ML20084J276

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Ao:On 730504,during Local Leak Rate Testing,Torus to Reactor Bldg Vacuum Breaker Lines Failed to Hold Pressure Between Isolation Valves V-26-17 & 18.Caused by Butterfly Valve V-26-18 Leakage.Valve Linkage Adjusted
ML20084J276
Person / Time
Site: Oyster Creek
Issue date: 05/15/1973
From: Ross D
JERSEY CENTRAL POWER & LIGHT CO.
To: Anthony Giambusso
US ATOMIC ENERGY COMMISSION (AEC)
References
NUDOCS 8305120379
Download: ML20084J276 (2)


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M ADISoN AVENUE AT PUNCH BOWL Ro AD e MoRRISToWN. N.J. 07960 e 539 6111 May 15, 1975

$1 Mr. A. Giariousso N,/

Deputy Director for Reactor Projects MD

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Dear Mr. Giambusso:

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Subject:

Oyster Creek Station 7,

Docket No. 50-219 Nv i Failure of Torus to Reactor Building Vacuum Relief Valve V-26-18 This event is considered to be an abnormal occurrence as j

Q defined in the Technical Specifications, Paragraph 1.15.F.

Notifica.

i tion of tinis event, as required by the Technical Specifications, Para-

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graph 6.6.B, was made to AEC Region I, Directorate of Regulatory Opera-

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y tions, on Friday, May 4, 1973.

i While performing local leak rate testing, it was found that l

one of the torus to reactor building vacuum breaker lines would not d]'

hold pressure between the isolation valves (V-26-17 6 18). The lack of j

air Icakage through check valve (V-26-17) indicated that the Icakage was f

through the butterfly valve (V-26-18).

l Details of the valve are as follows:

Air Operated Butterfly, Rockwell E

Size - 20" Rating - 150 psi Operator - Conoflow Corp.

Inspection of V-26-18 showed that the valve was 0.010 inches

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off the seat, indicating that the linkage on the valve arm required adj usttrent.

The valve was inspected and the boot seat and butterfly disc I

were found in good ~ condition. The valve was found to be 0.010 inches off the seat. The boot seat and butterfly disc were cleaned and the valve

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, i linka,ge was adjusted to position the zalve disc properly on the seat.

"The adjustment consisted of increasing the stroke in the close direction.

i The line between the isolation valves was then pressurized and the

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1eakage was calculated to be 0.492 SCFH well within the technical specifi-

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cation limit. The cause of the change in linkage adjustment has not been determined, t

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There was no safaty significance associated with this occurrence since the redundant component (check valve V-26-17) was shown to be Icakage tight. This is implied by the fact that the check valve was not j

moved during the testing period, so that the maximum possible Icakage through the check valve was 0.492 SCFH.

r To prevent a reoccurrence of this type problem, indicating marks were placed on the disc shaft.

Several operating tests will be perfonned prior to plant startup to verify repeatability of linkage and valve I

position based on these markings.

Also, additional leak rate measurements will be performed prior to plant startup to verify the adequacy of re-

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lying on these new markings to ensure the valve has closed properly i

following future operability surveillmice tests.

Very truly yours, i

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Donald A. Ross Manager, Nuclear Generatir.g Stations cs Enclosures (40) 6 f

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Mr. J. P. O'Reilly, Director

.j Directorate of Regulatory Op rations, Region 1 t

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