ML18024B179

From kanterella
Revision as of 07:18, 4 October 2018 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
RO 50-296/79-19:on 791204,during Augmented Ultrasonic Insp of Core Spray Piping,Indication Located Adjacent to safe-end to Core Spray Pipe Weld.Caused by Stress Corrosion Cracking.Piping Replaced W/Carbon Steel
ML18024B179
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 12/05/1979
From: ABERCROMBIE H
TENNESSEE VALLEY AUTHORITY
To:
References
NUDOCS 7912190554
Download: ML18024B179 (4)


See also: IR 05000296/1979019

Text

REGULAT INFORMATION

DISTRIBUTION

STER (ADIOS).ACCESSION NBR:7912190554

DOC.DATE: 79/FACIL:50 259 drowns Ferry i~luclear Power 50=2o0~owns

Pet ry Nuclear Power 50 299r'owns Ferry Nuclear Power A~~cs r4 AU T HUH AFF IL I A T ION AbE<CHONUIE~H, Tennessee Valley 4uthor RECIP,NA~E

RECIPIENT AFFILIATION

12/05 NOTARIZEDa.

NO Stations Unit 1r Tennessee Station<Unit 2i Tennessee Stations Unit 3i Tennessee ity DOCKET 05000259 05000260 0500029o I SUBJECT: RO 50 296/79-19:on

791204iduring

auqmented ul trasonic insp of units 3 core spray piping<indication

located adjacent to safe end to core spray pipe weld.Caused

oy stress corrosion cracxing.Piping

replaced w/carbon steel.orsr~rsvrros

coos:.aaars covrzs r scsrvso:era

/soccer srzs:~I'I1Lk.: Ltfc.(Uackf i t)NOTES: REC IP IEN l ID CODE/NAKE INTEHNALa 0 R G FrlE 04 I NSIC S HANAUEH COPIES LTl'R ENCL 1~2 1 1 HEC IP IEN T Iu CODt/NAi~E

02 hHC PDR HPA H IRELAND COPIES LTTh ENCL 1 1 1 txTERNAL: 03 LPDR TOTAL NUh]HER OF COPIES RE4UIRtD: L TTR 9 E!')CL gag

3XLECOPY'K)RRC 12/5/79 l.'-..8, Huc1ear Regulatory

Coamission

Reg,ion 4X 101 Nazietta Street Suk.te 3100 Atlanta, Georgia 30303 AFRO-50-296/>919

P'.',=,:;jRC

RFCI'-!ANTP..".-'.-~g gpss 5 AIf;00 i P.O'RBLLY.'C.M.UPRIGHl'0 CHENDLMj lV.S.RENTAL, F.J.LONG E, Q.E.MURPHY ,9.T.SUTHERLAND

K M.C RK Reported under Technical Specification 6.7.2.a(9)

Date of Occurrence;

12/4/79 Time of Occurrence:

9:30 a,m.Unit 3'reehnical

Speci.frication

involved: Hone Conditions

Prior to Occurrence:

Unit.3 in refueling mutate.Vases 1 and 2 in normal operation at 995 MVe and 735 Yde, respectkvelr.

58entffication

and Deacr'i tioa 6f.Occurrence:

QiHe perfomfr;g

an'augmented

uLtrasonic

inspection

of unit 3 coze spray piping, sn bd%cat5on was locet~ad3scent to the safe-end to core sprsy pipe~~M (weld Ho.DC&-3-l8)~fnspection

was performed et>en though chks piping var being rap~sc:ed during the exfsting.scheduled outage.There veze no resulting significant

occur" fences, no previous similar events, and no danger to the health or safeL)'f'the pub1ic.A grant Cause of Occurrence.

Subseouent

metallurgica1

analysis of the removed ultrasonic

indication

area revealed stress-corrosion

cracking.in the weld heat-affected'cone

ek gabe%0-inc>diameter, scb Gute 80, P-~>less-stee1

pipei A detai1ed metaLLurgical

report, is forthcoTair~

Qtbez Related Events:%e potent%ax foz stress-cozz.Agon

cracking, in certai>stain ess-steeK P.ping, his been previousl)

ibex'iie5 Cenectt.ve

Action T'eken nr Planned;Piping oa unit 3 was chansed out and replaced with carbon steel, L>nit 2 core spray piping vas chST'.ged to c-rhnn itee1 on a previous outage.LTnit X zefueliag.

outage begins DanuaTy 2, LSM, at>+feb time we will perform an insenCce inspection

to deterTnine

iK indi-cations ex%st.If indications

are observed,.

eweKuatMa and sobseqeent

repafra aa necessa~&El be performed.

r<8 i..AberczoTUbie

Tosser'Plant Superintendent

%res Vert'y Huclear PLaat P 001'18190 QS$g/g

T