and classified

appropriately. However, as previously described, a similar number of focus

group participants expressed frustration that they were not fully aware of site

performance improvement plans or how they could make an individual

contribution.

When the team raised the issue of accountability in focus groups, personnel

expressed a strong willingness to be held accountable for individual and site

performance but were frustrated by what they perceived as the failure of past

senior management and some of their middle-managers to be accountable to

them. The context for these comments was generally in relation to having the

resources to fix equipment and procedures, obtain training, replace personnel

who had left their work groups, and the ability to perform work to their standards

without excessive schedule or cost-containment pressures or interference with

their views of the right way to perform a task. Several individuals reported that

they had used the recently disseminated standards and expectations and

industry safety culture principles booklets to challenge management decisions or

actions they perceived as being inconsistent with the goals expressed in the

documents.

Interviewees also discussed the difficulties of holding co-workers accountable in

the face of the many long-standing personal and professional relationships they

have developed at the site and in the community (20 years or more among the

majority of the workforce). Interviewees discussed the barriers to challenging the

work products and behavior of long-term colleagues who have become close

friends when those work products or behaviors were professionally

unacceptable. Some personnel self-reported the choice to accept inadequate

work products and behavior to avoid conflict in these close relationships.

Conversely, interviewees also noted the long-standing adverse effects of past

interpersonal conflicts that had not been resolved. In these instances,

interviewees described conscious efforts to avoid interacting with the individuals

- 140 - Enclosure

with whom they had previous conflicts. The team noted that these conflict-

avoidant behaviors contributed to the observed siloing (i.e., lack of cooperation)

between some functional groups, as well as the failure of staff to hold one

another accountable for meeting their own and the new managements

standards. However, during the inspection, several interviewees reported that

they were changing their conflict-avoidant behavior to support the need for

performance improvement. These individuals described incidents in which they

had personally rejected work products from other organizations that did not meet

their standards and worked with the other organization to provide an acceptable

product.

The team determined that the behavior of site personnel did not consistently

reflect the strong, positive attitudes they expressed regarding their willingness to

hold themselves accountable as well as to be held accountable by management.

The examples of human performance deficiencies described earlier in this report

indicated that personnel had not yet internalized senior managements new

standards and expectations in individual behavior.

Licensee safety culture assessment. The team determined that the licensees

safety culture assessment adequately captured these issues.

b.6 Corrective Action Program

The team identified several concerns in the corrective action safety culture

component associated with problem identification, evaluation, and effective

corrective actions. This safety culture component was assessed primarily

through direct inspection activities.

Specific problem identification concerns during this inspection involved

implementation of emergency action levels, the emergency exercise critique

process, and solenoid valve performance in the auxiliary feedwater system. As

previously discussed in this report, the team identified an apparent reluctance or

inability among some personnel to identify issues as conditions adverse to quality

without prompting. The team determined that this reluctance or inability was a

safety culture weakness.

Specific problem evaluation concerns during this inspection involved condensate

storage tank temperatures, scaffolding procedures, post-accident monitoring

instruments, emergency diesel generator oil leaks, emergency action levels,

operability determinations, and the conduct of the corrective action review board

and ARRC. The team noted that the licensees problem evaluations lacked

depth and rigor and were generally inconsistent with current industry standards

and practices. The team determined that the observed lack of depth and rigor

was a safety culture weakness.

Specific corrective action concerns during this inspection involved high lead

levels in a low pressure safety injection pump bearing, 4160 and 480V motor

terminations, establishment of maintenance rule criteria, and multiple databases

to track deficient conditions. The team noted that corrective actions for these

issues had not been completed or had not been effective, which the team

determined represented a safety culture weakness.

- 141 - Enclosure

Multiple substantive crosscutting aspects associated with problem identification,

evaluation and resolution have existed since 2004. Corrective actions have

continued to be ineffective in improving performance as noted by effectiveness

reviews, external industry reviews, and NRC inspections.

The team determined that the licensees CAP, while complicated and

cumbersome, contained the basic elements of an effective program. Licensee

personnel often recognized appropriate problem identification, evaluation and

resolution fundamentals and behaviors when interviewed; however, this

knowledge and understanding of expectations was not consistently demonstrated

in meetings or in the field over the course of the inspection.

