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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML19343C2181975-12-23023 December 1975 AO 50-219/75-33:on 751212,during 6-month Load Test on Station a batteries,125 Volt Dc Distribution Ctr de-energized.Caused by Personnel Error in Following Procedure.Distribution Ctr re-energized ML20090C9991975-12-12012 December 1975 AO 75-33:on 751212,125-volt Dc Distribution Ctr of Station a Battery Inadvertently de-energized.Caused by Failure to Establish Proper Breaker Lineup Preparation for Conducting Battery Load Test.Procedure changed.W/751219 Memo ML19343C2191975-12-11011 December 1975 AO 50-219/75-32:on 751203,during Testing,Emergency Diesel Generator 1 Failed to Start When Simulated Loss of Power Condition Applied to Fast Start Logic Circuit.Caused by Failure of Relay to Operate Due to Varnish on Armature ML20126E8281975-12-0303 December 1975 AO 50-219/75-31:on 751124,during Operability Test of Torus to Drywell Vacuum Breakers,Alarm Sys 2 Failed to Annunciate in Control Room When V-26-4 Opened.Caused by Failure of Relay Due to Contacts Being Detective.Relay Replaced ML20090D0071975-11-25025 November 1975 AO 75-31:on 751124,drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-4 Opened. Caused by Component Failure.Corrective Action Under Investigation ML20090D0161975-11-0707 November 1975 AO 75-30:on 751106,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17 a & C Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability.Pressure Switches Recalibr ML20090D0601975-11-0606 November 1975 AO 75-29:on 751027,torus Drywell Vacuum Breakers Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened. Caused by Sticking Microswitch ML20090D0761975-10-28028 October 1975 AO 75-29:on 751027,torus to Drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened.Caused by Component Failure.Corrective Action Under Investigation ML20090D0941975-10-24024 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil Replaced ML20090D1141975-10-17017 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1041975-10-16016 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil replaced.W/751016 ML20090D1341975-10-0808 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressures Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1501975-09-23023 September 1975 AO 75-26:on 750923,emergency Svc Water Pump 52C Failed to Start Automatically During Routine Surveillance Test of Containment Spray Sys Ii.Caused by Failure of Contact Switch in Time Delay Relay 16 K4B.Relay Replaced ML20090D2071975-09-0808 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML19291C2641975-09-0808 September 1975 AO 73-19:when Closing Signal Was Applied to Breaker S1A,loss of Power Occurred at 4160-volt Ac Bus 1A Causing Trip of Various Pumps.Caused by Incorrect Setting of Current Transformer Ratio Matching Taps.Taps Set Properly ML20090D1941975-09-0808 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2151975-09-0202 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML20090D2011975-09-0202 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2241975-08-21021 August 1975 AO 75-23:on 750817-20,stack Effluent for Iodine & Particulates Not Monitored.Caused by Personnel Error.Filter Installed in Operating Stack Gas Sampling Train ML20090D2261975-08-11011 August 1975 Preliminary AO-50-219/75-22:on 750810,stack Gas Sample Line Low Flow Alarm Received.Caused by Stack Gas Sample Pump a Not Running.Thermal Overload Protection Reset ML20090D2471975-08-0404 August 1975 Preliminary AO-50-219/75-21:on 750801,during Routine Surveillance on B Isolation Condensor Sys,Steam Line Valve V-14-32 Failed to Close on Simulation of Steam Line High Flow.Caused by Low Torque Switch Setting.Torque Increased ML20090D2521975-07-17017 July 1975 AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D, A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20090D2561975-07-0909 July 1975 Preliminary AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D,A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20084E1151975-07-0101 July 1975 RO 50-219/75-18:on 750623,two 8-1/2 Inch Handhole Covers in Standby Gas Treatment Filter Train Not in Place.Cause Unknown.Handhole Covers Repositioned & Secured ML20090D2741975-06-27027 June 1975 AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2661975-06-24024 June 1975 Preliminary AO 50-219/75-18:on 750623,handhole Covers in Standby Gas Treatment Filter Train 1-1 Not in Place.Cause Under Investigation.Covers Repositioned & Secured ML20090D2781975-06-24024 June 1975 AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83P & E Tripped at Pressures Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D2731975-06-19019 June 1975 Preliminary AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2901975-06-16016 June 1975 Preliminary AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83B & E Tripped at Pressure Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D6561975-06-0606 June 1975 AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned & Repaired ML20090D2971975-06-0606 June 1975 AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D2981975-06-0202 June 1975 Preliminary AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D6581975-05-30030 May 1975 Preliminary AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned ML20090D6611975-05-14014 May 1975 AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6641975-05-0707 May 1975 Preliminary AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6531975-05-0606 May 1975 AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17B & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatablilty.Switches Recalibr ML20090D6701975-04-28028 April 1975 Preliminary AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 178 & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatability.Switches Recalibr ML20090D6751975-04-18018 April 1975 AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7001975-04-14014 April 1975 AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure.Valves Adjusted &/Or Repaired ML20090D6811975-04-11011 April 1975 Preliminary AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7131975-04-0808 April 1975 AO-50-219/75-09:on 750329,breaker 1C Tripped Resulting in Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7061975-04-0707 April 1975 Preliminary AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure. Valves Adjusted &/Or Repaired ML20090D7271975-04-0303 April 1975 AO-50-219/75-08:on 750325,power Operation Continued W/ Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate.Caused by Failure to Properly Monitor Reactor Core.Rate Reduced ML20090D7211975-03-31031 March 1975 Preliminary AO-50-219/75-09:on 750329,breaker 1C Tripped Due to Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7651975-03-27027 March 1975 AO-50-219/75-07:on 750319,during Standby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Differential Relay Installed ML20090D7361975-03-26026 March 1975 Preliminary AO-50-219/75-08:on 750325,power Operation Continued W/Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate. Caused by Improper Reactor Core Monitoring.Rate Reduced ML20090D7761975-03-20020 March 1975 Preliminary AO-50-219/75-07:on 750319,during Stanby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Relay Installed ML20090D7801975-03-19019 March 1975 AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Continuously Monitor Stack Releases While Reactor in Unisolated Condition.Caused by Circuit Design.Request to Modify Circuit for Stack Gas Sample Pumps Submitted ML20090D7901975-03-13013 March 1975 AO-50-219/75-05:on 750306,during Monthly Surveillance Test, Containment Spray Pump 51A Failed to Start When Subjected to Simulated Signals.Caused by Breaker Trip Bar Failing to Reset After Previous Breaker Trip.Trip Bar Bushings Cleaned ML20090D7811975-03-11011 March 1975 Preliminary AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Monitor Stack Releases While Reactor in Unisolated Condition.Caused by faulty-circuit Design 1975-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
[Table view] |
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%j % .a ro: Jene P. O'Failly Directorate cf Pegulatory Operation.;
Peglen I 631 Park Avent:c King of Prtcsia, Fcansylvenia 1940S i
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Oysta.r Crc:k Nuclear. Generating Station ,
Docket #50-219 Forketl River; New Jersey 08731 .
l Obj e ct - ALnorm1 Occurrence Report No. 50-219/74/35 The following is a prolicinary report being subultted in coeplicnce tritt. the TecJmical Specifications, paragraph 6.6.2.
Pratininary Approval: i T
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Initial Written ' Tina of
1540 Report Date: 7/ri/74< .c _ ' ' " 0ccurrence t.-
OYSTER CREEK NUCLEAR GENERATING STATION
- FORKED RIVI!R, NHH JERSEY 09731
/unorcal Occurrenco Report No. 50-219/74/ 35 IDENTIFICKfl0M > Violation of the Technical Specifications, parar,raph 2.3.7, OF OCCURRENCfl:
Ifnin Steam Lino low Pressure Switches Pf23B, C, ::nd D.ucre found to trip at pressures less then .the etnic:tn required value of 850 psig.
This event is considdred to be ' ne abnormal occurrence as de- j fined in the Technical Specifications, paragraph 1.15A. :
1 CGiDITIONS PRIOR Steady Stato Power P,outino Shutdown TO OCCURRENCE: llot. Steadby Operation ;
Cold Shutdown Load Omngos During Refueling Shirtdown Routine Power Operation i I
X Routine Stortty 0ther (Specify)
Operation _ _ _
Power: Reactor,;.12.40 F4 l" w Elec., 399'lafe Flo'4 : Recirc. , 8.6 x 10 gp:2 Feed., 4.5 iit 108 1b/he Reactor Pressure: 1020 psig TESCRIPTIW OF Oa Friday, July 5,1974, at 1540, while perforcing a routino OCCURRENCE:
survoillance test on the four J Main Steam Line Low Pressure Switches, it was discovered th'at switches P.E23B, C, and D tripped at 845, 857, and 854 pslNhehp{ctiv0!y.
i Those values I are holow the rinirem required trip point 'of 860 psig which is derived by adding to the Technical Specification limit of 850 psig a 10 psig head correction factor.
