ML20040E664

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LER 81-020/03L-0:on 811226,borated Water Storage Tank Channel a Level Instrumentation Declared Inoperable Due to Erratic Indication.Cause Undetermined Due to Intermittent Occurrence of Erratic Indication.Instrument Returned to Svc
ML20040E664
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 01/25/1982
From: Kutzer J
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20040E663 List:
References
LER-81-020-03L-02, LER-81-20-3L-2, NUDOCS 8202050220
Download: ML20040E664 (1)


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