Licensee response: The licensees plan to improve the corrective action program

was incomplete at the time of the inspection. However, the draft plan available

for review addressed the majority of the teams concerns.

Licensee safety culture assessment. The team determined that the licensees

safety culture assessment adequately captured these issues.

b.7 Work Practices

The team identified several concerns in the work practices area. This safety

culture component was primarily assessed through direct inspection activities.

Work practice human performance concerns observed during this inspection

included: (1) Poor human error prevention techniques involving transient

combustibles in the containment building and temporary shielding installation;

(2) poor procedure compliance findings involving transient combustibles in the

auxiliary building and radiological surveys; (3) inadequate management oversight

for findings involving compliance with Technical Specification Surveillance

Requirement 3.0.3, and rigging of the Unit 3 air lock door; and (4) operations

personnel conduct of operations weaknesses, including turnovers, three-way

communications, alarm response, crew briefs, control room logs, and oversight of

switchyard activities.

Work practice concerns have also been a longstanding issue and performance

improvement actions have not sustained improvement as noted by effectiveness

reviews, external industry reviews, and NRC inspections. In particular, the

licensees effectiveness review for human performance concluded that corrective

actions were not well defined and there were no actions for implementation,

monitoring, reinforcement, adjustment, or for managing the transfer of

responsibility for human performance program changes. Furthermore, the

corrective actions for past human performance problems were not fully

implemented.

Interviews indicated that some personnel had begun implementing new work

practice standards and expectations. For example, several interviewees

described recent incidents during which they had stopped work in the face of

uncertainty (e.g., an incorrect procedure or work order instructions that did not

apply to the specific job) or what they perceived to be unsafe job conditions.

However, the team noted that these and other desirable work practices were not

yet consistently implemented by site personnel.

- 142 - Enclosure

b.8 Work Control

The team identified several concerns in the work control area. This safety culture

component was primarily assessed through direct inspection activities. Work

control human performance concerns observed during this inspection included

weaknesses in communications between fire protection, operations, engineering,

and maintenance, which contributed to findings associated with transient

combustible material controls, switchyard maintenance activities, establishment

of compensatory measures for incorrectly installed sprinklers, establishing

performance criteria for plant systems, and installing emergency lighting in

containment.

Work control concerns have been a longstanding issue and performance

improvement actions have not sustained improvement as noted by effectiveness

reviews, external industry reviews, and NRC inspections. In particular, the

licensees effectiveness review for human performance concluded that corrective

actions were not well defined and there were no actions for implementation,

monitoring, reinforcement, adjustment, or transfer of human performance

ownership change. Furthermore, the corrective actions were either not fully

implemented or not implemented as intended.

b.9 Operating Experience

The team identified several concerns in the OE area. This safety culture

component was assessed through direct inspection activities. OE opportunities

were frequently missed, ignored or misapplied. A lack of technical rigor was

frequently cited in component design basis reviews and self assessments with

respect to the application of OE. The station did not appear to have a sense of

the importance and benefits of a strong OE program. The failure to incorporate

OE into daily activities is an open issue from the Yellow finding. In addition, the

failure to effectively use OE contributed to several performance deficiencies

identified by the team. Specific examples of ineffective use of OE during the

inspection involved AF TT&V, Target Rock reed switches, Borg Warner check

valves, and switchyard maintenance activities.

b.10 Self and Independent Assessments

The team identified several concerns with self assessments. This safety culture

component was assessed through direct inspection activities. Self-assessments

conducted by Palo Verde personnel often lacked depth and did not effectively

specify or implement corrective actions. As a result, the self-assessment

program seldom resulted in improved organizational performance. Self-

assessment corrective actions were not always tracked nor were corrective

action documents always written to track the expected actions. The team noted

that self assessments conducted by a mix of Palo Verde and industry personnel

led to more meaningful results.

Specific examples of poor self assessment implementation involved vague

recommendations in the November 2006 operational decision-making self-

assessment; the March 2007 work management self-assessment concluded only

that the assessment needed to be re-performed later in 2007; the self-

- 143 - Enclosure

assessment of the maintenance rule program did not recognize that unavailability

and reliability performance criteria could not be validated, that numerous systems

had non-conservative performance criteria, and that switchyard risk reviews were

not consistently performed; and deficiencies from the assessment of the safety

injection system and the assessment of the environmental qualification program

were not entered into the CAP.

b.11 Environment for Raising Concerns

The team determined that the environment for raising concerns was healthy.

