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Other: L-85-291, Advises That Schedule for Responding to NRC 850621 & 0711 Requests for Addl Info Re TMI Action Item II.D.1 Will Be Provided by 851031.Info Must Be Obtained from NSSS & Ae, L-85-397, Advises That Util Will Provide Response to NRC 850621 & 0711 Requests for Info Re Relief & Safety Valve Test Requirements Per TMI Item II.D.1 by 860315, L-89-225, Informs That Resolution of Items Outlined in Section 5.2 of Technical Evaluation Repts Re NUREG-0737,Item II.D.1, Performance Testing of Relief & Safety Valves Will Be Completed by 891215, L-89-455, Discusses NUREG-0737,Item II.D.1, Performance Testing of Relief & Safety Valves. Due to Significant Addl Analytical Work Required for Item 8 of Ser,Completion Schedule Extended Until Aug 1990
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MONTHYEARML17216A2311985-06-21021 June 1985 Forwards Request for Addl Info Re Response to TMI Action Item II.D.1, Relief & Safety Valve Test Requirements. Response Requested within 30 Days Project stage: RAI L-85-291, Advises That Schedule for Responding to NRC 850621 & 0711 Requests for Addl Info Re TMI Action Item II.D.1 Will Be Provided by 851031.Info Must Be Obtained from NSSS & Ae1985-07-26026 July 1985 Advises That Schedule for Responding to NRC 850621 & 0711 Requests for Addl Info Re TMI Action Item II.D.1 Will Be Provided by 851031.Info Must Be Obtained from NSSS & Ae Project stage: Other L-85-397, Advises That Util Will Provide Response to NRC 850621 & 0711 Requests for Info Re Relief & Safety Valve Test Requirements Per TMI Item II.D.1 by 8603151985-10-18018 October 1985 Advises That Util Will Provide Response to NRC 850621 & 0711 Requests for Info Re Relief & Safety Valve Test Requirements Per TMI Item II.D.1 by 860315 Project stage: Other ML20247F5211989-05-11011 May 1989 NPDES Noncompliance Notification:On 890309,effluent Ph of Unit 1 Sewage Treatment Plant Observed to Be 3.6 Std Units. Unknown Quantity of Effluent W/Ph Less than 6.0 Std Units Discharged.Sodium Carbonate Added to Correct Ph to 6.2 Project stage: Request L-89-225, Informs That Resolution of Items Outlined in Section 5.2 of Technical Evaluation Repts Re NUREG-0737,Item II.D.1, Performance Testing of Relief & Safety Valves Will Be Completed by 8912151989-06-23023 June 1989 Informs That Resolution of Items Outlined in Section 5.2 of Technical Evaluation Repts Re NUREG-0737,Item II.D.1, Performance Testing of Relief & Safety Valves Will Be Completed by 891215 Project stage: Other L-89-455, Discusses NUREG-0737,Item II.D.1, Performance Testing of Relief & Safety Valves. Due to Significant Addl Analytical Work Required for Item 8 of Ser,Completion Schedule Extended Until Aug 19901989-12-13013 December 1989 Discusses NUREG-0737,Item II.D.1, Performance Testing of Relief & Safety Valves. Due to Significant Addl Analytical Work Required for Item 8 of Ser,Completion Schedule Extended Until Aug 1990 Project stage: Other 1985-07-26
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DESCRIPTION OF THE EVENT The following is a description of a non-conformance event'which occurred at the St.
Lucie Plant.
This event was reported to Priscilla Oliver of EPA by telephone on March 9, 1989.
At 10:20 a.m.,
on March 9, 1989, the effluent pH of the Unit #1 sewage treatment plant was observed to be 3.6 standard units (su).
On the previous day at 9:15 a.m.,
the pH'was 6.5 su.
Addition of sodium carbonate corrected the pH to 6.2 su by 11:00 a.m.
Influent water was observed to be 8.8 su.
While there was no actual flow from the plant to the intake canal at that time an unknown quantity of effluent (less than 7,500 gallons) with a pH of less than 6.0 su had been discharged since the previous day's sample.
Average daily flow for the previous week was approximately 0.0075 MGD.
This effluent is diluted by approximately 720 MGD of sea water flow which is. pumped by once-through cooling water pumps through the Unit #1' Power Plant.
l While a definite cause for the low pH has not been determined, it is suspected that an acidic solution was disposed of into the Unit
- 1 sewage system.
There were presently 1,000 extra people on site for the Unit #2 refueling work.
A letter was distributed to all employees, including temporary employees, that no chemical should be discarded down any drain.
No adverse effects to the environment were observed.
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8905300095 890511 PDR ADOCK 05000335 R
PDC
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