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 Issue dateTitleTopic
ML18039A66631 December 1998Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable StatusPost Accident Monitoring
ML18032A4182 July 1987Ro:On 870227 & 0505 Oil Spills Occurred Resulting in Oil Sheens.Spilled Matl Did Not Involve PCB-contaminated Oil. Feb Spill Went to Plant Intake Forebay & May Spill Went Directly Into Tennessee River
ML18031B28531 March 1987Special Rept:On 870321,loss of Seismic Monitoring Instrumentation Discovered.Caused by Inadequacy in Instructions & Training.All Instruments Removed from Site Will Be Repaired & Restored to Operation
ML20024C06129 June 1983Telecopy Ro:On 830613 & 14,train B Discovered Inoperable & Operability of Standby Gas Treatment Sys Trains Exceeded Tech Specs for Approx 6 H.Caused by Malfunctioning Square Root Converter.Plant Instruction Rev in Progress
ML18025B7249 February 1982Ro:On 820104,suspended Solids Samples Exceeded Daily Max Limit of 100 Mg/L.Caused by High Increase in Turbidity & Suspended Solids Due to 3.4 Inches of Rainfall.No Corrective Action Taken Because Occurrences Not Typical
ML20009F66930 June 1981Ro:On 810629,during Refueling Outage,Ultrasonic Test Insp Revealed Reactor Water Cleanup Sys Inboard Primary Containment Isolation Valve Indication.Cause Unknown. Indication Will Be Removed & Weld Repaired
ML20010B8635 March 1981RO 50-259/81-09:on 810304,during Evaluation of IE Info Notice 80-45,mode Selector Switch Had Same Deficiency Identified in Notice.Apparently Caused by Circuitry Design Deficiency.Procedure Revisions Will Be Made
ML19343C11410 February 1981Environ RO BFRO-50-259/8105:on 810131,combined Discharge of Spent Demineralizer Regenerants from Makeup Water Treatment Plant & Biothermal Research Facility Had Ph Value of 9.2, Exceeding Tech Spec Limits.Caused by Natural Phenomena
ML20049A4642 February 1981RO 50-259/8105:on 810131,during Normal Operation,Ph of Reservoir Was in Excess of Discharge Limit.Cause Unknown. Discharge of Demineralizer Regenerants Was Stopped.Raw Water Samples Were Taken & Analyzed for Ph
ML20049A46327 January 1981RO 50-259/8103:on 810124,during Normal Operation, Notification Was Received That 1-inch Vent Line on Scram Discharge Vol Was Not Seismically Qualified.Caused by Nonconformance to Design Requirements.Restraints Installed
ML18025B3635 December 1980Ro:On 801205,w/unit in Operation,Rhr Heat Exchanger 2C Was Removed from Svc Due to Leakage.Cause Is Undetermined. Surveillance Testing Was Performed Per Tech Specs
ML19345B97426 November 1980RO 50-260/80-47:on 801107,chlorine Residual Reached 0.49 mg/1 Exceeding Max Allowable of 0.05 mg/1.Caused by Failure of Main Condenser Cooling Water Pumps to Provide Adequate Dilution.Chlorination Stopped.Procedures Revised
ML19347B5958 October 1980Limiting Conditions of Operations Violation Rept:On 800928 & 29,Wheeler Reservoir Water Temp Exceeded Tech Spec Limit. Caused by Thermal Monitoring Sys Error.Unit 3 Sys Placed on Cooling Tower.Design Change Requests Being Prepared
ML19347B6298 October 1980Environ RO 50-259/8073:on 800928 & 29,temp Rise of Wheeler Reservoir Between Upstream & Downstream Thermal Monitors Exceeded Tech Specs.Caused by Extensive Rainfall & Lower than Normal Ambient Temp,Adding to Errors in Prediction
ML20049A3296 October 1980Ro:On 801004,w/unit Operating at 749 Mw,Load Limited,Hpci Declared Inoperable Due to High Level Indication in Exhaust Drain Pot Indicating Blockage of Drain Line.Caused by Faulty O-ring in Level Sensing Line
ML20049A3316 October 1980Ro:On 801006,faulty Indication on Outboard Isolation Valve of Reactor Coolant Isolation Sys Would Not Allow Operator to Be Aware of Actual Valve Position.Caused by Open Circuit in Valve Position Indication.Surveillance Testing Performed
ML19326D85615 July 1980RO 50-259/8054:on 800706,river Temp Exceeded Max Limitation for Over 1-h at Downstream Monitor.Caused by Computer Error. Predictive Computer Program Underestimated Max Downstream Temp by 2 F.Cooling Towers Used,Station Load Reduced
ML19330A9758 July 1980Ro:On 800708,during Routine Surveillance Instruction,Pcv 73-43,which Controls Cooling Water to Gland Seal Condensor & Lube Oil Cooler,Was Found Stuck in Closed Position.Cause Unknown.Equipment Expected to Be Returned to Svc by 800708
IR 05000296/198002430 June 1980RO-BFRO-50-296/8024:on 800628,during Routine Maint Shutdown, Approx 68 of 185 Control Rods Failed to Fully Insert When Reactor Was Manually Tripped.Unit Is Shut Down Until Cause Determined & Corrective Action Taken
ML18025A95930 June 1980RO-BFRO-50-296/8024:on 800628,during Routine Maint Shutdown, Approx 68 of 185 Control Rods Failed to Fully Insert When Reactor Was Manually Tripped.Unit Is Shut Down Until Cause Determined & Corrective Action Taken
