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{{#Wiki_filter:4A.JDOV6.IJREGULRTOINFORMATION DISTRIBUTION NTEM(RIDS))ACCESSION NBR:9703100241 DOC.DATE:
{{#Wiki_filter:4A.J DOV6.I J REGULRTOINFORMATION DISTRIBUTION NTEM (RIDS))ACCESSION NBR:9703100241 DOC.DATE:~~~NOTARIZED:
~~~NOTARIZED:
NO DOCKET N FACIL:50-397 WPPSS Nuclear'Project, Unit 2, Washington Public Powe ,05000397~~~~~~~~~AUTH.NAME AUTHOR AFFILIATION EBRING,R.L.
NODOCKETNFACIL:50-397 WPPSSNuclear'Project, Unit2,Washington PublicPowe,05000397
Washington Public Power Supply System RECIP.NAME
~~~~~~~~~AUTH.NAMEAUTHORAFFILIATION EBRING,R.L.
Washington PublicPowerSupplySystemRECIP.NAME
'ECIPIENT AFFILIATION
'ECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
"AnnualOperating Reptfor1996."W/970228ltr.DISTRIBUTION CODE:IE47DCOPIESRECEIVED:LTR ENCLSIZE:TITLE:50.59Annual,ReportofChanges,TestsorExperiments MadeNOTES:cQWoutApprov@RECIPIENT IDCODE/NAME PD4-2PDINTERNAL:
"Annual Operating Rept for 1996." W/970228 ltr.DISTRIBUTION CODE: IE47D COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.59 Annual, Report of Changes, Tests or Experiments Made NOTES: c Q W out Approv@RECIPIENT ID CODE/NAME PD4-2 PD INTERNAL: ACRS RGN4 FILE 01 EXTERNAL: NOAC COPIES LTTR ENCL 1,~0 1 1 1 1 1 1 RECIPIENT ID CODE/NAME COLBURN,T FILE CENTER NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 0~'C E NOTE TO ALL"RIDSM RECIPIENTS:
ACRSRGN4FILE01EXTERNAL:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, I ROOM OWFN 5D-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 7 ENCL, 6 0 0 WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~Richland, Washington 99352-0968 February 28, 1997 G02-97-043 Docket No.50-397 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
NOACCOPIESLTTRENCL1,~0111111RECIPIENT IDCODE/NAME COLBURN,T FILECENTERNRCPDRCOPIESLTTRENCL1111110~'CENOTETOALL"RIDSMRECIPIENTS:
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,IROOMOWFN5D-5(EXT.
415-2083)
TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!TOTALNUMBEROFCOPIESREQUIRED:
LTTR7ENCL,6 00 WASHINGTON PUBLICPOWERSUPPLYSYSTEMP.O.Box968~Richland, Washington 99352-0968 February28,1997G02-97-043 DocketNo.50-397U.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Gentlemen:


==Subject:==
==Subject:==
WNP-2,OPERATING LICENSENPF-21ANNUALOPERATING REPORT1996
WNP-2, OPERATING LICENSE NPF-21 ANNUAL OPERATING REPORT 1996


==References:==
==References:==


1)Title10,CodeofFederalRegulations, Part50.59(b)2)WNP-2Technical Specifications 4.8.1.1.3, 6.9.1.4and6.9.1.53)Regulatory Guide1.16,Reporting ofOperating Information, AppendixA4)NEIGuideline forManagingNRCCommitments Inaccordance withthereferences, theSupplySystemherebysubmitstheannualoperating reportforcalendaryear1996;Ifyouhaveanyquestions ordesireadditional information pertaining tothisreport,pleasecontactMs.LourdesFernandez at(509)377-4147.
1)Title 10, Code of Federal Regulations, Part 50.59(b)2)WNP-2 Technical Specifications 4.8.1.1.3, 6.9.1.4 and 6.9.1.5 3)Regulatory Guide 1.16, Reporting of Operating Information, Appendix A 4)NEI Guideline for Managing NRC Commitments In accordance with the references, the Supply System hereby submits the annual operating report for calendar year 1996;If you have any questions or desire additional information pertaining to this report, please contact Ms.Lourdes Fernandez at (509)377-4147.Respectfully, R.L.Webring Vice President, Operations Support/PIO Mail Drop JE08 JDA/lm~0003'ttachment cc:-.EW Merschoff, NRC-Region IV KE Perkins, NRC-Region IV, WCFO TG Colburn, NRC-NRR REIRS Project Manager, NRC-NRR 970310024i 961231 PDR'DOCK OS000397 R-PDR NRC Resident Inspector (MD 927N)DL Williams-BPA (MD 399)NS Reynolds-Winston&Strawn!!!!![]!!!lllMII!!!Illljllt!!!
Respectfully, R.L.WebringVicePresident, Operations Support/PIO MailDropJE08JDA/lm~0003'ttachment cc:-.EWMerschoff, NRC-RegionIVKEPerkins,NRC-RegionIV,WCFOTGColburn,NRC-NRRREIRSProjectManager,NRC-NRR970310024i 961231PDR'DOCKOS000397R-PDRNRCResidentInspector (MD927N)DLWilliams-BPA(MD399)NSReynolds-Winston&Strawn!!!!![]!!!lllMII!!!Illljllt!!!
IIIIII!Illl  
IIIIII!Illl  


WASHINGTON NUCLEARPLANTNO.2ANNUALOPERATING REPORT1996DOCKETNO.50-397FACILI'IY OPERATING LICENSENO.NPF-21Washington PublicPower.SupplySystem"'P.O.Box968Richland, Washington 99352 1l~~h0
WASHINGTON NUCLEAR PLANT NO.2 ANNUAL OPERATING REPORT 1996 DOCKET NO.50-397 FACILI'IY OPERATING LICENSE NO.NPF-21 Washington Public Power.Supply System"'P.O.Box 968 Richland, Washington 99352 1 l~~h 0


==1.0INTRODUCTION==
==1.0 INTRODUCTION==


TABLEOFCONTEXTS1.11996CapacityFactors1.21996LoadProfile2.0REPORTS2.1AnnualPersonnel ExposureandMonitoring Report2.2'eactorCoolantSpecificActivityLevels2.3MainSteamLineSafety/Relief ValveChallenges 2.4SummaryofPlantOperations 2.5Significant Corrective Maintenance Performed onSafety-Related Equipment 2.6FuelPerformance 2.710CFR50.59 Changes,TestsandExperiments
TABLE OF CONTEXTS 1.1 1996 Capacity Factors 1.2 1996 Load Profile 2.0 REPORTS 2.1 Annual Personnel Exposure and Monitoring Report 2.2'eactor Coolant Specific Activity Levels 2.3 Main Steam Line Safety/Relief Valve Challenges 2.4 Summary of Plant Operations
.2.7.1PlantModifications 2.7.2Temporary Modifications/Instrument SetpointChanges2.7.3FSARChanges2.7.4ProblemEvaluations 2.7.5PlantTestsandExperiments 2.7.6PlantProcedure Changes2.7.7Miscellaneous 2.8DieselGenerator Failures2.9Regulatory Commitment Changes(NEIProcess)=~
 
===2.5 Significant===
Corrective Maintenance Performed on Safety-Related Equipment 2.6 Fuel Performance 2.7 10CFR50.59 Changes, Tests and Experiments
.2.7.1 Plant Modifications 2.7.2 Temporary Modifications/Instrument Setpoint Changes 2.7.3 FSAR Changes 2.7.4 Problem Evaluations 2.7.5 Plant Tests and Experiments 2.7.6 Plant Procedure Changes 2.7.7 Miscellaneous 2.8 Diesel Generator Failures 2.9 Regulatory Commitment Changes (NEI Process)=~
td!~  
td!~  


==1.0 lXIRODUCTXON==
==1.0 lXIRODUCTXON==
The1996AnnualOperating ReportofWashington PublicPowerSupplySystemPlantNumber2(WNP-2)issubmitted pursuanttotherequirements ofFederalRegulations andFacilityOperating LicenseNPF-21.Theplantisa3486MWt,BWR-5,whichbegancommercial operation onDecember13,1984.OnMarch2,1996WNP-2hadoperatedcontinuously for242consecutive dayswhentheplantwastakenofflineattherequestoftheBonneville PowerAdministration, customerforWNP-2electricity.
The 1996 Annual Operating Report of Washington Public Power Supply System Plant Number 2 (WNP-2)is submitted pursuant to the requirements of Federal Regulations and Facility Operating License NPF-21.The plant is a 3486 MWt, BWR-5, which began commercial operation on December 13, 1984.On March 2, 1996 WNP-2 had operated continuously for 242 consecutive days when the plant was taken off line at the request of the Bonneville Power Administration, customer for WNP-2 electricity.
The242consecutive dayrunwasjust15shortoftheplant'srecordmarkof257days,setbetweenAugust.1993 andApril1994.Thisalsorepresented thefirstbreaker-to-breakerrun.Theplantwasmaintained inthisreserveshutdowncondition formorethanonemonthbeforetherefueling outagescheduled startdateduetoanabundance ofrelatively inexpensive powerfromtheFederalColumbiaRiverPowerSystem.OnApril13,1996theplantofficially enteredthe1996Maintenance andRefueling Outage(R-11)asscheduled.
The 242 consecutive day run was just 15 short of the plant's record mark of 257 days, set between August.1993 and April 1994.This also represented the first breaker-to-breaker run.The plant was maintained in this reserve shutdown condition for more than one month before the refueling outage scheduled start date due to an abundance of relatively inexpensive power from the Federal Columbia River Power System.On April 13, 1996 the plant officially entered the 1996 Maintenance and Refueling Outage (R-11)as scheduled.
TheplantendedtheannualoutageonJune21,1996.Following startup,theplantwasmanuallyscrammedfrom28.5percentpoweronJune24,1996duetoanunexpected plantresponseduringtestingoftherecently-installed DigitalFeedwater LevelControlSystem.Theunexpected responsewasduetoadigitalfeedwater controller error.Achangewasmadetothecontroller softwareandplantstartupresumed.FromJune1996throughAugust1996,powerproduction waslimitedduetoproblemsassociated withtherecently-installed ReactorRecirculation SystemPumpAdjustable SpeedDriveandDigitalFeedwater LevelControlSystems.Powerproduction continued tobeperiodically limitedduringtheremainder oftlieyearduetoproblemswiththeadjustable speeddrives.TheBonneville PowerAdministration, duetoabnormally highrun-offconditions onseveraloccasions throughout theremainder oftheyear,alsorequested thatWNP-2reducepowerlevelssothatthefederalpowermarketing agencycouldmaximizeitsgenerating capability fromtheregion'shydroelectric projects.
The plant ended the annual outage on June 21, 1996.Following startup, the plant was manually scrammed from 28.5 percent power on June 24, 1996 due to an unexpected plant response during testing of the recently-installed Digital Feedwater Level Control System.The unexpected response was due to a digital feedwater controller error.A change was made to the controller software and plant startup resumed.From June 1996 through August 1996, power production was limited due to problems associated with the recently-installed Reactor Recirculation System Pump Adjustable Speed Drive and Digital Feedwater Level Control Systems.Power production continued to be periodically limited during the remainder of tlie year due to problems with the adjustable speed drives.The Bonneville Power Administration, due to abnormally high run-off conditions on several occasions throughout the remainder of the year, also requested that WNP-2 reduce power levels so that the federal power marketing agency could maximize its generating capability from the region's hydroelectric projects.The eleventh refueling outage was successfully completed during 1996.Significant planned and emergent activities included:~Installation of an Adjustable Speed Drive System for the Reactor Recirculation System pump motors.J~, Installation of a Digital Feedwater'Level Control System: l I~g I' Installation of clamps on each of the jet pump sensing lines.The 80 n'w clamps (four on each line)supplement welded supports and were installed in support of the Adjustable Speed Drive System modification.
Theeleventhrefueling outagewassuccessfully completed during1996.Significant plannedandemergentactivities included:
~Full core off-load to support the jet pump sensing line modification.
~Installation ofanAdjustable SpeedDriveSystemfortheReactorRecirculation Systempumpmotors.J~,Installation ofaDigitalFeedwater'Level ControlSystem:lI~gI' Installation ofclampsoneachofthejetpumpsensinglines.The80n'wclamps(fouroneachline)supplement weldedsupportsandwereinstalled insupportoftheAdjustable SpeedDriveSystemmodification.
~Core refuel with Asea Brown-Boveri (ABB)assemblies.
~Fullcoreoff-loadtosupportthejetpumpsensinglinemodification.
This represented ABB's first refuel load for a U.S.commercial nuclear power plant.~Visual inspection of the Reactor Pressure Vessel.~Cleaning of Main Condenser tubes.~Refurbishment of 20 Control Rod Drive Mechanisms.
~CorerefuelwithAseaBrown-Boveri (ABB)assemblies.
~Inspection of the Moisture Separator Reheater During December 1996, a new power generation record was set.The gross generation for the month was 882,470 megawatt-hours and net generation equalled 850,855 megawatt-hours.
Thisrepresented ABB'sfirstrefuelloadforaU.S.commercial nuclearpowerplant.~Visualinspection oftheReactorPressureVessel.~CleaningofMainCondenser tubes.~Refurbishment of20ControlRodDriveMechanisms.
The.previous record of 868,390 megawatt-hours gross and 837,936 megawatt-hours net occurred in October 1995.
~Inspection oftheMoistureSeparator ReheaterDuringDecember1996,anewpowergeneration recordwasset.Thegrossgeneration forthemonthwas882,470megawatt-hours andnetgeneration equalled850,855megawatt-hours.
1.1 Capacity Factors-1996 The 1996 capacity factors, based on net electrical energy output are listed below.January Pebruary March>>April>>*97.8 82.1 0 0 June>>>>>>0.8 July 58.6" August September 61.6'6.5 October November'-December 96.2 99.3 103.3 57.1 Entered Economic Dispatch Reserve Shutdown Condition Started Maintenance and Refueling Outage Ended Maintenance and Refueling Outage  
The.previousrecordof868,390megawatt-hours grossand837,936megawatt-hours netoccurredinOctober1995.
1.1CapacityFactors-1996The1996capacityfactors,basedonnetelectrical energyoutputarelistedbelow.JanuaryPebruaryMarch>>April>>*97.882.100June>>>>>>0.8July58.6"AugustSeptember 61.6'6.5OctoberNovember'-December96.299.3103.357.1EnteredEconomicDispatchReserveShutdownCondition StartedMaintenance andRefueling OutageEndedMaintenance andRefueling Outage  


LoadProfile-19960Generation QEconOisp1,0000FEBMARAPRJUN1,000Z'JULAUGSEP'.OCTNOVDEC4 2.0RIM'ORTSThereportsinthissectionareprovidedpursuantto:1)therequirements ofTechnical Specifications 6.9.1.4and'6.9.1.5, "AnnualReports,"
Load Profile-1996 0 Generation Q Econ Oisp 1,000 0 FEB MAR APR JUN 1,000 Z'JUL AUG SEP'.OCT NOV DEC 4 2.0 RIM'ORTS The reports in this section are provided pursuant to: 1)the requirements of Technical Specifications 6.9.1.4 and'6.9.1.5,"Annual Reports," 2)the requirements of Technical Specification 4.8.1.1.3,"Reports" (Electrical Power System Surveillance Requirements), 3)the requirements of 10CFR50.59,"Changes, Tests, and Experiments," 4)the guidance contained in Regulatory Guide 1.16,"Reporting of Operating Information," Revision 4-August 1975, and 5)the guidance contained in the NEI Guideline for Managing NRC Commitments, Revision 2, December 1995.Technical Specifications 6.9.1.4 and 6.9.1.5 require that the following reports for the previous calendar year be submitted prior to March 1 of each year:~A tabulation on an annual basis of the number of station, utility, and other personnel (including contractors) receiving exposures greater than 100 mrems/year and their associated man-rem exposure according to work and job functions.
2)therequirements ofTechnical Specification 4.8.1.1.3, "Reports" (Electrical PowerSystemSurveillance Requirements),
I Documentation of a11 challenges to main steam line safety/relief valves.The results of specific activity analysis in which the primary coolant exceeded the limits of Specification 3.4.5.The limits are, Less than or equal to 0.2 microcuries per gram DOSE EQUIVALENT I-131," and"Less than or equal to 100/E-Bar microcuries per grBII1.Technical Specification 4.8.1.1.3 requires reporting of all diesel generator failures, valid or non-.valid.This report is made pursuant to Specification 6.9.1,"Routine Reports." Regulation 10CFR50.59 requires that licensees submit, as specified in 10CFR50.4, a report containing a brief description of any changes, tests or experiments, including a summary of the safety evaluation of each.The report may be submitted annually or at shorter intervals.
3)therequirements of10CFR50.59, "Changes, Tests,andExperiments,"
Regulatory Guide 1.16 states that routine operating reports covering the operation of the unit~during the previous calendar year should be submitted prior to March 1 of each year.Each annual operating report should include: 1~A narrative summary of operating experience during the report period relating to the safe operation of the facility, including safety-related maintenance not covered elsewhere.
4)theguidancecontained inRegulatory Guide1.16,"Reporting ofOperating Information,"
For each outage or forced reduction in power of over 20 percent of design power level where the reduction extends for-more than four hours: (a)The proximate cause and the system and major component involved (if the outage or forced reduction in power involved equipment malfunction).
Revision4-August1975,and5)theguidancecontained intheNEIGuideline forManagingNRCCommitments, Revision2,December1995.Technical Specifications 6.9.1.4and6.9.1.5requirethatthefollowing reportsforthepreviouscalendaryearbesubmitted priortoMarch1ofeachyear:~Atabulation onanannualbasisofthenumberofstation,utility,andotherpersonnel (including contractors) receiving exposures greaterthan100mrems/year andtheirassociated man-remexposureaccording toworkandjobfunctions.
v 0 (b)A brief discussion (or reference to reports)of any reportable occurrences pertaining to the outage or reduction.(c)Corrective action taken to reduce the probability of recurrence, if appropriate.
IDocumentation ofa11challenges tomainsteamlinesafety/relief valves.TheresultsofspecificactivityanalysisinwhichtheprimarycoolantexceededthelimitsofSpecification 3.4.5.Thelimitsare,Lessthanorequalto0.2microcuries pergramDOSEEQUIVALENT I-131,"and"Lessthanorequalto100/E-Bar microcuries pergrBII1.Technical Specification 4.8.1.1.3 requiresreporting ofalldieselgenerator
'd)Operating time lost as a result of the outage or power reduction.(e)A description of major safety-related corrective maintenance performed during the outage or power reduction', including system and component involved,and identification of the critical path activity dictating the length of the outage or power reduction.(f)A report of any=single release of radioactivity or single exposure specifically
: failures, validornon-.valid.ThisreportismadepursuanttoSpecification 6.9.1,"RoutineReports."
-associated with the outage which accounts for more than ten percent of the allowable annual values.A tabulation on an annual basis of the number of station, utility and other personnel (including contractors) receiving exposures greater than 100 mrem/year and their associated man-rem exposure according to work and job functions.
Regulation 10CFR50.59 requiresthatlicensees submit,asspecified in10CFR50.4, areportcontaining abriefdescription ofanychanges,testsorexperiments, including asummaryofthesafetyevaluation ofeach.Thereportmaybesubmitted annuallyoratshorterintervals.
~'ndications of failed fuel resulting from irradiated fuel examinations, including eddy current tests, ultrasonic tests, or visual examinations completed during the report period.~~~~~~~~~~~~~The NEI Guideline for Managing NRC Commitments is a commission-endorsed method for licensees to follow for managing or changin'g NRC commitments.
Regulatory Guide1.16statesthatroutineoperating reportscoveringtheoperation oftheunit~duringthepreviouscalendaryearshouldbesubmitted priortoMarch1ofeachyear.Eachannualoperating reportshouldinclude:1~Anarrative summaryofoperating experience duringthereportperiodrelatingtothesafeoperation ofthefacility, including safety-related maintenance notcoveredelsewhere.
As part of this process and for commitments that satisfy one of the five NEI decision criteria not involving a codified regulatory process, the NEI guidance specifies periodic staff notification, either annually or along'with the FSAR updates as required by 10CFR50.71(e).
Foreachoutageorforcedreduction inpowerofover20percentofdesignpowerlevelwherethereduction extendsfor-morethanfourhours:(a)Theproximate causeandthesystemandmajorcomponent involved(iftheoutageorforcedreduction inpowerinvolvedequipment malfunction).
The NEI g'uideline further specifies that commitments dispositioned through the NEI process that satisfy none of the NEI decision criteria do not need to be reported in the licensee's periodic report because their regulatory and safety significance is negligible.  
v0 (b)Abriefdiscussion (orreference toreports)ofanyreportable occurrences pertaining totheoutageorreduction.
(c)Corrective actiontakentoreducetheprobability ofrecurrence, ifappropriate.
'd)Operating timelostasaresultoftheoutageorpowerreduction.
(e)Adescription ofmajorsafety-related corrective maintenance performed duringtheoutageorpowerreduction',
including systemandcomponent involved,and identification ofthecriticalpathactivitydictating thelengthoftheoutageorpowerreduction.
(f)Areportofany=singlereleaseofradioactivity orsingleexposurespecifically
-associated withtheoutagewhichaccountsformorethantenpercentoftheallowable annualvalues.Atabulation onanannualbasisofthenumberofstation,utilityandotherpersonnel (including contractors) receiving exposures greaterthan100mrem/year andtheirassociated man-remexposureaccording toworkandjobfunctions.
~'ndications offailedfuelresulting fromirradiated fuelexaminations, including eddycurrenttests,ultrasonic tests,orvisualexaminations completed duringthereportperiod.~~~~~~~~~~~~~TheNEIGuideline forManagingNRCCommitments isacommission-endorsed methodforlicensees tofollowformanagingorchangin'g NRCcommitments.
Aspartofthisprocessandforcommitments thatsatisfyoneofthefiveNEIdecisioncriterianotinvolving acodifiedregulatory process,theNEIguidancespecifies periodicstaffnotification, eitherannuallyoralong'with theFSARupdatesasrequiredby10CFR50.71(e).
TheNEIg'uideline furtherspecifies thatcommitments dispositioned throughtheNEIprocessthatsatisfynoneoftheNEIdecisioncriteriadonotneedtobereportedinthelicensee's periodicreportbecausetheirregulatory andsafetysignificance isnegligible.  


