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Issue date | Title | Topic | |
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ML20084C916 | 2 August 1974 | AO 50-219/74/42:on 740725,main Steam Line Low Pressure Switches RE23A,B,C & D Found to Trip at Pressures Less than Min of 860 Psig.Caused by Switch Repeatability.Setpoint Accuracy & Tolerence Under Investigation | Fuel cladding |
ML20084C917 | 26 July 1974 | AO 50-219/74/41:on 740719,main Steam Line Low Pressure Switches RE23C & D Found to Trip at Pressures Less than Min of 860 Psig.Caused by Lack of Setpoint Tolerances in Tech Specs.Setpoint Accuracy & Tolerance Under Investigation | Fuel cladding |
ML20084C921 | 16 July 1974 | AO 50-219/74/40:on 740715,one Bergen-Paterson Hydraulic Shock & Sway Arrestor on South Core Spray Sys in Drywell Noted Inoperable.Caused by Loss of Hydraulic Fluid.Unit Replaced | |
ML20084D013 | 16 July 1974 | AO 50-219/74/39:on 740714,electromatic Relief Valve Pressure Switches IA83A,B,C & E Found to Trip at Pressures in Excess of Max Allowable Value of 1070 Psig.Caused by Setpoint Repeatability.Switches Reset | |
ML20084D026 | 16 July 1974 | AO 50-219/74/38:MSIV NS04B Failed to Close in Less than 10 S.Cause Under investigation.Four-way Valve in Pilot Valve Assembly Cleaned & Relubricated | |
ML20084D031 | 12 July 1974 | AO 50-219/74/37:on 740712,main Steam Line Low Pressure Switches RE23A,B,C & D Found to Trip at Pressures Less than Min Value of 860 Psig.Caused by Switch Repeatability. Corrective Actions Continuing | Fuel cladding |
ML20084D050 | 10 July 1974 | AO 50-219/74/36:on 740710,reactor Pressure Sensor REO3D Failed to Trip at Point Corresponding to Reactor Pressure of 1060 Psig.Cause Under Investigation.Sensor Recalibr | |
ML20084D062 | 8 July 1974 | AO 50-219/74/35:on 740705,main Steam Line Low Pressure Switches RE23B,C & D Found to Trip at Pressures Less than Min of 860 Psig.Caused by Switch Repeatability.Problem Under Investigation | Fuel cladding |
ML20084D185 | 30 May 1974 | AO 50-219/74/34:on 740529,indications of Coolant Leakage Existing in Area of in-core Flux Monitor Reactor Vessel Housing Noted.Cause Not Determined | Hydrostatic |
ML20084D199 | 22 May 1974 | AO 50-219/74/32:on 740521,core Spray Booster Pump Pressure Switch RV4OD Failed in Permissive Position.Cause Under Investigation | |
ML20084D205 | 20 May 1974 | AO 50-219/74/31:on 740519,one Bergen-Paterson Hydraulic Shock & Sway Arrestor on South Core Spray Sys Found Inoperable.Caused by Loss of Hydraulic Fluid.Seven Units Replaced W/Units Equipped W/Ep Seals | Design basis earthquake |
ML20084D213 | 15 May 1974 | AO-50-219/74/30:on 740514,generator Load Rejection Scram Failed to Operate at Turbine Steaming Rates Greater than 40% of Rated While in Run Mode.Cause Under Investigation. Switch Recalibr | |
ML20084D219 | 1 May 1974 | AO-50-219/74/28:on 740423,electromatic Relief Valve Pressure Switches 1A83B & D Found to Trip at Pressures in Excess of Max of 1070 Psig.Caused by Setpoint Repeatability.Switches Reset & Will Be Surveyed Each Time Reactor Shut Down | |
ML20084D224 | 19 April 1974 | Preliminary AO 50-219/74/28:on 740419,motor Operated Suction Valve v-20-4 Failed to Open Electrically After Closing Electrically During Surveillance Testing on Core Spray Sys. Cause Under Investigation | |
ML20084D228 | 18 April 1974 | Preliminary AO 50-219/74/27:on 740417,three Hydraulic Shock & Sway Arrestors Failed.Caused Not Identified.Units Will Be Replaced W/Units Rebuilt W/Ethylene Propylene Matl | |
ML20084D239 | 12 April 1974 | Preliminary AO 50-219/74/26:on 740412,emergency Svc Water Pump 52C Failed to Start.Cause Under Investigation | |