None of the licensee employees interviewed by the team indicated they were

hesitant to raise nuclear safety issues and about 25 percent of those interviewed

gave examples of occasions where they had willingly raised an issue multiple

times. These included occasions when the individuals believed that the CAP had

failed to prioritize an issue appropriately or had not timely or effectively resolved

an issue. The large majority of interviewees perceived that their managers were

receptive to concerns and willing to address them, although they also reported

frustration with the organizations ineffectiveness at resolving longstanding issues

such as obtaining replacements for out-dated equipment, completing repairs on

equipment within an acceptable timeframe, and delays in hiring and qualifying

personnel in time to replace those who had left their work groups or the site.

The team identified very few examples of recent incidents or perceptions of

retaliation for raising safety concerns. Some interviewees described isolated

examples of past incidents that created a perception of retaliation but the

licensee had effectively mitigated those perceptions.

Almost all of the interviewees stated that if they were not satisfied with the

response from their immediate supervisor, they would feel free to escalate the

concern. The interviewees uniformly described positive experiences when

bringing issues to their supervisors and could name several other avenues for

raising concerns. The majority of interviewees explained that approaching their

supervisors and using the CAP to raise concerns had been generally effective to

communicate the concerns (although less effective in resolving them), and

therefore, they have not had the need to use other alternative avenues.

The team noted some differences in the willingness of contractors to raise

concerns compared to licensee employees. About 5 percent of the contractors in

the focus groups stated that they had not been trained in how to write a PVAR or

expressed reluctance to doing so for fear of being viewed as a troublemaker.

Consistent with these perceptions, the Employee Concerns Program (ECP) had

received several concerns involving contractor personnel in the month before the

team arrived on site. In response to those concerns, the licensee reinforced

expectations for maintaining a safety conscious work environment (SCWE) in all

contract organizations. The ECP sent a letter describing the appropriate SCWE

duties and obligations to each contract organization, which became a part of the

contracts terms and conditions. In addition, senior management took steps to

integrate contractor supervisors and managers into alignment and other

meetings to better communicate SCWE expectations.

- 144 - Enclosure

b.12 Preventing, Detecting, and Mitigating Perceptions of Retaliation

Palo Verde had an Integrated Issues Resolution Process (IIRP) comprising the

ECP, the Differing Professional Opinions (DPO) Program, the Management

Issues Tracking Resolution (MITR) program, and the PVAR. A fifth, recently

implemented corporate-level program, called EthicsPoint, was available for

raising ethical concerns or conflicts with the corporate code of conduct, although

no-one at the site had used EthicsPoint since it was implemented in early 2007.

The combined IIRP included these five alternative avenues for raising concerns

at Palo Verde.

Employee Concerns Program. Most individuals interviewed by the team were

aware of the ECP. Interviews indicated that a few groups, primarily contractors,

had not heard of the ECP or received any information or training about the

program. Many interviewees did not have personal experience with the ECP

because they had not needed to use the program. The majority of those

interviewed said that they would raise an issue through their chain-of-command

first, and if that didnt work they would take their concern to the companys DPO

program instead of using the ECP. The inspection team identified a

misconception about the purpose of the ECP among many of the staff

interviewed. The most common view was that the ECP is to be used for human

resource (HR) issues, which the licensee normally processes through the MITR

program, rather than for nuclear safety concerns. When the inspection team

discussed this issue with the ECP manager, she indicated that she was aware of

the issue and believed this misconception may exist because she formerly was

the HR manager. Some interviewees thought that the ECP was not objective

because it was linked to senior management. Also, several interviewees told the

team that they did not trust the ECP, but were unable to give examples to

support the distrust. Personnel interviewed who had used the ECP in the past

indicated that the experience was positive, and that they would not hesitate to

use the ECP again if needed. No interviewees were aware of any breaches of

confidentiality.

The team reviewed 36 ECP files from 2007 related to SCWE issues. The team

determined that the concerns had been reviewed thoroughly and dispositioned

appropriately.

The ECP manager had received approval from senior management to conduct

extensive benchmarking at other nuclear facilities. This effort has been funded in

the 2008 budget. The ECP manager planned to contact the ECP managers at

several other sites to obtain information about how other programs write reports,

apply policies and guidelines, and advertise their programs. The effort will

include reviewing performance indicators and methods for using the programs

metrics to better educate management about resolution of issues. One of the

other areas to be pursued is how other sites integrate safety issues into their

CAPs without compromising confidentiality.