10CFRPART20MASHIMCTON PUBLICPOMERSUPPLYSISTEMRADIATION EXPOSURERECORDSMORNANDJOBtUNCTIONREPORTReportforCalendarYeari1996'7S'7TotalHAM-RCH!349.890--yeartoDateDose-ItationUtility-contractots EsployeesEcployees andOthers1735105951486715,7950,3810+1633.4290.0930.9311,29900871+0658061189663243.8560.664121'304.0800.0000.4499430,28516'773,5690.04625992.96923926.5660,3160,0004,1920.0000.0000.0000,0040,0000,00800050,0000,079003101490527ILLAMCEMaintenance Personnel operatinq tersonnel HealththyslcsPersonnel supervlsocy Personnel Eagineering Personnel Maintenance Personnel Operatinq Personnel HealthPhysicsPersonnel supervisory Personnel Engineering Personnel Maintenance Personnel opecatinq Personnel HealthPhysicsPersonnel Supervisory tersonnel Engineering Personnel Nalntenanee Persoanel Opsratinq Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Pecsonnel Naintenance I'ersonnel opecetinq Personnel HealththysiesPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel operatinq personnel HealthPhysicsPersonnel Supecvlsohcy Personnel Engineering Personnel 0.99ISSe900,000170,67I5~170,385446.3217180,006o340F000.000,000,07000Oo07033072ROUTINEHAINTENAMCE 5501'317342'55.82INSERVICE INSPECTION Oe55000002002010SPECIALMAINTENANCE
10 CFR PART 20 MASHIMCTON PUBLIC POMER SUPPLY SISTEM RADIATION EXPOSURE RECORDS MORN AND JOB tUNCTION REPORT Report for Calendar Yeari 1996'7S'7 Total HAM-RCH!349.890--year to Date Dose-I tation Utility-contractots EsployeesEcployees and Others 17 351 0 595 14 867 15,795 0,381 0+163 3.429 0.093 0.931 1,299 0 087 1+065 806 1 189 6 632 43.856 0.664 121'30 4.080 0.000 0.4 4 9 943 0,285 16'77 3,569 0.046 2 599 2.969 2 392 6.566 0,316 0,000 4,192 0.000 0.000 0.000 0,004 0,000 0,008 0 005 0,000 0,079 0 031 0 149 0 527 ILLAMCE Maintenance Personnel operatinq tersonnel Health thyslcs Personnel supervlsocy Personnel Eagineering Personnel Maintenance Personnel Operatinq Personnel Health Physics Personnel supervisory Personnel Engineering Personnel Maintenance Personnel opecatinq Personnel Health Physics Personnel Supervisory tersonnel Engineering Personnel Nalntenanee Persoanel Opsratinq Personnel Health Physics Personnel Supervisory Personnel Engineering Pecsonnel Naintenance I'ersonnel opecetinq Personnel Health thysies Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel operatinq personnel Health Physics Personnel Supecvlsohcy Personnel Engineering Personnel 0.99 ISSe90 0,00 0 17 0,67 I5~17 0,38 5 44 6.32 17 18 0,00 6o34 0 F 00 0.00 0,00 0,07 0 00 Oo07 0 33 0 72 ROUTINE HAINTENAMCE 55 0 1'3 17 34 2'5 5.82 INSERVICE INSPECTION Oe55 0 00 0 02 0 02 0 10 SPECIAL MAINTENANCE
{Snattachedsheets)0,0240,000lo2260.0000.0000,060.00le070+00Oooo0+4820.0250,6190.000'.135 18II30,83707751.3510.2410420,00Oooo0,000.0705920.0000,00000000.0270+710,000+700,000.05HASTEPROCESSISO6,4150,0003,3680,003091011o030+0010.2000073'20,0080,0000,0000,2280~590REPUELINO 20+070.03040Oooo1210.003'90,86;Oo752+94~aaorandTotalstvNalntenance Personnel Operatinq Personnel HealththyelesPersonnel Supervisory Personnel Engineering Personnel 159.743414395816.4924.31274.37i.873.'22I5022918o46353rOSlo0060199+6268elo30o34.491+96844920o9015916+2270291348351.859160.022038105770378219100.3613+746I47121+0067450207e261tacilitya 02Thisreportuasproduceduithdirectreadingdosieeter dataNuabero!personsReceiving over100eilllraais--NnherotIndividuals
{Sn attached sheets)0,024 0,000 lo226 0.000 0.000 0,06 0.00 le07 0+00 Oooo 0+482 0.025 0,619 0.000'.135 18 II3 0,837 0 775 1.351 0.241 0 42 0,00 Oooo 0,00 0.07 0 592 0.000 0,000 0 000 0.027 0+71 0,00 0+70 0,00 0.05 HASTE PROCESS ISO 6,415 0,000 3,368 0,003 0 910 11o03 0+00 10.20 0007 3'2 0,008 0,000 0,000 0,228 0~590 REPUELINO 20+07 0.03 0 40 Oooo 1 21 0.00 3'9 0,86;Oo75 2+94~aaorand Totals tv Nalntenance Personnel Operatinq Personnel Health thyeles Personnel Supervisory Personnel Engineering Personnel 159.74 34 14 39 58 16.49 24.31 274.37 i.87 3.'22 I 50 2 29 18o46 353rOS lo00 60 19 9+62 68elo 30o34.491+96 84 49 20o90 15 91 6+22 7029 134 835 1.859 160.022 0 381 0 577 0 378 21 910 0.361 3+746 I 471 21+006 7 450 207e261 tacilitya 02 This report uas produced uith direct reading dosieeter data Nuaber o!persons Receiving over 100 eilllraa is--Nnher ot Individuals
-ItatlonUtilityContraetols Eaployees Eaployees andOthersOPERATIONS AMDSURVE69.493e4391~3131.863+22O.S316.450.833~6810.23,054,0413.8I83825'4'el8OOcng'pBg95',OOc)k~gs~OOgOO8,PAIDO(gOgFLD~eC6g~.POO.o~O' IJ WASHINGTON PUBLICPOWERSUPPLYSYSTEMRADIATION EXPOSURERECORDSWORKANDJOBFUNCTIONREPORT10CFRPART20Facilitys 02Thisreportwasproducedwithdirectreadingdosimeter dataReportforCalendarYears1996SPECIALMAINTENANCE
-I tatlon Utility Contraetols Eaployees Eaployees and Others OPERATIONS AMD SURVE 69.49 3e43 91~31 31.86 3+22 O.S3 16.45 0.83 3~68 10.23 ,05 4,04 13.8I 8 38 25'4'el 8 O O cn g'p Bg 9 5', O O c)k~gs~OO g O O 8, PA ID O (g O g FL D~e C6 g~.P O O.o~O' IJ WASHINGTON PUBLIC POWER SUPPLY SYSTEM RADIATION EXPOSURE RECORDS WORK AND JOB FUNCTION REPORT 10 CFR PART 20 Facilitys 02 This report was produced with direct reading dosimeter data Report for Calendar Years 1996 SPECIAL MAINTENANCE
--NumberofIndividuals
--Number of Individuals
--II---YeartoDateDose---tation'Utilitycontractof sStationUtilitycontracto Employees Employees andOthers"Employees Employees andOthe1.InstallVibration Mitigation Clamp,JetPumpSensingLine2.ReactorRecirculation andResidualHeatRemovalVibration Testing3..TubePlugging.
--I I---Year to Date Dose---tation'Utility contractof s Station Utility contracto Employees Employees and Others" Employees Employees and Othe 1.Install Vibration Mitigation Clamp, Jet Pump Sensing Line 2.Reactor Recirculation and Residual Heat Removal Vibration Testing 3..Tube Plugging.Condenser7Neat.
Condenser7Neat.
Exchanger 9i C Water Box 4.Adjustable Speed Drive Implementation 5.Source Rance Monitor Drive B Gearbox Replacement 6.Adjust Main Steam Jet Pump Set Screw Oaps 7.Reactor Recirculation Valve 68A, Repair Leak 8.Remove Stellite Control Rod Blade Rollers/Velocity Limiters and Clean Spent Fuel Pool Maintenance Personnel operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervi.sory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel 2'13 0>>00 2>>32 0>>00 0 16 0.00 0>>00 D>>OD 0>>00.0 00 4.60 0.00 0>>'32 0>>00 2'5 0>>00 0.00 0.00 0>>00 0 00 2'8 0>>00 0>>00 0>>00 0>>00 0.00 0.00 0>>40 0.00 0>>00 0>>00 0.00 0>>00 0>>00 0.00 0>>00 0>>00 0>>48 0>>00 Q>>00 0.00 0.00 0.00 0.00 0.00 0>>00 0>>00 0>>00 0>>00 0>>00 0.00 0.00 0.00 0 F 00 0>>42 0>>00 0.00 0,00 0.00 0.00 0>>00 0 00 0.00 0.00 0 00 0>>00 0>>00 0.00 0>>00 0>>QO 0 F 00 Q>>00 0 F 00 0.00 0 00 0.00 0.00 0.00 0>>00 0'.00 12.19 0.00 0.00 0.00 6 40 12 39 0>>00 0.00 0.00 6.52 1.12 0 00 0 00 0 00 1 03 8>>14 0>>00 0>>00 0.00 0>>00 0.67 0>>00 0.00 0.00 0.64 1.54 0>>00 0.00 0>>00 1 06 1 30 0.00 0.00 0.00 0 94 0.75 0.00 0.00 0>>00 0.71 0.634 0 000 0 690 0.000 0.047 0,000 0 000 0.000 0.000 0>>000 1~366 0.000 0.094 0 000 0.876 0,000 0,000 0.000 0 000 Q>>000 0 767 0.000 0.000 0.000 0 000 0.000 0'.000 0.118 0 000 0.000 0,000 0'.000 0 000 0 000 0 000 0.000 0 000 0>>142 0 000 0>>000 0.000 0.000 0.000 0.000 0.000 0.000 0 000 0 000 0.000 0.000 0.000 0.000 0.000 0.000 0 124 0~000 0.000 0 000 0 000 0.000 0.000 0.000 0 000 0.000 0'.000 0.000 0'.000 0 000 0~000 0'.000 0~000 0.000 0.000 0 000 0.000 0.000 0.000 0.000 0.000 0.000 3.623 0.000 0.000 0.000 1.901 3.681 0 000 0>>000 0.000 1 937 0.334 0 000 0.000 0~000 0.305 2.419 0~000 0.000 0.000 0'.000 0.199 0.000 0~000 0~000 0.190 0.457 0.000 0.000 0 000 0'15 0 385 0.000 0.000 0.000 0.279 0.222 0.000 0.000 0~000 0.210  
Exchanger 9iCWaterBox4.Adjustable SpeedDriveImplementation 5.SourceRanceMonitorDriveBGearboxReplacement 6.AdjustMainSteamJetPumpSetScrewOaps7.ReactorRecirculation Valve68A,RepairLeak8.RemoveStelliteControlRodBladeRollers/Velocity LimitersandCleanSpentFuelPoolMaintenance Personnel operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervi.sory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel 2'130>>002>>320>>000160.000>>00D>>OD0>>00.0004.600.000>>'320>>002'50>>000.000.000>>000002'80>>000>>000>>000>>000.000.000>>400.000>>000>>000.000>>000>>000.000>>000>>000>>480>>00Q>>000.000.000.000.000.000>>000>>000>>000>>000>>000.000.000.000F000>>420>>000.000,000.000.000>>000000.000.000000>>000>>000.000>>000>>QO0F00Q>>000F000.000000.000.000.000>>000'.0012.190.000.000.0064012390>>000.000.006.521.120000000001038>>140>>000>>000.000>>000.670>>000.000.000.641.540>>000.000>>001061300.000.000.000940.750.000.000>>000.710.634000006900.0000.0470,00000000.0000.0000>>0001~3660.0000.09400000.8760,0000,0000.0000000Q>>00007670.0000.0000.00000000.0000'.0000.11800000.0000,0000'.0000000000000000.00000000>>14200000>>0000.0000.0000.0000.0000.0000.000000000000.0000.0000.0000.0000.0000.00001240~0000.000000000000.0000.0000.00000000.0000'.0000.0000'.00000000~0000'.0000~0000.0000.00000000.0000.0000.0000.0000.0000.0003.6230.0000.0000.0001.9013.68100000>>0000.00019370.33400000.0000~0000.3052.4190~0000.0000.0000'.0000.1990.0000~0000~0000.1900.4570.0000.00000000'1503850.0000.0000.0000.2790.2220.0000.0000~0000.210  


9.hBBFuelDebrisFilterRemoval.10.Paint/Label ReactorBuildingRHRhtB>'42211.'501ReactorBide,coatingHallsandDoors12.ReworkPenetration Seals,QC16214.Miscellaneous Projects13.Temporary Shieldi.ng forEquipment Drain8ResidualHeatRemovalPipesMaintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel rMaintenance Personnel Operating Personnel HealthPhysicsPersonnel Bupervisory Personnel Bngineering Personnel Maintenance Personnel, Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Bngineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel HealthPhysicsPersonnel Supervisory Personnel Engineering Personnel 0.000,550000.000.301290000.000000001.170000.000000000.000.000.000000000,61"0,000000OD0~001240000350000.340.000.00Oooo0~000+000.000.000.000+000+000+00o'.aa0.000,00OoooOroo0+00oooo0+000+000+000+00oroa0+000.00o.oa0F000,000.00Oooo0.000F000+000.000+000.000F000.000000+000.00a.ao0.000F000.000.730.000000000+702.050000000DD1333.530.00000Oioa2~120+00001640.00000000+09003830~0000.0000.0000.0000,3480~000Ooaoo0.000a'.ooo0.00000000+ODD',000 0~0000.18200000.0000,0000.000~0~368Ooaoo0.104Ooooo0.1010.0000.0000.000000000000.0000.0000.0000000D.DDD0.0000.0000.0000.00000000.00000000.00000000.0000.0000.0000.0000,0000+0000.0000.0000.0000.0000.0000.0000~0000.00000000.0000.0000.0000.00000000ODD0.0000.0000.0000.0000.0000.2170000000000000.2080.6090.0000.0000.0000~3961.0480.0000.0000~0000630 I'
9.hBB Fuel Debris Filter Removal.10.Paint/Label Reactor Building RHR htB>'422 11.'501 Reactor Bide, coating Halls and Doors 12.Rework Penetration Seals, QC 162 14.Miscellaneous Projects 13.Temporary Shieldi.ng for Equipment Drain 8 Residual Heat Removal Pipes Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel r Maintenance Personnel Operating Personnel Health Physics Personnel Bupervisory Personnel Bngineering Personnel Maintenance Personnel, Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Bngineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel 0.00 0,55 0 00 0.00 0.30 1 29 0 00 0.00 0 00 0 00 1.17 0 00 0.00 0 00 0 00 0.00 0.00 0.00 0 00 0 00 0, 61" 0,00 0 00 0 OD 0~00 1 24 0 00 0 35 0 00 0.34 0.00 0.00 Oooo 0~00 0+00 0.00 0.00 0.00 0+00 0+00 0+00 o'.aa 0.00 0,00 Oooo Oroo 0+00 oooo 0+00 0+00 0+00 0+00 oroa 0+00 0.00 o.oa 0 F 00 0,00 0.00 Oooo 0.00 0 F 00 0+00 0.00 0+00 0.00 0 F 00 0.00 0 00 0+00 0.00 a.ao 0.00 0 F 00 0.00 0.73 0.00 0 00 0 00 0+70 2.05 0 00 0 00 0 DD 1 33 3.53 0.00 0 00 Oioa 2~12 0+000 0 164 0.000 0 000 0+090 0 383 0~000 0.000 0.000 0.000 0,348 0~000 Ooaoo 0.000 a'.ooo 0.000 0 000 0+ODD',000 0~000 0.182 0 000 0.000 0,000 0.000~0~368 Ooaoo 0.104 Ooooo 0.101 0.000 0.000 0.000 0 000 0 000 0.000 0.000 0.000 0 000 D.DDD 0.000 0.000 0.000 0.000 0 000 0.000 0 000 0.000 0 000 0.000 0.000 0.000 0.000 0,000 0+000 0.000 0.000 0.000 0.000 0.000 0.000 0~000 0.000 0 000 0.000 0.000 0.000 0.000 0 000 0 ODD 0.000 0.000 0.000 0.000 0.000 0.217 0 000 0 000 0 000 0.208 0.609 0.000 0.000 0.000 0~396 1.048 0.000 0.000 0~000 0 630 I'
2.2ReactorCoolantSpecificActivityLevelsThissectioncontainsinformation pertaining toreactorcoolantdose-equivalent iodine.Thespecificactivityoftheprimarycoolantwassignificantly lessthan0.2microcuries pergram'ose-equivalent I-131and100/E-Bar microcuries pergramasrequiredby~Technical Specification 3.4.5.Thisdataisprovidedsolelyforinformational purposesandeaseofreference.
2.2 Reactor Coolant Specific Activity Levels This section contains information pertaining to reactor coolant dose-equivalent iodine.The specific activity of the primary coolant was significantly less than 0.2 microcuries per gram'ose-equivalent I-131 and 100/E-Bar microcuries per gram as required by~Technical Specification 3.4.5.This data is provided solely for informational purposes and ease of reference.
Technical Specification 6.9.1.5.c onlyrequiresreporting whentheresultsofspecificactivityanalysisofprimarycoolantexceedthelimitsofSpecification 3.4.5..-~I-hh10
Technical Specification 6.9.1.5.c only requires reporting when the results of specific activity analysis of primary coolant exceed the limits of Specification 3.4.5..-~I-h h 10


MainSteamLineSafety/Relief ValveChallenges Thissectioncontainsinformation pertaining tomainsteamlinesafety/relief valvechallenges andisincludedpursuanttoTechnical Specification 6.9.1.5(b).
Main Steam Line Safety/Relief Valve Challenges This section contains information pertaining to main steam line safety/relief valve challenges and is included pursuant to Technical Specification 6.9.1.5(b).
Themainsteamlinesafety/relief valvechallenges (actuation events)areshownonthefollowing tables.Thedataincludesallin-situtests.Foreaseofreference, thefoHowingdescriptive codesareusedforeachactuation orfailureto'actuate:
The main steam line safety/relief valve challenges (actuation events)are shown on the following tables.The data includes all in-situ tests.For ease of reference, the foHowing descriptive codes are used for each actuation or failure to'actuate:
TypeofActuation A=Automatic B=RemoteManualC=SpringCause/Reason forActuation
Type of Actuation A=Automatic B=Remote Manual C=Spring Cause/Reason for Actuation~.B=C=D=E=Overpressure ADS or other safety Test Inadvertent (Accidental/Spurious)
~.B=C=D=E=Overpressure ADSorothersafetyTestInadvertent (Accidental/Spurious)
Manual relief Reactor Operating Condition Prior to Lift A=B=C=D=E=F=G=H=Construction Preoperational, startup or power ascension tests in progress Routine startup Routine shutdown Steady state operations Load changes during routine operation Shutdown (hot or cold), except refueling Refueling~Failures and Reports A=B=:C=D=Failure of electrical or other components not considered part of the valve assembly-No SRVS failure report required-Failure of any part of the valve-SRVS failure report will be filed No failures occurred-No SRVS failure report required LER Submitted-Report LER number in Item 316 NPRDS will be submitted 11  
ManualreliefReactorOperating Condition PriortoLiftA=B=C=D=E=F=G=H=Construction Preoperational, startuporpowerascension testsinprogressRoutinestartupRoutineshutdownSteadystateoperations Loadchangesduringroutineoperation Shutdown(hotorcold),exceptrefueling Refueling
~I NOTE: lneludes all ln-Situ Tests For Each Actuation or Failure'o Actuate: S/R Valve Serial Number Component ID (Location)
~FailuresandReportsA=B=:C=D=Failureofelectrical orothercomponents notconsidered partofthevalveassembly-NoSRVSfailurereportrequired-Failureofanypartofthevalve-SRVSfailurereportwillbefiledNofailuresoccurred-NoSRVSfailurereportrequiredLERSubmitted
MS-RV-1B MS-RV-lc 63790404140 63790404139 63790404049 MS-RV-1A MS-RV-1D MS-RV-2B 63790404134 63790404050 Date of Actuation (Mo/Da/Yr)
-ReportLERnumberinItem316NPRDSwillbesubmitted 11  
Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Ult (Code)Rx Power level Prior to Lift (%Rated nrermal)Time Rcq'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number" Reading and Units Rx Prcssure Prior to Actuation (PSIG)tF AVAILABLE/tF APPLlCABLE Reseat Pressure At Valve Closure (PSIG),Duration of This Actuation (Minutes, Seconds)Failures.Rcporlts (Code)LER Number (5 Digit Number)Comments Regarding This Aetuaiion Auaehcd7 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A 1257 15 NIA Process Computer OPEN 919 NIA 6 SEC.NIA 3/2/96 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A 3/2/96 1257 15 NIA Process Computer OPEN ,919 N/A 4 SEC.N/A 3/2/96 1257 15~NIA Process Computer OPEN 919 NIA 6 SEC.NIA 0
~I NOTE:lneludesallln-SituTestsForEachActuation orFailure'o Actuate:S/RValveSerialNumberComponent ID(Location)
NOTE: Includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404122 63790404054 63790404138 63790404053
MS-RV-1BMS-RV-lc63790404140 63790404139 63790404049 MS-RV-1AMS-RV-1DMS-RV-2B63790404134 63790404050 DateofActuation (Mo/Da/Yr)
.63790404124 Component ID (Location)
TimeofDay(24HourClock)TypeofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortoUlt(Code)RxPowerlevelPriortoLift(%Ratednrermal)TimeRcq'dforTailpipeTemptoReturntoNormalOtherInstrumentation Type(Code)OtherInstrumentation Number"ReadingandUnitsRxPrcssurePriortoActuation (PSIG)tFAVAILABLE/tF APPLlCABLE ReseatPressureAtValveClosure(PSIG),Duration ofThisActuation (Minutes, Seconds)Failures.
Date of Actuation (Mo/Da/Yr)
Rcporlts(Code)LERNumber(5DigitNumber)CommentsRegarding ThisAetuaiion Auaehcd7125715NIAProcessComputerOPEN919NIA4SEC.N/A125715NIAProcessComputerOPEN919NIA6SEC.NIA3/2/96125715NIAProcessComputerOPEN919NIA4SEC.N/A3/2/96125715NIAProcessComputerOPEN,919N/A4SEC.N/A3/2/96125715~NIAProcessComputerOPEN919NIA6SEC.NIA 0
Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior td LIR (Code)Rx Power Level Prior to LIR (%Rated Thermal)Time Reel'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Prcssure Prior to Aetualton (PSIG)tF AVAILABLB/tF APPL'ICABLB Reseat Pressure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation At taehed7 MS-RV-2C 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A MS-RV-2A 1257 15 NIA'Process Computer OPEN 919 NIA 4 SEC.C, NIA MS-RV-2D 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.NIA MS-RV-3B 3/2/96 1257 15 NIA Process Computer OPEN 919 N/A 4 SEC.IA MS-RV-3C 1257 15 NIA Process Computer OPEN 919 NIA 6 SEC.N/A 13 0,
NOTE:IncludesallIn-SituTestsForEachActuation orFailuretoActuate:S/RValveSerialNumber63790404122 63790404054 63790404138 63790404053
NOTE: Includes all In Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404058 63790404126 63790404137 63790404056 63790404135 Component ID (Location)
.63790404124 Component ID(Location)
Date of Actuation (Mo/Da/Yr)
DateofActuation (Mo/Da/Yr)
Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated Thermal)Time Rcq'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLE/IF APPLICABLE Reseat Prcssure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation Attached?MS-RV-3A 1257 C D NIA Procea Computer OPEN 919 NIA 6 SEC.N/A MS-RV-3D C NIA.Process Computer OPEN 919 N/A 4 SEC.N/A hIS.RVAB 12S7 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A MS-ROC 1257 15 NIA Process Computer OPEN 919 N/A 4 SEC.N/A MS.RVAA IS NIA Process Computer OPEN 919 NIA 4 SEC.N/A 14
TimeofDay(24HourClock)TypeofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortdLIR(Code)RxPowerLevelPriortoLIR(%RatedThermal)TimeReel'dforTailpipeTemptoReturntoNormalOtherInstrumentation Type(Code)OtherInstrumentation NumberReadingandUnitsRxPrcssurePriortoAetualton (PSIG)tFAVAILABLB/tF APPL'ICABLB ReseatPressureAtValveClosure(PSIG)DurationofThisActuation (Minutes, Seconds)Failures.
Reports(Code)LERNumber(5DigitNumber)CommentsRegarding ThisActuation Attaehed7MS-RV-2C125715NIAProcessComputerOPEN919NIA4SEC.N/AMS-RV-2A125715NIA'ProcessComputerOPEN919NIA4SEC.C,NIAMS-RV-2D125715NIAProcessComputerOPEN919NIA4SEC.NIAMS-RV-3B3/2/96125715NIAProcessComputerOPEN919N/A4SEC.IAMS-RV-3C125715NIAProcessComputerOPEN919NIA6SEC.N/A13 0,
NOTE:IncludesallInSituTestsForEachActuation orFailuretoActuate:S/RValveSerialNumber63790404058 63790404126 63790404137 63790404056 63790404135 Component ID(Location)
DateofActuation (Mo/Da/Yr)
TimeofDay(24HourClock)TypeofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortoLift(Code)RxPowerLevelPriortoLift(%RatedThermal)TimeRcq'dforTailpipeTemptoReturntoNormalOtherInstrumentation Type(Code)OtherInstrumentation NumberReadingandUnitsRxPressurePriortoActuation (PSIG)IFAVAILABLE/IF APPLICABLE ReseatPrcssureAtValveClosure(PSIG)DurationofThisActuation (Minutes, Seconds)Failures.
Reports(Code)LERNumber(5DigitNumber)CommentsRegarding ThisActuation Attached?
MS-RV-3A1257CDNIAProceaComputerOPEN919NIA6SEC.N/AMS-RV-3DCNIA.ProcessComputerOPEN919N/A4SEC.N/AhIS.RVAB12S715NIAProcessComputerOPEN919NIA4SEC.N/AMS-ROC125715NIAProcessComputerOPEN919N/A4SEC.N/AMS.RVAAISNIAProcessComputerOPEN919NIA4SEC.N/A14
'
'
NOTE:IncludesallIn.SituTestsForEachActuation orFailuretoActuate:S/RValveSerialNumber63790404060 63790404136 63790404062 Component ID(Location)
NOTE: Includes all In.Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404060 63790404136 63790404062 Component ID (Location)
DateofActuation (Mo/Da/Yr)
Date of Actuation (Mo/Da/Yr)
TimeofDay(24HourClock)TypeofActuation (Code)Cause/Reason forAc(uation (Code)RxOperating Condition PriortoLIft(Code)RxPaverLevelPriortoLIII(%RatedThermal)TimeReq'dforTailpipeTemptoReturntoNormalOtherInstrumentation Type(Code)OtherInstrumentation NumberReadingandUnitsRxPressurePriortoActuation (PSIG)IFAVAILABLBIF AFFUCASLE ReseatPressureAtValveClosure(PSIG)Durationol'ThisActuation (Minutes, Seconds)Failures.
Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Ac(uation (Code)Rx Operating Condition Prior to LIft (Code)Rx Paver Level Prior to LIII (%Rated Thermal)Time Req'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLBIF AFFUCASLE Reseat Pressure At Valve Closure (PSIG)Duration ol'This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Nuinbcr)Comments Regarding This Actuation At tachcd?MS.RVAD 1257 D.N/A Process Computer OPEN 919 NIA 4 SEC.NIA MS-RV-SB N/A Process Computer OPEN 919 NIA 4 SEC.N/A MS-RV-SC 1257 D IS NIA Process Computer OPEN 919 NIA 6 SEC.
Reports(Code)LERNumber(5DigitNuinbcr)CommentsRegarding ThisActuation Attachcd?MS.RVAD1257D.N/AProcessComputerOPEN919NIA4SEC.NIAMS-RV-SBN/AProcessComputerOPEN919NIA4SEC.N/AMS-RV-SC1257DISNIAProcessComputerOPEN919NIA6SEC.
U NOTE: Includes all ln-Situ Tests For Each Actuation or Failure'o Actuate: S/R Valve Serial Number 63790404052 2 63790404126 4 63790404055 637 9040406 l 63790404059 Component ID (Location)
U NOTE:Includesallln-SituTestsForEachActuation orFailure'oActuate:S/RValveSerialNumber63790404052 263790404126 463790404055 6379040406l63790404059 Component ID(Location)
Date of Actuation (Mo/Da/Yr)
DateofActuation (Mo/Da/Yr)
Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated Thermal)Time Req'd for Tailpipe Temp to Rctutn to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSlG)IF AVAILABLMF APPLICABLE Reseat Pressure At Valve Closure (PSiG)Duration of fhis Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation At tached?MS-RV-3C 5/28/96 N/A B 0 N/A OPEN 0 NIA NIA MS-RV-3D 5/28/96 NIA B 0 NIA OPEN'0 N/A NIA MS-RV4B 5/28/96 NIA B 0 NIA OPEN 0 NIA NIA'S-RYE 5/28/96 NIA'0 NIA Process Computcr-OPEN 0 N/A NIA MS-RV-5B 5/28/96 NIA B 0 NIA Process Computer OPEN 0 NIA NIA 0
TimeofDay(24HourClock)TypeofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortoLift(Code)RxPowerLevelPriortoLift(%RatedThermal)TimeReq'dforTailpipeTemptoRctutntoNormalOtherInstrumentation Type(Code)OtherInstrumentation NumberReadingandUnitsRxPressurePriortoActuation (PSlG)IFAVAILABLMF APPLICABLE ReseatPressureAtValveClosure(PSiG)DurationoffhisActuation (Minutes, Seconds)Failures, Reports(Code)LERNumber(5DigitNumber)CommentsRegarding ThisActuation Attached?MS-RV-3C5/28/96N/AB0N/AOPEN0NIANIAMS-RV-3D5/28/96NIAB0NIAOPEN'0N/ANIAMS-RV4B5/28/96NIAB0NIAOPEN0NIANIA'S-RYE 5/28/96NIA'0NIAProcessComputcr-OPEN0N/ANIAMS-RV-5B5/28/96NIAB0NIAProcessComputerOPEN0NIANIA 0
N(yfE: Includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404045 63790404057 637904040S l 63790404048 63790404135 Component ID (Location)
N(yfE:IncludesallIn-SituTestsForEachActuation orFailuretoActuate:S/RValveSerialNumber63790404045 63790404057 637904040S l63790404048 63790404135 Component ID(Location)
Date of Actuation (Mo/Da/Yr)
DateofActuation (Mo/Da/Yr)
'IIme of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated'Ibermal)Time Req'd for Tailpipe Temp to Return m Normal Other Instrumentation Type (Code)Other Instrumentation Number.Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAKABLEIIF APPLICABLE Rcscat Pressure At Valve Closure (PSIG)Duration of'Ibis Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (S Digit Number)Comments Regarding This Actuation At'tacbcd7 MS-RV-1C S/28/96 NIA B NIA" OPEN 0 N/A NIA MS-ROC 5/28/96 NIA B 0 N/A Process Computer OPEN 0 NIA NIA MS-RV-3B 5/28/96'IA B 0 N/A OPEN 0 NIA N/A MS-RV-lA NIA~B 0 NIA Process Computer OPEN N/A NIA MS-RVAA N/A B 0 NIA Process Computer OPEN NIA NIA 17 0
'IImeofDay(24HourClock)TypeofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortoLift(Code)RxPowerLevelPriortoLift(%Rated'Ibermal)
NOTE: Includes all In-Situ Tests For Each Actuation or Failure to Actuatet S/R Valve Serial Number 63790404062 63790404051 63790404045 63790404057 63790404051 Component ID (Location)
TimeReq'dforTailpipeTemptoReturnmNormalOtherInstrumentation Type(Code)OtherInstrumentation Number.Reading andUnitsRxPressurePriortoActuation (PSIG)IFAVAKABLEIIF APPLICABLE RcscatPressureAtValveClosure(PSIG)Durationof'IbisActuation (Minutes, Seconds)Failures, Reports(Code)LERNumber(SDigitNumber)CommentsRegarding ThisActuation At'tacbcd7 MS-RV-1CS/28/96NIABNIA"OPEN0N/ANIAMS-ROC5/28/96NIAB0N/AProcessComputerOPEN0NIANIAMS-RV-3B5/28/96'IAB0N/AOPEN0NIAN/AMS-RV-lANIA~B0NIAProcessComputerOPENN/ANIAMS-RVAAN/AB0NIAProcessComputerOPENNIANIA17 0
Date of Actuation (Mo/Da/Yr)
NOTE:IncludesallIn-SituTestsForEachActuation orFailuretoActuatetS/RValveSerialNumber63790404062 63790404051 63790404045 63790404057 63790404051 Component ID(Location)
Time of Day (24 Hour Clock)Type of Actuation (Code)Cause&eaton for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated Thermal)Time Req'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLKIIF APPLICABLE Rcscat Pressure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments Regarding%us Actuation Attachcd7 MS-RV-5C NIA B 0 NIA OPEN 0 NIA N/A MS-RV-3B NIA B C 0 NIA Process Computer OPEN 0 NIA NIA MS-RV-1C 6/8/96 N/A B 0 N/A Process Computer OPEN"0 NIA NIA MS-ROC NIA B 0 NIA OPEN 0 NIA.5 min NIA MS-RV-3B 6/8/96 NIA B 0~N/A Process Computer OPEN 0 NIA NIA 18 NOTE: includes all In.Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Ser J Number 1~<63790404045 63790404048 63790404051 63790404052 63790404126 Component 1D (Location)
DateofActuation (Mo/Da/Yr)
Date of Actuation (Mo/Dept/r)
TimeofDay(24HourClock)TypeofActuation (Code)Cause&eaton forActuation (Code)RxOperating Condition PriortoLift(Code)RxPowerLevelPriortoLift(%RatedThermal)TimeReq'dforTailpipeTemptoReturntoNormalOtherInstrumentation Type(Code)OtherInstrumentation NumberReadingandUnitsRxPressurePriortoActuation (PSIG)IFAVAILABLKIIF APPLICABLE RcscatPressureAtValveClosure(PSIG)DurationofThisActuation (Minutes, Seconds)Failures.
Time of Day (24 Hour Clock)~of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Litt (Code)Rx Psaver Level Prior to Lilt (%Rated'Ihermal)Time Rcq'd for Tailpipe Temp to Return to Normal Other lnsttumcntation Type (Code)Other lnsttumcntation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLE/IF APPLICASLE Rcscat Pressure At Val ve Closure (PSIG)Duration of Ihis Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation Attached?MS-RV-1C 6/16/96 N/A OPEN N/A NIA MS-RV-1A 6/16/96 0346 C N/A Process Computer OPEN NIA NIA MS-RV-3B 6/16/96 3 N/A OPEN NIA NIA MS-RV-3C 6/16/96 C~8/A OPEN NIA N/A MS-RV-3D 6/16/960352 3 N/A OPEN 919 NIA NIA 19
Reports(Code)LERNumber(5DigitNumber)CommentsRegarding
%usActuation Attachcd7 MS-RV-5CNIAB0NIAOPEN0NIAN/AMS-RV-3BNIABC0NIAProcessComputerOPEN0NIANIAMS-RV-1C6/8/96N/AB0N/AProcessComputerOPEN"0NIANIAMS-ROCNIAB0NIAOPEN0NIA.5minNIAMS-RV-3B6/8/96NIAB0~N/AProcessComputerOPEN0NIANIA18 NOTE:includesallIn.SituTestsForEachActuation orFailuretoActuate:S/RValveSerJNumber1~<63790404045 63790404048 63790404051 63790404052 63790404126 Component 1D(Location)
DateofActuation (Mo/Dept/r)
TimeofDay(24HourClock)~ofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortoLitt(Code)RxPsaverLevelPriortoLilt(%Rated'Ihermal)
TimeRcq'dforTailpipeTemptoReturntoNormalOtherlnsttumcntation Type(Code)Otherlnsttumcntation NumberReadingandUnitsRxPressurePriortoActuation (PSIG)IFAVAILABLE/IF APPLICASLE RcscatPressureAtValveClosure(PSIG)DurationofIhisActuation (Minutes, Seconds)Failures, Reports(Code)LERNumber(5DigitNumber)CommentsRegarding ThisActuation Attached?
MS-RV-1C6/16/96N/AOPENN/ANIAMS-RV-1A6/16/960346CN/AProcessComputerOPENNIANIAMS-RV-3B6/16/963N/AOPENNIANIAMS-RV-3C6/16/96C~8/AOPENNIAN/AMS-RV-3D6/16/9603523N/AOPEN919NIANIA19


