ML20084C921

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AO 50-219/74/40:on 740715,one Bergen-Paterson Hydraulic Shock & Sway Arrestor on South Core Spray Sys in Drywell Noted Inoperable.Caused by Loss of Hydraulic Fluid.Unit Replaced
ML20084C921
Person / Time
Site: Oyster Creek
Issue date: 07/16/1974
From: Carroll J, Parsall R
JERSEY CENTRAL POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
AO-50-219-74-40, NUDOCS 8304080350
Download: ML20084C921 (3)


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i Initial Telephone Date o 3 Ituport Dat e : 7/16/74 Occurrence: 7/15/74 4 q Initial 1lritt en Tir:e of j Report Dat e : 7/16/74 Occurrence: 1400 OYST!ilt CREEL: NUCLEAR CliNIIRATING STATION FORKED RIVli!t, NE!! JEllSEY 08731 Nmomal Occurrence Report No. 50-219/74/ 40 r IlEN f1FI CAT 10:; Inoperability of one Bergen-Paterson !!ydraulic Shock and Swdy OF OCCU!!!1:CE Arrest or locat ed on the scutt' core spray systen in the drvwell; This event in considered to be an abnornal occurrence as de-fined in the Tech: 'c,1 9 'c!4 ! c ra ! cr.s, p ra3raph

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t OJ'.!H T10XS Hu O'. TO OCCIE:RIN Ct Steady State i;o.eer ~ Operation Routine Shutde..in llot Standby I Cold Shutde n 1.oad Changes During _ _ tciuclin .,auido.u emo r,,m "e.7er ope r:.ti er, lloutine Startup x Othc r (Speci fy) Operation The reactor vas shutdcen.i t h react m c to ta p rature ~ 1 ] css than 21:0F. DESCRI PTION An inspection of the dryuel] shock and sway arrestors, 0F OCCURRENCE. ' erf c: Pat erson Type IF."A~ 13, J ocnted rn inoperabic unit en the south core spray system. The inoperable unit was installed e in the drywell during t he Snring hefueling Out ar,e a ft er i t hr..i 1, rel 1 -{ 1; Ai7id 'V: !9 ~ < Pre e6re l 0:- (L L'l; 4: 1.'

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3 Abnormal Occurrence Rep art I,'o. 50-219/74/40 Par,e 2 1 The cause of the snubber inoperability was due to loss of l hydraulic fluid. Examination of the unit revealed two small cuts on the rain cylinder shaft U-cup caused by burrs on the piston. K1ALYSIS OF The s a fe t '.,i gnifi cance of this occurrence was a partial loss OCCURRENCE: of seisnic restrainine ability for the affected systen. 11ad l the plant suf fered.. der.ign bases carthquake, the probabili ty 1h;t the enn h core spra wsten unuid have suffered structe,' w u, ao: l CORRECTIVE The failed unit was replaced with an identical snubber which f ACr101: } .-s Ichuilf 1:ith et Im1 on.. pynpy1ogn r,-tr~j7,1 333 779,, 3 3 7c test ed to 4,000 psi. FAf LllllE InTA: Manufacturc - !!e rg en - P - m l 'l ype - IISS 't-1 C i Serial Ke:.ber - 487F i i s i i 4 s i i i i I l l .iq r, 9 'ccparcd hv .\\.J.1 N'. h (.'L8 6. q )k n 1 Dat n ; 7/l f,/ 74 y .}}