Potentially Unqualified Component in Certain Allen Bradley Timing RelaysML16232A604 |
Person / Time |
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Site: |
Millstone, Browns Ferry, Nine Mile Point, Perry, Saint Lucie, North Anna, River Bend, Ginna, South Texas, Fort Calhoun |
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Issue date: |
08/15/2016 |
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From: |
Bolt T AZZ / NLI Nuclear Logistics |
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To: |
Document Control Desk, Office of Nuclear Reactor Regulation |
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References |
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51030 |
Download: ML16232A604 (9) |
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Category:Deficiency Report (per 10CFR50.55e and Part 21)
MONTHYEARML23348A3942023-12-14014 December 2023 Interim Part 21 Report of a Potential Deviation or Failure to Comply Associated with Starter Contactors for the High Pressure Coolant Injection Suppression Pool Inboard Suction Valve ML23335A0722023-12-0101 December 2023 Interim Report of a Deviation or Failure to Comply Associated with a Relay in the Unit 2 Reactor Core Isolation Cooling Condensate Pump ML23320A2542023-11-16016 November 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump ML23282A0022023-10-0606 October 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump ML23279A0612023-10-0505 October 2023 Paragon Energy Solutions LLC, Part 21 Final Report Re Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) ML23254A0242023-09-0606 September 2023 Paragon Energy Solutions LLC, Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) ML23241A0022023-08-25025 August 2023 Paragon Final Part 21 Report on Defect with Eaton/Cutler Hammer Size 4 and 5 Freedom Series Contactors Modified by Paragon with Special Coils And/Or with RTV to Improve the Securing of Shading Coils RBG-48245, Part 21 Notification of a Failure to Comply Identified During Preinstallation Testing on a Motor Driven Relay2023-08-24024 August 2023 Part 21 Notification of a Failure to Comply Identified During Preinstallation Testing on a Motor Driven Relay ML23221A3702023-08-0303 August 2023 Paragon Energy Solutions, 10CFR Part 21 Initial Notification: P21-08032023-IN, Rev. 0 ML23207A0762023-07-14014 July 2023 EN 56557 - Update to Part 21 Report Re Potential Defect with Trane External Auto/Stop Emergency Stop Relay Card Pn: XI2650728-06 ML23192A0622023-06-30030 June 2023 Engine Systems, Inc., 10CFR21 Reporting of Defects and Non-Compliance, Report No. 10CFR21-0136, Rev. 0 ML23187A4722023-06-30030 June 2023 56603-EN 56603 - Engine Systems, Inc., Report No. 10CFR21-0136, Rev. 0 Re Voltage Regulator Chassis ML23100A1072023-04-10010 April 2023 Framatome Part 21 Report Re Erroneous Change of State for Circuit Breaker ML23066A2212023-03-0707 March 2023 Velan, Inc. - Revised Part 21 Notification Re Butterfly Valves Found to Have a Number of Fasteners Loose ML23038A0192023-02-0606 February 2023 Curtiss-Wright Part 21 Notification for Qualtech Np Supplied Eaton TMR5 Timing Relays ML22341A0322022-11-30030 November 2022 10 CFR Part 21 Notification from Curtiss-Wright Nuclear Division for Qualtech Np Supplied Eaton TRM5 Timing Relays ML22301A1742022-10-28028 October 2022 Global Nuclear Fuel Americas, LLC (GNF) - Part 21 60-Day Interim Report Notification: GNF3 Raised Water Rod (SC-22-04 Rt) ML22208A0042022-06-17017 June 2022 Nutherm International, Inc., USNRC 10CFR Part 21 Notification Reference: Arnold Magnetics Power Supply Part Number PBM-24-106 ML22153A0792022-04-0707 April 2022 10CFR Part 21 Notification for Curtiss-Wright Supplied RCS-Dresser Actuator P/N: SURE-24-10-4 ML22019A1762021-12-28028 December 2021 Lake Engineering Company - Interim Notification Per 10 CFR Part 21: Degraded Snubber SF1154 Hydraulic Fluid Batch No . 