NIXIE:IncludesallIn-SituTestsForEachActuanonorFailuretoActuate:S/RValveSeriaNumber63790404055 63790404061 63790404059 63790404057 63790404135 Component ID(Location)
NIXIE: Includes all In-Situ Tests For Each Actuanon or Failure to Actuate: S/R Valve Seria Number 63790404055 63790404061 63790404059 63790404057 63790404135 Component ID (Location)
DateofActuation (Mo/Da/Yr)
Date of Actuation (Mo/Da/Yr)
T1meofDayg4HourClock)'PypeofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortoIJft(Cod)RxPowerLevelPriortoLiR(%RatedThermal)TimeReq'dforTailpipeTemptoRenuntoNormalOtherInstrumentation Type(Code)Otherinstrumentation NumberReadingandUnitsRxPrcssurePriortoActuation (PSIG)IFAYiQLA$1E/IFAPPLICABIE ReseatPressureAtValveClosure(PS1G)DurationofThisActuation (Minutes, Seconds)Failures, Reports(Code)LERNumber(5DigitNumber)Conuncnts Regarding ThisActuation Attached7
T1me of Day g4 Hour Clock)'Pype of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to IJft (Cod)Rx Power Level Prior to LiR (%Rated Thermal)Time Req'd for Tailpipe Temp to Renun to Normal Other Instrumentation Type (Code)Other instrumentation Number Reading and Units Rx Prcssure Prior to Actuation (PSIG)IF AYiQLA$1E/IF APPLICABIE Reseat Pressure At Valve Closure (PS1G)Duration of This Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (5 Digit Number)Conuncnts Regarding This Actuation Attached7 ,MS-RYE 6/16/96 0353 NIA OPEN N/A 4 scc NIA MS-RYE 6/16/96 NIA OPEN NIA C N/A MS-RV-SB 6/16/96 0359 N/A OPEN NIA NIA MS-RYE 6/16/96 0355 N/A OPEN NIA A NIA MS-RYE 6/20/96 B 15 NIA OPEN NIA 1 min, 20 scc NIA 20
,MS-RYE6/16/960353NIAOPENN/A4sccNIAMS-RYE6/16/96NIAOPENNIACN/AMS-RV-SB6/16/960359N/AOPENNIANIAMS-RYE6/16/960355N/AOPENNIAANIAMS-RYE6/20/96B15NIAOPENNIA1min,20sccNIA20


NOTE:includesallIn-SituTestsForEachActuation orFailuretoActuate:S/RValveSerialNumber63790404055 63790404057 63790404126 63790404059 63790404062 Component ID(Location)
NOTE: includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404055 63790404057 63790404126 63790404059 63790404062 Component ID (Location)
DateofActuation (Mo/Da/Yr)
Date of Actuation (Mo/Da/Yr)
TimeofDay(24HourClock)TypeofActuation (Code)Cause/R'eaton forActuation (Code)RxOperating Condition PriortoLift(Code)RxPowerLevelPriortoLift(%Rated'Ihermal)
Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/R'eaton for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated'Ihermal)Time Req'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Cab)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)tF AVAKABLMF APPUCAttLE.
TimeReq'dforTailpipeTemptoReturntoNormalOtherInstrumentation Type(Cab)OtherInstrumentation NumberReadingandUnitsRxPressurePriortoActuation (PSIG)tFAVAKABLMF APPUCAttLE.
Reseat Pressure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments'Regarding Mis Actuation Attachcd7 MS-RVAB 6/20/96 B 15 NIA OPEN NIA 1 min, 7 scc NIA MS-RYE 6/20/96 B C NIA OPEN NIA 1 min, 16 sec N/A MS-RV-3D 6/20/96 B 15 NIA NIA 1 min, 12 scc NIA MS-RV-SB 6/20/96 12S I B 15 N/A OPEN NIA NIA MS-RV-SC 6/20/96 1253 B 1$NIA Process Computer OPEN NIA 1 min, 5 sec NIA lii, I~i~21~8 i i~~  
ReseatPressureAtValveClosure(PSIG)DurationofThisActuation (Minutes, Seconds)Failures.
Reports(Code)LERNumber(5DigitNumber)Comments'Regarding MisActuation Attachcd7 MS-RVAB6/20/96B15NIAOPENNIA1min,7sccNIAMS-RYE6/20/96BCNIAOPENNIA1min,16secN/AMS-RV-3D6/20/96B15NIANIA1min,12sccNIAMS-RV-SB6/20/9612SIB15N/AOPENNIANIAMS-RV-SC6/20/961253B1$NIAProcessComputerOPENNIA1min,5secNIAlii,I~i~21~8ii~~  