The ECP manager was actively working to increase the awareness of the

program by making the program more visible at the site. The ECP manager had

recently hired two new ECP investigators, and was planning to hire a third with

- 145 - Enclosure

greater technical knowledge to better ensure that each concern is assessed

appropriately. Interviewees indicated that the ECP staff was well known, well

liked, and approachable.

The ECP was developing a plan to re-market the program. Since its integration

into the IIRP, the ECP has lost some of its identity to the Palo Verde staff. The

ECP manager planned to work with the communications department to develop a

new way to communicate the purpose of the ECP without losing integration with

the IIRP.

Differing Professional Opinions Program. The DPO program was an avenue for

resolving technical disagreements between staff members. The process

required an independent third party with appropriate technical knowledge to

review both sides of the issue and negotiate an acceptable resolution to the

problem. After the review is complete, both parties have the option to agree with

the resolution. If there is no agreement, the initiator may choose to escalate the

issue to the senior management team for resolution where the final decision will

be made by the site vice president/CNO. The team reviewed seven recently

closed DPO files and concluded that the DPO process was effective.

Management Issues Tracking Resolution Process. The MITR process was

designed to resolve personnel issues arising between management and staff and

was managed by the HR department. As previously mentioned, the team noted

some confusion among the staff as to the purpose of this process and took

personnel issues or concerns to the ECP more frequently than to HR. Many of

those interviewed had never heard of the MITR process. The team reviewed all

MITR files from 2007 and determined that the issues had been investigated and

resolved effectively.

Retaliation and the Disciplinary Review Board. Approximately 98 percent of the

interviewees stated that they had not experienced, nor heard of any issues of

retaliation, harassment, intimidation or discrimination at Palo Verde. Some

interviewees expressed concern that new accountability standards for industrial

safety might lead to future perceptions of retaliation, but the team noted that the

licensee was working to quell those impressions.

The licensees Disciplinary Review Board (DRB) screened disciplinary actions for

evidence of retaliation. The team reviewed several examples of the DRBs

efforts to ensure that controversial terminations were not viewed by staff as being

retaliatory. One example was a case where an individual had been terminated

because of a fitness-for-duty (FFD) violation. Management worked with the line

organization to explain the FFD process and the reasons why an employee might

be fired for violating FFD standards. This communication successfully diffused

the rumors surrounding this particular termination.

At the time of the inspection, the DRB did not review actions involving contractor

personnel, but the ECP and HR were assessing the need to expand the scope of

the program. Both organizations were benchmarking disciplinary review

processes at other sites to better understand how Palo Verde can revise its own

process to include contractor actions and ensure that all disciplinary actions are

thoroughly reviewed for perceptions of retaliation.

- 146 - Enclosure

Employee Dispute Resolution Process. The Employee Dispute Resolution

(EDR) process was a corporate-level program that allows an employee to dispute

a disciplinary action. There were three steps in the process. The first step

requires the individual to present the dispute and request resolution from his or

her direct supervisor. If the employee does not agree with the supervisors

response, the employee can appeal the issue to the HR manager. At this second

step, the HR manager assigns a representative to investigate the dispute and

propose a solution that is acceptable to both the employee and supervisor.

When a disciplinary action or termination takes place, or if the result of Step 2 is

not acceptable to the individual, he or she has a choice to request a review of the

action taken by either the APS Corporate Vice President of HR or from a review

panel. Employees may dispute the nature or severity of the impending discipline.

During the review, the management team will try to ensure that the employee is

able to openly discuss their opposition to the action. Once the review takes

place, the decision to change the disciplinary action must be made within 10

working days.

The teams review of the EDR process indicated that the EDR generally reduced

the level of discipline applied, but there were no terminations that had been

reversed as a result of the process. The team determined that this process was

effective in resolving employee disputes involving disciplinary actions.

b.13 Safety Policies

The team concluded that Palo Verdes safety policies and training related to

safety culture and the safety conscious work environment were appropriate.