+ The "as fotnd" cad "as loft" switch settings were:
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Abnormal Occurrence Poport No. 50-219/74/35 PO'!C 2 "As Fcund" Settin o "As Inft" Settiy a FI23A c54 psig 864 psig FI23B S45 psig E62 psig RE23C E57 psig 863 psig DB23D 054 psig 862 psig APPAPDTT CAUSE X Design Proceduro GF OCCUEENCE: 1:anufacturc Unusual Service Conditien Installation / Inc. Enviren" ental Constructica ~~
Corp;nent Failura Operator Other (Spccify)
Suitch repentability is a recogni cd prchlea and work is in j r .
progress to forr.ulato a final soluticn.
i ANALYsrG OF M indicated in the bases of the TechMen! Specifications, f CCCUPffSG:
"iho tou pressure isolotion of the !!ain Stcen Lines at E50 i
psig was provided to give protection arrinat ft:st reactor I depressurizatica und the resultmt rapid cooldewn of the vessel. Adv ntage uns tcken of the scica fonture which occurs when the M2in Stean Inolation Valves cro clor.ed to provide for reactor shutdcma so thct high power operation at Icw reacter pressure dacs not occur, thus providing protec- 4 tien for the fml cladding integrity safety lielt." g f
The adverso consequences of reactor lostation occurring at recetor presrure approxitately 15 psig beloa the s >ccified )
a vininum value of 860 psig in lic.ited to those effects atten-d1nt to a greater than norn:a1 ronctor cooldcun rato. lho 1
fuel cladding integrity safety licit only con.cs into effect I 5,
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ihnor:aal Occurrence noport No. 50-219/74/55 Pog: 3 for pwer operctica at reacter pn'snures less than 600 psig or for pser operation greater than 354 Kit with less then 10% recirculation flou. Thorufore, the connequences of n IE. psig lower then nornni reactor isolction und scrcn set-point hcs no threatening effect whatsoever on the fuel clsMin;; int egrity.
The effects of a too rapid ecoldown due to the Icwer isoln-tien presnure nre ir. consequential ninee there iq. Icss than 212 difference between the saturation terport.ture for USO 4
psig end 835 psig, i C1UJLCr1VE . C7tinuing cpunctive actions being trken Lt this tir arc
/ Cfl0?i:
ns staten in A5nacol Occurrence Report Hos. 74-9, 74-10, 74-12, and 74-?2, and as restnted horcin: I 4
1 Investigation is being ccaducted into the basis for the stenn line 1w pressure sett!nh of E$0 psig. Developrznt of a Technical Specification chango to lover the sotpoint will fcilou if results of trcnsient annlyses indicste this possibility. (See Ibnorcal Occurrence Hopert No. 73-39.)
- 2. Re.co::c:andations to possibly reduce or clininate the sensor L a
setpoint change pmblen have bocn roccived. It was re-l il '
ported thot General Electric tests on a pulenting line I to sinninto plant conditions sher that pre-cycled Dads- 3 1
dalo switches show improvecent but that tho switches still i do not rect 14 repe!!tabill ty. Gcncral Bloctric, therefore, I
t.
s Abnormal Occurrenco <
,Rspidt No. 50-219/74/35O *. O +'. race-4 -
recow, ended an Ashicroft switch as it is more accurate.
The Ashcroft catalog mi-ber'is 61 S 6080_ DN20-06L-1028 ,
I As a result, one switch of each type. (pre-cycled Barks- ,
I-dale and Ashcroft) has been purchased ~ for. test and ]
evaluation at Oyster Creek. An Ashcroft switch is cur-rently on hand end undergoing evaluation. 4 i -
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PA1WPE DATA: Manufacturer data pertinent to these' switches are as follows:
Heletron corp. (subsidiaryfor Darksdale) ,
i Los Angeles, Californi'a Pressure Actuated Switch Model 372' Catalog #372-6SS49A-293 Rango 20-1400 psig -
Proof Psi.1750 G 1.f Provious Abnormal Occurrence Reports involving these switches are:
- 1. Letter to Mr. A. Gia::busso from Mr. D. A. Ross, dated Deccre.ber 24, 1973,
- 2. Abnornal Occurrence Report No. 74-l'.
