ML20052H695

From kanterella
Jump to navigation Jump to search
LER 82-007/01T-0:on 820428,during Final Reactor Bldg Insp, One Vertical Tendon in Secondary Shield Wall Was Found Broken.Caused by Stress Corrosion of post-tensioning Wires Near Stressing Washers Due to Water
ML20052H695
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 05/12/1982
From: Kutzer J
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20052H689 List:
References
LER-82-007-01T, LER-82-7-1T, NUDOCS 8205210347
Download: ML20052H695 (1)


Text

.

M AC PoAsa 34 U. S. NUCLEAR RECULATORY coa 4MassJoas mm IJCENSEE EVENT REPORT EXHIBIT A coninot stoco l l l l l cetzAss enmr on Tveir att. nscusato moona4Ancm i l .!@

$. l S l C. lucw N u.[Ecoo. lE l 2 [g.0 l 0l- l 0 l ucwn

.. 3 0 l 0~v-na l 010l- l 0 l 0a lg{= 4l ucan 1l 1 l nn 1(1a lg[i,c.r.g l l

.; r. T l,j!.lL.J Z @.la 0 l5 l 0 l 01 .. oocOl

.r 2 uu lna7 l 0 @l0 = l !4evaar12 caral 8[ 812@l0 l 511l2

1. is aercaroar.l812 l@

EVENT QEscDWDON ANO PmosAELE CoNsECUENCES O'o o l_On April 28, 1982,.during the final Reactor Building inspection, oac vertical [

, tendon in the secondary shield wall was found broken. Subsequent detailed

, , ,inspectio'n of Units 2 and 3 found one additional failed tendon in Unit 2 and ,

[TTT1 I some rusted vertical tendons in Units 2 and 3. The primary structural integrity; o e lof the wall system and its abilftv to nerform its deslen function are consideredt o , lto be intact; thus, this event did not have a significant effect on the health 9 l

L,o_L.J. .l and safety of the public. _

=

"cnii . 'c^e' J.^M'. .ui'"o;.

c JOM.

a .

l XI x lg t..sj@ L,," J@ I X I Ii'Y.1=co.I IX x!x[ g g g g g S.out wilAL oCCUA*ENCE 2. PORT ASVISion.

u nimo 8YEMf VEAA REPOR r 864L coo 8 rype apCL

@ , agar l 8l 2j [--.j [ Ol0 l 7 l y 10l1I Q g @

n u o s. u u a a a u u Of" ".ci'"J cA'A'Ur 'SZs" . ^".'57t"ra'

. ,o"0% '"J"Aci"/-

l.c"lu",7..

Q u lGl@-

l C [g a l=A [@ ul0l4lJ@l6l . W@ l. N[@ lLl@

.. . l P [ 316 l 2l@ .,

cAusa oescairnoN ANo coamEenvE AencNs

,The apparent cause of this occu encewasstresscorrosionofthepost-tensioning g l wires near the stressing washers caused by water in the bottom of the vertical ,

g [ tendon sheaths. Defective tendons will be replaced and bottom grease caps ,

E lmodified to allow water drainace. A tendon surveillance program will be imple- l

, , [mented ,

P8 sco-en orwensrAru. @ " E in i

oi covenycasemirnon @

li Is l W@ l OIO ln l@[ Hot shutdown l' lA l@l Operator observation l

. *Enviry co'Siswr '* " ** ** "

AMOUNrof ACnViry @ l NA LOcArlomof AEttAss @

t a =et

[yjASE@o CP mgLtAsg[7J@l NA l l naso ==et enrosUses nn o nc..no,. @

i 7 l I-lu....2l' O!@W@l Maintenance - 6.7 Rem l reaso==e't nuu'lias **

wuu.en ossemenoa@

Q l0l0l0l@[

NA l

l 'oss on on oEaceSo a.ciury /~h nre c asca.eno= c X^

L,LL*J. L. EJ@l ..

l

@ IS3uf

, . L. N,J

@l IICEFUO88 i.

NA I Illl!lll lllll S

h O

, . . __ _ _