ML20027B462

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LER 82-009/01T-0:on 820804,during Refueling Insp of Reactor Coolant Pump,Five Closure Studs Found Degraded in Size Below Tech Spec Min.Caused by Boric Acid Corrosion Due to Closure Gasket Leakage.Studs Replaced
ML20027B462
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 09/10/1982
From: Petty J
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20027B461 List:
References
LER-82-009-01T-01, LER-82-9-1T-1, NUDOCS 8209210048
Download: ML20027B462 (1)


Text

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N C FORM 366 U.S. NUCLE AR R EGULATOR Y COMMISSION APPROVED BY OME l'"

LICENSEE EVENT REPORT $'EPIAEE4ao4:

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l 0 l2 l lDurinc a refuelinn insnection of Reactor Coolant Pimn (PCP) closuro grud nn l lol3ll August 4, 1982 at 1000, it was determined that five closure studs, two on 3Al l lo l4 l land three on 3A2, on Unit 3's RCPs had been degraded in size below the minimum l

,,,,;l acceptable diameter of 3.250 inches. This was reportable per T.S. 6.6.2.1.a. (9)[.

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[d@y @ l Zl@ l Zl@ l 0 j 0 l 0@l 0l [Nj @l Nl Q l Lj @ l Bl2 l6 j 5 l 33 34 5. 34 3, 4. 41 42 45 44 er CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i j o l lThe closure studs degraded because of boric acid corrosion due to a closure l

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