IR 05000260/198002517 June 1980RO-BFRO-50-260/8025:on 800617,Dresser Industries Safety Valves Identified as Possibly Having Guides W/Cracks. Condition Identified in Similar Valves Loaned to Another Util from Browns Ferry.Cause Unknown
ML18025A95117 June 1980RO-BFRO-50-260/8025:on 800617,Dresser Industries Safety Valves Identified as Possibly Having Guides W/Cracks. Condition Identified in Similar Valves Loaned to Another Util from Browns Ferry.Cause Unknown
ML18024B3491 February 1980RO 50-259/511:on 800201,w/Unit 1 in Cold Shutdown & Units 2 & 3 Operating Normally,Discovered Potential Loss of Secondary Containment If Primary Containment Purging Is Conducted During Hot Standby.Caused by Pressure Surge
ML19290C68118 January 1980RO 50-259/804:on 800118,w/Unit 1 in Refueling Outage,Water Cleanup Sys Inboard Primary Containment Isolation Valve 69-1 Had Indication Requiring Repair.Cause Unknown.Indication Removed
ML19290C68218 January 1980RO 50-259/805:on 800118,during Insp,Determined That Seismic Restraints Not Installed on Reactor Bldg closed-cooling Water Lines Inside Drywell.Restraints Will Be Installed
IR 05000296/197902111 December 1979RO 50-296/79-21:on 791208,w/load Approx 200 Mwe Following Return to Svc After Fuel Outage,Difficulty Occurred in Maintaining drywell-to-torus Pressure Differential.Caused by Leak Around Equipment Hatch Seal.Fasteners RetightenedBackfit
ML18024B22911 December 1979RO 50-296/79-21:on 791208,w/load Approx 200 Mwe Following Return to Svc After Fuel Outage,Difficulty Occurred in Maintaining drywell-to-torus Pressure Differential.Caused by Leak Around Equipment Hatch Seal.Fasteners RetightenedBackfit
ML18024B1795 December 1979RO 50-296/79-19:on 791204,during Augmented Ultrasonic Insp of Core Spray Piping,Indication Located Adjacent to safe-end to Core Spray Pipe Weld.Caused by Stress Corrosion Cracking.Piping Replaced W/Carbon Steel
ML18024B17329 November 1979RO-50-259/79-32:on 791128,during Insp of Restraints,Typical Hanger Identified as Possibly Unacceptable.Caused by Possible Misapplication of Hanger.Insp & Analyses Will Be Conducted to Determine Effect on Sys
IR 05000259/197903229 November 1979RO-50-259/79-32:on 791128,during Insp of Restraints,Typical Hanger Identified as Possibly Unacceptable.Caused by Possible Misapplication of Hanger.Insp & Analyses Will Be Conducted to Determine Effect on Sys
IR 05000296/19790182 November 1979RO-50-296/79-18:on 791030,during Logic Testing Per LPCI Mods,Simultaneous Starting of Two RHR Pumps Occurred.Caused by Mismatch Between Current Transformer Ratios on Normal Supply to Shutdown Boards.Transformers Will Be Changed
ML18024B1972 November 1979RO-50-296/79-18:on 791030,during Logic Testing Per LPCI Mods,Simultaneous Starting of Two RHR Pumps Occurred.Caused by Mismatch Between Current Transformer Ratios on Normal Supply to Shutdown Boards.Transformers Will Be Changed
ML18024A84730 May 1979RO 50-260/79-011 on 790526:rod Inadvertently Pulled Three Notches During Attempt to Reach Criticality.Cause Not Established.Operator Interviewed
IR 05000260/197901130 May 1979RO 50-260/79-011 on 790526:rod Inadvertently Pulled Three Notches During Attempt to Reach Criticality.Cause Not Established.Operator Interviewed
ML18024A5756 December 1978RO-50-296/782:Bendix Connectors Used Inside Primary Containment Which Failed post-aging Environ Test Were Modified by Potting Plug & Receptacle Portion of Connectors & Passed 10 Year Qualifying Tests
ML18024A5218 November 1978Supplementary Reportable Occurence Rept BFRO-50-296/7822: on 780822,during Startup at 3 Percent Thermal Pwr,Msrv 1-4 Opened & Did Not Completely Close Resulting in Excessive Cooldown Rate.Caused by Excessive Pilot Leakage
ML18024A5238 November 1978Supplementary Reportable Occurrence Rept#BFRO-50-296/7821 on 780817.Following Reactor Scram,Cooldown Rate Was Exceeded Due to Safety Valves Actuating & Not Completely Closing. Caused by Excessive Pilot Leakage
IR 05000296/19780218 November 1978Supplementary Reportable Occurrence Rept#BFRO-50-296/7821 on 780817.Following Reactor Scram,Cooldown Rate Was Exceeded Due to Safety Valves Actuating & Not Completely Closing. Caused by Excessive Pilot Leakage
ML18024A5388 November 1978RO#50-296/7822 on 780822:during Startup at 3% Thermal Pwr, MSRV 1-4 Opened & Did Not Reclose Completely,Resulting in Excessive Vessel Cooldown Rate,Due Apparently to Excessive Pilot & second-stage Leakage in the Valves
IR 05000296/19780228 November 1978RO#50-296/7822 on 780822:during Startup at 3% Thermal Pwr, MSRV 1-4 Opened & Did Not Reclose Completely,Resulting in Excessive Vessel Cooldown Rate,Due Apparently to Excessive Pilot & second-stage Leakage in the Valves