ML20009C136

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LER 81-003/01X-1:on 810226,steam Generator B Was Pressurized to 550 Psig.Caused by Procedural Deficiency.Valves Opened to Lower Once Through Steam Generator Pressure.Condensate & Feedwater Procedure Will Be Revised
ML20009C136
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 06/10/1981
From: Jackie Jones
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009C128 List:
References
LER-81-003-01X, LER-81-3-1X, NUDOCS 8107200314
Download: ML20009C136 (1)


Text

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l Evewrnascairtion On February 26,AnoemosAat.scosssacueness 1981, the "B" Steam @ Generator was pressurized to 550gpsig.

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No systems or piping were damaged by this incident. The integrity of the

main steam lines, hangers, and the OTSG itself were v.erified.'~hus, this g g , incident was of no significance with respect to safe operation, and the g g ; health and safety of the public was not affected. p

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,,,,,l The major cause of the incident was the result of a procedural deficiency. ,

,,,,,, Valves 3SD-5 and 3SD-290 were opened in order to Jowe,r the OTSG. pressure. ,

, The Condensate and Feedwater procedure will be revised to lower OTSG level to

between 50% and 80% on the operating range prior to initiating FDW recirculation

[ A note will also be added to close the start-up block valves if the control ,

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  • (704) 373-8197 8107200314 810610 PMCN :

PDR ADOCK 05000287 S PDR

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