Interviews indicated that the new senior management team was generally

perceived as believable in their emphasis on nuclear safety and as walking the

talk. Focus group participants who had exercised the new senior managers

invitations to send an email or other communication regarding concerns or

suggestions commented favorably that their issues were taken seriously and, in

most cases, resulted in action. Consistent with the results of the licensees

safety culture assessment, the NRC team determined that most personnel

interviewed were cautiously optimistic that the new senior management team

can be trusted to improve performance at the site.

9.0 REVIEW OF YELLOW FINDING - CONTAINMENT SUMP VOIDING

Before commencing the inspection, the licensee informed the NRC that they were not

prepared to support a closure review of the corrective actions associated with the Yellow

finding. Consequently, the team only reviewed the licensees progress in addressing the

Yellow findings performance concerns.

The team identified that the licensee was unable to effectively track the completion of

corrective actions associated with the two NRC IP 95002 supplemental inspections and

had not evaluated the effectiveness of corrective actions taken for this item. The inability

of the licensee to resolve the Yellow finding performance deficiencies contributed to

several of the violations documented in this report.

- 147 - Enclosure

a. Inspection Scope

The team reviewed the status of the implementation and completion of corrective

actions associated with a Yellow finding previously issued to Palo Verde regarding the

voiding of ECCS piping in all three units. The team evaluated the results of previous

NRC IP 95002 inspections related to this finding, as well as prior Palo Verde

performance improvement plans and corrective action plans. The team also reviewed

a recent audit of these corrective actions conducted by Palo Verde.

b. Observations and Findings

On October 24, 2007, the team reviewed the July 2004 Yellow finding to determine if

the associated corrective actions had been completed and if they had been assessed

by the licensee as effective. The root cause analysis for the Yellow finding identified

several deficiencies which were segregated into 10 focus areas. These 10 focus

areas were assigned to individual licensee managers or focus area owners. The

December 12, 2005, and the October 11, 2006, NRC IP 95002 inspections determined

that the corrective actions for these deficiencies were not completed. The areas of

concern involved questioning attitude, technical rigor, technical review, the

establishment of performance measures and metrics, and the use of OE. PVNGS

responded to the NRC in a November 16, 2006, letter detailing further commitments in

completing these corrective actions by March 30, 2007.

In June 2007, the licensee completed an IP 95002 effectiveness review and concluded

that they had not maintained current documentation of the project which precluded an

accurate status assessment of the corrective actions. The checklist used for this

effectiveness review described several reasons for non-completion of the corrective

actions, including: improper alignment of the corrective action to the root cause;

corrective actions not assigned as CRDRs and CRAIs (which did not allow for

assessment of corrective action completion); CRDR and CRAI completion dates being

extended several months past original due dates; and the lack of metrics to measure

effectiveness (originally scheduled for completion by December 1, 2006). An

additional issue was that no effectiveness reviews (effectiveness reviews of

engineering products was originally scheduled to be complete by February 1, 2007)

were conducted to insure proper closure of corrective actions.

Following discussions with the licensee, the team determined that in early 2007, when

it was known that Unit 3 was entering Column 4, the focus area owners assumed that

the IP 95002 corrective actions would be integrated into the IP 95003 process. During

this period a new senior management team was arriving and it was assumed by the

focus area owners that a new plan would be developed for site improvement. As a

result, the IP 95002 corrective actions were administratively forgotten as stated in the

evaluation report and PVAR 3030058, which identified this deficiency on

June 19, 2007. The licensee initiated CRDR 3031092 to resolve their inability to

address the Yellow finding performance concerns.

10 REVIEW OF WHITE FINDING - EMERGENCY DIESEL GENERATOR K-1 RELAY

Prior to the performance of the inspection, the licensee indicated they had not completed

the effectiveness reviews of the root causes and corrective actions associated with the K-1

relay failure. Consequently, the team reviewed the licensees progress and did not

- 148 - Enclosure

complete an assessment using IP 95001. A subsequent inspection will be completed

using IP 95001 as part of the NRCs review of the items described in the Confirmatory

Action Letter dated June 21, 2007.

a. Inspection Scope

The team reviewed the licensees assessment of the White finding associated with the

Unit 3 K-1 relay to assure that the root causes and contributing causes of the risk

significant performance issues were understood. In addition, the team reviewed the

extent of condition and corrective actions to verify that they were sufficient to address

the root causes and contributing causes, and to prevent recurrence.