ML20084D289 | 10 April 1974 | Preliminary AO 50-219/74/25:on 740409,loss of Primary Integrity W/Reactor Critical & Reactor Water Temp Greater than 212 F Occurred.Cause Unknown.Valves Properly Seated & Successfully Leak Tested & Power Increased to Initial Value | |
ML20084D307 | 10 April 1974 | Preliminary AO 50-219/74/24:on 740409,stack Gas Particulate Filter in Svc from 740328-31 Not Analyzed for Gross Beta, Alpha & Lambda.Cause Under Investigation | |
ML20084E038 | 18 March 1974 | Preliminary AO 50-219/74-23:on 740315,high Flow Isolation Setpoint for Isolation Condenser Condensate Line Break Sensors Found to Actuate at Differential Pressures in Excess of Tech Specs.Caused by Sensor Drift | |
ML20084E040 | 18 March 1974 | Preliminary AO 50-219/74/22:on 740315,low Pressure Main Steam Line Pressure Switch RE23D Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability. Recommendations to Eliminate Setpoint Problem Received | Fuel cladding |
ML20084E060 | 11 March 1974 | AO 50-219/74/19:on 740309,primary Containment Integrity Not Maintained W/Reactor Water Temp Above 212 F & Fuel in Reactor Vessel.Caused by Equipment Malfunction & Operator Error | |
ML20084E115 | 1 July 1975 | RO 50-219/75-18:on 750623,two 8-1/2 Inch Handhole Covers in Standby Gas Treatment Filter Train Not in Place.Cause Unknown.Handhole Covers Repositioned & Secured | |
ML20084E851 | 5 October 1970 | Telecopy Ao:On 701004,gape Valve 852B Only Opened Halfway. Caused by Loose Stem Nut of Limitorque Operator.Nut Replaced | |
ML20084E863 | 14 October 1970 | Telecopy Message of Ao:On 701014,gate Valve 851A Failed to Fully Close.Caused by Loose Stem Nut Locking.Lock Tightened & Stem Lubricated | |
ML20084F163 | 11 October 1973 | Preliminary AO-73-26:on 731006,average Power Range Monitor (APRM) Scram & Rod Block Setpoints Not Set to Tech Spec Values.Caused by Communication Problem.Aprm Adjusted | |
ML20084F227 | 1 October 1973 | Preliminary AO 73-25:on 730929,during Surveillance Test, Contacts on Relay 6K12 Failed to Open within Preset Time Delay.Cause Unknown.Relay Replaced | |
ML20084H968 | 28 September 1973 | Preliminary AO-73-24:on 730927,MSIVs NA04A & B Failed to Meet Acceptable Leakage Limit.Caused by Leakage Past Valve Packing | |
ML20084J076 | 10 September 1973 | Preliminary AO-73-22:on 730909,during MSIV NS03B Test Following Reactor Scram,Leakage Found in Excess of Tech Spec Limit.Cause Unknown Steam Measurements Taken on Valves | |
ML20084J079 | 10 September 1973 | Preliminary AO-73-21:on 730908,several Hydraulic Shock & Sway Arrestors on Piping Sys in Drywell Failed.Caused by Inoperable Snubbers Due to Hydraulic Fluid Loss.Hydraulic Shock & Sway Arrestors Replaced | |
ML20084J081 | 10 September 1973 | Preliminary AO-73-20:on 730909,during Last Stages of Plant Cooldown,Isolation Condenser NE01A Condensate Return Valve V-14-34 Failed to Operate.Caused by Tripped Overloads for Starting Contactor.Overloads Reset | |
ML20084J084 | 10 September 1973 | Preliminary AO-73-19:on 730908,setting on Base Differential Monitoring Relay C of Startup Transformers Considered Inoperable.Caused by Incorrect Setting of Transformer Ratio Matching Taps.Taps Set Properly | |
ML20084J086 | 31 August 1973 | AO-73-18:on 730823,max Amount of Radioactivity Contained in Outside Radwaste Storage Tanks Exceeded Tech Spec Limits. Caused by Failure to Recirculate Tank for Sufficient Time to Eliminate Stratification.Tanks Will Be Cleaned Out | |
ML20084J089 | 2 April 1974 | Supplementary AO: Beginning 740112,during Plant Shutdown, Hydraulic Shock & Sway Arrestor Insp Found 30 Affected Snubbers.Surveillance Program Outlined on 731207 Will Continue Until Satisfactory Solution Is Found | |
