ML20084J712

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Ao:On 730310,recirculation Loop Started When Coolant Temp & Reactor Coolant Temp Exceeded 50 F Differential.Caused by Personnel Error.Recirculation Sys Operating & Emergency Procedures Revised
ML20084J712
Person / Time
Site: Oyster Creek
Issue date: 03/23/1973
From: Ross D
JERSEY CENTRAL POWER & LIGHT CO.
To: Anthony Giambusso
US ATOMIC ENERGY COMMISSION (AEC)
References
NUDOCS 8305180677
Download: ML20084J712 (3)


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Jersey Contral P ' wer & Light Company

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M ADISoN AVENUE AT PUNCH BOWL Ro AD 9 McRRISToWN, N.J. 07960 e 539-611 t March 23, 1973

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-a Mr. A. Giambuss M

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Deputy Director for Reactor Projects y bggd' j

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Dear Mr. Giambusso:

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Subject:

Oyster Creek Station

'M Docket No. 50-219 Technical Specification Violation c

The purpose of this letter is to report a violation of our Technical Specifications, Paragraph 3.3.C.2 whereas a recirculation loop was started when its coolant temperature and the reactor coolant temperature exceeded a 50 F differential.

This event is considered an abnormal occurrence as defined in Technical Specifications, Paragraph 1.15.0 and Paragraph 1.15.C.

Notification of this event, as required by the Technical Specifications, was made to ti e AEC Region 1, Directorate of Regulatory Operations, on Mard 12, 1973.

y On March 10, 1973, the B reactor recirculation pump was removed from service to permit replacement of worn brushes on its

! associated motor generator set.

Upon ccapletion of the maintenance work, the pump was restarted.

During the restart, a flux spike was observed on the APIG1 channels - along with a. momentary rod block and

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high flux alarm. The shift foreman, upon investigating the flux

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spike, observed that the B loop temperatures had decreased to approximately 407 F from the normal 524 F during the time interval

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the pump was out of service.

Since the plant was operating at

" q N' reduced power at the time, only the high flux alarms were received I 'p f

even though APPJ1 channels 4 and 7 recorded approximately an 8% flux

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spike and APICI channel 5 recorded approximately a 20% flux spike.

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This event occurred due to the failure of operating F

t personnel to use existing procedures which 'contain a precaution against starting a recirculation pump if its associated loop temperature is not within 50*F of the reactor coolant temperature.

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Mr. A. hbbusso V

The mechanism which caused the temperature difference to occur is associated with the B recirculation loop piping connections associated with the cleanup system.

Figure 1 shows a sketch of the B recirculation loop piping arrangement.

When the recirculation pump was removed from service, the two-inch discharge bypass valve is opened, the discharge valve is closed, and the pump suction valve remains open.

This valve line up normally allows reactor vessel water to flow back through the pump and associated piping to maintain its temperature at near reactor coolant temperatures.

On the B recirculation loop, however, the cleanup system draws water from the pump suction line and returns same to the reactor vessel via the pump discharge line at a temperature of approximately 450 F.

With the B recirculation pump in service, this water is mixed with circulating reactor coolant water at the pump discharge.

It is now recognized that when the B pump is not in service, a flow path is set up which allows the cooler cicanup system return flow to be drawn back through the pump and into the suction piping leading back to the cleanup system thus causing that water volume to slowly cool down.

During the PORC review of this event and after questioning the individuals involved, it became evident that this situation has occurred on at least five previous occasions when the B recirculation pump was secured for brush maintenance or had tripped off due to other causes.

Subsequent action included contacting the reactor designer in an effort to evaluate the significance of the above event.

By comparison with the Zir.mcr Statica recirculaticn out1ct nozzle analysis for improper start of a cold recirculation loop (400*F T for 26 seconds vs. Oyster Creek 117"F for approximately 5 seconds) showed only skin stresses, which were easily accounted for by the fatigue analysis.

On this basis, we have i

been advised it can be concluded that the described transient for Oyster

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Creek is insignificant and may be ignored. This evaluation will be supported by calculations of recirculation loop nozzle stresses specific

{f to the Oyster Creek design.

We presently plan to have these calcula-tions completed and made availabic to the AEC within ninety days from this date.

Further, the recirculation system operating procedure and h'

associated emergency procedure will be revised to include the precaution related to the observed effects of the cleanup system operation on the B recirculation loop.

We are enclosing forty copies of this report.

Very truly yours, O

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Donald A. Ross Manager, Nuclear Generating Stations Pk Enclosures cc: Mr. J. P. O'Reilly, Director Directorate of Regulatory Operations, Region 1 k.

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