Specifically, CRDR 2926830, Unit 3 Diesel Generator K1 Contactor Repeat Failure,

Revision 3, dated September 20, 2007, was reviewed using the guidance provided in

IP 95001. CRDR 2926830, incorporated the results of the Palo Verde ImPACT Team

review to correct inadequacies in the previous revision of the root cause investigation.

In addition, Revision 2 of this document was reviewed, along with APS

Correspondence 102-05626-CDM/SAB/JAP/CJS from D. Mauldin to US NRC, dated

January 9, 2007, responding to NRC Inspection Report 05000528; 05000529;

05000530/2006012 and a draft copy of the K-1 Relay Issue Problem Development

Sheet, dated July 26, 2007, used by the licensee to evaluate and address the

inadequacies in earlier root cause investigations of this problem.

b. Observations and Findings

The team considered the technical analysis provided in the root cause investigation

analysis to be adequate. However, the team observed several examples where the

investigation could have been more technically rigorous or the investigators should

have had a more questioning attitude. Specifically:

1) Root Cause 1 stated that the K1 relay was treated as a single replaceable

component; however, there were no design documents or drawings of this safety-

related relay found in the PVNGS nuclear records as stated in the Overview of K1

Contactor History.

2) The discovery, during troubleshooting, of variations of straight and bent actuator

arms without corroborating drawings may have indicated that field modifications

had been made at some time in the past and thus may have invalidated the original

equipment qualification.

3) The decision to "adjust and field straighten" the actuator arms may have

invalidated the equipment qualification. Metal fatigue and spring compression

issues are mentioned; however, other qualification issues such as seismic

qualification were not.

4) The report was not rigorous in documenting the extent of condition. Specifically,

the K1 relay condition could have also existed in the other two units at the same

time; thereby, having an impact on plant risk at the other two units. The Safety

Significance section, as it was written, potentially indicated a lack of appreciation

by the licensee of the impact that the inoperability of safety systems and

components had on plant risk.

- 149 - Enclosure

11 LICENSEE-IDENTIFIED VIOLATIONS

The following violations of very low significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI.A of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs:

a. Technical Specification 5.4.1.a requires written procedures to be established,

implemented, and maintained covering the activities specified in Regulatory

Guide 1.33, Quality Assurance Program Requirements (Operations), dated

February 1978. Regulatory Guide 1.33, Appendix A, Item 1.l, Plant Fire Protection

Program, requires, in part, procedures for plant fire protection. Procedures

14DP-0FP34, Fire Watch Duties, and 14DP-0FP36, Hot Work Permit, stated that in

the event of a fire, notify the fire department by calling the site emergency extension

(i.e., contact security who contacts the control room). Contrary to this requirement,

personnel notified the site fire department via the normal fire department extension

vice the site emergency extension following a small fire in Unit 3 on October 5, 2007.

This resulted in the control room not being notified of the fire until several hours after

the fire started, which impacted the ability of the SM to implement the EAL assessment

process. The licensee subsequently determined that no EAL classification would have

been required since the fire lasted less than five minutes. The licensee entered this

item into the CAP as PVARs 3071922 and 3071994. This finding was determined to

be of very low safety significance because it did not result in a missed emergency

classification.

b. 10 CFR Part 50, Appendix B, Criteria XVI, Corrective Action, requires the licensee to

take appropriate and timely corrective action for conditions adverse to quality. The

inspectors reviewed CRAI 2942350 that addressed training for chemistry personnel on

changes to the 10 CFR 50.59 Guidance Manual. Some Chemistry personnel had not

attended the training and the CRAI was closed as complete. This corrective action

was in response to the ESP chemistry issues which resulted in the fouling of the EDG

heat exchanger in 2006. The licensee did review procedures that were revised by

these personnel that had not attended this training. The licensee performed an extent

of condition and found one individual that was not qualified on applicability

determinations had performed applicability determinations with supervisor permission

because they thought the individual was qualified to perform applicability

determinations after attending chemistry training in November 2006. Additionally, as a

follow up to PVAR 3009064, dated May 4, 2007, the team reviewed an additional nine

CRDRs reported in 2005, four CRDRs in 2006 and eleven CRDRs as of

October 5, 2007 related to personnel performing safety-related and non-safety-related

activities without proper qualifications. No items of significance were identified. This

event was documented in the licensees CAP as PVARs 3073306 and 3082659. This

finding is of very low safety significance because the licensee concluded that the

procedures that were changed and the tasks that were performed did not contain

significant errors and had not resulted in the need to perform an evaluation for

applicability determinations.