ML20084J212 | 17 August 1973 | AO-73-17:on 730808,during Surveillance Insp of Diesel Generator 1,two Starting Motors Failed to Engage.Caused by Bushing Which Slipped Out of Position & Prevented Pinion Gear from Engaging Ring Gear.Starter Motor Replaced | |
ML20084J222 | 6 August 1973 | Ao:On 730721,during Plant Shutdown,Eight Drywell Snubbers Discovered Missing Hydraulic Fluid.Caused by Seal Failure Creating Leakage Path.Snubbers Replaced.Forwards Snubber Repair Activities..., Summary Rept | Earthquake |
ML20084J241 | 25 July 1973 | Preliminary AO-73-15:on 730725,during Closure Timing & Scram Checks,Msiv NS04B Closed in Less than 3 S.Caused by Insufficient Oil in Hydraulic Dashpot.Seal Cartridge Assembly Replaced | |
ML20084J248 | 31 July 1973 | AO-73-14:on 730723,plot of Absorption Pool (Torus) Water Level Developed.Caused by Feedwater Leak Around Check Valve Hinge Pin Seal Plugs.Erosion of Seating Surface on Valve Body Machined Out | |
ML20084J253 | 28 June 1973 | AO-73-11:from 730609-13,reactor Coolant Not Analyzed for Total Radioactive Iodine Content.Caused by Failure of Multichannel Analyzer.Analyzer Repaired | Grab sample |
ML20084J266 | 28 June 1973 | AO-73-12:on 730618,containment Spray Sys 2 Automatic Reset Circuitry Failed.Caused by Relay Coil 16K22B Failure.Coil & Relay Series Resistor Replaced | |
ML20084J276 | 15 May 1973 | Ao:On 730504,during Local Leak Rate Testing,Torus to Reactor Bldg Vacuum Breaker Lines Failed to Hold Pressure Between Isolation Valves V-26-17 & 18.Caused by Butterfly Valve V-26-18 Leakage.Valve Linkage Adjusted | |
ML20084J284 | 22 June 1973 | Followup of 730424 AO Rept Re Failure of Electromatic Relief Valve NR-108-B During Operability Test.Addl Investigation Revealed Failure Due to Solenoid Core Guide Pin.New 304SS Guide Pins Machined to Proper Dimensions | |
ML20084J547 | 5 July 1973 | AO-73-13:on 730621,during Power Operation,Diesel Generator 2 Failed to Fully Operate.Caused by Three Transformer Fuses Blowing During Lightning Storm.Two Fuses Replaced & One Jumped | |
ML20084J550 | 5 June 1973 | Ao:On 730522,during Leakage Testing for MSIV NSO4B,vol Between NOS3B & 4 Could Not Be Drained.Caused by Leak in NSO3B.Valve Stem Replaced | |
ML20084J551 | 30 May 1973 | Ao:On 730518,during Refueling Outage Test,Liquid Poison Pump NP01A Failed.Caused by Blown Logic Control Power Fuse. Fuse Locations Tagged or Identified for Proper Size | Squib |
ML20084J563 | 22 June 1973 | AO-73-10:on 730611,during Surveillance Test,Diesel Generator 1-1 Failed to Assume Load.Caused by Engine Governors Not Set for 60 Hz Unloaded Operation.Generator Properly Synchronized | |
ML20084J607 | 5 June 1973 | Ao:On 730527,drywell Head Manhole Cover Double Gasket Seal Failed to Meet Acceptable Leakage Specified in Tech Specs. Caused by Brittle Outer Gasket.Gasket Replaced | |
ML20084J675 | 24 April 1973 | Ao:On 730424,during Surveillance Test of B Isolation Condensor Motor Operated Condensate Return Valve V-14-35, Breakaway from Closed Motor Current of 75 Amps Observed. Cause Undetermined.Torque Applied to Handwheel Freed Disc | |
ML20084J712 | 23 March 1973 | Ao:On 730310,recirculation Loop Started When Coolant Temp & Reactor Coolant Temp Exceeded 50 F Differential.Caused by Personnel Error.Recirculation Sys Operating & Emergency Procedures Revised | |
ML20084T882 | 15 June 1970 | Ao:On 700605,turbine electro-hydraulic Control Sys Transient Caused Turbine Trip & Reactor Scram,Followed by Inadvertently Opened Safety Valves.Two Safety Valves Failed to Close,Releasing Primary Coolant to Containment | |
ML20084U950 | 2 January 1975 | AO 50-265/74-29:on 741223,cracks at Welds in 4 Inch Reactor Recirculation Discharge Valve Bypass Lines Indicated.Cause Undetermined.Piping on a & B Loops to Be Completely Replaced |