NOTE:IncludesallIn-SituTestsForEachActuation orFailuretoActuate:S/RValveSerialNumberComponent ID(Location)
NOTE: Includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number Component ID (Location)
DateofActuation (Mo/Da/Yr)
Date of Actuation (Mo/Da/Yr)
RimeofDay(24HourClock)TypeofActuation (Code)Cause/Reason forActuation (Code)RxOperating Condition PriortoLI(t(Code)RxPcnverLevelPriortoLilt(%Rated'Ihermal)
Rime of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to LI(t (Code)Rx Pcnver Level Prior to Lilt (%Rated'Ihermal)Time Req'd for Tailpipe Temp to Rctum to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IP AVAILABLE/IF APPLICABLE Reseat Pressure At Valve Closure (PSIG)Duration of%his Actuation.(Minutes, Seconds)Failures, Reports (Code)63790404061 MS-RV4D 1622 B N/A OPEN N/A I min.l scc LER Number (5 Digit Number)Comments Regarding'Ihis Actuation Attached?N/A 22 2.4 Summary of Plant Operations This section contains a narrative summary of operating experience and is included pursuant to Regulatory Guide 1.16, Sections C.l.b.(1)and C.l.b.(2).
TimeReq'dforTailpipeTemptoRctumtoNormalOtherInstrumentation Type(Code)OtherInstrumentation NumberReadingandUnitsRxPressurePriortoActuation (PSIG)IPAVAILABLE/IF APPLICABLE ReseatPressureAtValveClosure(PSIG)Durationof%hisActuation.
January 1996 At the begimnng of the month, the plant was operating at full power.From January 12, 1996 through part of January 16, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.
(Minutes, Seconds)Failures, Reports(Code)63790404061 MS-RV4D1622BN/AOPENN/AImin.lsccLERNumber(5DigitNumber)CommentsRegarding
During this time power was reduced to about 60 percent.Following economic dispatch, the plant returned" to full power operation on January 16, 1996.On January 19, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.
'IhisActuation Attached?
During this time power was reduced to about 60 percent.Following economic dispatch, the plant returned to full power operation on January 22, 1996 and operated at or near full power for the remainder of the month.February 1996 At the beginning of the month, the plant was operating at full power.On February 3, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.
N/A22 2.4SummaryofPlantOperations Thissectioncontainsanarrative summaryofoperating experience andisincludedpursuanttoRegulatory Guide1.16,SectionsC.l.b.(1) andC.l.b.(2).
During this time power was reduced to about 80 percent.r I On February 4, 1996 the plant was maneuvered into a planned downpower for Main Condenser maintenance.
January1996Atthebegimnngofthemonth,theplantwasoperating atfullpower.FromJanuary12,1996throughpartofJanuary16,1996theplantwasplacedoneconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministration.
FoHowing condenser work, the plant returned to full power operation.
Duringthistimepowerwasreducedtoabout60percent.Following economicdispatch, theplantreturned" tofullpoweroperation onJanuary16,1996.OnJanuary19,1996theplantwasplacedoneconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministration.
II On February 10 and 16, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.
Duringthistimepowerwasreducedtoabout60percent.Following economicdispatch, theplantreturnedtofullpoweroperation onJanuary22,1996andoperatedatornearfullpowerfortheremainder ofthemonth.February1996Atthebeginning ofthemonth,theplantwasoperating atfullpower.OnFebruary3,1996theplantwasplacedoneconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministration.
During this time power was reduced to about 75 and 55 percent respectively.
Duringthistimepowerwasreducedtoabout80percent.rIOnFebruary4,1996theplantwasmaneuvered intoaplanneddownpower forMainCondenser maintenance.
Following economic dispatch, the plant was returned to full power and operated at or near full power until February 27, 1996 when it was placed on economic dispatch goad following)
FoHowingcondenser work,theplantreturnedtofullpoweroperation.
'at the request of the Bonneville Power Administration.
IIOnFebruary10and16,1996theplantwasplacedoneconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministration.
During this time pow'er was reduced to about 80 percent.-The.plant returned to full power operation (100 percent)on February 28, 1996.~p r, F g*-.23  
Duringthistimepowerwasreducedtoabout75and55percentrespectively.
~On February 28, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administratio'n.
Following economicdispatch, theplantwasreturnedtofullpowerandoperatedatornearfullpoweruntilFebruary27,1996whenitwasplacedoneconomicdispatchgoadfollowing)
During this time power was reduced to about 80 percent.Tlie plant returned to full power operation (100 percent)on February 29, 1996.On February 29, 1996 the plant was placed on economic dispatch.goad following) at the request of the Bonneville Power Administration.
'attherequestoftheBonneville PowerAdministration.
During this time power was reduced to about 60 percent.~At the beginning of the month the plant continued to operate at reduced power due to economic dispatch goad following) at the request of the Bonneville Power Administration.
Duringthistimepow'erwasreducedtoabout80percent.-
During this time power generation was about 70 percent.~On March 2, 1996 the Main Turbine Generator was removed from service and the plant.was shutdown for economic dispatch goad following) at the request of the Bonneville Power Administration.
The.plantreturnedtofullpoweroperation (100percent)onFebruary28,1996.~pr,Fg*-.23  
The plant remained in a reserve shutdown condition until the beginning of the annual planned maintenance and refueling outage.April 1996~At the beginning of the month the plant continued to be in a reserve shutdown condition.
~OnFebruary28,1996theplantwasplacedoneconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministratio'n.
On April 13, 1996 the plant entered the annual maintenance and refueling outage.May 1996 The plant was in the annual maintenance and refueling outage for the entire month.June 1996 C The plant ended the annual maintenance and refueling outage on June 21, 1996.Following restart, the plant was manually scrammed on June 24, 1996 due to an unexpected plant response during testing of a recently-installed Digital Feedwater Level Control System.The reason for the unexpected plant response was due to a digital reactor feedwater controller error.A change was made to the controller software and plant startup resumed.At the end of-the month, the plant was operating at 25 percent power and continuing with.startup testing following the maintenance and,refueling outage.-0 24 July 1996 At the beginning of the month the plant was ramped up to 68 percent power.Power was maintained at this level due to problems encountered during testing of the recently-instaHed Reactor Recirculation System Pump Adjustable Speed Drives and the Digital Feedwater Level Control System.~At the end of the month the plant was operating at 68 percent power and continuing with startup testing foHowing the maintenance and refueling outage.August 1996 At the beginning of the month, startup testing following the maintenance and refueling outage was still in progress with the focus on the recently-installed Reactor Recirculation System Pump Adjustable Speed Drives and the Digital Feedwater Level Control System.Power was maintained at 64 percent power.On August 10, 1996 the plant continued to operate as a severe transient coursed through the interconnected electrical transmission grids in the Western United States.l During the evening of August 10, 1996, on-line Reactor Recirculation (RRC)System Pump RRC-P-IB"ran back" from approximately 50 Hi to 15 Hz during testing on part of the Adjustable Speed Drive System for the pump.Reactor power decreased from 64 percent to 48 percent.Reactor power was subsequently restored to'65 percent.On August 11, 1996 an unanticipated increase of approximately two percent power occurred due to an apparent failure of a portion of the control for both reactor recirculation pumps.The part of the computer control involved in the failure was removed from the control circuitry and local reactor recirculation pump control was established.
Duringthistimepowerwasreducedtoabout80percent.Tlieplantreturnedtofullpoweroperation (100percent)onFebruary29,1996.OnFebruary29,1996theplantwasplacedoneconomicdispatch.
Testing'and troubleshooting efforts were suspended pending a thorough review of a Reactor Recirculation System Pump Adjustable Speed Drives and Digital Feedwater Level Control System test plan.On August 29, 1996 following development of a revised plan, testing was resumed and the power level was increased to support the effort.At the end of the month the plant was operating at 69 percent power and testing continued.
goadfollowing) attherequestoftheBonneville PowerAdministration.
25 September 1996~The lan p t entered the month at about 69 percent power as testing of the Reactor Recirculation System Pump Adjustable Speed Drives and.the Digital Feedwater Level Control System continued.
Duringthistimepowerwasreducedtoabout60percent.~Atthebeginning ofthemonththeplantcontinued tooperateatreducedpowerduetoeconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministration.
On September 5, 1996, following successful testing efforts, reactor power was raised to 100 percent.On September 13, 1996 power was reduced to approximately 52 percent for economic dispatch goad following) at the request of the Bonneville Power Administration.
Duringthistimepowergeneration wasabout70percent.~OnMarch2,1996theMainTurbineGenerator wasremovedfromserviceandtheplant.wasshutdownforeconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministration.
On September 15, 1996, during routine turbine valve testing, a turbine stop valve Med to open.On September 16, 1996 power was reduced to 25 percent to perform repairs to the Turbine Stop Valve Control System.~Following successful repair efforts, the plant resumed 100 percent power operation on September 17, 1996.~On September 20, 1996 power was reduced to 60 percent power@plug a leaking tube~in the Main Coridenser and to replace some scram solenoid pilot valves.FoHowing repairs, the plant resumed fuH power operation on September 22, 1996 and operated at or near 100 percent power for the remainder of the month.October 1996 The plant entered the month at 100 percent power.On October 9, 1996 power was reduced to approximately 55 percent to repair an Adjustable Speed Drive channel that experienced a Med resistivity meter.On October 10, 1996 the plant resumed 100 percent power On October 11, 1996 power w'as reduced to approximately 75 percent power to perform scram time and turbine valve testing, and then to 60 percent for digital feedwater system testing.Following a firmware change on each of the reactor feedwater pumps and subsequent testing, the plant resumed 100 percent power on October 13, 1996.The plant operated at or near fuH power until October 23, 1996 when power was reduced to repair an Adjustable Speed Drive channel that experienced a failed resistivity meter.During power ascension foHowing,repairs, the same channel tripped on overspeed.
Theplantremainedinareserveshutdowncondition untilthebeginning oftheannualplannedmaintenance andrefueling outage.April1996~Atthebeginning ofthemonththeplantcontinued tobeinareserveshutdowncondition.
3 At the end of the month'the plant was operating at 92 percent power,26 November 1996~The lan p t entered the month at approximately 92 percent power due to a channel failure in the Adjustable Speed Drive System.On November 1, 1996 power was reduced to approximately 49 percent to perform repairs on Adjustable Speed Drive Channel 1A/2.Following successful repair efforts, plant power was increased to 100 percent on November 3, 1996.On November 9, 1996 a power reduction to 75 percent was commenced to perform monthly turbine valve testing.During this evolution, Main Steam (MS)'System Turbine Intercept Valve MS-V-165C would not re-open during testing.Accordingly, power was reduced to 62 percent as prescribed by the Technical Specifications.
OnApril13,1996theplantenteredtheannualmaintenance andrefueling outage.May1996Theplantwasintheannualmaintenance andrefueling outagefortheentiremonth.June1996CTheplantendedtheannualmaintenance andrefueling outageonJune21,1996.Following restart,theplantwasmanuallyscrammedonJune24,1996duetoanunexpected plantresponseduringtestingofarecently-installed DigitalFeedwater LevelControlSystem.Thereasonfortheunexpected plantresponsewasduetoadigitalreactorfeedwater controller error.Achangewasmadetothecontroller softwareandplantstartupresumed.Attheendof-themonth,theplantwasoperating at25percentpowerandcontinuing with.startuptestingfollowing themaintenance and,refueling outage.-024 July1996Atthebeginning ofthemonththeplantwasrampedupto68percentpower.Powerwasmaintained atthislevelduetoproblemsencountered duringtestingoftherecently-instaHedReactorRecirculation SystemPumpAdjustable SpeedDrivesandtheDigitalFeedwater LevelControlSystem.~Attheendofthemonththeplantwasoperating at68percentpowerandcontinuing withstartuptestingfoHowingthemaintenance andrefueling outage.August1996Atthebeginning ofthemonth,startuptestingfollowing themaintenance andrefueling outagewasstillinprogresswiththefocusontherecently-installed ReactorRecirculation SystemPumpAdjustable SpeedDrivesandtheDigitalFeedwater LevelControlSystem.Powerwasmaintained at64percentpower.OnAugust10,1996theplantcontinued tooperateasaseveretransient coursedthroughtheinterconnected electrical transmission gridsintheWesternUnitedStates.lDuringtheeveningofAugust10,1996,on-lineReactorRecirculation (RRC)SystemPumpRRC-P-IB"ranback"fromapproximately 50Hito15HzduringtestingonpartoftheAdjustable SpeedDriveSystemforthepump.Reactorpowerdecreased from64percentto48percent.Reactorpowerwassubsequently restoredto'65percent.OnAugust11,1996anunanticipated increaseofapproximately twopercentpoweroccurredduetoanapparentfailureofaportionofthecontrolforbothreactorrecirculation pumps.Thepartofthecomputercontrolinvolvedinthefailurewasremovedfromthecontrolcircuitry andlocalreactorrecirculation pumpcontrolwasestablished.
On November 10, power was further reduced to 55 percent to repair the valve.The air solenoid and internal o-rings were replaced.~Following successful repair efforts, plant power was increased to 100 percent on ,.November 13, 1996.~With the exception of a few short downpowers for'outine maintenance, the plant operated at or near 100 percent power during the remainder of the month.December 1996 The plant operated at or near 100 percent power during the month.I 27 2.S Significant Corrective Maintenance Performed on Safety-Related Equipment~~~This section contains a description of major, safety-related corrective maintenance performed during outages or power reductions and is included pursuant to Regulatory Guide 1.16, Section C.l.b(2)(e).
Testing'and troubleshooting effortsweresuspended pendingathoroughreviewofaReactorRecirculation SystemPumpAdjustable SpeedDrivesandDigitalFeedwater LevelControlSystemtestplan.OnAugust29,1996following development ofarevisedplan,testingwasresumedandthepowerlevelwasincreased tosupporttheeffort.Attheendofthemonththeplantwasoperating at69percentpowerandtestingcontinued.
The following descriptions consist of summaries of information provided through the Nuclear Plant Reliability Data System (NPRDS).In addition to safety-related equipment, components considered to be essential for power generation are also included.~APRM-F/U-A During the annual maintenance and refueling outage, an alarm was received on the Average Power Range Monitor (APRM)"A" flow unit: During investigation of the problem, the"C" flow unit was taken to bypass and the"A" unit alarm cleared and did not return until after the"C" flow unit was removed from the bypass mode.The cause of the problem was indeterminate.
25 September 1996~Thelanptenteredthemonthatabout69percentpowerastestingoftheReactorRecirculation SystemPumpAdjustable SpeedDrivesand.theDigitalFeedwater LevelControlSystemcontinued.
The test monitor switch was replaced and tested.No further problems were noted.(Failure Date: 06/18/96)CAC-EHO-FCV/4A 0 During testing of a Containment Atmosphere Control (CAC)System flow control valve, it was discovered that a normally closed limit switch on the electro-hydraulic operator was in the open'position.
OnSeptember 5,1996,following successful testingefforts,reactorpowerwasraisedto100percent.OnSeptember 13,1996powerwasreducedtoapproximately 52percentforeconomicdispatchgoadfollowing) attherequestoftheBonneville PowerAdministration.
The cause of the problem was due to an incorrectly wired connection in.the limit switch.The miswiring apparently occurred during previous maintenance activities.
OnSeptember 15,1996,duringroutineturbinevalvetesting,aturbinestopvalveMedtoopen.OnSeptember 16,1996powerwasreducedto25percenttoperformrepairstotheTurbineStopValveControlSystem.~Following successful repairefforts,theplantresumed100percentpoweroperation onSeptember 17,1996.~OnSeptember 20,1996powerwasreducedto60percentpower@plugaleakingtube~intheMainCoridenser andtoreplacesomescramsolenoidpilotvalves.FoHowingrepairs,theplantresumedfuHpoweroperation onSeptember 22,1996andoperatedatornear100percentpowerfortheremainder ofthemonth.October1996Theplantenteredthemonthat100percentpower.OnOctober9,1996powerwasreducedtoapproximately 55percenttorepairanAdjustable SpeedDrivechannelthatexperienced aMedresistivity meter.OnOctober10,1996theplantresumed100percentpowerOnOctober11,1996powerw'asreducedtoapproximately 75percentpowertoperformscramtimeandturbinevalvetesting,andthento60percentfordigitalfeedwater systemtesting.Following afirmwarechangeoneachofthereactorfeedwater pumpsandsubsequent testing,theplantresumed100percentpoweronOctober13,1996.TheplantoperatedatornearfuHpoweruntilOctober23,1996whenpowerwasreducedtorepairanAdjustable SpeedDrivechannelthatexperienced afailedresistivity meter.Duringpowerascension foHowing,repairs, thesamechanneltrippedonoverspeed.
I The wiring error was corrected and the switch'was adjusted.No further problems were noted.(Failure Date: 02/24/96), CAC-FCV-4B During the performance of a local leak rate test, leakage in excess of allowable limits was discovered on Containment Atmosphere Control (CAC)System Valve CAC-FCV-4B.The cause of the problem was due to line and valve rust which degraded seat.integrity.
3Attheendofthemonth'the plantwasoperating at92percentpower,26 November1996~Thelanptenteredthemonthatapproximately 92percentpowerduetoachannelfailureintheAdjustable SpeedDriveSystem.OnNovember1,1996powerwasreducedtoapproximately 49percenttoperformrepairsonAdjustable SpeedDriveChannel1A/2.Following successful repairefforts,plantpowerwasincreased to100percentonNovember3,1996.OnNovember9,1996apowerreduction to75percentwascommenced toperformmonthlyturbinevalvetesting.Duringthisevolution, MainSteam(MS)'SystemTurbineIntercept ValveMS-V-165C wouldnotre-openduringtesting.Accordingly, powerwasreducedto62percentasprescribed bytheTechnical Specifications.
The rust was removed and the valve seat was machined and lapped.Following completion of a successful post-maintenance local leak rate test, no further problems were noted.(Failure Date: 05/16/96)28  
OnNovember10,powerwasfurtherreducedto55percenttorepairthevalve.Theairsolenoidandinternalo-ringswerereplaced.
~Following successful repairefforts,plantpowerwasincreased to100percenton,.November13,1996.~Withtheexception ofafewshortdownpowers for'outine maintenance, theplantoperatedatornear100percentpowerduringtheremainder ofthemonth.December1996Theplantoperatedatornear100percentpowerduringthemonth.I27 2.SSignificant Corrective Maintenance Performed onSafety-Related Equipment
~~~Thissectioncontainsadescription ofmajor,safety-related corrective maintenance performed duringoutagesorpowerreductions andisincludedpursuanttoRegulatory Guide1.16,SectionC.l.b(2)(e).
Thefollowing descriptions consistofsummaries ofinformation providedthroughtheNuclearPlantReliability DataSystem(NPRDS).Inadditiontosafety-related equipment, components considered tobeessential forpowergeneration arealsoincluded.
~APRM-F/U-A Duringtheannualmaintenance andrefueling outage,analarmwasreceivedontheAveragePowerRangeMonitor(APRM)"A"flowunit:Duringinvestigation oftheproblem,the"C"flowunitwastakentobypassandthe"A"unitalarmclearedanddidnotreturnuntilafterthe"C"flowunitwasremovedfromthebypassmode.Thecauseoftheproblemwasindeterminate.
Thetestmonitorswitchwasreplacedandtested.Nofurtherproblemswerenoted.(FailureDate:06/18/96)
CAC-EHO-FCV/4A 0DuringtestingofaContainment Atmosphere Control(CAC)Systemflowcontrolvalve,itwasdiscovered thatanormallyclosedlimitswitchontheelectro-hydraulic operatorwasintheopen'position.
Thecauseoftheproblemwasduetoanincorrectly wiredconnection in.thelimitswitch.Themiswiring apparently occurredduringpreviousmaintenance activities.
IThewiringerrorwascorrected andtheswitch'was adjusted.
Nofurtherproblemswerenoted.(FailureDate:02/24/96)
,CAC-FCV-4B Duringtheperformance ofalocalleakratetest,leakageinexcessofallowable limitswasdiscovered onContainment Atmosphere Control(CAC)SystemValveCAC-FCV-4B.Thecauseoftheproblemwasduetolineandvalverustwhichdegradedseat.integrity.
Therustwasremovedandthevalveseatwasmachinedandlapped.Following completion ofasuccessful post-maintenance localleakratetest,nofurtherproblemswerenoted.(FailureDate:05/16/96) 28  


CAC-V-4TDuringtheperformance ofalocalleakratetest,aleakrateinexcessofallowable limitswasdiscovered onContainment Atmosphere Control(CAC)SystemValveCAC-V-4.Thecauseoftheproblemwasduetolineandvalverustwhichdegradedseatintegrity.
CAC-V-4 T During the performance of a local leak rate test, a leak rate in excess of allowable limits was discovered on Containment Atmosphere Control (CAC)System Valve CAC-V-4.The cause of the problem was due to line and valve rust which degraded seat integrity.
Therustwasremovedandthevalveseatwasmachinedandlapped.Following completion ofasuccessful post-maintenance localleakratetest,nofurtherproblemswerenoted.(FailureDate:05/18/96)
The rust was removed and the valve seat was machined and lapped.Following completion of a successful post-maintenance local leak rate test, no further problems were noted.(Failure Date: 05/18/96)~COND-DM-1B During power operation, Condensate (COND)System Demineralizer COND-DM-1B failed its resin bleed-through test.There was evidence of resin trachng across the rubber washers at the bayonet fitting on 35 of the septa.New septa (35)were installed in the area immediately adjacent to the draft tube and no further problems were noted.(Failure Date: 08/13/96)COND-DM-1E During routine inspections while at power operation, it was observed that the resin strainer differential pressure on Condensate (COND)System Demineralizer COND-DM-1E had increased from ten psid to 15 psid.Following troubleshooting efforts and additional inspections, it was discovered that the draft tube was loose and not latched.In addition, most of the septa on the inner ring were damaged.The cause of the problem was attributed to fiow-induced vibration or other failure mechanism.
~COND-DM-1B Duringpoweroperation, Condensate (COND)SystemDemineralizer COND-DM-1B faileditsresinbleed-through test.Therewasevidenceofresintrachngacrosstherubberwashersatthebayonetfittingon35ofthesepta.Newsepta(35)wereinstalled intheareaimmediately adjacenttothedrafttubeandnofurtherproblemswerenoted.(FailureDate:08/13/96)
e'elded lochng devices were added to the draft tube and new septa were installed.
COND-DM-1E Duringroutineinspections whileatpoweroperation, itwasobservedthattheresinstrainerdifferential pressureonCondensate (COND)SystemDemineralizer COND-DM-1Ehadincreased fromtenpsidto15psid.Following troubleshooting effortsandadditional inspections, itwasdiscovered thatthedrafttubewaslooseandnotlatched.Inaddition, mostoftheseptaontheinnerringweredamaged.Thecauseoftheproblemwasattributed tofiow-induced vibration orotherfailuremechanism.
No further problems were noted.(Failure Date: 02/27/96).~COND-HX-2A During full power operation', it was noted that the level control valve for Condensate (COND)System Heat Exchanger COND-HX-2A was open further than normal.This was an indication of a tube leak in the heat exchanger.
e'eldedlochngdeviceswereaddedtothedrafttubeandnewseptawereinstalled.
The cause of the problem was attributed to normal wear.The heat exchanger was drained and nondestructive examinations were performed.
Nofurtherproblemswerenoted.(FailureDate:02/27/96)
Leaking tubes were plugged and no further problems were noted.(Failuie Date: 03/04/96)  
.~COND-HX-2A Duringfullpoweroperation',
itwasnotedthatthelevelcontrolvalveforCondensate (COND)SystemHeatExchanger COND-HX-2A wasopenfurtherthannormal.Thiswasanindication ofatubeleakintheheatexchanger.
Thecauseoftheproblemwasattributed tonormalwear.Theheatexchanger wasdrainedandnondestructive examinations wereperformed.
Leakingtubeswerepluggedandnofurtherproblemswerenoted.(FailuieDate:03/04/96)  


COND-HX-9 Duringroutinesampling-at fullpoweroperation, anincreaseinreactorsulfatelevelswasobserved.
COND-HX-9 During routine sampling-at full power operation, an increase in reactor sulfate levels was observed.The reason for the increase was determined to be a condenser tube leak in Condensate (COND)'System Heat Exchanger COND-HX-9.
Thereasonfortheincreasewasdetermined tobeacondenser tubeleakinCondensate (COND)'System HeatExchanger COND-HX-9.
The exact cause of the tube leak was indeterminate.
Theexactcauseofthetubeleakwasindeterminate.
The tube was plugged and no further problems were noted.(Failure Date: 02/02/96)COND-HX-9 During main condenser inspection efforts, damage was noted on spray baskets", welds and a strong back for Condensate (COND)System Heat Exchanger COND-HX-9.
Thetubewaspluggedandnofurtherproblemswerenoted.(FailureDate:02/02/96)
The cause of the problem was attributed to normal usage and stresses.AH damaged components were either repaired or replaced and no further problems were noted.(Failure Date: 05/07/96)COND-HX-9 During power operation, an increase in reactor sulfate levels were observed.The reason for the increase was determined to be a condenser tube leak in Condensate (COND)System Heat Exchanger COND-HX-9.
COND-HX-9 Duringmaincondenser inspection efforts,damagewasnotedonspraybaskets",
The exact cause of the tube leak was indeterminate.
weldsandastrongbackforCondensate (COND)SystemHeatExchanger COND-HX-9.
The tube was plugged and no further problems were noted.(Failure Date: 09/10/96)COND-P-2A During power operation, inboard and outboard seal leakage was discovered on Condensate (COND)System Pump COND-P-2A.
Thecauseoftheproblemwasattributed tonormalusageandstresses.
The cause of the problem was determined to be a casting defect in the bearing assembly that resulted in premature failure of the bearing.A new bearing, bearing body and bearing caps were installed.
AHdamagedcomponents wereeitherrepairedorreplacedandnofurtherproblemswerenoted.(FailureDate:05/07/96)
Following completion of post-maintenance testing, no further problems were noted.(Failure Date: 08/18/96)COND-P-2B During power operation, mechanical seal leakage was observed on Condensate (COND)System Pump COND-P-2B.
COND-HX-9 Duringpoweroperation, anincreaseinreactorsulfatelevelswereobserved.
The cause of the problem was determined to be.normal usage and.wear.'0  
Thereasonfortheincreasewasdetermined tobeacondenser tubeleakinCondensate (COND)SystemHeatExchanger COND-HX-9.
Theexactcauseofthetubeleakwasindeterminate.
Thetubewaspluggedandnofurtherproblemswerenoted.(FailureDate:09/10/96)
COND-P-2A Duringpoweroperation, inboardandoutboardsealleakagewasdiscovered onCondensate (COND)SystemPumpCOND-P-2A.
Thecauseoftheproblemwasdetermined tobeacastingdefectinthebearingassemblythatresultedinpremature failureofthebearing.Anewbearing,bearingbodyandbearingcapswereinstalled.
Following completion ofpost-maintenance testing,nofurtherproblemswerenoted.(FailureDate:08/18/96)
COND-P-2B Duringpoweroperation, mechanical sealleakagewasobservedonCondensate (COND)SystemPumpCOND-P-2B.
Thecauseoftheproblemwasdetermined tobe.normalusageand.wear.
'0  


Theinboardandoutboardseals'and theoutboardshaftsleevewerereplaced.
The inboard and outboard seals'and the outboard shaft sleeve were replaced.No further problems were noted.(Failure Date: 07/31/96)COND-PC V~During the annual maintenance and refueling outage, it was noted that the valve stem was worn on Condensate (COND)System Pressure Control Valve COND-PCV-40.
Nofurtherproblemswerenoted.(FailureDate:07/31/96)
The cause of the problem was attributed to normal usage and wear.The valve stem, plug, seat ring, gaskets and packing were replaced.Following completion of successful diagnostic testing, no further problems were noted.(Failure Date: 04/23/96)COND-V-141 A During the annual maintenance and refueling outage, Engineering personnel were informed by the vendor for Conderihate (COND)System Valve COND-V-141A that the potential existed for failure of the anti-rotation collar due to key misalignment or lack of a set screw.The cause of the problem was attributed to manu'facturer assembly practices.
COND-PCV~Duringtheannualmaintenance andrefueling outage,itwasnotedthatthevalvestemwaswornonCondensate (COND)SystemPressureControlValveCOND-PCV-40.
A new key was fabricated and installed on the valve.(Failure Date: 05/21/96)During power operation, an increased temperature was observed on a load side fuse clip in Containment Return Air (CRA)Motor ControHer CRA-42-8B6B for a fan in the primary containment cooling system.The cause of the problem was that the fuse clip had separated from the bakelite support, causing a higher resistance which resulted in the" temperature increase.The fuse block was replaced and no"further problems were noted.(Failure Date: 09/24/96)CRA-FN-SB During the annual maintenance and refueling outage, Maintenance personnel observed Containment Return Air (CRA)Fan CRA-FN-SB rotating in the incorrect direction during performance of preventive maintenance.
Thecauseoftheproblemwasattributed tonormalusageandwear.Thevalvestem,plug,seatring,gasketsandpackingwerereplaced.
The cause of the problem was due to reversed phase lead connections.
Following completion ofsuccessful diagnostic testing,nofurtherproblemswerenoted.(FailureDate:04/23/96)
The lead reversal apparently occurred during previous maintenance activities.
COND-V-141 ADuringtheannualmaintenance andrefueling outage,Engineering personnel wereinformedbythevendorforConderihate (COND)SystemValveCOND-V-141A thatthepotential existedforfailureoftheanti-rotation collarduetokeymisalignment orlackofasetscrew.Thecauseoftheproblemwasattributed tomanu'facturer assemblypractices.
tp 31 0 The leads were re-connected to the correct configuration and no further problems were noted.(Failure Date: 05/16/96)CRD-HCU-2215 During the annual maintenance and refueling outage, Control Rod Drive (CRD)System Hydraulic Control Unit CRD-HCU-2215 level switch failed to actuate during surveillance testing.The cause of the problem was attributed to mechanical binding in the actuating mechanism.
Anewkeywasfabricated andinstalled onthevalve.(FailureDate:05/21/96)
A new level switch was installed and no further problems were noted..(Failure Date: 03/28/96)CRD-HCU-2623 During operation with the plant at 80 percent power, water leakage past the piston was noted on the accumulator for Control Rod Drive (CRD)System Hydraulic Control Unit CRD-HCU-2623.
Duringpoweroperation, anincreased temperature wasobservedonaloadsidefuseclipinContainment ReturnAir(CRA)MotorControHer CRA-42-8B6B forafanintheprimarycontainment coolingsystem.Thecauseoftheproblemwasthatthefusecliphadseparated fromthebakelitesupport,causingahigherresistance whichresultedinthe"temperature increase.
The cause of the problem was attributed to normal wear or aging of the piston sealing mechanism.
Thefuseblockwasreplacedandno"further problemswerenoted.(FailureDate:09/24/96)
The piston sealing mechanism.was replaced and no further problems were noted.(Failure Date: 02/04/96)~CRD-HCU-3443 During the annual maintenance and refueling outage, hydrogen leakage was noted past the packing and around the stem on a valve associated with Control Rod Drive (CRD)System Hydraulic Control Unit CRD-HCU-3443.
CRA-FN-SB Duringtheannualmaintenance andrefueling outage,Maintenance personnel observedContainment ReturnAir(CRA)FanCRA-FN-SB rotatingintheincorrect direction duringperformance ofpreventive maintenance.
The cause of the problem was attributed to normal wear.The valve was replaced with a new valve and no further problems were noted.(Failure Date: 04/18/96)~CRD-'P-1B During power operation, minor leakage was observed on'he positive seal supply lirie and casing drain plug for Control Rod Drive (CRD)System Pump CDR-P-1B.The cause of the problem was attributed to normal wear.The line was disassembled and a new union joint was installed.
Thecauseoftheproblemwasduetoreversedphaseleadconnections.
No further problems were noted., (Failure Date: 10/30/96)32  
Theleadreversalapparently occurredduringpreviousmaintenance activities.
tp31 0Theleadswerere-connected tothecorrectconfiguration andnofurtherproblemswerenoted.(FailureDate:05/16/96)
CRD-HCU-2215 Duringtheannualmaintenance andrefueling outage,ControlRodDrive(CRD)SystemHydraulic ControlUnitCRD-HCU-2215 levelswitchfailedtoactuateduringsurveillance testing.Thecauseoftheproblemwasattributed tomechanical bindingintheactuating mechanism.
Anewlevelswitchwasinstalled andnofurtherproblemswerenoted..(FailureDate:03/28/96)
CRD-HCU-2623 Duringoperation withtheplantat80percentpower,waterleakagepastthepistonwasnotedontheaccumulator forControlRodDrive(CRD)SystemHydraulic ControlUnitCRD-HCU-2623.
Thecauseoftheproblemwasattributed tonormalwearoragingofthepistonsealingmechanism.
Thepistonsealingmechanism.was replacedandnofurtherproblemswerenoted.(FailureDate:02/04/96)
~CRD-HCU-3443 Duringtheannualmaintenance andrefueling outage,hydrogenleakagewasnotedpastthepackingandaroundthestemonavalveassociated withControlRodDrive(CRD)SystemHydraulic ControlUnitCRD-HCU-3443.
Thecauseoftheproblemwasattributed tonormalwear.Thevalvewasreplacedwithanewvalveandnofurtherproblemswerenoted.(FailureDate:04/18/96)
~CRD-'P-1B Duringpoweroperation, minorleakagewasobservedon'hepositivesealsupplylirieandcasingdrainplugforControlRodDrive(CRD)SystemPumpCDR-P-1B.
Thecauseoftheproblemwasattributed tonormalwear.Thelinewasdisassembled andanewunionjointwasinstalled.
Nofurtherproblemswerenoted.,(FailureDate:10/30/96) 32  


DLO-P-3A2 Duringfullpoweroperation, abrokencouplingoccurredonDieselGenerator LubeOil(DLO)PumpDLO-P-3A'2.
DLO-P-3A2 During full power operation, a broken coupling occurred on Diesel Generator Lube Oil (DLO)Pump DLO-P-3A'2.
Thecausewasattributed tohighvibration duetoinadequate pumpmountingsupp'orts.
The cause was attributed to high vibration due to inadequate pump mounting supp'orts.
Thehighvibration'resulted inincreased stresseswhichledtocrackdevelopment.
The high vibration'resulted in increased stresses which led to crack development.
Thecouplingwasreplacedandpumpsofsimilardesignwereinspected andadditional couplings werereplaced.
The coupling was replaced and pumps of similar design were inspected and additional couplings were replaced.A re-design of the support structure was not performed.
Are-design ofthesupportstructure wasnotperformed.
This decision was based on a cost benefit analysis.Couplings are to be inspected and replaced when necessary.(Failure Date: 01/05/96)~DLO-P-3B2 During operation with the plant at 60 percent power, a broken coupling occurred on Diesel Generator Lube Oil (DLO)Pump DLO-P-3B2.
Thisdecisionwasbasedonacostbenefitanalysis.
The cause was attributed to inadequate design for the effects of resonance, cold spring and differential thermal expansion on coupling alignment.
Couplings aretobeinspected andreplacedwhennecessary.
The coupling was replaced and flex hoses were installed to dampen vibrations.
(FailureDate:01/05/96)
No further problems were noted.(Failure Date: 02/18/96)8)R-V-3 During the annual maintenance and refueling outage, leakage was observed on'adioactive Floor Drain (FDR)System Valve FDR-V-3.The cause of the problem was.determined to be normal usage,and wear.A contributing cause was line rust which degraded the seat.The..valve was cleaned and a new seat was installed.(Failure Date: 04/26/96)8)R-V-3 During the annual maintenance and refueling.
~DLO-P-3B2 Duringoperation withtheplantat60percentpower,abrokencouplingoccurredonDieselGenerator LubeOil(DLO)PumpDLO-P-3B2.
outage, Radioactive Floor Drain (FDR)System Valve FDR-V-3 failed to close during local leak rate testing.The cause of the problem was determined to be binding in the stem seal area.The stem nut had apparently been over-tightened during previous maintenance work.The stem nut was loosened and no f'urther valve stroking problems related to this event were noted.(Failure Date: 05/19/96)0 33' During power operation, Radioactive Floor Drain (FDR)System Valve FDR-V-3 exceeded the closing time limit during stroke time testing.The cause of the problem was determined to be foreign material and debris that had collected in the seat area.The source was loop seal piping debris that lodged into the seat from increased flow during a drain down of the undervessel drywell FDR sump.The valve was disassembled and cleaned.No further problems were noted with this particular valve.(Failure Date: 07/06/96)FDR-V-4 During power operation, Radioactive Floor Drain (FDR)System Valve FDR-V-4 exceeded the closing time limit during stroke time testing.The cause of the problem was attributed to foreign material and debris that had collected in the seat area.The source , was from loop seal piping debris that lodged into the seat from increased flow during a drain down of the undervessel drywell FDR sump.A contributing cause was loose set screws that allowed the coupling to shift out of alignment.
Thecausewasattributed toinadequate designfortheeffectsofresonance, coldspringanddifferential thermalexpansion oncouplingalignment.
The valve was disassembled and cleaned.Existing set screws were tightened and an additional set were installed.
Thecouplingwasreplacedandflexhoseswereinstalled todampenvibrations.
No further problems were noted.(Failure Date: 08/01/96)h During power operation, high vibration readings were noted on the bearings for High Pressure Core.Spray (HPCS)System Discharge Piping Fill Pump HPCS-P-3.The cause of the problem was determined to be normal wear leading to bearing degradation.
Nofurtherproblemswerenoted.(FailureDate:02/18/96) 8)R-V-3Duringtheannualmaintenance andrefueling outage,leakagewasobservedon'adioactive FloorDrain(FDR)SystemValveFDR-V-3.Thecauseoftheproblemwas.determined tobenormalusage,and wear.Acontributing causewaslinerustwhichdegradedtheseat.The..valve wascleanedandanewseatwasinstalled.
Th'e pump was disassembled and the shaft, sleeve, bearings, seals and o-rings were replaced.No furtherproblemswerenoted.(FailureDate:
(FailureDate:04/26/96) 8)R-V-3Duringtheannualmaintenance andrefueling.
09/11/96)~IRM-EMSQ401F During testing efforts while at power operation, it was noted that positive and negative adjustments could not be made to Intermediate Range Monitor (IRM)15-volt Power supply IRM-EMSQ-601F.
outage,Radioactive FloorDrain(FDR)SystemValveFDR-V-3failedtocloseduringlocalleakratetesting.Thecauseoftheproblemwasdetermined tobebindinginthestemsealarea.Thestemnuthadapparently beenover-tightened duringpreviousmaintenance work.Thestemnutwasloosenedandnof'urthervalvestrokingproblemsrelatedtothiseventwerenoted.(FailureDate:05/19/96) 033' Duringpoweroperation, Radioactive FloorDrain(FDR)SystemValveFDR-V-3exceededtheclosingtimelimitduringstroketimetesting.Thecauseoftheproblemwasdetermined tobeforeignmaterialanddebristhathadcollected intheseatarea.Thesourcewasloopsealpipingdebristhatlodgedintotheseatfromincreased flowduringadraindownoftheundervessel drywellFDRsump.Thevalvewasdisassembled andcleaned.Nofurtherproblemswerenotedwiththisparticular valve.(FailureDate:07/06/96)
The cause of the problem was attributed to a defective circuit card in the power supply.The power supply was replaced and no further problems were noted.(Failure Date: 08/01/96)34  
FDR-V-4Duringpoweroperation, Radioactive FloorDrain(FDR)SystemValveFDR-V-4exceededtheclosingtimelimitduringstroketimetesting.Thecauseoftheproblemwasattributed toforeignmaterialanddebristhathadcollected intheseatarea.Thesource,wasfromloopsealpipingdebristhatlodgedintotheseatfromincreased flowduringadraindownoftheundervessel drywellFDRsump.Acontributing causewasloosesetscrewsthatallowedthecouplingtoshiftoutofalignment.
Thevalvewasdisassembled andcleaned.Existingsetscrewsweretightened andanadditional setwereinstalled.
Nofurtherproblemswerenoted.(FailureDate:08/01/96) hDuringpoweroperation, highvibration readingswerenotedonthebearingsforHighPressureCore.Spray(HPCS)SystemDischarge PipingFillPumpHPCS-P-3.
Thecauseoftheproblemwasdetermined tobenormalwearleadingtobearingdegradation.
Th'epumpwasdisassembled andtheshaft,sleeve,bearings, sealsando-ringswerereplaced.
Nofurtherproblemswerenoted.
(FailureDate:
09/11/96)
~IRM-EMSQ401F Duringtestingeffortswhileatpoweroperation, itwasnotedthatpositiveandnegativeadjustments couldnotbemadetoIntermediate RangeMonitor(IRM)15-voltPowersupplyIRM-EMSQ-601F.
Thecauseoftheproblemwasattributed toadefective circuitcardinthepowersupply.Thepowersupplywasreplacedandnofurtherproblemswerenoted.(FailureDate:08/01/96) 34  


LPRM-DEJA/57 Duringpoweroperation, severalspuriousalarmswereobservedwithLocalPowerRangeMonitor(LPRM)LPRM-DET-40/75.
LPRM-DEJA/57 During power operation, several spurious alarms were observed with Local Power Range Monitor (LPRM)LPRM-DET-40/75.
Thecauseoftheproblemwasattributed.
The cause of the problem was attributed.
toadefective auxiliary circuitcard.Theauxiliary circuitcardwasreplacedandnofurtherproblemswerenoted.(Failure.
to a defective auxiliary circuit card.The auxiliary circuit card was replaced and no further problems were noted.(Failure.Date: 02/04/96)MS-ABC During the annual maintenance and refueling outage, an air leak was observed between the valve and manifold for Main Steam (MS)System Valve Air Operator MS-AO-4C.The cause of the problem was due to failed o-rings due to normal wear and usage.Four o-rings were replaced and no further problems were noted.(Failure Date: 05/28/96)MS-PS-47A During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47A was out of tolerance in the conservative direction.
Date:02/04/96)
The cause of the problem was that the piessure switch case had not been vented.The pressure'switch case was vented and no further problems were noted.(Failure Date: 11/26/96)During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47B was out of tolerance in the conservative direction.
MS-ABCDuringtheannualmaintenance andrefueling outage,anairleakwasobservedbetweenthevalveandmanifoldforMainSteam(MS)SystemValveAirOperatorMS-AO-4C.
The cause of the problem was that the pressure switch case had not been vented.The pressure switch case was vented and no further problems were noted.(Failure Date:~11/26/96)MS-PS-47C During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47C was out of tolerance in=the conservative direction.
Thecauseoftheproblemwasduetofailedo-ringsduetonormalwearandusage.Fouro-ringswerereplacedandnofurtherproblemswerenoted.(FailureDate:05/28/96)
The cause of the.problem was that the pressure switch case had not been vented.The pressure switch case was vented and no further problems were noted.:(Failure Date: 11/26/96)
MS-PS-47A Duringpoweroperation, itwasdiscovered thatthesetpointforMainSteam(MS)SystemPressureSwitchMS-PS-47A wasoutoftolerance intheconservative direction.
MS-PS-47D During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47D was out of tolerance in the conservative direction.
Thecauseoftheproblemwasthatthepiessureswitchcasehadnotbeenvented.Thepressure'switchcasewasventedandnofurtherproblemswerenoted.(FailureDate:11/26/96)
The cause of the problem was that the pressure switch case had not been vented.The pressure switch case was vented and no further problems were noted.(Failure Date: 11/26/96)MS-V-165 C During testing efforts while at power operation, it was noted that Main Steam (MS)System Intercept Valve MS-V-165C would not re-open when a test button was released.The cause of the problem was attributed to poor manufacturing practices resulting in particu1ates in the assembly.The particulates caused binding in the solenoid.The air solenoid valve was replaced.(Failure Date: 09/15/96)MS-V-165 C h During power bperation, it,was again noted that Main Steam (MS)System Intercept Valve MS-V-165C would not re-open during testing.The cause of the problem was attributed to either particulate contamination or problems with the sealing o-rings.The air solenoid and o-rings internal to the valve were replaced.No further problems were noted.(Failure Date: 11/09/96)MS-V-37K During the annual maintenance and refueling outage, it was noted that Main Steam (MS)System Valve MS-V-37K would not properly return to the full-closed position during vacuum breaker operability testing.The cause of the problem was attributed to foreign material buildup (hardened lubricant) at the hinge area which resulted in valve binding.The material buildup was filed down and no further problems were noted.(Failure Date: 05/03/96)MS-V-37V During the annual maintenance and refueling outage, it was noted that Main Steam (MS)System Valve MS-V-37V would not pr'operly, return to the full-closed position during vacuum breaker operability testing.The cause of the problem was attributed to foreign material buildup (hardened lubricant) at the hinge area which resulted.in valve binding.=.36 e
Duringpoweroperation, itwasdiscovered thatthesetpointforMainSteam(MS)SystemPressureSwitchMS-PS-47B wasoutoftolerance intheconservative direction.
The material buildup was filed down and no further problems were noted (Failure Date: 05/03/96)~RCIC-MO-110 During the annual maintenance and refueling outage, the yoke-to-valve collar for Reactor Core Isolation Cooling (RCIC)System Valve Motor Operator RCIC-MO-110 was found'o be loose and the operator could be rotated by hand.The cause of the problem was attributed to vibration.
Thecauseoftheproblemwasthatthepressureswitchcasehadnotbeenvented.Thepressureswitchcasewasventedandnofurtherproblemswerenoted.(FailureDate:~11/26/96)
The yoke was torqued to 110 ft-lbs and no further problems were noted.(Failure Date: 06/02/96)RCIC-V-66 During local leak rate testing in the annual maintenance and refueling outage, leakage in excess of allowable limits was discovered for Reactor Core Isolation Cooling (RCIC)System Valve RCIC-V-66.
MS-PS-47C Duringpoweroperation, itwasdiscovered thatthesetpointforMainSteam(MS)SystemPressureSwitchMS-PS-47C wasoutoftolerance in=theconservative direction.
The cause of the problem was attributed to a loose packing follower and an eroded shaft and carbon bushing due to normal aging and abnormal wear during usage.The shaft, bushing and packing set were replaced.No further problems were noted.(Failure Date 04/16/96)RFW-DT-1B During the annual maintenance and refueling outage, it was discovered that the inboard bearing for Reactor Feedwater (RPV)System Turbine RFW-DT-1B prematurely failed.The cause"of the problem was indeterminate.
Thecauseofthe.problemwasthatthepressureswitchcasehadnotbeenvented.Thepressureswitchcasewasventedandnofurtherproblemswerenoted.:(Failure Date:11/26/96)
New bearing pads and housing were installed and no further problems were noted.(Failure Date: 04/27/96)RFW-FR-607 During power operation, it was noted that a pen would stick on Reactor Feedwater (RFW)System Flow Recorder RFW-FR-607 when either increasing or decreasing flow.The cause was isolated problems with the rotor assembly.The pen slide bar was cleaned and the rotor..assembly replaced.No further problems were noted.-(Failure Date: 09/11/96).37 RFW-LS-624B During power operation, a Reactor Pressure Vessel Level-8 trip signal was received from Reactor Feedwater (RFW)System Level Switch RFW-LS-624B.
MS-PS-47D Duringpoweroperation, itwasdiscovered thatthesetpointforMainSteam(MS)SystemPressureSwitchMS-PS-47D wasoutoftolerance intheconservative direction.
The signal was received concurrent with a Station Battery Bl-2 ground alarm.The cause of the problem was indeterminate.
Thecauseoftheproblemwasthatthepressureswitchcasehadnotbeenvented.Thepressureswitchcasewasventedandnofurtherproblemswerenoted.(FailureDate:11/26/96)
The level switch was replaced and no further problems were noted.(Failure Date: 07/08/96)RHR-DPIS-12A During surveillance testing while at power operation, it was noted that Residual Heat Removal (RHR)System Differential Pressure Switch RHR-DPIS-12A could not be properly calibrated.
MS-V-165CDuringtestingeffortswhileatpoweroperation, itwasnotedthatMainSteam(MS)SystemIntercept ValveMS-V-165C wouldnotre-openwhenatestbuttonwasreleased.
The cause of the problem was.attributed to normal aging and usage..The pressure switch was replaced and no further problems were noted.(Failure Date: 08/22/96)RHR-P-3 During power operation, Residual Heat Removal (RHR)System Water Leg Pump RHR-P-3 tripped on electrical thermal overload.The cause of the thermal overload trip was due to a failure of the pump thrust bearing.The vibration-induced fatigue failure of the bearing was due to inadequate design and service application.
Thecauseoftheproblemwasattributed topoormanufacturing practices resulting inparticu1ates intheassembly.
The pump bearings and shaft were replaced with components of an updated design.No further problems were noted.(Failure Date: 10/16/96)RHR-TRS-601 During power operation, it was observed that the display was gradually failing on Residual Heat Removal (RHR)System Temperature Recorder RHR-TRS-601.
Theparticulates causedbindinginthesolenoid.
The cause of the problem was attributed to normal aging and usage.A new display was installed and no further problems were noted.(Failure Date: 06/24/96)RPS-EPA-3E During surveillance testing while at Hot Standby, it was noted the Reactor Protection System (RPS)Electrical Protection Assembly RPS-EPA-3E could not be calibrated.
Theairsolenoidvalvewasreplaced.
The cause was isolated to a problem with the logic board.38 The logic board was replaced and no further problems were noted.(Failure Date: 03/07/96)~RPS-RLY-K16B During the annual maintenance and refueling outage, it was noted that Reactor Protection System (RPS)Relay RPS-RLY-K16B was in a degraded condition and failing.The cause of the problem was attributed to normal aging and usage.The relay was replaced and no further problems were noted.(Failure Date: 05/14/96)~RRC-PS-18A During testing while at power operation, it was noted that the as-found trip setpoint for Reactor Recirculation (RRC)System Pressure Switch RRC-PS-18A was well below the administrative limit and could not be restored to within the required tolerances.
(FailureDate:09/15/96)
The cause of the problem was indeterminate.
MS-V-165ChDuringpowerbperation, it,wasagainnotedthatMainSteam(MS)SystemIntercept ValveMS-V-165C wouldnotre-openduringtesting.Thecauseoftheproblemwasattributed toeitherparticulate contamination orproblemswiththesealingo-rings.Theairsolenoidando-ringsinternaltothevalvewerereplaced.
The pressure switch was replaced and no further problems were noted.(Failure Date: 08/15/96)e~SLC-LT-1 During power operation, it was observed that Standby Liquid Control (SLC)Level Transmitter SLC-LT-1 appeared to be providing erroneous indication of SLC tank level.The cause of the problem was due to a plugged sensing line (bubbler tube)which resulted in air backpressure influencing the output of the level transmitter.
Nofurtherproblemswerenoted.(FailureDate:11/09/96)
The bubbler tube was rodded out and the transmitter was returned to service.No further problems were noted.(Failure Date: 10/06/96)~SLC-TS-3 During surveillance testing while at 58 percent, power, it was noted that Standby Liquid Control (SLC)System Temperature Switch SLC-TS-3 could not be calibrated.
MS-V-37KDuringtheannualmaintenance andrefueling outage,itwasnotedthatMainSteam(MS)SystemValveMS-V-37Kwouldnotproperlyreturntothefull-closed positionduringvacuumbreakeroperability testing.Thecauseoftheproblemwasattributed toforeignmaterialbuildup(hardened lubricant) atthehingeareawhichresultedinvalvebinding.Thematerialbuildupwasfileddownandnofurtherproblemswerenoted.(FailureDate:05/03/96)
The cause of the problem was indeterminate.
MS-V-37VDuringtheannualmaintenance andrefueling outage,itwasnotedthatMainSteam(MS)SystemValveMS-V-37Vwouldnotpr'operly, returntothefull-closed positionduringvacuumbreakeroperability testing.Thecauseoftheproblemwasattributed toforeignmaterialbuildup(hardened lubricant) atthehingeareawhichresulted.
The temperature switch was-replaced and no further problems were noted.(Failure Date: 02/04/96)I~~39 2.6 Fuel Performance This section contains information relative to fuel integrity.
invalvebinding.=.36 e
This input is provided solely for informational purposes and ease of reference.
Thematerialbuildupwasfileddownandnofurtherproblemswerenoted(FailureDate:05/03/96)
There were no indications of failed fuel during 1996.Regulatory Guide 1.16, Section C.l.b.(4), only requires reporting where, based on examination, there are indications of failed fuel.Bachground During 1995 the Supply System modified a WNP-2 FSAR commitment pertaining to surveillance of post-irradiated fuel.As part of our routine fuel inspection program that was described in the WNP-2 FSAR, a visual examination was to be performed on five to ten percent of the highest burnup assemblies of the discharged fuel after each refueling.
~RCIC-MO-110 Duringtheannualmaintenance andrefueling outage,theyoke-to-valve collarforReactorCoreIsolation Cooling(RCIC)SystemValveMotorOperatorRCIC-MO-110 wasfound'obelooseandtheoperatorcouldberotatedbyhand.Thecauseoftheproblemwasattributed tovibration.
-The visual examination was for the detection of indications of generic gross cladding defects or anomalies that may have occurred during operation.
Theyokewastorquedto110ft-lbsandnofurtherproblemswerenoted.(FailureDate:06/02/96)
This commitment was accepted by the NRC in the WNP-2 Safety Evaluation Report, as adequately addressing the issue of post-irradiation surveillance.
RCIC-V-66 Duringlocalleakratetestingintheannualmaintenance andrefueling outage,leakageinexcessofallowable limitswasdiscovered forReactorCoreIsolation Cooling(RCIC)SystemValveRCIC-V-66.
As an alternate approach, the Supply System evaluated post-irradiation fuel inspection activities and determined that it would be acceptable to perform visual inspection only on discharged fuel where there was indication of either actual or suspected gross cladding defects or anomalies.
Thecauseoftheproblemwasattributed toaloosepackingfollowerandanerodedshaftandcarbonbushingduetonormalagingandabnormalwearduringusage.Theshaft,bushingandpackingsetwerereplaced.
Examples of such indications include increased Offgas System activity and negative impacts on water chemistry paiameters.
Nofurtherproblemswerenoted.(FailureDate04/16/96)
This change to the post-irradiation surveillance program was incorporated, into Amendment 50 (August 1995)to the WNP-2 FSAR.1996 Results Based.on plant operational indicators, there was-no evidence of fuel performance problems'during Cycle 11.Accordingly, a visual inspection of the discharged fuel was determined to be unnecessary.
RFW-DT-1B Duringtheannualmaintenance andrefueling outage,itwasdiscovered thattheinboardbearingforReactorFeedwater (RPV)SystemTurbineRFW-DT-1B prematurely failed.Thecause"oftheproblemwasindeterminate.
40 This section contains summaries of the Safety Evaluations (SE)completed for activities implemented during 1996 and is included pursuant to 10CFR50.59.
Newbearingpadsandhousingwereinstalled andnofurtherproblemswerenoted.(FailureDate:04/27/96)
Federal Regulation 10CFR50.59 and Supply System Operating License NPF-21 allow changes to be made to the facility and procedures as described in the safety analysis report, and tests or experiments to be conducted which are not described in the safety analysis report without prior Nuclear Regulatory Commission approval, unless the proposed change, test or experiment involves a change in the technical specifications incorporated in the license or an unreviewed safety question.A proposed change, test or experiment is deemed to involve an unreviewed safety question if 1)the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased, or 2)a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be created, or 3)the margin of safety as defined in the basis for any technical specification is reduced.Each change summarized in the following sections was evaluated and determined to neither represent an unreviewed safety question nor require a change to the WNP-2 Technical~~~~~~~~~~~~Specifications.
RFW-FR-607 Duringpoweroperation, itwasnotedthatapenwouldstickonReactorFeedwater (RFW)SystemFlowRecorderRFW-FR-607 wheneitherincreasing ordecreasing flow.Thecausewasisolatedproblemswiththerotorassembly.
~g In certain instances, a single safety.evaluation was used for several implementing activities.
Thepenslidebarwascleanedandtherotor..assembly replaced.
This is allowed by procedure only where an existing evaluation adequately covers the specific change being considered.
Nofurtherproblemswerenoted.-(FailureDate:09/11/96)
If*the activity extends beyond the plant mode bounds, then a separate evaluation is required.A separate evaluation is also required if out-of-service equipment, equipment lineups, modifications or temporary alterations are in place that invalidate the existing evaluation.
.37 RFW-LS-624B Duringpoweroperation, aReactorPressureVesselLevel-8tripsignalwasreceivedfromReactorFeedwater (RFW)SystemLevelSwitchRFW-LS-624B.
41 2.7.1 Plant Modifications The section contains information pertaining to implemented Plant Modification Records (PMRs)and is included pursuant to 10CFR50.59.
Thesignalwasreceivedconcurrent withaStationBatteryBl-2groundalarm.Thecauseoftheproblemwasindeterminate.
~PNIR 864525-7 (SE 95-084)This PMR provided for snubber optimization of Main Steam System, Loop C, inside the primary containment drywell and containment exhaust purge bypass piping in the reactor building.This modification involved the removal and subsequent replacement of snubbers with rigid struts.It was concluded from the safety evaluation that the affected piping systems, components and supports were reanalyzed and remain qualified to applicable ASME Code and WNP-2 design basis requirements.
Thelevelswitchwasreplacedandnofurtherproblemswerenoted.(FailureDate:07/08/96)
Pressure boundary integrity of the piping systems and primary containment are maintained and engineered safety features used in mitigating transients will remain operable.The only possible accidents'are those associated with reactor pressure boundary and containment isolation.
RHR-DPIS-12A Duringsurveillance testingwhileatpoweroperation, itwasnotedthatResidualHeatRemoval(RHR)SystemDifferential PressureSwitchRHR-DPIS-12A couldnotbeproperlycalibrated.
Since the piping and component analyses meet all design requirements and no new pipe breaks are created in main steam piping, then the pressure boundary is maintained.
Thecauseoftheproblemwas.attributed tonormalagingandusage..Thepressureswitchwasreplacedandnofurtherproblemswerenoted.(FailureDate:08/22/96)
The containment exhaust purge piping is exempt from postulated pipe rupture due to the ASME exemption criteria of being less than or equal to one-inch in diameter.All equipment will remain functional to maintain containment isolation.
RHR-P-3Duringpoweroperation, ResidualHeatRemoval(RHR)SystemWaterLegPumpRHR-P-3trippedonelectrical thermaloverload.
PMR 87-0244-6 (SE 93-200)This PMR provided modification of the Reactor Recirculation (RRC)System by installing Adjustable Speed Drives (ASD)to control recirculation pump speed.This modification also provided direction for ASD interconnections to the Main Control Room.The ASD System is a functional replacement for a hydraulically-controlled flow control valve arrangement.
Thecauseofthethermaloverloadtripwasduetoafailureofthepumpthrustbearing.Thevibration-induced fatiguefailureofthebearingwasduetoinadequate designandserviceapplication.
It was concluded from the safety evaluation that the RRC System has no active safety function.Its primary relation to the design analyses is as an initiator of events.This modification does not alter assumptions pertaining to RRC pump response during transients or accidents.
Thepumpbearingsandshaftwerereplacedwithcomponents ofanupdateddesign.Nofurtherproblemswerenoted.(FailureDate:10/16/96)
The coast-down characteristics are similar to all.previous analyses of recirculation system events.A 42 0  
RHR-TRS-601 Duringpoweroperation, itwasobservedthatthedisplaywasgradually failingonResidualHeatRemoval(RHR)SystemTemperature RecorderRHR-TRS-601.
'I The design of the ASD interlocks and limiters will prevent operation of the system outside of acceptable operating parameters.
Thecauseoftheproblemwasattributed tonormalagingandusage.Anewdisplaywasinstalled andnofurtherproblemswerenoted.(FailureDate:06/24/96)
Installation activities would occur during the refueling outage.Any potential failures that could occur during post-modification testing are bounded by previous analyses.~PMR 87-0282-0 (SE 95-098)This PMR provided for the installation of an additional steam tunnel fan/coil air cooling unit to provide for improved peak summer load performance and as backup protection for the existing units.It was concluded from the safety evaluation that the seismically-mounted backup unit provides no safety function.The unit would be installed to meet applicable design requirements preserving the important to safety function of equipment located in the vicinity.All associated mechanical and electrical components:
RPS-EPA-3E Duringsurveillance testingwhileatHotStandby,itwasnotedtheReactorProtection System(RPS)Electrical Protection AssemblyRPS-EPA-3E couldnotbecalibrated.
would also be installed to appropriate standards commensurate with this activity to ensure that no important to safety functions are affected.No previously evaluate'd transients or operator post-accident responses are adversely impacted by the change.r PMR 89-0299-6 (SE 95-100)This.PMR provided for the replacement of flow transmitters in the Containment Atmosphere Control (CAC)System with units of an improved design.It was concluded from the safety evaluation that the five new replacement transmitters would be procured to Quality Class 1 requirements and installed such that the original design function will be maintained.
Thecausewasisolatedtoaproblemwiththelogicboard.38 Thelogicboardwasreplacedandnofurtherproblemswerenoted.(FailureDate:03/07/96)
The new transmitters do not change the function or configuration of the CAC System in response to a design basis accident.All measurement ranges, indications and recording and alarm functions remain the same as prior to the change.PMR 91-0438-0 (SE 94-209)This PMR provided for the replacement of Reactor Feedwater (RFW)analog control system components with a digital control system upgrade.This change was made due to'shortcomings with the.existing system, which had significant impact on plant performance.
~RPS-RLY-K16B Duringtheannualmaintenance andrefueling outage,itwasnotedthatReactorProtection System(RPS)RelayRPS-RLY-K16B wasinadegradedcondition andfailing.Thecauseoftheproblemwasattributed tonormalagingandusage.Therelaywasreplacedandnofurtherproblemswerenoted.(FailureDate:05/14/96)
The RFW Level Control System controls the discharge of the RFW pumps into the reactor pressure:vessel to maintain.leyel within predetermined limits.~~~~43 It was concluded from the safety evaluation that the modification to the RFW Level Control System and associated Turbine Governor Control System would not increase the probability of a previously evaluated transient or impact the outage safety'plan.
~RRC-PS-18A Duringtestingwhileatpoweroperation, itwasnotedthattheas-foundtripsetpointforReactorRecirculation (RRC)SystemPressureSwitchRRC-PS-18A waswellbelowtheadministrative limitandcouldnotberestoredtowithintherequiredtolerances.
The RFW System is a non-safety related system that is used to control reactor vessel water~level during normal"operation.
Thecauseoftheproblemwasindeterminate.
The system is.physically isolated when the core is flooded during a refueling outage.The level trips and plausible accidents are bounded by the automatic response of the Reactor Protection System.Implementation of the new level control system reduces operator burden by providing direct and consolidated control of turbine speed.and enabling earlier introduction of the feedwater pumps during startup valve/feedwater pump crossover.
Thepressureswitchwasreplacedandnofurtherproblemswerenoted.(FailureDate:08/15/96) e~SLC-LT-1Duringpoweroperation, itwasobservedthatStandbyLiquidControl(SLC)LevelTransmitter SLC-LT-1appearedtobeproviding erroneous indication ofSLCtanklevel.Thecauseoftheproblemwasduetoapluggedsensingline(bubblertube)whichresultedinairbackpressure influencing theoutputoftheleveltransmitter.
The change does not result in the possibility of increased challenges to important to safety systems.The upset range level indicator or feedwater flow indicators mentioned in Regulatory Guide 1.97 are not changed by this modification.
Thebubblertubewasroddedoutandthetransmitter wasreturnedtoservice.Nofurtherproblemswerenoted.(FailureDate:10/06/96)
~PNIR 5Q-0085-0 (SE 96-002)This PMR provided for modification of Containment Atmosphere Control (CAC)System push-button"valve test" switches CAC-RMS-PBA and CAC-RMS-PBB on the hydrogen recombiner control panel.The push-buttons were replaced with maintained-contact control keylock switches.This change prevents the bypassing of the pressure suppression function of the drywell downcomers in the event of single test switch failure or inadvertent depressing of the push-button.
~SLC-TS-3Duringsurveillance testingwhileat58percent,power,itwasnotedthatStandbyLiquidControl(SLC)SystemTemperature SwitchSLC-TS-3couldnotbecalibrated.
This modification also corrected an operator"work-around" by elimination of the need to install a jumper around the CAC"valve.test" switch during valve testing, rather than depressing the push-button for extended periods.It was concluded from the safety evaluation that the new switches would not introduce~any new failure modes that could increase the consequences of previously evaluated transients.
Thecauseoftheproblemwasindeterminate.
The keylock feature was added to prevent inadvertent actuation during normal plant operation.
Thetemperature switchwas-replaced andnofurtherproblemswerenoted.(FailureDate:02/04/96)
There is no'impact on design basis bypass leakage rates.The addition of two switches in series serves as an additional bariier to single failure of any one switch.The replacement device serves an equivalent function, with improved performance characteristics.
I~~39 2.6FuelPerformance Thissectioncontainsinformation relativetofuelintegrity.
Thisinputisprovidedsolelyforinformational purposesandeaseofreference.
Therewerenoindications offailedfuelduring1996.Regulatory Guide1.16,SectionC.l.b.(4),
onlyrequiresreporting where,basedonexamination, thereareindications offailedfuel.Bachground During1995theSupplySystemmodifiedaWNP-2FSARcommitment pertaining tosurveillance ofpost-irradiated fuel.Aspartofourroutinefuelinspection programthatwasdescribed intheWNP-2FSAR,avisualexamination wastobeperformed onfivetotenpercentofthehighestburnupassemblies ofthedischarged fuelaftereachrefueling.
-Thevisualexamination wasforthedetection ofindications ofgenericgrosscladdingdefectsoranomalies thatmayhaveoccurredduringoperation.
Thiscommitment wasacceptedbytheNRCintheWNP-2SafetyEvaluation Report,asadequately addressing theissueofpost-irradiation surveillance.
Asanalternate
: approach, theSupplySystemevaluated post-irradiation fuelinspection activities anddetermined thatitwouldbeacceptable toperformvisualinspection onlyondischarged fuelwheretherewasindication ofeitheractualorsuspected grosscladdingdefectsoranomalies.
Examplesofsuchindications includeincreased OffgasSystemactivityandnegativeimpactsonwaterchemistry paiameters.
Thischangetothepost-irradiation surveillance programwasincorporated, intoAmendment 50(August1995)totheWNP-2FSAR.1996ResultsBased.onplantoperational indicators, therewas-noevidenceoffuelperformance problems'duringCycle11.Accordingly, avisualinspection ofthedischarged fuelwasdetermined tobeunnecessary.
40 Thissectioncontainssummaries oftheSafetyEvaluations (SE)completed foractivities implemented during1996andisincludedpursuantto10CFR50.59.
FederalRegulation 10CFR50.59 andSupplySystemOperating LicenseNPF-21allowchangestobemadetothefacilityandprocedures asdescribed inthesafetyanalysisreport,andtestsorexperiments tobeconducted whicharenotdescribed inthesafetyanalysisreportwithoutpriorNuclearRegulatory Commission
: approval, unlesstheproposedchange,testorexperiment involvesachangeinthetechnical specifications incorporated inthelicenseoranunreviewed safetyquestion.
Aproposedchange,testorexperiment isdeemedtoinvolveanunreviewed safetyquestionif1)theprobability ofoccurrence ortheconsequences ofanaccidentormalfunction ofequipment important tosafetypreviously evaluated inthesafetyanalysisreportmaybeincreased, or2)apossibility foranaccidentormalfunction ofadifferent typethananyevaluated previously inthesafetyanalysisreportmaybecreated,or3)themarginofsafetyasdefinedinthebasisforanytechnical specification isreduced.Eachchangesummarized inthefollowing sectionswasevaluated anddetermined toneitherrepresent anunreviewed safetyquestionnorrequireachangetotheWNP-2Technical
~~~~~~~~~~~~Specifications.
~gIncertaininstances, asinglesafety.evaluation wasusedforseveralimplementing activities.
Thisisallowedbyprocedure onlywhereanexistingevaluation adequately coversthespecificchangebeingconsidered.
If*theactivityextendsbeyondtheplantmodebounds,thenaseparateevaluation isrequired.
Aseparateevaluation isalsorequiredifout-of-service equipment, equipment lineups,modifications ortemporary alterations areinplacethatinvalidate theexistingevaluation.
41 2.7.1PlantModifications Thesectioncontainsinformation pertaining toimplemented PlantModification Records(PMRs)andisincludedpursuantto10CFR50.59.
~PNIR864525-7(SE95-084)ThisPMRprovidedforsnubberoptimization ofMainSteamSystem,LoopC,insidetheprimarycontainment drywellandcontainment exhaustpurgebypasspipinginthereactorbuilding.
Thismodification involvedtheremovalandsubsequent replacement ofsnubberswithrigidstruts.Itwasconcluded fromthesafetyevaluation thattheaffectedpipingsystems,components andsupportswerereanalyzed andremainqualified toapplicable ASMECodeandWNP-2designbasisrequirements.
Pressureboundaryintegrity ofthepipingsystemsandprimarycontainment aremaintained andengineered safetyfeaturesusedinmitigating transients willremainoperable.
Theonlypossibleaccidents'are thoseassociated withreactorpressureboundaryandcontainment isolation.
Sincethepipingandcomponent analysesmeetalldesignrequirements andnonewpipebreaksarecreatedinmainsteampiping,thenthepressureboundaryismaintained.
Thecontainment exhaustpurgepipingisexemptfrompostulated piperuptureduetotheASMEexemption criteriaofbeinglessthanorequaltoone-inchindiameter.
Allequipment willremainfunctional tomaintaincontainment isolation.
PMR87-0244-6 (SE93-200)ThisPMRprovidedmodification oftheReactorRecirculation (RRC)Systembyinstalling Adjustable SpeedDrives(ASD)tocontrolrecirculation pumpspeed.Thismodification alsoprovideddirection forASDinterconnections totheMainControlRoom.TheASDSystemisafunctional replacement forahydraulically-controlled flowcontrolvalvearrangement.
Itwasconcluded fromthesafetyevaluation thattheRRCSystemhasnoactivesafetyfunction.
Itsprimaryrelationtothedesignanalysesisasaninitiator ofevents.Thismodification doesnotalterassumptions pertaining toRRCpumpresponseduringtransients oraccidents.
Thecoast-down characteristics aresimilartoall.previous analysesofrecirculation systemevents.A42 0  
'IThedesignoftheASDinterlocks andlimiterswillpreventoperation ofthesystemoutsideofacceptable operating parameters.
Installation activities wouldoccurduringtherefueling outage.Anypotential failuresthatcouldoccurduringpost-modification testingareboundedbypreviousanalyses.
~PMR87-0282-0 (SE95-098)ThisPMRprovidedfortheinstallation ofanadditional steamtunnelfan/coilaircoolingunittoprovideforimprovedpeaksummerloadperformance andasbackupprotection fortheexistingunits.Itwasconcluded fromthesafetyevaluation thattheseismically-mounted backupunitprovidesnosafetyfunction.
Theunitwouldbeinstalled tomeetapplicable designrequirements preserving theimportant tosafetyfunctionofequipment locatedinthevicinity.
Allassociated mechanical andelectrical components:
wouldalsobeinstalled toappropriate standards commensurate withthisactivitytoensurethatnoimportant tosafetyfunctions areaffected.
Nopreviously evaluate'd transients oroperatorpost-accident responses areadversely impactedbythechange.rPMR89-0299-6 (SE95-100)This.PMRprovidedforthereplacement offlowtransmitters intheContainment Atmosphere Control(CAC)Systemwithunitsofanimproveddesign.Itwasconcluded fromthesafetyevaluation thatthefivenewreplacement transmitters wouldbeprocuredtoQualityClass1requirements andinstalled suchthattheoriginaldesignfunctionwillbemaintained.
Thenewtransmitters donotchangethefunctionorconfiguration oftheCACSysteminresponsetoadesignbasisaccident.
Allmeasurement ranges,indications andrecording andalarmfunctions remainthesameaspriortothechange.PMR91-0438-0 (SE94-209)ThisPMRprovidedforthereplacement ofReactorFeedwater (RFW)analogcontrolsystemcomponents withadigitalcontrolsystemupgrade.Thischangewasmadedueto'shortcomings withthe.existingsystem,whichhadsignificant impactonplantperformance.
TheRFWLevelControlSystemcontrolsthedischarge oftheRFWpumpsintothereactorpressure:vessel tomaintain.leyel withinpredetermined limits.~~~~43 Itwasconcluded fromthesafetyevaluation thatthemodification totheRFWLevelControlSystemandassociated TurbineGovernorControlSystemwouldnotincreasetheprobability ofapreviously evaluated transient orimpacttheoutagesafety'plan.
TheRFWSystemisanon-safety relatedsystemthatisusedtocontrolreactorvesselwater~levelduringnormal"operation.
Thesystemis.physically isolatedwhenthecoreisfloodedduringarefueling outage.Theleveltripsandplausible accidents areboundedbytheautomatic responseoftheReactorProtection System.Implementation ofthenewlevelcontrolsystemreducesoperatorburdenbyproviding directandconsolidated controlofturbinespeed.andenablingearlierintroduction ofthefeedwater pumpsduringstartupvalve/feedwater pumpcrossover.
Thechangedoesnotresultinthepossibility ofincreased challenges toimportant tosafetysystems.Theupsetrangelevelindicator orfeedwater flowindicators mentioned inRegulatory Guide1.97arenotchangedbythismodification.
~PNIR5Q-0085-0 (SE96-002)ThisPMRprovidedformodification ofContainment Atmosphere Control(CAC)Systempush-button "valvetest"switchesCAC-RMS-PBA andCAC-RMS-PBB onthehydrogenrecombiner controlpanel.Thepush-buttons werereplacedwithmaintained-contact controlkeylockswitches.
Thischangepreventsthebypassing ofthepressuresuppression functionofthedrywelldowncomers intheeventofsingletestswitchfailureorinadvertent depressing ofthepush-button.
Thismodification alsocorrected anoperator"work-around" byelimination oftheneedtoinstallajumperaroundtheCAC"valve.test"switchduringvalvetesting,ratherthandepressing thepush-button forextendedperiods.Itwasconcluded fromthesafetyevaluation thatthenewswitcheswouldnotintroduce
~anynewfailuremodesthatcouldincreasetheconsequences ofpreviously evaluated transients.
Thekeylockfeaturewasaddedtopreventinadvertent actuation duringnormalplantoperation.
Thereisno'impact ondesignbasisbypassleakagerates.Theadditionoftwoswitchesinseriesservesasanadditional bariiertosinglefailureofanyoneswitch.Thereplacement deviceservesanequivalent
: function, withimprovedperformance characteristics.
k  
k  
~PMR92-0209(SE95-102)ThisPMRprovidedforinstallation ofJetPumpSensingLine(JPSL)mitigation supportassemblies onthesensinglinesofeachofthe20existingjetpumpdiffusers.
~PMR 92-0209 (SE 95-102)This PMR provided for installation of Jet Pump Sensing Line (JPSL)mitigation support assemblies on the sensing lines of each of the 20 existing jet pump diffusers.
FouroftheJPSLsupportswererequiredoneachofthesensinglines.Thepurposeofthismodification wastoreducetheresonantvibration responses oftheJPSLsbyshiftingthenaturalfrequencies ofthelineintoabandwhichwillnotcoincidewiththevanepassingfrequency associated withrecirculation pumpspeed.Itwasconcluded fromthesafetyevaluation thatthismodification improvesthesecurityoftheJPSLsandreducestheprobability ofsensinglinefailure.Themitigation clampshavebeenseismically analyzedtoensuretheywouldnotfailinamannerthatcoulddamagesafety-related structures intheeventofanearthquake.
Four of the JPSL supports were required on each of the sensing lines.The purpose of this modification was to reduce the resonant vibration responses of the JPSLs by shifting the natural frequencies of the line into a band which will not coincide with the vane passing frequency associated with recirculation pump speed.It was concluded from the safety evaluation that this modification improves the security of the JPSLs and reduces the probability of sensing line failure.The mitigation clamps have been seismically analyzed to ensure they would not fail in a manner that could damage safety-related structures in the event of an earthquake.
Basedontheresultsofstressanalysis, loosepartsanalysis, andmaterialcompatibility itwasdetermined thatthereisnocrediblefailuremodeassociated withtheclampassemblythatcouldimpactpreviously evaluated accidents.
Based on the results of stress analysis, loose parts analysis, and material compatibility it was determined that there is no credible failure mode associated with the clamp assembly that could impact previously evaluated accidents.
~PMR93-0049-0 (SE95-015)ThisPMRprovidedformodification ofthecontrolcircuitry forHighPressureCoreSpraySystem(HPCS)ValvesHPCS-V-10 andHPCS-V-11 bytheadditionoftime-delay onthedrop-outtimers.Thismodification willallowtrappedrotorfluxtodecayfollowing movementtoafullwpenpositionandpreventinadvertent circuitbreakertripping.
~PMR 93-0049-0 (SE 95-015)This PMR provided for modification of the control circuitry for High Pressure Core Spray System (HPCS)Valves HPCS-V-10 and HPCS-V-11 by the addition of time-delay on the drop-out timers.This modification will allow trapped rotor flux to decay following movement to a fullwpen position and prevent inadvertent circuit breaker tripping.It was concluded from the safety evaluation that the safety function of these valves would not be impacted by the change.The valves are normally closed, except during testing, and the passive component function (electrical integrity) is maintained with the new: relays.There would be no change in HPCS accident response time or support of secondary containment bypass leak rate.The added time delay simply prevents inadvertent circuit breaker tripping when the valves are immediately taken to the closed position when initially traveling in the open direction.
Itwasconcluded fromthesafetyevaluation thatthesafetyfunctionofthesevalveswouldnotbeimpactedbythechange.Thevalvesarenormallyclosed,exceptduringtesting,andthepassivecomponent function(electrical integrity) ismaintained withthenew:relays.TherewouldbenochangeinHPCSaccidentresponsetimeorsupportofsecondary containment bypassleakrate.Theaddedtimedelaysimplypreventsinadvertent circuitbreakertrippingwhenthevalvesareimmediately takentotheclosedpositionwheninitially traveling intheopendirection.
~PMR 93-0065-0 (SE 96-101)This PMR provided for deletion of the lead-lag function of Radwaste Building Chillers WCH-CR-51A and WCH-.CR-51B and modification of the control circuitry to allow the two chillers to run independently.
~PMR93-0065-0 (SE96-101)ThisPMRprovidedfordeletionofthelead-lagfunctionofRadwasteBuildingChillersWCH-CR-51A andWCH-.CR-51B andmodification ofthecontrolcircuitry toallowthetwochillerstorunindependently.
" This change will allow the chillers to be controlled independently from their own individual chilled water sensors;rather than from a common sensor.45  
"Thischangewillallowthechillerstobecontrolled independently fromtheirownindividual chilledwatersensors;ratherthanfromacommonsensor.45  