18CLVS431 ML21306A1802021-10-28028 October 2021 United Controls International - Part 21 Notification for York Pin: TCM-1 a Temperature Control Modules ML21294A0292021-10-0404 October 2021 Flowserve Part 21 Notification for Limitorque Supplied DC Motor ML21271A2342021-09-23023 September 2021 EN 55282 (Updated) - Framatome Part 21 Reportable Defect - Vacuum Breakers ML21260A0072021-09-0909 September 2021 Ametek Solidstate Controls, Notification of Potential Defect - 10CFR Part 21 Report Re Omron Timer Relay ML21225A0812021-08-0404 August 2021 Lake Engineering Co., Final Report Per 10 CFR Part 21 Degraded Snubber SF1154 Hydraulic Fluid Batch No. 17BLVS293 ML21181A2202021-06-29029 June 2021 Part 21 Written Notification - P21-03302021 Rev. 2 - Failures of Size 1 and 2 Freedom Series Full Voltage Reversing Starters ML21168A2172021-06-17017 June 2021 GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors M210077, GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors2021-06-17017 June 2021 GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors ML21126A1722021-04-29029 April 2021 Paragon Energy Solutions Failures of Size 1 and 2 Freedom Series Full Voltage Reversing Starters ML20366A0482020-12-0707 December 2020 10CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. 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Report No. 10 CFR21-0127, Rev. 0, Emd Fuel Injectors - Seized Plunger and Bushing ML19253A0532019-08-29029 August 2019 Azz Nuclear - Report of Potential 1O CFR Part 21, Eaton Size 1 and 2 A200 Series Starters/Contactors ML19199A0342019-07-0505 July 2019 Lake Engineering Co., Third Interim Notification Per 10 CFR Part 21 Degraded Snubber SF1154 Hydraulic Fluid Batch No. ZJS1518 ML19120A1062019-04-17017 April 2019 Interim Report of Potential 10 CFR Part 21, Eaton Size 1 and 2 A200 Series Starters/Contactors ML19121A1552019-04-15015 April 2019 Curtiss-Wright Nuclear Division, Enertech - 10 CFR Part 21 Notification for SF-1154 Hydraulic Fluid ML19080A0592019-03-0808 March 2019 Interim Report of Potential 10CFR Part 21, Eaton A200 Series Starters/Contactors ML19072A0632019-03-0606 March 2019 10 CFR Part 21 Report Notification of a Defect with Target Rock Modulating Valve Positioner; Model 810000-X ML19071A1122019-03-0101 March 2019 Lake Engineering Co., Corrected Potentially Degraded Snubber SF1154 Hydraulic Fluid Batch 11KLVS146 Final Report, Per 10 CFR Part 21 2023-09-06
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0811512016 U.S. Nuclear Regulatory Commission Operations Center Event Report Pagel Part 21 (PAR) Event# 51030 Rep,Org: AZZ/NLI NUCLEAR LOGISTICS, INC Notification Date I Time: 05/01/2015 13:32 (EDT)
Supplier: ALLEN BRADLEY Event Date I Time: 04/30/2015 (CDT)
Last Modification: 08/15/2016 Region: 4 Docket#:
City: FORT WORTH Agreement State: Yes County: License #:
State: TX NRC Notified by: TRACY BOLT Notifications: MEL GRAY R1DO HQ Ops Officer: DANIEL MILLS FRANK EHRHARDT R2DO.
Emergency Class: NON EMERGENCY ROBERTORLIKOWSKI R3DO 10 CFR Section: GEOFFREY MILLER R4DO 21.21(d)(3)(i) DEFECTS AND NONCOMPLIANCE PART 21/50.55 REACTORS EMAiL POTENTIALLY UNQUALIFIED COMPONENT IN CERTAIN ALLEN BRADLEY TIMING RELAYS The following is an excerpt from a document received from the licensee via email:
"Report of potential 10 CFR Part 21, Allen Bradley: Timing Relay Model 700RTC "Pursuant to 10 CFR 21.21 (d)(3)(ii), AZZ/NLI is providing written notification of the identification of a potential failure to comply.