- 3. Abnormal Occurrenco Report No' . 74-0,
- 4. Abnorm 1 Occurrence Report No. 74-10,
- 5. Abnor:asl Occurrence Report No; 74-12.'
- 6. Abnormal Occurrence Report No. 74-22-.
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Jersey Central Power & Light Company 3
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- MADISON AVENUE AT PUNCH BOWL ROAD
- 201-539-6111 General g{*, Public Utilities Corporation 4
July 15, 1974 VI A
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Mr. A. Giambusso u.ai(M www'""' q' y
Deputy Director for Reactor Proj.ects Directorate of Licensing g t.pm D3 ** ,
United States Atomic Energy Commission s N
T Washington, D. C. 20545 '
Dear Mr. Giambusso:
Subject:
Oyster Creek Station Docket No. 50-219 fincr= 1 00:urr:ne: ..:p;rt "
MO. 50 210/71/25 The purpose of this letter is to forward to you the attached Abnormal Occurrence Rep' ort in compliance with paragraph 6.6.2.a of the Technical Specifications.
Enclosed are forty copics of this submittal.
Very truly yours,
,uszbl ., %;
Donald A. Ross Manager, Nuclear Generating Stations es Enclosures i cc: Mr. J. P. O'Reilly, Director .
Directorate of Regulatory Operations, Region I
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a$1 Jersey Central Power & Light Company ($=f {f MADISON AVENUE AT PUNCH DOWL ROAD e MORRISTOWN, N.J.07960
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General, ', Pubhc Utahties Co,poration OYSTI!R CREEK NUCLEAR GENERATING STATION 1:0RKl!D RIVER, NEW JERSEY 08731 Abnormal Occurrence $ bMg Report No. 50-219/74/35 '
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lleport Date 'l pg t i]/1 - 5
, I'j July 15,1974 i, a -
Occurrence Date sc / ; iN_ ? t-July 5, 1974 Identification of Occurrence Violation of the Technical Specifications, paragraph 2.3.7, main steam line low pressure switches itE23Ii, C, and D were found to trip at pressures less ti t an the minimum required value of 860 psig. 'Ihis event is considered to be an abnormal occurrence as defined in the Technical Specifications, paragraph 1
1.15A.
i Conditions Prior to Occurrence The plant was in a routine startup.
The major plant parameters at the time of the event were:
Power: Reactor,1200 FMt Electric, 399 FMc Flow: Recirculation, 8.6 x 104 gpm I cedwater, 4.5 x 10 6 lb/hr Reactor Pressure: 1020 psig Description of Occurrence On Friday, July 5, 1974, at 1540, while performing a routine surveillance test on the four main steam line low pressure switches, it was discovered that switches RE23B, C, and D tripped at 845, 857, and 854 psig, respectively. These (e.-.~,;3 D~.
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Abnormal Occurrence No. 50-219/74/35 Page 2 values are below the minimum required trip point of 860 psig which is derived by adding to the Technical Specification limit of 850 psig a 10 psig head cocrection factor.
The "as found" and "as left" switch settings were:
"As Found" Settings "As Left" Settings RE23A 864 psig 864 psig RE23B 845 psig 862 psig RE23C 857 psig 863 psig RE23D 854 psig 862 psig Apparent Cause of Occurrence Design is considered to be a major factor contributing to this event. Switch repeatability is a recognized problem and work is in progress to formulate a final solution.
Analysis of Occurrence As indicated in the bases of the Technical Specifications, "The low pressure isolation of the Main Steam Lines at 850 psig was provided to give protection against fast reactor depressurization and the resultant rapid cooldown of the vessel. Advantage was taken of the scram feature which occurs when the Main Steam Isolation Valves are closed to provide the reactor shutdown so that high power operation at low reactor pressure does not occur, thus providing protection for the fuel cladding integrity safety limit."