Itwasconcluded from'thesafetyevaluation thattheavailability ofthechillerswillnotbeaffectedbyremovalofthelead-lagfunctionfromthe.controlsystem.ThecoolingfunctionnormallyprovidedbythechillerswouldbeassumedbytheServiceWaterSystemuntilsuchtimethattheunitswerereturnedtoservice.Theaffectedequipment isnon-safety related,doesnothaveanaccidentmitigation
It was concluded from'the safety evaluation that the availability of the chillers will not be affected by removal of the lead-lag function from the.control system.The cooling function normally provided by the chillers would be assumed by the Service Water System until such time that the units were returned to service.The affected equipment is non-safety related, does not have an accident mitigation function, does not have an off-site dose reduction function and is not a credited system which supports equipment important to safety.~PMR 93-0157-2 (SE 95-097)This PMR provided for replacement of Reactor Building to Wetwell Vacuum Relief Valves CSP-V-S, CSP-V-6 and CSP-V-9.The valves were replaced with components of an improved design to more reliably meet allowable leakage requirements.
: function, doesnothaveanoff-sitedosereduction functionandisnotacreditedsystemwhichsupportsequipment important tosafety.~PMR93-0157-2 (SE95-097)ThisPMRprovidedforreplacement ofReactorBuildingtoWetwellVacuumReliefValvesCSP-V-S,CSP-V-6andCSP-V-9.Thevalveswerereplacedwithcomponents ofanimproveddesigntomorereliablymeetallowable leakagerequirements.
It was concluded from the safety evaluation that the safety function of these CSP valves is to prevent excessive vacuum from developing in primary containment from such cases as inadvertent containment spray actuation.
Itwasconcluded fromthesafetyevaluation thatthesafetyfunctionoftheseCSPvalvesistopreventexcessive vacuumfromdeveloping inprimarycontainment fromsuchcasesasinadvertent containment sprayactuation.
The new valves were procured and installed to Quality Class 1 and Seismic Category 1 standards.
Thenewvalveswereprocuredandinstalled toQualityClass1andSeismicCategory1standards.
There was no change in valve opening time, leak-tightness, quality and seismic requirements.
Therewasnochangeinvalveopeningtime,leak-tightness, qualityandseismicrequirements.
System interfaces were also unchanged.
Systeminterfaces werealsounchanged.
There were no changes from the original valve function, other than a seal design which will allow for a tighter seal.The ability to seal consistently when in a containment isolation mode would decrease the consequences of an accident.~PNIR 94-0057-0 (SE 94-074)This PMR provided for mechanically blochng Reactor Recirculation (RRC)System Flow Control Valves RRC-V-60A and RRC-V-60B in the full-open position and removal of the associated hydraulic system.This modification was performed in support of the installation of an Adjustable Speed Drive System on the RRC pump motors.It was concluded from the safety evaluation that this change would not have an adverse impact on the reactor coolant pressure boundary.Stress analyses performed on the RCC piping show that piping stresses will not be increased as a result of modifying the flow control valves.The final configuration of the modification would not introduce any new failure modes or operational transients.
Therewerenochangesfromtheoriginalvalvefunction, otherthanasealdesignwhichwillallowforatighterseal.Theabilitytosealconsistently wheninacontainment isolation modewoulddecreasetheconsequences ofanaccident.
Reactor protection trip delay time and pump/motor inertia would also not change.The.Adjustable Speed Drive System was designed to ensure that acceptable fuel thermal margins are maintained in the event of a reactor protection trip.46 PMR 94-0332-1 (SE'95-103)
~PNIR94-0057-0 (SE94-074)ThisPMRprovidedformechanically blochngReactorRecirculation (RRC)SystemFlowControlValvesRRC-V-60A andRRC-V-60B inthefull-open positionandremovaloftheassociated hydraulic system.Thismodification wasperformed insupportoftheinstallation ofanAdjustable SpeedDriveSystemontheRRCpumpmotors.Itwasconcluded fromthesafetyevaluation thatthischangewouldnothaveanadverseimpactonthereactorcoolantpressureboundary.
This PMR provided for the installation of a zinc injection system.The addition of depleted zinc reduces the buildup of Co-60 on primary piping and components.
Stressanalysesperformed ontheRCCpipingshowthatpipingstresseswillnotbeincreased asaresultofmodifying theflowcontrolvalves.Thefinalconfiguration ofthemodification wouldnotintroduce anynewfailuremodesoroperational transients.
The modification consisted of the installation of'a vendor-supplied skid for the injection of dissolved zinc oxide into the Reactor Feedwater~V)System.It was concluded from the safety evaluation that zinc levels of less than or equal to 65 ppb would not have an adverse affect on the intergrannular stress corrosion cracking characteristics of primary system components.
Reactorprotection tripdelaytimeandpump/motor inertiawouldalsonotchange.The.Adjustable SpeedDriveSystemwasdesignedtoensurethatacceptable fuelthermalmarginsaremaintained intheeventofareactorprotection trip.46 PMR94-0332-1 (SE'95-103)
Based on information received from the vendor, it was determined that this modification would not impact'RFW pump seals, RFW nozzles or RFW flow measurement instrumentation.
ThisPMRprovidedfortheinstallation ofazincinjection system.TheadditionofdepletedzincreducesthebuildupofCo-60onprimarypipingandcomponents.
There would also be no"detrimental impact to the fuel assemblies.
Themodification consisted oftheinstallation of'avendor-supplied skidfortheinjection ofdissolved zincoxideintotheReactorFeedwater
Installation and testing of the skid would not interfere with plant operations.
~V)System.Itwasconcluded fromthesafetyevaluation thatzinclevelsoflessthanorequalto65ppbwouldnothaveanadverseaffectontheintergrannular stresscorrosion crackingcharacteristics ofprimarysystemcomponents.
The skid is also isolatable from plant components by the use of double isolation valves.PMR 94-0346-0 (SE 95-066)This PMR provided for the rework and modification of fire-rated penetration seals to support current fire tests and restore the penetrations to an acceptable configuration.
Basedoninformation receivedfromthevendor,itwasdetermined thatthismodification wouldnotimpact'RFW pumpseals,RFWnozzlesorRFWflowmeasurement instrumentation.
This effort was associated with an ongoing penetration seal upgrade project.The upgrade project was implemented based on the results of an analysis which revealed that not all of the installed configurations are supported by current fire tests or acceptable evaluations.
Therewouldalsobeno"detrimental impacttothefuelassemblies.
It was concluded from the safety evaluation that penetration seal design variations have no impact on design basis accidents, only events.The design of the seals is int'ended to mitigate the effects of fires and, in some installations, other design basis events.The changes made by this modification have no impact on the ability of safety systems to perform during accident conditions, nor do they increase challenges to safety systems.The fire barriers and seals within the scope of this modification are currently declared, inoperable and an hourly fire tour has been implemented as a compensatory action.The fire tours will not be removed until the seals and barriers have been declared operable.During the restoration efforts, required safe shutdown systems and components will be maintained in accordance with licensing basis documents.
Installation andtestingoftheskidwouldnotinterfere withplantoperations.
Theskidisalsoisolatable fromplantcomponents bytheuseofdoubleisolation valves.PMR94-0346-0 (SE95-066)ThisPMRprovidedforthereworkandmodification offire-rated penetration sealstosupportcurrentfiretestsandrestorethepenetrations toanacceptable configuration.
Thiseffortwasassociated withanongoingpenetration sealupgradeproject.Theupgradeprojectwasimplemented basedontheresultsofananalysiswhichrevealedthatnotalloftheinstalled configurations aresupported bycurrentfiretestsoracceptable evaluations.
Itwasconcluded fromthesafetyevaluation thatpenetration sealdesignvariations havenoimpactondesignbasisaccidents, onlyevents.Thedesignofthesealsisint'ended tomitigatetheeffectsoffiresand,insomeinstallations, otherdesignbasisevents.Thechangesmadebythismodification havenoimpactontheabilityofsafetysystemstoperformduringaccidentconditions, nordotheyincreasechallenges tosafetysystems.Thefirebarriersandsealswithinthescopeofthismodification arecurrently
: declared, inoperable andanhourlyfiretourhasbeenimplemented asacompensatory action.Thefiretourswillnotberemoveduntilthesealsandbarriershavebeendeclaredoperable.
Duringtherestoration efforts,requiredsafeshutdownsystemsandcomponents willbemaintained inaccordance withlicensing basisdocuments.
47  
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PMR94-0364-0 (SE96-006)'ThisPMRprovidedforinstallation ofapermanent curtainshielding supportstructure aroundaportionofReactorRecirculation (RRC)System,Loop"A"pipingforALARAconsiderations.
PMR 94-0364-0 (SE 96-006)'This PMR provided for installation of a permanent curtain shielding support structure around a portion of Reactor Recirculation (RRC)System, Loop"A" piping for ALARA considerations.
Thepermanent structure eliminated theneedtoassembletube-lock scaffolding andinstallshielding duringeveryoutage.Itwasconcluded fromthesafetyevaluation thatinstallation oftheshielding andtheshielding supportsystemwouldnotaffectanysystem,structure orcomponent.
The permanent structure eliminated the need to assemble tube-lock scaffolding and install shielding during every outage.It was concluded from the safety evaluation that installation of the shielding and the shielding support system would not affect any system, structure or component.
thatmitigates theconsequences ofadesignbasisaccident.
that mitigates the consequences of a design basis accident.The shielding support structure meets Seismic Category 1M requirements to prevent adverse II/I interactions with important to safety systems, structures and components.
Theshielding supportstructure meetsSeismicCategory1Mrequirements topreventadverseII/Iinteractions withimportant tosafetysystems,structures andcomponents.
3 The shielding and support structure was also designed to withstand all applicable loads, including pipe breaks and missiles.The shielding, which is located in primary containment, does not restrict access to vital areas or otherwise impede actions to.mitigate the consequences of design basis accidents.
3Theshielding andsupportstructure wasalsodesignedtowithstand allapplicable loads,including pipebreaksandmissiles.
PMR 94-0364-1 (SE 96-010)This PMR provided for installation of a permanent curtain shielding support structure around a portion of Reactor Water Cleanup (RWCU)piping for ALARA considerations.
Theshielding, whichislocatedinprimarycontainment, doesnotrestrictaccesstovitalareasorotherwise impedeactionsto.mitigatetheconsequences ofdesignbasisaccidents.
The permanent structure eliminated the need to assemble tube-lock scaffolding and instaH shielding during every outage.It was concluded from the safety evaluation that installation of the shielding and the shielding support system would not affect any system, structure or component that mitigates the consequences of a design basis accident.The shielding support structure meets Seismic Category 1M requirements to prevent adverse II/I interactions with important to safety systems, structures and components.
PMR94-0364-1 (SE96-010)ThisPMRprovidedforinstallation ofapermanent curtainshielding supportstructure aroundaportionofReactorWaterCleanup(RWCU)pipingforALARAconsiderations.
The shielding and support structure was also designed to withstand all applicable loads, including pipe breaks and missiles.The shielding, which is located in primary containment, does not restrict access to vital areas or otherwise impede actions to mitigate the consequences of design basis accidents.
Thepermanent structure eliminated theneedtoassembletube-lock scaffolding andinstaHshielding duringeveryoutage.Itwasconcluded fromthesafetyevaluation thatinstallation oftheshielding andtheshielding supportsystemwouldnotaffectanysystem,structure orcomponent thatmitigates theconsequences ofadesignbasisaccident.
~PMR 95-0174-0 (SE 95-099)This PMR provided for the installation of an iron injection system.The addition of iron oxalate reduces the buildup" of'Co;.60 on.primary piping and components.
Theshielding supportstructure meetsSeismicCategory1Mrequirements topreventadverseII/Iinteractions withimportant tosafetysystems,structures andcomponents.
The modification
Theshielding andsupportstructure wasalsodesignedtowithstand allapplicable loads,including pipebreaksandmissiles.
'consisted of a permanent stainless steel injection point that was welded to the 36-inch condensate booster pump, suction, line.48 0
Theshielding, whichislocatedinprimarycontainment, doesnotrestrictaccesstovitalareasorotherwise impedeactionstomitigatetheconsequences ofdesignbasisaccidents.
It was concluded from the safety evaluation that, although iron concentration will be increased in the reactor feedwater, the level would still be well below the design basis value of 5.0 ppb.Increasing the iron concentration from 0.1 ppb to 0.5 ppb would not adversely impact any safety-related structure, system or component.
~PMR95-0174-0 (SE95-099)ThisPMRprovidedfortheinstallation ofanironinjection system.Theadditionofironoxalatereducesthebuildup"of'Co;.60on.primarypipingandcomponents.
It was determined that this modification would not impact the performance of reactor feedwater heaters or flow nozzles.The new piping that is installed will be compatible with the existing piping design pressures and temperatures.
Themodification
The increase in iron concentration will also not affect the integrity of the fuel cladding.The cladding would not become embrittled or experience any wall thinning.PMR 95-0236-0 (SE 95-092)This PMR provided for the replacement of eight top-entry Local Power Range Monitor (LPRM)detector assemblies with bottom-entry models of a better design.This modification was made to provide for improved efficiencies during refueling outages.It was concluded from the safety evaluation that the new LPRM detectors meet or exceed the design requirements of the original detectors.
'consisted ofapermanent stainless steelinjection pointthatwasweldedtothe36-inchcondensate boosterpump,suction,line.48 0
All of the replacement compone'nts, including cable and connectors, are qualified for the environment in which they would be.installed.
Itwasconcluded fromthesafetyevaluation that,althoughironconcentration willbeincreased inthereactorfeedwater, thelevelwouldstillbewellbelowthedesignbasisvalueof5.0ppb.Increasing theironconcentration from0.1ppbto0.5ppbwouldnotadversely impactanysafety-related structure, systemorcomponent.
No activities are included which would impact systems arid result in challenges to safety-related equipment.
Itwasdetermined thatthismodification wouldnotimpacttheperformance ofreactorfeedwater heatersorflownozzles.Thenewpipingthatisinstalled willbecompatible withtheexistingpipingdesignpressures andtemperatures.
Following changes to the processing software to compensate for the different sensitivity of the new LPRM detectors, the.function will be identical to the existing system.1 PMR 96-0043-0 (SE 96-015)This PMR provided for the modification to Radwaste Building Release Duct Radiation Monitor Sample Racks WEA-SR-25 and WEA-SR-25A to prevent overheating of the system blower.This change was made to increase the reliability of Sample Rack WEA-SR-25 by reducing flow restrictions to lower exhaust air sample blower operating temperature.
Theincreaseinironconcentration willalsonotaffecttheintegrity ofthefuelcladding.
The blower had been operating at a higher than design temperature and required periodic replacement due to premature failure.Loss of the blower would result in the sample racks becoming inoperable.
Thecladdingwouldnotbecomeembrittled orexperience anywallthinning.
It was concluded from the safety evaluation that this modification would not alter safety-related system response to an accident condition.
PMR95-0236-0 (SE95-092)ThisPMRprovidedforthereplacement ofeighttop-entry LocalPowerRangeMonitor(LPRM)detectorassemblies withbottom-entry modelsofabetterdesign.Thismodification wasmadetoprovideforimprovedefficiencies duringrefueling outages.Itwasconcluded fromthesafetyevaluation thatthenewLPRMdetectors meetorexceedthedesignrequirements oftheoriginaldetectors.
The change will ensure that the radiation monitors perform any required post-accident function for the duration of the transient..
Allofthereplacement compone'nts, including cableandconnectors, arequalified fortheenvironment inwhichtheywouldbe.installed.
Environmental conditions withinthe rack area are bounded by current radiation and temperature limits.Post modification testing would also verify final operability.
Noactivities areincludedwhichwouldimpactsystemsaridresultinchallenges tosafety-relatedequipment.
of the sample racks.49  
Following changestotheprocessing softwaretocompensate forthedifferent sensitivity ofthenewLPRMdetectors, the.functionwillbeidentical totheexistingsystem.1PMR96-0043-0 (SE96-015)ThisPMRprovidedforthemodification toRadwasteBuildingReleaseDuctRadiation MonitorSampleRacksWEA-SR-25 andWEA-SR-25A topreventoverheating ofthesystemblower.Thischangewasmadetoincreasethereliability ofSampleRackWEA-SR-25byreducingflowrestrictions tolowerexhaustairsamplebloweroperating temperature.
Theblowerhadbeenoperating atahigherthandesigntemperature andrequiredperiodicreplacement duetopremature failure.Lossoftheblowerwouldresultinthesampleracksbecominginoperable.
Itwasconcluded fromthesafetyevaluation thatthismodification wouldnotaltersafety-relatedsystemresponsetoanaccidentcondition.
Thechangewillensurethattheradiation monitorsperformanyrequiredpost-accident functionforthedurationofthetransient..
Environmental conditions withinthe rackareaareboundedbycurrentradiation andtemperature limits.Postmodification testingwouldalsoverifyfinaloperability.
ofthesampleracks.49  


