ML17223A359

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NPDES Noncompliance Notification:On 890803 & 04,plant Discharge Canal Temp Exceeded 113 F Limit.Unit 1 down- Powered to Clean Condenser Water Boxes
ML17223A359
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 10/16/1989
From: Sager D
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-89-368, NUDOCS 8910240217
Download: ML17223A359 (7)


Text

DOCKET 05000335

SUBJECT:

NPDES noncompliance notification:on 890803 6 04,plant discharge canal temp exceeded 113 F limit.Util down-powered.

DISTRIBUTION CODE: IE25D COPIES RECEIVED:LTR ENCL SIZE: TITLE: Environmental Monitoring Rept (per Tech Specs)NOTES: ACCELERATED DI BUTION DEMONSTRATION SYSI'EM REGULAT INFORMATION DISTRIBUTION STEM (RIDS)ACCESSION NBR:8910240217 DOC.DATE: 89/10/16 NOTARIZED:

NO FACIL:50-335 St.Lucie Plant, Unit 1, Florida Power 6 Light Co.AUTH.NAME AUTHOR AFFILIATION SAGER,D.A.

Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)RECIPIENT ID CODE/NAME PD2-2 LA NORRISiJ, INTERNAL: ACRS IRM TECH ADV~REP RPB 10 RE XT 01 LE 02 COPIES L'gTR ENCL 3 3 1'1 1 1 1 2 2 1 1 1 1 RECIPIENT.ID.CODE/NAME PD2-2 PD AEOD/DSP/TPAB NRR ROTHMANgR NUDOCS-ABSTRACT RGN2 DRSS/RPB COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 h EXTERNAL EGSG S IMPSON i F NRC PDR 2 2 1 1 LPDR 1 1 h TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19 P.O.Box14000, Juno Beach, FL 33408-0420 oCTOBHR i 6 19B9 L-89-368 U.S.'uclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:

Re: St.Lucie Unit 1 Docket No.50-335 Environmental Protection Plan Report-National Pollutant Dischar e Elimination S stem NPDES Re ortable Event In accordance with Section 3.2.1.of the St.Lucie Unit 1 Environmental Protection Plan, attached is a copy of the Discharge Monitoring Report (DMR)required by the St.Lucie Plant NPDES Permit with respect to a reportable event.Additionally, a description of the event is provided.Very truly yours,<ad D.A.ger Vice sident St.Lucie Plant DAS/MSD/gp Attachments cc: Stewart D.Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, St.Lucie Plant I se>02O02>7 S9iOib PDR ADOCK 05000335'q g PNu an FPL Group company f t PERMITTEE NAMEIADDRESS llnklnch Fnrirlrie lenrkk/Lorn r ion ff djffkrknrl NAME Q~t~rl~~~-~ol e L!L n ADDREss~~tati lre~i~t A+I-A+I?S ail~eM t"~cj.i FACILITY LOCATION'TTN: To Ro FAIR PARAMETER (32-3T)NATIONAL POLLUTANT DISCHARGE ELIMINATION SYSTF M (NPDES J DISCHARGE MONITORING REPORT(DER)

(2-)6J ((7-)9)FL0002200 001 1 PERMIT NUMBER DISCHARGE NUMBER Form Apptovrd F-FINAL CONU t;AUX COOLING'yf'A~V~.FL, 334 0d MAJOR (SU&i?JA)NOTE: Read Instructions before completing this form.(26.27)(2(f-29)(3M(J (20.2!)(22-23J (2C-25)(C Crrrd Only)(3(f45)(3 Card OrtlTJ QUANTITY OR LOADING (C6.53J (jdidl J OUALITY OR CONCENTRATION (Cd 53)(5C4)J FREQUENCY OF ANALYSIS (dd J58J NO.EX SAMPLE TYPE MAXIMUM AVERAGE UNITS AVERAGE MAXIMUM MINIMUM UNITS 6MB (69.Tft)MONITORING PERIOD YEAR MO DAY Y 0 D Y FROM y u v TO TEMP ERATURL'-v>>A1 f-.t,~L(FAH,'?Eidlii.1 1'30011 1 0 0 UENT GR(ISu VALUE.I LHP~DIFF~ULI I(ELif~AN o t UP iT ILf'i UE--~f-uoV13 1)0 L FF ULeN1 dict)SS V ALUI.SAMPLE MEASUREMENT PERMIT REQUIREMENT SAMPLE MEASUREMENT PERMIT REQUIREMENT Ar AA hr rrV~Y P~OOPVVA A A A A A Y Y'Y Y V A r A VtpffteXhtv h A A vvh v rv r'ip p A J 4 P'Ir AAAA vvv r AA vv rvvv rpv AA A 4'P YYYV'P Yv r INST,HX DEAF INST'X DLGoF./(Hc 3I?ON 9 TIJTAI (AS:)..I 1022 2 4'Ni I V.nL Jtr SAMPLE MEASUREMENT PERMIT REQUIREMENT AA AAAA r Y rv.r~hAAJ'PPVP~e JttetA J y A A h A r Vh'rff AAAAAA vvvv rff~0 INST, MX HG/L BATCH VX IL',EINTS s TOTAL.Ai=SIDUAL 94044 P 0 U)CIDENlst Tt)TAL ftt.SI DUAL I4t)44 Q 0 0 I'i~SAMPLE MEASUREMENT PERMIT REQUIREMENT SAMPLE MEASUREMENl'ERMIT REQUIREMENT AA AA YVV YVV 4 AJ A hA lf'pep e 4A A A VV Per P P AAA~ff h AA AAA er ff VVY~J 4 A'Y V'V A A vrr A AA rvv Y A J AAAA r Yvv YC POOha AAAA J A YVAV P P'P qietrh JeA A A A rvff vfr r AA AA 4 Vfft p per<, o 0~3 INST'HX XG/L Onl INST MX.HG/L Q 1A.OM UOUS Ol IN VOUS 0 0 OX10ENTSv FRE'-s\VAI LAUL-34045 I?0 0 f3XI t)FI4TS v FRI:=AVAILAt)L~