The adverse consequences of reactor isolation occurring at reactor pressure approximately 15 psig below the specified minimum value of 860 psig is limited to those effects attendant to a greater than normal reactor cooldown rate. 'Ihe fuel cladding integrity safety limit only comes into effect for power operation at reactor pressures less than 600 psig or for power operation greater than 354 MWt with less than 10". recirculation flow. Therefore, the consequences of a 15 psig lower than normal reactor isolation and scram setpoint has no threatening effect whatsoever on the fuel cladding integrity.
The effects of a too rapid cooldown due to the lower isolation pressure are inconsequential since there is less than 2*F difference between the saturation temperature for 850 psig and 835 psig.
Corrective Action
'the corrective actions being taken at this time are:
- 1. l'ormal correspondence was initiated with General Electric Company on March 26, 1974 following numerous attempts at informal resolution of this problem. Since then, additional follow up conversation and correspond-ence, as recent as June 4, 1974, has ensued. General Elcetric has been
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. ,%, j ~ p O o Abnormal Occurrence No. 50-219/74/35 Page 3 requested to investigate the feasibility of a change to the Technical Specifications which would allow for tolerances or deviations on all instrumentation connected with safety systems and protective functions.
If this approach cannot be technically justified, General Electric has i been requested to develop a basis for a Technical Specification change to '
reduce the main steam low pressure setpoint considerably lower than the present 850 psig but with an acceptable margin to the 600 psig fuel cladding integrity limit for power operation. The above actions, if taken, will resolve the problem of the main steam line low pressure deviations.
Unfortunately, the approach and response by General Electric has not been entirely satisfactory and has caused delay in our resolution of the matter.
- 2. The Ashcroft switch that was reported in Abnormal Occurrence Nos. 50-219/74/10, 50-219/74/12, and 50-219/74/22 to have been undergoing tests, has been found to give excellent repeatability under controlled conditions. Ilowever, under conditions similar to that presently found during the surveillance of the Barksdale switches, the repeatability of the Ashcroft switches vary within their design limitations (+ _
1** of full scale). hhereas they may be somewhat superior to the Barksdale switches, they still are unsatisfactory for the Technical Specification limiting safety system settings.
Testing is continuing. Consequently, the above stated results are still considered to be preliminary in nature.
l 3. 'lhe General Office lleview Board has been involved in every instance of l instrument setpoint repeatability and has assigned to the General Public i
Utilities Service Corporation's Electrical Engineering Department the task of problem investigation. The item has been pursued in various General l
Office Review Board meetings when appropriate abnormal occurrences have
! been discussed, and the General Office Review Doard, as well as the Plant l Operations Review Committee, is committed to following the problem to a final solution. To date, a total of thirteen abnormal occurrences have i been identified this year to be the result of instrumentation repeatability l p rob lems . Most, if not all of the setpoint inaccuracies, however, fall
! within the manufacturer stated tolerances for the instrument involved. This l implies that repeatability as such is not in questi:,n. Consequently, the preferred action identified in "1" above would appear, at this time, to be the only reasonable solution for this condition. Six of the thirteen i reports have been generated as a result of " repeatability" of the main steam line low pressure switches. In this case, the alternate action in "1" above will be pursued in the event that the preferred action is not feasibic.
j Additionally, the General Public Utilities Service Corporation's Electrical Engineering Department has identified other means of monitoring this l parameter and has made recommendations to correct the problem, all of which l involve redesign of the monitoring network frem either a mechanical and/or electrical standpoint. The Jersey Central Power f, Light Company Generation Engineering Department is currently investigating with General Electric Company the feasibility of several of these alternate plans recommended by both General Public Utilities Service Corporation and the plant staff.
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Abnormal Occurrence No. 50-219/74/35 Page 4 Planufacturer data pertinent to these switches are as follows:
Ffeletron Corporation (subsidiary of Barksdale)
Los Angeles, California Pressure Actuated Switch blodel 372 Catalog #372-6SS49A-293 Range 20-1400 psig Proof psi 1750 G Previous abnormal occurrence reports involving these switches are:
- 1. Letter to Mr. A. Giambusso from Mr. D. A. Ross, dated December 24, 1973,
- 2. Abnormal Occurrence Report No. 50-219/74/1
- 3. Abnormal Occurrence Report No. 50-219/74/9
- 4. Abnormal Occurrence Report No. 50-219/74/10
- 5. Abnormal Occurrence Report No. 50-219/74/12
- 6. Abnormal Occurrence Report No. 50-219/74/22}}