During.theimplementation phase,compensatory alternate samplingmethodswouldbeimplemented andthesampleracksnotreturnedtooperablestatusuntilthemodification andassociated follow-up testingwerecompleted.
During.the implementation phase, compensatory alternate sampling methods would be implemented and the sample racks not returned to operable status until the modification and associated follow-up testing were completed.
~PMR96-0057-0 (SE96-034)ThisPMRprovidedforremovaloftheDemineralized Water(DW)Systemflushcapability fortheResidualHeatRemoval(RHR)Loops"A"and"B"samplelines.Thismodification alsoprovidedforinstallation ofadditional isolation valvesinthejetpumpsamplelines,betweentheDWSystemandPostAccidentSamplingSystem(PASS).Thereasonforthemodification wastominimizerecurrence ofcontamination oftheDWSystemthroughthePASSbymeansofthedemineralized waterflushinglines.Itwasconcluded fromthesafetyevaluation thatremovalofaportionoftheDWSystemflushcapability slightlyincreases thepotential forincreased dose.However,calculations haveshownthisslightchangeindosewouldhaveanegligible effectintotalareadose.Thepotential increaseindosewithinthesecondary containment envelopewasreviewed'nd foundtobewithincurrentdesignrequirements andlimits.Allcreditedaccidentmitigation equipment andsystemswouldremainfunctional andoperablewiththeimplementation ofthismodification.
~PMR 96-0057-0 (SE 96-034)This PMR provided for removal of the Demineralized Water (DW)System flush capability for the Residual Heat Removal (RHR)Loops"A" and"B" sample lines.This modification also provided for installation of additional isolation valves in the jet pump sample lines, between the DW System and Post Accident Sampling System (PASS).The reason for the modification was to minimize recurrence of contamination of the DW System through the PASS by means of the demineralized water flushing lines.It was concluded from the safety evaluation that removal of a portion of the DW System flush capability slightly increases the potential for increased dose.However, calculations have shown this slight change in dose would have a negligible effect in total area dose.The potential increase in dose within the secondary containment envelope was reviewed'nd found to be within current design requirements and limits.All credited accident mitigation equipment and systems would remain functional and operable with the implementation of this modification.
ThePASSfunctionwillnotbeimpactedforpost-accident samplingandtheabilitytoobtaindataforpost-accident evaluation, sheltering orrecoveryactionswouldstillbemaintained.
The PASS function will not be impacted for post-accident sampling and the ability to obtain data for post-accident evaluation, sheltering or recovery actions would still be maintained.
50  
50  