"On the basis of our evaluation, it is determined that AZZ/NLI does not have sufficient information to determine if the subject condition would, or has, created a Substantial Safety Hazard or would have created a Technical Specification Safety Limit violation as it relates to the subject plant applications.
"The specific part which fails to comply or contains a defect:
"As of 2009-2010, Allen Bradley relays base model 700RTC, contain an unevaluated CPLD (Complex Programmable Logic Device). This was an unpublished design change that was implemented to replace an obsolete integrated circuit chip. Th13 undocumented design change did not result in a part number change from Allen-Bradley. There was no change to the appearance of the relay that would identify any design changes were made to the relay configuration. Therefore, NLI qualification/dedication of the relays after 2009 have not included additional testing for the new CPLD component.
"The timing relay model 700RTC has been dedicated/qualified for multiple applications for various plants.
"Between 2009-2010 Allen Bradley made a design change without changing the part number of the commercial .
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0811512016 U.S. Nuclear Regulatory Commission Operations Center Event Report Page 2 relay or providing any documented evidence of a design change. The manufacturer specification data sheets maintain the classification that the relays are 'solid state', which would imply that there are no digital devices installed in the relay. However, after inspection of the internals of the timing relay (Figure 2), it has been identified that the unit does contain a CPLD which meets the definition of a digital device under the guidance of NEI 01-01."
Potentially affected plants include Browns Ferry, Ginna, Millstone, Nine Mile Point, North Anna, Ft. Calhoun, Perry, River Bend, South Texas Project, and St. Lucie.
- AZZ/NLI Nuclear Logistics provided additional information regarding Part 21 Report No: P21-04302015, Rev. 1.
Notified R1 DO (Rogge), R2DO (Nease), R3DO(Skokowski), R4DO (Kellar), and PART 21/50.55 REACTORS via email.
- AZZ/NLI Nuclear Logistics provided Revision 2 to Part 21 Report No: P21-04302015 to correct the referenced EPRI TR-102323 Rev. 3 to Rev. 4 and change 'timing' contacts to 'instantaneous' contacts as shown below:
"(vii) The corrective action which has been, is being, or will be taken; the name of the individual or organization responsible for the action; and the length of time that has been or will be taken to complete the action.
"The relays that are currently in stock at NU have been placed on hold until after the units have been determined to be qualified for the specific application. NU has completed the EMC qualification testing per the requirements of EPRI TR-102323 Rev. 4 for the following tests, as applicable: CE101, CE102, RE101, RE102, RS101, RS103, CS101, CS114, CS115 and CS116.
"The results were satisfactory with exception of the following condition: During Conducted Susceptibility CS114 onto the power lines, with the timing circuit in operation, the instantaneous contacts exhibited chatter in the range of 2.6 MHz to 20.3 MHz. The unit requires a ferrite to be installed onto the input power lines of the relay with 3 turns through the ferrite core. In this modified configuration, the relay was not susceptible to Conducted Susceptibility and successfully passed the required test per CS114."
Notified R1 DO (Lilliendahl), R2DO (Guthrie), R3DO(Kunowski), R4DO (Werner), and PART 21/50.55 REACTORS via email.
- UPDATE FROM TRACY BOLT TO DONG PARK AT 1807 EDT ON 8/15/16 * *
- AZZ/NLI Nuclear Logistics provided additional information regarding Part 21 Report No: P21-04302015, Rev. 3, correcting the date the change occurred to October 2008.
Notified R1 DO (Jackson), R2DO (Shaeffer), R3DO (Riemer), R4DO (Proulx), and PART 21/50.55 REACTORS via email.