ML20084J089
ML20084J089 | |
Person / Time | |
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Site: | Oyster Creek |
Issue date: | 04/02/1974 |
From: | Ross D JERSEY CENTRAL POWER & LIGHT CO. |
To: | Giambusso A US ATOMIC ENERGY COMMISSION (AEC) |
Shared Package | |
ML20084J091 | List: |
References | |
NUDOCS 8305100068 | |
Download: ML20084J089 (2) | |
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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML19343C2181975-12-23023 December 1975
[Table view]AO 50-219/75-33:on 751212,during 6-month Load Test on Station a batteries,125 Volt Dc Distribution Ctr de-energized.Caused by Personnel Error in Following Procedure.Distribution Ctr re-energized ML20090C9991975-12-12012 December 1975 AO 75-33:on 751212,125-volt Dc Distribution Ctr of Station a Battery Inadvertently de-energized.Caused by Failure to Establish Proper Breaker Lineup Preparation for Conducting Battery Load Test.Procedure changed.W/751219 Memo ML19343C2191975-12-11011 December 1975 AO 50-219/75-32:on 751203,during Testing,Emergency Diesel Generator 1 Failed to Start When Simulated Loss of Power Condition Applied to Fast Start Logic Circuit.Caused by Failure of Relay to Operate Due to Varnish on Armature ML20126E8281975-12-0303 December 1975 AO 50-219/75-31:on 751124,during Operability Test of Torus to Drywell Vacuum Breakers,Alarm Sys 2 Failed to Annunciate in Control Room When V-26-4 Opened.Caused by Failure of Relay Due to Contacts Being Detective.Relay Replaced ML20090D0071975-11-25025 November 1975 AO 75-31:on 751124,drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-4 Opened. Caused by Component Failure.Corrective Action Under Investigation ML20090D0161975-11-0707 November 1975 AO 75-30:on 751106,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17 a & C Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability.Pressure Switches Recalibr ML20090D0601975-11-0606 November 1975 AO 75-29:on 751027,torus Drywell Vacuum Breakers Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened. Caused by Sticking Microswitch ML20090D0761975-10-28028 October 1975 AO 75-29:on 751027,torus to Drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened.Caused by Component Failure.Corrective Action Under Investigation ML20090D0941975-10-24024 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil Replaced ML20090D1141975-10-17017 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1041975-10-16016 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil replaced.W/751016 ML20090D1341975-10-0808 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressures Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1501975-09-23023 September 1975 AO 75-26:on 750923,emergency Svc Water Pump 52C Failed to Start Automatically During Routine Surveillance Test of Containment Spray Sys Ii.Caused by Failure of Contact Switch in Time Delay Relay 16 K4B.Relay Replaced ML20090D2071975-09-0808 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML19291C2641975-09-0808 September 1975 AO 73-19:when Closing Signal Was Applied to Breaker S1A,loss of Power Occurred at 4160-volt Ac Bus 1A Causing Trip of Various Pumps.Caused by Incorrect Setting of Current Transformer Ratio Matching Taps.Taps Set Properly ML20090D1941975-09-0808 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2151975-09-0202 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML20090D2011975-09-0202 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2241975-08-21021 August 1975 AO 75-23:on 750817-20,stack Effluent for Iodine & Particulates Not Monitored.Caused by Personnel Error.Filter Installed in Operating Stack Gas Sampling Train ML20090D2261975-08-11011 August 1975 Preliminary AO-50-219/75-22:on 750810,stack Gas Sample Line Low Flow Alarm Received.Caused by Stack Gas Sample Pump a Not Running.Thermal Overload Protection Reset ML20090D2471975-08-0404 August 1975 Preliminary AO-50-219/75-21:on 750801,during Routine Surveillance on B Isolation Condensor Sys,Steam Line Valve V-14-32 Failed to Close on Simulation of Steam Line High Flow.Caused by Low Torque Switch Setting.Torque Increased ML20090D2521975-07-17017 July 1975 AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D, A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20090D2561975-07-0909 July 1975 Preliminary AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D,A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20084E1151975-07-0101 July 1975 RO 50-219/75-18:on 750623,two 8-1/2 Inch Handhole Covers in Standby Gas Treatment Filter Train Not in Place.Cause Unknown.Handhole Covers Repositioned & Secured ML20090D2741975-06-27027 June 1975 AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2661975-06-24024 June 1975 Preliminary AO 50-219/75-18:on 750623,handhole Covers in Standby Gas Treatment Filter Train 1-1 Not in Place.Cause Under Investigation.Covers Repositioned & Secured ML20090D2781975-06-24024 June 1975 AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83P & E Tripped at Pressures Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D2731975-06-19019 June 1975 Preliminary AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2901975-06-16016 June 1975 Preliminary AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83B & E Tripped at Pressure Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D6561975-06-0606 June 1975 AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned & Repaired ML20090D2971975-06-0606 June 1975 AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D2981975-06-0202 June 1975 Preliminary AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D6581975-05-30030 May 1975 Preliminary AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned ML20090D6611975-05-14014 May 1975 AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6641975-05-0707 May 1975 Preliminary AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6531975-05-0606 May 1975 AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17B & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatablilty.Switches Recalibr ML20090D6701975-04-28028 April 1975 Preliminary AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 178 & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatability.Switches Recalibr ML20090D6751975-04-18018 April 1975 AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7001975-04-14014 April 1975 AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure.Valves Adjusted &/Or Repaired ML20090D6811975-04-11011 April 1975 Preliminary AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7131975-04-0808 April 1975 AO-50-219/75-09:on 750329,breaker 1C Tripped Resulting in Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7061975-04-0707 April 1975 Preliminary AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure. Valves Adjusted &/Or Repaired ML20090D7271975-04-0303 April 1975 AO-50-219/75-08:on 750325,power Operation Continued W/ Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate.Caused by Failure to Properly Monitor Reactor Core.Rate Reduced ML20090D7211975-03-31031 March 1975 Preliminary AO-50-219/75-09:on 750329,breaker 1C Tripped Due to Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7651975-03-27027 March 1975 AO-50-219/75-07:on 750319,during Standby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Differential Relay Installed ML20090D7361975-03-26026 March 1975 Preliminary AO-50-219/75-08:on 750325,power Operation Continued W/Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate. Caused by Improper Reactor Core Monitoring.Rate Reduced ML20090D7761975-03-20020 March 1975 Preliminary AO-50-219/75-07:on 750319,during Stanby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Relay Installed ML20090D7801975-03-19019 March 1975 AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Continuously Monitor Stack Releases While Reactor in Unisolated Condition.Caused by Circuit Design.Request to Modify Circuit for Stack Gas Sample Pumps Submitted ML20090D7901975-03-13013 March 1975 AO-50-219/75-05:on 750306,during Monthly Surveillance Test, Containment Spray Pump 51A Failed to Start When Subjected to Simulated Signals.Caused by Breaker Trip Bar Failing to Reset After Previous Breaker Trip.Trip Bar Bushings Cleaned ML20090D7811975-03-11011 March 1975 Preliminary AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Monitor Stack Releases While Reactor in Unisolated Condition.Caused by faulty-circuit Design 1975-09-08 Category:TEXT-SAFETY REPORT MONTHYEAR05000219/LER-1998-011, :on 980914,three Small Bore Pipe Lines Did Not Meet Design Bases for Seismic & Thermal Allowables.Caused by Inadequate Structural Piping Analysis.Two 1/2 Sdcs Lines Were Modified During 17R RFO & 3rd Was Modified During 19991999-09-30030 September 1999
[Table view]
ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B7331998-08-13013 August 1998 Safety Evaluation Supporting Amend 196 to License DPR-16 ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station 05000219/LER-1997-013, Has Been Canceled1998-06-30030 June 1998 Has Been Canceled 1999-09-30 |
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.ersey Central Power & Light Company lk['M cv QQ9 MADISON AVENUE AT PUNCH BOWL ROAD
- MORRISTOWN, N.J.079GO
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/[,yjj, Poc utm::e3 corcarat en cenerai D b7E M April 2, 1974 Mr. A. Giambusso
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Deputy Director for Reactor Projects i'
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United States Atomic Energy Commission Washington, D. C. 20545 0,.
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Dear Mr. Giambusso:
VC'.
Subject:
Oyster Crcok Station Docket No. 50-219 Hydraulic Shock and Sway Arrestor Inspection -
January 1974 The purpose of this letter is to forward to you supplementary in-formation regarding the seals of five " failed" hydraulic shock and sway arrestors (snubbers) found in the drywell during the plant shutdown which began on January 12, 1974. The initial report on the January inspection of the snubbers in the drywell was forwarded by letter dated February 19, 1974.
A visual inspection of the seals removed from the five failed snubbers indicated that several types of material were used in each unit. To determine which of the materials had failed, the seals were sent to the GPU System Lcboratory for material identification analyses using infrared scans and microscopic examinations. The results of the naterial analysis can be sunnari::ed as follows:
1.
Only three seals in cach snubber werc of the recommended polyethylene-propylene (PEP) material.
2.
None of the PEP seals showed any sign of failure.
3.
Two types of polvurethane were used in the failed snubbers.
These were the millabic gun and the cast polyurethane.
4.
One fiber seal was also discovered in two of the snubbers.
Both of these units were of an old seri.es which could not be rebuilt completely. The fiber seals had probably never been changed out at the tine the snubbers were rebuilt or they were cut from new unidentified gasket material.
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'\\..l w.j Mr. Giambusso April 2, 1974 5.
One other seal used in the two old series snubbers could not be identified. The material is believed to be teflon.
6.
The seals which, because of their physical characteristics, had visually appeared to be failed before the laboratory analysis are now identified to be millable gum polyurethane.
We believe the results of the laboratory analyses provide further evidence that ethylene-propylene is the material best suited for replacement seals in the hydraulic snubbers located in the drywell and in the reactor building.
Enclosed are forty copics of this submittal.
Very truly yours,
'7
'jfV,%Lh Donald A. Ross Manager, Nuclear Generating Stations es Enclosures cc:
Mr. J. P. O'Reilly, Director Directorate of Regulatory Operations, Region I
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