Temporary Modifications andInstrument SetpointChangesThissectioncontainsinformation pertaining toimplemented'Temporary Modification Requests(TMRs)andInstrument SetpointChangeRequests(ISCRs)andisincludedpursuantto10CFR50.59.
Temporary Modifications and Instrument Setpoint Changes This section contains information pertaining to implemented'Temporary Modification Requests (TMRs)and Instrument Setpoint Change Requests (ISCRs)and is included pursuant to 10CFR50.59.
ISCR1280(SE96-014)ThisISCRprovidedforachangetothesetpoints fortheisolation signalduetocondenser vacuumforMainSteam(MS)SystemPressureSwitchesMS-PS-56A, MS-PS-56B, MS-PS-56CandMS-PS-56D.
ISCR 1280 (SE 96-014)This ISCR provided for a change to the setpoints for the isolation signal due to condenser vacuum for Main Steam (MS)System Pressure Switches MS-PS-56A, MS-PS-56B, MS-PS-56C and MS-PS-56D.
Thenewsetpoints werechangedbymeansofacalculation and;willallowlesslossofvacuumpriortoinitiating anMSIVisolation.
The new setpoints were changed by means of a calculation and;will allow less loss of vacuum prior to initiating an MSIV isolation.
Itwasconcluded fromthesafetyevaluation thatallowingforlesslossofvacuumprior'oinitiating anMSIVisolation wouldresultinareduction inoperating margin.Thelowvacuumfunctionisprovidedtoisolatethemainsteamsystemintheeventofalossofmaincondenser vacuumwhichwouldremovetheeffective capability ofthecondenser asaheatsink.Thereduction inoperating marginwouldnotincreasetheprobability ofalossofcondenser vacuumevent.However,itcouldslightlyincreasetheprobability ofanMSIVisolation event.Itwasdetermined thatanycontribution totheincreaseintheprobability oftheMSIVisolation eventduetothedecreaseinoperating margincausedbythemoreconservative setpointipsignificantly lessthantheprobability oftheMSIVisolation event.Inaddition, thissmallincreaseintheprobability oftheMSIVisolation eventdoesnotcontribute toanmcreaseinfrequency.
It was concluded from the safety evaluation that allowing for less loss of vacuum prior'o initiating an MSIV isolation would result in a reduction in operating margin.The low vacuum function is provided to isolate the main steam system in the event of a loss of main condenser vacuum which would remove the effective capability of the condenser as a heat sink.The reduction in operating margin would not increase the probability of a loss of condenser vacuum event.However, it could slightly increase the probability of an MSIV isolation event.It was determined that any contribution to the increase in the probability of the MSIV isolation event due to the decrease in operating margin caused by the more conservative setpoint ip significantly less than the probability of the MSIV isolation event.In addition, this small increase in the probability of the MSIV isolation event does not contribute to an mcrease in frequency.
ISCR1284(SE96-041)ThisISCRprovidedforrevisiontotheANALYZEcomputerprogramconfiguration filetoturnoffthezerostabilizer functionforstackmonitorintermediate andhighrangedetectors PRM-RE-1B andPRM-RE-1C.
ISCR 1284 (SE 96-041)This ISCR provided for revision to the ANALYZE computer program configuration file to turn off the zero stabilizer function for stack monitor intermediate and high range detectors PRM-RE-1B and PRM-RE-1C.
Itwasdetermined thatthezerostabilizer functioncouldfailathighcountratesandresultinanincorrect indication ofsystemfailureinthemaincontrolroom.Itwasconcluded fromthesafetyevaluation thatthissystemisapost-accident systemwithnocontrolfunctions.
It was determined that the zero stabilizer function could fail at high count rates and result in an incorrect indication of system failure in the main control room.It was concluded from the safety evaluation that this system is a post-accident system with no control functions.
Information fromthissystemisusedfordecisions pertaining toaccident"follow-up actions.However,theinformation usedbyOperations personnel inthesescenarios willnotbeaffected, bythischange.-'=~~51~tl,  
Information from this system is used for decisions pertaining to accident"follow-up actions.However, the information used by Operations personnel in these scenarios will not be affected, by this change.-'=~~51~tl,  


Thechangeaffectsonlythezerostabilization functionofthemulti-channel analyzersystemandhasnoimpactonanyotherpartofthesystemortheplant.Thezerostabilizer functionofthestackmonitormulti-channel analyzerprovidesautomatic correction forsmallchangesinthezerovalueofthespectrum.
The change affects only the zero stabilization function of the multi-channel analyzer system and has no impact on any other part of the system or the plant.The zero stabilizer function of the stack monitor multi-channel analyzer provides automatic correction for small changes in the zero value of the spectrum.Turning off the function.will simply disable the testing of the zero stabilizer range.It will not affect the gain stabilizer function.The gain stabilizer function provides all of the automatic control that is required to maintain the multi-channel analyzer within required tolerances.
Turningoffthefunction.
This change has no affect on the gross count rate response of the system.Gross count rate indication is the information that is used for accident follow-up decisions.
willsimplydisablethetestingofthezerostabilizer range.Itwillnotaffectthegainstabilizer function.
~TMR 95-105 (SE 95-105)This TMR provided for modification of the suction and discharge lines foi Radwaste.Building HVAC (WOA)Sample Racks WOA-SR-18A, WOA-SR-18B, WOA-SR-19A and WOA-SR-19B to increase fio'w through the system.Increased flow was obtained by.merging.the intake and exhaust lines to the pump suction, and exhausting to the local atmosphere.
Thegainstabilizer functionprovidesalloftheautomatic controlthatisrequiredtomaintainthemulti-channel analyzerwithinrequiredtolerances.
The increased flow was necessary to reduce blower operating temperatures to preclude premature failure.It was concluded from the safety evaluation that the modification will ensure that the blowers are operating within vendor recommendations to ensure availability during the required post-accident operating time.The control room remote air intake radiation monitors are not the initiator of any previously evaluated transient.
Thischangehasnoaffectonthegrosscountrateresponseofthesystem.Grosscountrateindication istheinformation thatisusedforaccidentfollow-up decisions.
Based on testing results,.it was concluded that system flow would be increased by approximately.1.5 times the current value, which dropped temperatures within the recommended operating range.With this modification, the blowers could be expected to operate reliably during post-accident conditions.
~TMR95-105(SE95-105)ThisTMRprovidedformodification ofthesuctionanddischarge linesfoiRadwaste.BuildingHVAC(WOA)SampleRacksWOA-SR-18A, WOA-SR-18B, WOA-SR-19A andWOA-SR-19B toincreasefio'wthroughthesystem.Increased flowwasobtainedby.merging.theintakeandexhaustlinestothepumpsuction,andexhausting tothelocalatmosphere.
TMR 96-013 (SE 96-033)This TMR provided for removal of a tab from the indicator shaft for Reactor Core Isolation Cooling (RCIC)System Valve RCIC-V-66 to improve the operating characteristics of the valve.With the tab removed, the indicator shaft will not turn when the hanger arm rotates on the actuator shaft.This would then allow for the ability to sufficiently tighten indicator shaft packing to prevent leakage.It was concluded from the safety evaluation that the hanger arm and disc assembly.of the valve would continue to function a's designed to ensure rapid isolation in the event of an RCIC System line break.'he hanger arm and disc assembly will move more freely, being independent of.the indicator, shaft.52 Removal of the tab from the indicator shaft would not affect the system injection or containment isolation function of the valve.Because the indicator shaft will no longer turn in its packing, there is less probability of packing binding on the shaft or packing degradation due to wear.~TMR 96-023 (SE 96-066)This TMR provided for installation of a filtration system near the Standby Service Water (SSW)spray ponds to remove suspended solids from the spray pond water.The side stream filtration system is designed to remove organic material and silt present in the water, which will assist in maintaining the required heat transfer capability of the SSW System heat exchangers and reduce water treatment costs.It was concluded from the safety evaluation that the change is non-safety related.Potential impacts on important to safety systems and functions were evaluated and it was concluded none of those impacts'would result in the inability of those systems and components to meet their safety function.The impacts evaluated relate to seismic effects, spray pond water inventor requirements, tornado effects and the effects of localized flooding.The SSW system and ultimate heat sink would still be available with full capability to mitigate accidents.
Theincreased flowwasnecessary toreducebloweroperating temperatures toprecludepremature failure.Itwasconcluded fromthesafetyevaluation thatthemodification willensurethattheblowersareoperating withinvendorrecommendations toensureavailability duringtherequiredpost-accident operating time.Thecontrolroomremoteairintakeradiation monitorsarenottheinitiator ofanypreviously evaluated transient.
~TMR 96-029 (SE 96-100)This TMR provided for increasing the voltage applied to a Traversing Incore Probe (TIP)indexer.Indexer"B" would not move beyond channel one.This modification would increase the applied torque to the indexer mechanism and restore proper operation.
Basedontestingresults,.
It was concluded from the safety evaluation that the increase in motor voltage would not impact any of the analyzed transients.
itwasconcluded thatsystemflowwouldbeincreased byapproximately.1.5 timesthecurrentvalue,whichdroppedtemperatures withintherecommended operating range.Withthismodification, theblowerscouldbeexpectedtooperatereliablyduringpost-accident conditions.
The modification involves increasing the voltage to the indexer motor to a maximum of 200 VAC for no more than five seconds.The voltages and currents to be applied to the non-safety related indexer motor are within the design characteristics of the penetration module.53  
TMR96-013(SE96-033)ThisTMRprovidedforremovalofatabfromtheindicator shaftforReactorCoreIsolation Cooling(RCIC)SystemValveRCIC-V-66 toimprovetheoperating characteristics ofthevalve.Withthetabremoved,theindicator shaftwillnotturnwhenthehangerarmrotatesontheactuatorshaft.Thiswouldthenallowfortheabilitytosufficiently tightenindicator shaftpackingtopreventleakage.Itwasconcluded fromthesafetyevaluation thatthehangerarmanddiscassembly.
ofthevalvewouldcontinuetofunctiona'sdesignedtoensurerapidisolation intheeventofanRCICSystemlinebreak.'hehangerarmanddiscassemblywillmovemorefreely,beingindependent of.theindicator, shaft.52 Removalofthetabfromtheindicator shaftwouldnotaffectthesysteminjection orcontainment isolation functionofthevalve.Becausetheindicator shaftwillnolongerturninitspacking,thereislessprobability ofpackingbindingontheshaftorpackingdegradation duetowear.~TMR96-023(SE96-066)ThisTMRprovidedforinstallation ofafiltration systemneartheStandbyServiceWater(SSW)spraypondstoremovesuspended solidsfromthespraypondwater.Thesidestreamfiltration systemisdesignedtoremoveorganicmaterialandsiltpresentinthewater,whichwillassistinmaintaining therequiredheattransfercapability oftheSSWSystemheatexchangers andreducewatertreatment costs.Itwasconcluded fromthesafetyevaluation thatthechangeisnon-safety related.Potential impactsonimportant tosafetysystemsandfunctions wereevaluated anditwasconcluded noneofthoseimpacts'would resultintheinability ofthosesystemsandcomponents tomeettheirsafetyfunction.
Theimpactsevaluated relatetoseismiceffects,spraypondwaterinventorrequirements, tornadoeffectsandtheeffectsoflocalized flooding.
TheSSWsystemandultimateheatsinkwouldstillbeavailable withfullcapability tomitigateaccidents.
~TMR96-029(SE96-100)ThisTMRprovidedforincreasing thevoltageappliedtoaTraversing IncoreProbe(TIP)indexer.Indexer"B"wouldnotmovebeyondchannelone.Thismodification wouldincreasetheappliedtorquetotheindexermechanism andrestoreproperoperation.
Itwasconcluded fromthesafetyevaluation thattheincreaseinmotorvoltagewouldnotimpactanyoftheanalyzedtransients.
Themodification involvesincreasing thevoltagetotheindexermotortoamaximumof200VACfornomorethanfiveseconds.Thevoltagesandcurrentstobeappliedtothenon-safety relatedindexermotorarewithinthedesigncharacteristics ofthepenetration module.53  