c. Technical Specification 5.4.1.a requires, in part, that written procedures be

established, implemented, and maintained covering the activities specified in Appendix

A of Regulatory Guide 1.33, "Quality Assurance Program Requirements (Operations),"

dated February 1978. Regulatory Guide 1.33, Appendix A, Section 9a, requires

maintenance that can affect safety-related equipment be properly preplanned and

- 150 - Enclosure

12 MANAGEMENT MEETINGS

On December 19, 2007, a public meeting was held to present the results of the inspection

to Mr. R. Edington, Senior Vice President, Nuclear, and other members of the licensees

staff. The licensee acknowledged the inspection results. Proprietary information was

reviewed during the inspection. The proprietary information was returned to the licensee

and was not included in this inspection report.

On December 19, 2007, a public meeting was conducted following the IP 95003 exit

meeting to discuss the licensees performance improvement initiatives.

- 151 - Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

G. Andrews, Director, Performance Improvement

S. Bauer, Director, Regulatory Affairs

R. Bement, Vice President, Nuclear Operations

P. Borchert, Director, Operations

P. Brandjes, Department Leader, Maintenance

R. Buzard, Senior Consultant, Regulatory Affairs

D. Carnes, Director, Nuclear Assurance

P. Carpenter, Department Leader, Operations

R. Cavalieri, Director, Outages

K. Chavet, Senior Consultant, Regulatory Affairs

D. Coxon, Unit Department Leader, Operations

R. Edington, Senior Vice President, Nuclear

D. Elkington, Consultant, Regulatory Affairs

J. Gaffney, Director, Radiation Protection

T. Gray, Department Leader, Radiation Protection

K. Graham, Department Leader, Fuel Services

M. Grigsby, Unit Department Leader, Operations

M. Grissom, Section Leader, Reactor Engineering

J. Hesser, Vice President, Engineering

M. Karbasian, Director, Engineering

D. Marks, Section Leader, Regulatory Affairs

S. McKinney, Department Leader, Operations Support

J. Mellody, Department Leader, PV Communications

E. ONeil, Department leader, Emergency Preparedness

M. Radspinner, Section Leader, Systems Engineering

T. Radtke, General Manager, Emergency Services and Support

H. Ridenour, Director, Maintenance

F. Riedel, Director, Nuclear Training Department

M. Shea, Director, ImPACT Team

E. Shouse, Representative, EPE

M. Sontag, Department Leader, Performance Improvement

D. Straka, Senior Consultant, Regulatory Affairs

J. Taylor, Unit Department Leader, Operations

D. Vogt, Section Leader, OPS STA

T. Weber, Section Leader, Regulatory Affairs

J. Wood, Department Leader, Nuclear Training Department

NRC Personnel

M. Runyan, Senior Reactor Analyst

A-1 Attachment

Items Opened and Closed

Item Number Type Description

05000528; 05000529; NCV Eight Examples of the Failure to Implement the

05000530/2007012-01 Operability Determination Process

05000528; 05000529; NCV Failure to Implement Adequate Design Controls for

05000530/2007012-02 Condensate Storage Temp.05000530/2007012-03 NCV Inadequate Installation of Fire Sprinklers

05000528; 05000529; NCV Six Examples of a Failure to Implement the

05000530/2007012-04 Corrective Action Program Requirements

05000528; 05000529; NCV Failure to Evaluate Performance Monitoring Criteria

05000530/2007012-05 for Auxiliary Feedwater System

05000528; 05000529; NCV Failure to Meet Technical Specification Surveillance

05000530/2007012-06 Requirement 3.6.6.6

05000528; NCV Failure to Meet Technical Specification Surveillance

05000529/2007012-07 Requirement 3.0.3

05000530/2007012-08 NCV Two Examples of a Failure to Maintain Control of

Transient Combustibles05000530/2007012-09 FIN Failure to Install Emergency Lighting in Containment

