ML18106A947

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Forwards Suppl Rept on Corrective Measures to Be Taken to Reduce Potential of Future Occurrences,Per Discharge Confirmation Rept Submitted on 980709.Attached Pages to Be Inserted Into 980709 Rept & Previous Page Discarded
ML18106A947
Person / Time
Site: Salem  PSEG icon.png
Issue date: 10/22/1998
From: POWELL D R
Public Service Enterprise Group
To:
NEW JERSEY, STATE OF
References
LR-E98-0490, LR-E98-490, NUDOCS 9811040131
Download: ML18106A947 (4)


Text

e OPSfiG, Publfc Service F.Jectric and Gas Company P.O .. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear CERTIFIED MAIL RETURN RECEIPT REQUESTED ARTICLE NUMBER: Z 460 193 269 Bureau of Discharge Prevention New Jersey Department of Environmental Protection Station Plaza 4 22 South Clinton Avenue P.O. Box 424 Trenton, New Jersey 08625-0424 PSE&G SALEM GENERA TING STATION CASE NO. 98-06-12-0758-23 OCT IB 1998 LR-E98-0490 SUPPLEMENTAL DISCHARGE CONFIRMATION REPORT Per the Discharge Confirmation Report submitted on July 9, 1998 (LR-E980332), PSE&G is submitting this supplemental report on corrective measures to be taken to reduce the potential of future occurrences.

As discussed in the Discharge Confirmation Report, PSE&G discharged approximately 16 ounces of No. 2 fuel oil to the Delaware River. The discharge was from the Salem Generating Station oil/water separator (OWS) outfall, DSN 489. PSE&G has now completed an internal review of the events related to this discharge.

This internal review included recommended corrective actions. Enclosed are supplemental pages to the original Discharge Confirmation Report of July 9 with these corrective actions listed. These page.scan be inserted into the July 9 report and the previous page discarded.

\ Please contad Don Bowman of my staff at (609) 339-1477 if you have any questions.

\* Enclosure (1) LLS_QJJ_9_3 .. ===

981022 :

  • I ADOCK

! * . Sincerely, I. J // LJ. ;!. I I . David R. Powell Licensing/Regulation

& Fuels 9'i*2"68 REV 5 94 NJDEP LR-E98-0490 C Salem County Department of Health 98 Market Street Salem, NJ 08079 Attention:

James Warner U.S. Coast Guard Marine Safety Office/Group Philadelphia One Washington Avenue Philadelphia, PA 19147-4395 Attention:

Petty Officer Rich Lambert Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 . .

._. **

... OCT 18 1998

'** DISCHARGE CONFIRMATION REPORT CASE NO. 98-06-12-0758-23 CORRECTIVE; MEASURES:

The following corrective actions are being implemented:

(1) Engineering Design will redesign the OWS inlet chamber to minimize turbulent flow conditions prior to fluid entering the OWS. (2) Maintenance Services will track completion of soil erosion control methods in the yard area inside the security fence west of the OWS. (3) Engineering Design will provide adequate OWS venting mechanisms in accordance with vendor recommendations.

(4) Maintenance Services will develop a comprehensive maintenance procedure for the annual OWS cleaning and the periodic coalescer packs cleaning.

(5) Maintenance Services will procure equipment required to satisfactorily perform cleaning of the OWS, catch basins, skim tanks, and building sumps. (6) Engineering Design will provide adequate manway access to the OWS downstream of the parallel plate coalescers.

(7) Engineering Design will redesign OWS access platforms.

(8) Systems Engineering will create recurring tasks to clean building sumps, skim tanks, and yard catch basins. (9) Maintenance Services will provide training to all maintenance personnel on detergent and solvent usage upstream of the OWS. (10) Environmental Licensing will initiate remedial activities or maintenance based on videotape of yard piping upstream of the OWS. (11) Chemistry will revise applicable procedures to require both OWS tanks are in service simultaneously, with both inlet valves fully open, during normal operating conditions, and require inspections of sorbent material used throughout the OWS system. (12) Engineering Design will provide insulation to OWS sump pump discharge lines. (13) Engineering Design to evaluate reactivating the skim tanks in order to allow the settlement of solids and adequate retention of oils.

  • DISCHARGE CONFIRMATION REPORT CASE NO. 98-06-12-0758-23 INDIVIDUALS INVOLVED IN CONTAINMENT/CLEANUP:

The individuals responsible for the containment and cleanup of any contaminated material are: R. L. Black Nuclear Fire Protection Supervisor Public Service Electric and Gas Company Loss Prevention Department P. 0. Box 236, MIC X11 Hancock's Bridge, New Jersey 08038-0236 (609) 339-2800 A. W. Fisher Yard Supervisor Public Service Electric and Gas Company Maintenance Services P. 0. Box 236, M/C X12 Hancock's Bridge, New Jersey 08038-0236 (609) 339-1601 TYPE, QUANTITY, LOCATION AND DATE OF SAMPLES: Not applicable.

FINANCIAL RESPONSIBILITY:

-PSE&G satisfies the requirements for self-insurance established by NJAC 7:1 E-4.4(g) and has included appropriate documentation of this in its Discharge Cleanup and Removal (OCR) Plan as required by NJAC 7:1E-4.3(a)10.

1::7'::.;;; . --*