)4045 S 0 0 SAMPLE MEASUREMENT PERMIT REQUIREMENT SAMPLE MEASUREMEN'r PERMIT REQUIREMENT r AAA erff 4~p AA JIA 4A AAA VYMYVY J A JeAAA~ff'ff P'P Y AA AA A VrVVeff AAA AA A v p r"p lk'l v p p~AA A A Ie lr YV VVYff Vh t V'AA rvv r A AAA ff'vvv e v A J AAA N ht II OY~P ,o%0~2 DAILY AV ,p4 Oo2 DAILY AV Oe'5 INST HX HG/L Oe5;INST-(AX.XG/L EEKL EEKL DATE NAMBTITLE PRINCIPALEXECUTIVEOFFICER TELEPHONE I certify under penalty of law that this document and all attachments were prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel propedy gslher and evafuate the information submitted.

Based on my inquiry of the perSOn Or persons who manage the system.or those persons directly responsible for gathering the information, the Intorrnatfon submined Is.to the best ol my knowledge and belief.true.sccursle.snd complete.I sm aware thai there are signiticant penalilies lor submitting false information.

including the possibility of fine and Imprisonment for knowing violations.

SIGNA REOF PRINCIPAL CUTIVE OFFICER OR AUTHORIZED AGENT DAY Mo YEAR NUMBER TYPED OR PRINTED COMMENT AND EXPLANATION OF ANY VIOLATION:

AUX IL I Alv Y e r'i)ill)iliS tth Ik;)I-"Cti.'al.:.~

I'"t.i'-'"0 tr I FU,'+SE.V 4't'ItiCW~'L VCt c C-.UISCHA?Gt 9 H.=UN I f 1s S=UD IT 2 BORON HUNITORINb R'i='LJUIREO;v'HL:N I'ICTUS 44'HATLf?S TUr?A~'Ail'i~r ISO NOi'f Ai RATEi)Iv AT<:I HULO I Nio TANK~.p)r hr-t>ay$g...r r EPA Form 3320.1 (Rev.10-79)

PREvtous EDITloN Yo BEUsED IREPLACES EPA FORM T ao WHICH MAY NOT BE USED.)UNTIL SUPPLY IS EXHAUSIED.

01135/061409-045't PAGE 1 OF 4'V rQ DESCRIPTION OF THE EVENT The following is a description of an event which occurred at the St.Lucie Plant on August 3 and 4, 1989.This information was reported to Steve Scholfield of EPA by Ron Hix of FPL Environmental Affairs on August 7, 1989.Mr.Scholfield requested that this written report be submitted with the appropriate DMR.On the dates and times listed below, the St.Lucie Unit 1 discharge canal temperature exceeded the 113'F limit allowed for normal operation.

Au ust 3 1989 Au ust 4 1989 Time 1300 hrs 1400 1500 1600 1700 1800 1900~Tem 114'F 114 114 115 115 114 115 Time 1400 hrs 1500 1600 1700~Tem 115'F 114 114 114 During these periods, St.Lucie Unit 1 was experiencing severe condenser fouling.The St.Lucie Plant.NPDES Permit allows 117'F at the discharge terminus under these conditions.

Unit 1 was down-powered the evenings of August 4, 1989 and August 5, 1989 to clean condenser water-boxes.

Since that time discharge canal temperatures have returned to below 113'F.

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