Prior to Work Commencement

05000530/2007012-10 NCV Failure to Follow Procedures for Temporary

Shielding Installation

05000528; 05000529; NCV Inadequate Implementation of Risk Management

05000530/2007012-11 Actions and Risk Assessments for the Switchyard

05000530/2007012-12 NCV Incorrect Rigging of Personal Airlock Door

05000530/2007012-13 NCV Failure to Maintain Configuration Control of

Pressurizer Instrument Condensing Pot Support

Brackets

05000528; 05000529 NCV Failure to Implement Maintenance Rule

05000530/2007012-14 Requirements for the High Pressure Safety Injection

System

05000528; 05000529; NCV Inability to Implement Emergency Action Levels05000530/2007012-16

05000530/2007012-17 NCV Inadequate Briefings of Radiological Conditions05000529/2007012-18 NCV Failure to Periodically Update the Updated Final

Safety Analysis Report

Items Opened

05000528; 05000529; AV Failure to Correct a Risk Significant Planning

05000530/2007012-15 Standard

05000528; 05000529; URI Routine Heavy Use of Overtime

05000530/2007012-19

A-2 Attachment

List of Acronyms

ACC Arizona Corporate Commission

ACT Action Tracking System

ADAMS Agencywide Documents Access and Management System

ADV atmospheric dump valve

ALARA as low as reasonably achievable

AF auxiliary feedwater

APS Arizona Public Service

ARRC Action Request Review Committee

AT activity tracking

ATC at-the-controls

CAL Confirmatory Action Letter

CAP corrective action program

CAPR corrective action to prevent recurrence

CARB corrective action review board

CCDP conditional core damage probability

CDBR component design basis review

CDF core damage frequency

CFR Code of Federal Regulations

CRAI condition report action item

CRDR condition report/disposition request

CRS control room supervisor

CS containment spray

CST condensate storage tank

DPO differing professional opinion

DRB Disciplinary Review Board

EAL emergency action level

EC emergency coordinator

ECP Employee Concerns Program

ECCS emergency core cooling system

ECE engineering change evaluation

ED emergency director

EDG emergency diesel generator

EDR Employee Dispute Resolution

EOP emergency operating procedure

EP Emergency Plan

EPIP Emergency Plan Implementing Procedure

EQ environmental qualification

ESP essential spray pond

EW essential cooling water

FA functional assessment

FFD fitness-for-duty

FOP fundamental overall problem

FP fire protection

GPH gallons per hour

HEP human error probability

HPSI high pressure safety injection

A-3 Attachment

IIRP Integrated Issues Resolution Process

IMC Inspection Manual Chapter

ImPACT improved performance and cultural transformation

ISCPET Independent Safety Culture Performance Evaluation Team

ISLOCA intersystem loss of coolant accident

IP Inspection Procedure

JPM job performance measure

KART key attribute review team

LER Licensee Event Report

LERF large early release frequency

LPSI low pressure safety injection

LOCT licensed operation cycle training

LOOP loss of offsite power

MITR Management Issues Tracking Resolution

MR maintenance rule

NCR nonconformance report

NPSH net positive suction head

NRC U.S. Nuclear Regulatory Commission

O&M Operations & Maintenance

OD operability determination

ODMI operational decision making instruction

OE operating experience

PAL personnel airlock

PAR Protective Action Recommendation

PC performance criteria

PDS problem development statement

PI&R problem identification and resolution

PM preventative maintenance

PPM parts per million

PSF performance shaping factor

PSIA pounds per square inch absolute

PVAR Palo Verde action request

PVNGS Palo Verde Nuclear Generating Station

RP radiation protection

RVLMS reactor vessel level monitoring system

SCWE safety conscious work environment

SRP Salt River Project

SDC shutdown cooling

SGTR steam generator tube rupture

SIBP Site Integrated Business Plan

SIIP Site Integrated Improvement Plan

SM shift manager

SMART specific, measurable, achievable, reasonable, and timely

SPAR Standardized Plant Analysis Risk

SOV solenoid operated valve

SQFT square foot

SRO senior reactor operator

SSC structures, systems, and components

A-4 Attachment

STA shift technical advisor

SWMS site work management system

SWYD switchyard

TCCP transient combustible controls permit

TDS total dissolved solids

TID total integrated dose

TGO transmission/generation operations

T&TV trip and throttle valve

TS Technical Specification

TSSR Technical Specification Surveillance Requirement

UFSAR Updated Final Safety Analysis Report

URI unresolved item

WO work order

A-5 Attachment