ML18024B229

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RO 50-296/79-21:on 791208,w/load Approx 200 Mwe Following Return to Svc After Fuel Outage,Difficulty Occurred in Maintaining drywell-to-torus Pressure Differential.Caused by Leak Around Equipment Hatch Seal.Fasteners Retightened
ML18024B229
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 12/11/1979
From: Abercrombie H
TENNESSEE VALLEY AUTHORITY
To:
References
NUDOCS 8001140293
Download: ML18024B229 (4)


Text

REGULATORY ORMATION Ol'STRISUTION SYSl (RODS)

ACCESSION NBR:80011r10293 DOC ~ DATE: 79/12/11 NOTARIZED'O PACiL:50 296 Browns Perry Nuclear Power Stat>onr Onlt 3i Tennessee AOTH ~ NAME AUTHOR AFFILIATION ASPACROMBIEiH~ L Tennessee Val 1 ey Author f ty ABClP ~ NAME'ECIPIEblT'FFILIATION DOCKET 05000296

SUBJECT:

RO 50 296 retur n to ma i nta i ni by leak a

DISTRIBUTION CODE:

TifLEe NOTES:

/7921:on 791208rw/load approx 200 MNe following svc after fuel outageidifficulty occurred in ng drywell to.-torus pressure differential, Caused round equipment hatch seal,F'asteners ret19Rteneds M007S COPIES RECEIVED;L'TR g ENCL +

SIZE:

L LEA (Backfit)

REC IP I EN 1'D CODE/NAME INTE

~

01 REG ILE NSIC S

HANAUER EXTERNAL: 03 LPDR COPIES L'fiR ENCL 1

2i 1

RECIPIENT ID CODE/NAME 02 NRC PDR MPA R

IRELAND COPIES LlTA"ENCL 1

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TOTAL NUMBER OF COPIES REQUIRED; LTTR 9

ENCL

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Reports aa8er Technics Spec~gcaaf g 7

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XCma ae accorxence-Technical ByeciHcatiaa. hxvaiva8:

4 7 4,,2.g Candicions Pfior ca Occurrence I

Unit f. ac 970 Kfe, end-of-core eoastcbwn

,Unit 2 st S39 NMe, Hmitd bF 2'eactor feed pump maintenance.

Uakt 3 ibad at zpproxhuateiy 260 HWe foilevJng return ter service af the unit-fracn re&xeHng, cmtage st 163.5, k2/S/79 MC ia eeet p~reai I

Identifkaation and Descry tiom ef Qccnmence be%.ag eaKLskderod.

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Abercrombie

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Passer Flaa,e, Superintendent 8m~ F~~ NucIeax plume

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  • 4 DHHmBy in maintaining de'yeeXX & Axus pxessuxe cKHerenchQ ~~catect problems*with dryva21 leakage

. Farther invastigatfma. reveals

&mt. exceask~e d~kX Leakage,existed Leak psch. %8eatiHed cu4 repaired ae 0839>> XZ(9t79>

within 45 bc'ment par Yaebnicaf Speciff.cation 4 2 4 2 h(2)>

C.

~et Cause of Occurrence I

I XeA am& southeast equipaumt hatch esaX due tc heaenad fsscenees.

Retaught'en%us of faateaers fmmeNeceXy texmfaated %esker.

other Rebated Events -:'.., ', -',-

None I

Corrective Act$.on Takeo, or Pkannnk Retightening cf fasteners corrected Xaahage ocher. corrective sctien is

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