0FSARChangesThissectioncontainsinformation pertaining toFSARLicensing DocumentChangeNotices(LDCNS)andFSARChangeNotices(SCNs)andisincludedpursuantto10CFR50.59.
0 FSAR Changes This section contains information pertaining to FSAR Licensing Document Change Notices (LDCNS)and FSAR Change Notices (SCNs)and is included pursuant to 10CFR50.59.
LDCN-FSAR-96-063 (SE96-078)ThisLDCNprovidedforachangetotheFSARtoallowfortheuseofoptimumflowrateforiodinesamplingandsubstitution ofalocalalarmingcontinuous airmonitorforamobilemonitoring system.'Itwasconcluded fromthesafetyevaluation thatdoseavoidance duringthecourseofanaccidentinvolving radiation releaseswouldbeenhancedbythechangeduetoearlierandmorereliableindications ofiodineintheair.Amorereliablecontinuous airmonitorisalsobeingsubstituted forthecurrently-installed unit.Theuseofanoptimumflowrateforiodinesamplingandimplementation ofanimprovedairmonitoring systemdonotincreaseth'eprobability orconsequences ofanaccidentpreviously evaluated.
LDCN-FSAR-96-063 (SE 96-078)This LDCN provided for a change to the FSAR to allow for the use of optimum flow rate for iodine sampling and substitution of a local alarming continuous air monitor for a mobile monitoring system.'It was concluded from the safety evaluation that dose avoidance during the course of an accident involving radiation releases would be enhanced by the change due to earlier and more reliable indications of iodine in the air.A more reliable continuous air monitor is also being substituted for the currently-installed unit.The use of an optimum flow rate for iodine sampling and implementation of an improved air monitoring system do not increase th'e probability or consequences of an accident previously evaluated.
LOCN-FSAR-96-068 (SE96-091)ThisLDCNprovidedforachangetotheFSARtolowertheminimumdieselgenerator enginebaytemperature to40degreesfahrenheit.
LOCN-FSAR-96-068 (SE 96-091)This LDCN provided for a change to the FSAR to lower the minimum diesel generator engine bay temperature to 40 degrees fahrenheit.
Inaddition, thedescription ofthe'VACsystemfortheHighPressureCoreSpray(HPCS)Systembatteries wasmodifiedtoallowforuseofsupplemental, heatersorothermeanstomaintainbatterytemperature greaterthanorequalto60degreesfahrenheit.
In addition, the description of the'VAC system for the High Pressure Core Spray (HPCS)System batteries was modified to allow for use of supplemental, heaters or other means to maintain battery temperature greater than or equal to 60 degrees fahrenheit.
Itwasconcluded fromthesafetyevaluation thatloweringthedieselengineroomtemperature from70degreesto40degreeswouldnothaveanadverseaffectonthestartingcapability orreliabiTity oftheengines.Thedieselenginesupplierprovidedinformation totheeffectthat,aslongathecoolantandlubeoiltemperatures aremaintained atorabove85degreesbya"keepwarm"system,theenginescanachieveaten-second startinanambienttemperature of40degrees.Thebatterymanufacturer suppliedinformation totheeffectthattheHPCSbatteries willprovidefull-rated capacityaslongastheelectrolyte temperature isatorabove60degrees.'ecauselowering'of the.roomtemperature hasnoadverseimpactandthebatteries will.performasrequiredat60degrees,thecomponents willcontinuetofunctionasrequired='insupportofemergency corecoolingsystemaccident.
It was concluded from the safety evaluation that lowering the diesel engine room temperature from 70 degrees to 40 degrees would not have an adverse affect on the starting capability or reliabiTity of the engines.The diesel engine supplier provided information to the effect that, as long a the coolant and lube oil temperatures are maintained at or above 85 degrees by a"keep warm" system, the engines can achieve a ten-second start in an ambient temperature of 40 degrees.The battery manufacturer supplied information to the effect that the HPCS batteries will provide full-rated capacity as long as the electrolyte temperature is at or above 60 degrees.'ecause lowering'of the.room temperature has no adverse impact and the batteries will.perform as required at 60 degrees, the components will continue to function as required='in support of emergency core cooling system accident.mitigation.
mitigation.
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~LDCN-FSAR-96-077 (SE96-Q90)ThisLDCNprovidedforachangetothePSARtoreflectplannedorganizational changeswithinthePlantSupportServicesDepartment andtheadditionofnewALARAreview'riteria.
~LDCN-FSAR-96-077 (SE 96-Q90)This LDCN provided for a change to the PSAR to reflect planned organizational changes within the Plant Support Services Department and the addition of new ALARA review'riteria.
Itwasconcluded fromthesafetyevaluation that,fromanorganizational perspective, thechangeonlyinvolvesrealignment ofresponsibilities.
It was concluded from the safety evaluation that, from an organizational perspective, the change only involves realignment of responsibilities.
Currentfunctions suchassolidwasteprocessing havenotchanged.Clearcriteriafordetermiiiing theneedforanALARAreviewforprocedures wasalsoprovided.
Current functions such as solid waste processing have not changed.Clear criteria for determiiiing the need for an ALARA review for procedures was also provided.These changes are not in confiict with any licensing basis documentation or commitments.
Thesechangesarenotinconfiictwithanylicensing basisdocumentation orcommitments.
Although the review of procedures for ALARA considerations is an element of the ALARA Program, the specific review criteria are not part of any regulatory basis for radiological protection requirements.
Althoughthereviewofprocedures forALARAconsiderations isanelementoftheALARAProgram,thespecificreviewcriteriaarenotpartofanyregulatory basisforradiological protection requirements.
, LBCN-FSAR-96-079 (SE 96-097)This LDCN provided for a change to the FSAR to refIect updated actions that are to be taken following an earthquake.
,LBCN-FSAR-96-079 (SE96-097)ThisLDCNprovidedforachangetotheFSARtorefIectupdatedactionsthataretobetakenfollowing anearthquake.
It was concluded from the safety evaluation that the changes are consistent or conservative with EPRI guidance and a draft NRC regulatory guide pertaining to earthquake planning and follow-up actions.The recommended actions would ensure that conservative shutdown decisions are made and that the reliability of structures, systems, and components following an earthquake is not reduced.These changes affect only the criteria used to initiate a controlled manual reactor shutdown.No hardware is impacted.'
Itwasconcluded fromthesafetyevaluation thatthechangesareconsistent orconservative withEPRIguidanceandadraftNRCregulatory guidepertaining toearthquake planningandfollow-up actions.Therecommended actionswouldensurethatconservative shutdowndecisions aremadeandthatthereliability ofstructures, systems,andcomponents following anearthquake isnotreduced.Thesechangesaffectonlythecriteriausedtoinitiateacontrolled manualreactorshutdown.
LDCN-FSAR-96-080 (SE 96-092)" This LDCN provided for several changes to the Fire Protection Program to refiect updated compensatory measures and editorial enhancements.
Nohardwareisimpacted.'
It was concluded from the safety evaluation that previous fire protection analyses had concluded that compensatory measures could be altered under certain circumstances.
LDCN-FSAR-96-080 (SE96-092)"ThisLDCNprovidedforseveralchangestotheFireProtection Programtorefiectupdatedcompensatory measuresandeditorial enhancements.
This change allows Control Room Operators to act as a fire tour for inoperable wet-pipe sprinkler system and Halon confinement barriers..The change also allows for'eight hours to establish the operability of video and portable detection systems when sprinkler or-detection systems are inoperable in high radiation or contaminated areas.0-i These changes are consistent with previously-approved safety evaluations and provide reasonable assurance that adequate compensatoiy measures will still be implemented for the observation of fire or fire hazards in the areas of inoperable fire protection equipment.
Itwasconcluded fromthesafetyevaluation thatpreviousfireprotection analyseshadconcluded thatcompensatory measurescouldbealteredundercertaincircumstances.
LDCN-FSAR-96-081 (SE 96-099)This LDCN provided for a change to the FSAR to delete the requirement for Fast Flux Test Facility (FFI'F)personnel on the Hanford Reservation to provide direct WNP-2 Control Room notification of a sodium oxide release.Procedural arrangements are in place between FFTF and Supply System personnel for timely notification of the WNP-2 Control Room in the event of a sodium oxide release.It was concluded from the safety evaluation that changing the method of no'tifying the control room would have no impact on the probability or consequences of a previously-
ThischangeallowsControlRoomOperators toactasafiretourforinoperable wet-pipesprinkler systemandHalonconfinement barriers.
.evaluated accident.The original assumption of 55 minutes to notify the WNP-2 Control Room is still valid and provides adequate time for personnel to either isolate the control room or put on portable breathing equipment.
.Thechangealsoallowsfor'eight hourstoestablish theoperability ofvideoandportabledetection systemswhensprinkler or-detection systemsareinoperable inhighradiation orcontaminated areas.0-i Thesechangesareconsistent withpreviously-approved safetyevaluations andprovidereasonable assurance thatadequatecompensatoiy measureswillstillbeimplemented fortheobservation offireorfirehazardsintheareasofinoperable fireprotection equipment.
e e By continuing to provide ample waniin'g time, Supply System Operators would be able to respond accordingly and place the plant in a normal shutdown condition in the event of an accident.LDCN-FSAR-96-086 (SE 96-096)This LDCN provided for a change to the FSAR to reflect the downgrade of Standby Service Water (SSW)System Pumphouse Air Intake Fan POA-FN-2A from Quality Class-1 to Quality Class-Augmented (QC-A).It was concluded from the safety evaluation that the fan provides no active support for any equipment important to safety.The safety-related cooling function for the standby service water pumphouse HVAC system does not require the operation of POA-FN-2A.
LDCN-FSAR-96-081 (SE96-099)ThisLDCNprovidedforachangetotheFSARtodeletetherequirement forFastFluxTestFacility(FFI'F)personnel ontheHanfordReservation toprovidedirectWNP-2ControlRoomnotification ofasodiumoxiderelease.Procedural arrangements areinplacebetweenFFTFandSupplySystempersonnel fortimelynotification oftheWNP-2ControlRoomintheeventofasodiumoxiderelease.Itwasconcluded fromthesafetyevaluation thatchangingthemethodofno'tifying thecontrolroomwouldhavenoimpactontheprobability orconsequences ofapreviously-
The SSW pump and related equipment are cooled by a safety-related fan-coil unit.The potential loss of the intake fan would not result in pumphouse ambient temperatures.
.evaluated accident.
reaching the maximum normal operating limits for safety-related equipment.
Theoriginalassumption of55minutestonotifytheWNP-2ControlRoomisstillvalidandprovidesadequatetimeforpersonnel toeitherisolatethecontrolroomorputonportablebreathing equipment.
It was determined that a quality classification of QC-A is adequate for this component.
eeBycontinuing toprovideamplewaniin'gtime,SupplySystemOperators wouldbeabletorespondaccordingly andplacetheplantinanormalshutdowncondition intheeventofanaccident.
=e~SCN 95-058 (SE 96-035))+This SCN provided for a change to'the FSAR to reflect a revision to the Reactor Core Isolation Cooling (RCIC)System isolation time delay logic.Closure of RCIC System Primary Containment Isolation Valves RCIC-V-8, RCIC-V-63 and RCIC-'V-76 is delayed by logic time delay relays to prevent inadvertent isolation from high flow during system 56
LDCN-FSAR-96-086 (SE96-096)ThisLDCNprovidedforachangetotheFSARtoreflectthedowngrade ofStandbyServiceWater(SSW)SystemPumphouse AirIntakeFanPOA-FN-2A fromQualityClass-1toQualityClass-Augmented (QC-A).Itwasconcluded fromthesafetyevaluation thatthefanprovidesnoactivesupportforanyequipment important tosafety.Thesafety-related coolingfunctionforthestandbyservicewaterpumphouse HVACsystemdoesnotrequiretheoperation ofPOA-FN-2A.
TheSSWpumpandrelatedequipment arecooledbyasafety-related fan-coilunit.Thepotential lossoftheintakefanwouldnotresultinpumphouse ambienttemperatures.
reachingthemaximumnormaloperating limitsforsafety-related equipment.
Itwasdetermined thataqualityclassification ofQC-Aisadequateforthiscomponent.
=e~SCN95-058(SE96-035))+ThisSCNprovidedforachangeto'theFSARtoreflectarevisiontotheReactorCoreIsolation Cooling(RCIC)Systemisolation timedelaylogic.ClosureofRCICSystemPrimaryContainment Isolation ValvesRCIC-V-8, RCIC-V-63 andRCIC-'V-76 isdelayedbylogictimedelayrelaystopreventinadvertent isolation fromhighflowduringsystem56


~oinitiation whenthesteamflowtotheturbineismomentarily abovethehighflowsetpoint.
~o initiation when the steam flow to the turbine is momentarily above the high flow setpoint.The calculated time delay relay setpoint in each division was changed from a two-second nominal value to a three-second aHowable value.Process and instrument loop accuracies that were previously not.accounted for were included in the revised calculation.
Thecalculated timedelayrelaysetpointineachdivisionwaschangedfromatwo-second nominalvaluetoathree-second aHowablevalue.Processandinstrument loopaccuracies thatwerepreviously not.accounted forwereincludedintherevisedcalculation.
It was concluded from the safety evaluation that this change would not impact the overall function and accident response of the RCIC System.The safety function of these relays, during design basis event mitigation is to 1)isolate the system to limit mass energy blowdown for an RCIC System high energy line break, and 2)limit long-term secondary containment bypass leakage after'a system trip following a loss of coolant ac'cident.
Itwasconcluded fromthesafetyevaluation thatthischangewouldnotimpacttheoverallfunctionandaccidentresponseoftheRCICSystem.Thesafetyfunctionoftheserelays,duringdesignbasiseventmitigation isto1)isolatethesystemtolimitmassenergyblowdownforanRCICSystemhighenergylinebreak,and2)limitlong-term secondary containment bypassleakageafter'asystemtripfollowing alossofcoolantac'cident.
The allowable value of three seconds is derived from, and bounded by, the upper analytical limit of four seconds used in the event blowdown calculation.
Theallowable valueofthreesecondsisderivedfrom,andboundedby,theupperanalytical limitoffoursecondsusedintheeventblowdowncalculation.
The accident analysis assumes the four second delay (including process and loop inaccuracies) prior to the RCIC valves receiving a closure signal.SCN 95-062 (SE 95-095)This SCN provided for a change to the FSAR to describe changes to the new fuel storage vault.Deck plates were added to the vault racks and only allow fuel to be placed in alternate locations.
Theaccidentanalysisassumesthefourseconddelay(including processandloopinaccuracies) priortotheRCICvalvesreceiving aclosuresignal.SCN95-062(SE95-095)ThisSCNprovidedforachangetotheFSARtodescribechangestothenewfuelstoragevault.Deckplateswereaddedtothevaultracksandonlyallowfueltobeplacedinalternate locations.
These temporary plates constitute a template which limit placements of new fuel to alternate locations in the vault.This change allows for the safe and efficient handling of ABB re-load fuel.It was concluded from the safety evaluation that this activity has the effect of markedly increasing the space between the adjacent fuel assembHes.
Thesetemporary platesconstitute atemplatewhichlimitplacements ofnewfueltoalternate locations inthevault.Thischangeallowsforthesafeandefficient handlingofABBre-loadfuel.Itwasconcluded fromthesafetyevaluation thatthisactivityhastheeffectofmarkedlyincreasing thespacebetweentheadjacentfuelassembHes.
The additional spacing renders a criticality accident considerably less than the low probability arrangement previously employed in these racks.The proposed physical changes to the refuel floor to accommodate the change do not impact or increase the consequences of previously evaluated transients.
Theadditional spacingrendersacriticality accidentconsiderably lessthanthelowprobability arrangement previously employedintheseracks.Theproposedphysicalchangestotherefuelfloortoaccommodate thechangedonotimpactorincreasetheconsequences ofpreviously evaluated transients.
Items addressed included heavy crane load paths and seismic requirements.
Itemsaddressed includedheavycraneloadpathsandseismicrequirements.
SCN 95-064 (SE 95-091)This SCN provided for a change to the Fire Protection Program to reflect a revision of fire door surveillance requirements.
SCN95-064(SE95-091)ThisSCNprovidedforachangetotheFireProtection Programtoreflectarevisionoffiredoorsurveillance requirements.
The primary technical change consists of the performance of weekly position inspections for unlocked, unsupervised fire doors instead of the current inspection by, routine operator tours.It was concluded from the safety evaluation that the less frequent surveillance to nonessential and non-plant block doors will continue:to ensure their operability.
Theprimarytechnical changeconsistsoftheperformance ofweeklypositioninspections forunlocked, unsupervised firedoorsinsteadofthecurrentinspection by,routineoperatortours.Itwasconcluded fromthesafetyevaluation thatthelessfrequentsurveillance tononessential andnon-plant blockdoorswillcontinue:to ensuretheiroperability.
Nonessential fire'doors, by definition, are not credited with ensuring safe fire shutdown..
Nonessential fire'doors, bydefinition, arenotcreditedwithensuringsafefireshutdown..
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Thechangesinsurveillance frequency donotaffecttheoperation offireprotection systemequipment beyondthatpreviously evaluated.
The changes in surveillance frequency do not affect the operation of fire protection system equipment beyond that previously evaluated.
Sincethechangedoesnotalterfiredooroperation orcreatenewfailuremodes,extending theperiodbetweensurveillance testingwouldnotlowertheabilityoftheequip'ment tomitigateorpreventthepropagation offires.'CN 95-070(SE96-007)ThisSCNprovidedforachangetotheFSARtoreflectthattheHighPressureCoreSpray(HPCS)Systemdieselgenerator motor-driven aircompressor ispoweredfromMotorControlCenter(MCC)MC-6BinsteadoftheHPCSbus.'Itwasconcluded fromthesafetyevaluation thatsupplypowerfromnon-safety relatedMC-6BtoelectricmotordrivenDieselStartingAir(DSA)SystemAirCompressor DSA-.M-C/1Cwouldnotaffecttheconsequences orprobability ofapreviously evaluated accident.
Since the change does not alter fire door operation or create new failure modes, extending the period between surveillance testing would not lower the ability of the equip'ment to mitigate or prevent the propagation of fires.'CN 95-070 (SE 96-007)This SCN provided for a change to the FSAR to reflect that the High Pressure Core Spray (HPCS)System diesel generator motor-driven air compressor is powered from Motor Control Center (MCC)MC-6B instead of the HPCS bus.'It was concluded from the safety evaluation that supply power from non-safety related MC-6B to electric motor driven Diesel Starting Air (DSA)System Air Compressor DSA-.M-C/1C would not affect the consequences or probability of a previously evaluated accident.The air compressor is of an augmented quality class due to seismic requirements, but has no specific safety function.0'oss of the air compressor due to loss of MC-6B would not affect operation of the HPCS diesel generator.
Theaircompressor isofanaugmented qualityclassduetoseismicrequirements, buthasnospecificsafetyfunction.
Safety-related Diesel Starting Air Receivers DSA-AR-1C and DSA-AR-2C aie capable of maintaining system air pressure and capacity for starting of the diesel generator, regardless of the status of the air compressor.
0'ossoftheaircompressor duetolossofMC-6Bwouldnotaffectoperation oftheHPCSdieselgenerator.
SCN.,95-072 (SE 95-101)This SCN provided for a change to the FSAR to reflect updated secondary containment
Safety-related DieselStartingAirReceivers DSA-AR-1C andDSA-AR-2Caiecapableofmaintaining systemairpressureandcapacityforstartingofthedieselgenerator, regardless ofthestatusoftheaircompressor.
.bypass leakage paths.Some existing bypass paths were eliminated from consideration
SCN.,95-072 (SE95-101)ThisSCNprovidedforachangetotheFSARtoreflectupdatedsecondary containment
'nd others were added based on a technical evaluation.
.bypassleakagepaths.Someexistingbypasspathswereeliminated fromconsideration
The overall allowed bypass leak rate of 0;74 scfli was not changed by this SCN.It was concluded from the safety evaluation that revising the FSAR to reflect the potential bypass leakage paths for secondary containment would not impact previously evaluated transients.
'ndotherswereaddedbasedonatechnical evaluation.
The overall allowed leakage was not changed.Since the leak rate was not modified, the offsite and control room dose consequences would not be affected.The primary containment penetrations that were eliminated as secondary containment bypass leak paths were all analyzed to ensure that any leakage would be processed by the Standby Gas Treatment System.The valves eliminated from consideration as potential bypass leakage paths were containment isolation valves.The measured leakage would still be included in the Leak Rate Testing Program (Type B'and Type C).58  
Theoverallallowedbypassleakrateof0;74scfliwasnotchangedbythisSCN.Itwasconcluded fromthesafetyevaluation thatrevisingtheFSARtoreflectthepotential bypassleakagepathsforsecondary containment wouldnotimpactpreviously evaluated transients.
Theoverallallowedleakagewasnotchanged.Sincetheleakratewasnotmodified, theoffsiteandcontrolroomdoseconsequences wouldnotbeaffected.
Theprimarycontainment penetrations thatwereeliminated assecondary containment bypassleakpathswereallanalyzedtoensurethatanyleakagewouldbeprocessed bytheStandbyGasTreatment System.Thevalveseliminated fromconsideration aspotential bypassleakagepathswerecontainment isolation valves.ThemeasuredleakagewouldstillbeincludedintheLeakRateTestingProgram(TypeB'andTypeC).58  


~SCN96-005(SE96463)ThisSCNprovidedforachangetotheFSARandEmergency Plantoreflectcurrentbasesandmethodsforthecontrolling andmonitoring ofcontamination.
~SCN 96-005 (SE 96463)This SCN provided for a change to the FSAR and Emergency Plan to reflect current bases and methods for the controlling and monitoring of contamination.
Itwasconcluded fromthesafetyevaluation thatthechangewouldnotinvolvesystems,structures orcomponents anddoesnotimpactthephysicalbarriersthatprotectagainsttheuncontrolled releaseofradioactivity.
It was concluded from the safety evaluation that the change would not involve systems, structures or components and does not impact the physical barriers that protect against the uncontrolled release of radioactivity.
Controlshavebeenestablished toensurethereisnodetectable fixedorloosecontamination outsideoftheRadiologically Controlled Areaundernormalandemergency conditions.
Controls have been established to ensure there is no detectable fixed or loose contamination outside of the Radiologically Controlled Area under normal and emergency conditions.
Theintenttocontrollicensedmaterialhasnotbeenmodified.
The intent to control licensed material has not been modified.The current mix of isotopes in dry active waste are such that the other detector types will provide greater assurance that licensed radioactive material would be controlled in a manner consistent with ALARA considerations.
Thecurrentmixofisotopesindryactivewastearesuchthattheotherdetectortypeswillprovidegreaterassurance thatlicensedradioactive materialwouldbecontrolled inamannerconsistent withALARAconsiderations.
SCN 96-008 (SE 95-106)This SCN provided for a change to FSAR drawings to reflect an update of fire area boundaries and fire barriers.In some cases, essential and nonessential fire barriers have been downgraded.
SCN96-008(SE95-106)ThisSCNprovidedforachangetoFSARdrawingstoreflectanupdateoffireareaboundaries andfirebarriers.
However, the derated barriers are simply corrections or previous errors where no fire rating was actually required.It was concluded from the safety evaluation that the proposed changes do not lower the ability of safety systems to perform during accident conditions.
Insomecases,essential andnonessential firebarriershavebeendowngraded.
The changes in fire area boundaries do not affect the operation of, or become hazards to, accident mitigation equipment beyond that previously evaluated.
However,thederatedbarriersaresimplycorrections orpreviouserrorswherenofireratingwasactuallyrequired.
The proposed barrier changes do not increase radiological releases or exposures to.control room personnel since configuration controls exist to ensure secondary containment and control room ventilation boundary penetration seals are present, independent of the fire rating of the barrier.SCN 96-009 (SE 96-030)This SCN provided for changes to the FSAR and Emergency Plan to allow for removal of on-site Thermoluminescent Dosimeter (TLD)readers and to transfer the processing of exposure information.,to a certified local vendor.59 It was concluded from the safety evaluation that dose avoidance during the course of an accident involving radiation releases would be based on direct readout dosimeters.
Itwasconcluded fromthesafetyevaluation thattheproposedchangesdonotlowertheabilityofsafetysystemstoperformduringaccidentconditions.
The TLDs are processed as a follow-up after any dose has been received and the information is used as comparison to the direct dosimeter information.
Thechangesinfireareaboundaries donotaffecttheoperation of,orbecomehazardsto,accidentmitigation equipment beyondthatpreviously evaluated.
The results of TLD measurement of external doses to workers or the public would be available from the vendor within 48 hours upon request of the information.(SE 96-044)This SCN also provided for a change to the FSAR to allow for deletion.of reference to automatic radwaste drum processing (filling, storage and monitoring).
Theproposedbarrierchangesdonotincreaseradiological releasesorexposures to.controlroompersonnel sinceconfiguration controlsexisttoensuresecondary containment andcontrolroomventilation boundarypenetration sealsarepresent,independent ofthefireratingofthebarrier.SCN96-009(SE96-030)ThisSCNprovidedforchangestotheFSARandEmergency Plantoallowforremovalofon-siteThermoluminescent Dosimeter (TLD)readersandtotransfertheprocessing ofexposureinformation.,to acertified localvendor.59 Itwasconcluded fromthesafetyevaluation thatdoseavoidance duringthecourseofanaccidentinvolving radiation releaseswouldbebasedondirectreadoutdosimeters.
The current method for drum processing consists of a manual operation.
TheTLDsareprocessed asafollow-up afteranydosehasbeenreceivedandtheinformation isusedascomparison tothedirectdosimeter information.
It was'concluded from the safety evaluation that radwaste drum processing is a manual activity that would not increase the probability or consequences of an accident.The processing activity does not affect any safety-related or important to safety plant equipment.
TheresultsofTLDmeasurement ofexternaldosestoworkersorthepublicwouldbeavailable fromthevendorwithin48hoursuponrequestoftheinformation.
It was also concluded that the dose to the public from a manually filled drum would be the same as from the same drum filled in a remote manner.SCN 96-012 (SE 96-022)This SCN provided for a change to the WNP-2 Physical Security Plan to allow security officers who have left the protected area to re-enter the protected area without being subjected to a metal detector search.In addition, the plan was revised to allow for the removal of protected and vital area keys from the protected area when they are under the control and custody of on-duty security force personnel.
(SE96-044)ThisSCNalsoprovidedforachangetotheFSARtoallowfordeletion.
Changing the security plan to allow on-duty armed security officers to re-enter the protected area without being subjected to metal detector searches was endorsed by the NRC in Generic Letter 96-02,"Reconsideration of Nuclear Power Plant Security Requirements Associated with an Internal Threat." The staff considered that this change could be made to the security plans in accordance with the provisions of 10CFR50.54(p).
ofreference toautomatic radwastedrumprocessing (filling, storageandmonitoring).
I With regard to removal of keys from the protected area, it was concluded from the safety evaluation that the ability to protect vital equipment target sets continues to be maintained by prompt response to any vital area door alarm when an unauthorized access attempt's detected by the security system.
Thecurrentmethodfordrumprocessing consistsofamanualoperation.
The key control requirements identified in 10CFR73.55(d)(9) are still being met and have been incorporated into the security plan.There are no 10CFR73.55(d)(9) stipulations that these keys cannot leave the protected area when under the control of a security officer.It was also concluded that the likelihood of an attempt at radiological sabotage is not a function of whether or not a vital area key is taken off-site while under the control of an authorized on-duty security force officer.SCN 96-014 (SE 96-013)This SCN provided for clarification and consistency pertaining to seismic qualification of equipment and components.
Itwas'concluded fromthesafetyevaluation thatradwastedrumprocessing isamanualactivitythatwouldnotincreasetheprobability orconsequences ofanaccident.
The method for assessing valve clearance was also modified.It was concluded from the safety evaluation that the consequences of a previously analyzed seismic or dynamic accident would not be increased by these changes.Consequences can only increase if the equipment or components analyzed are damaged by the event.The proposed changes only involve analytical methods for seismic and dynamic qualification of equipment and components.
Theprocessing activitydoesnotaffectanysafety-related orimportant tosafetyplantequipment.
The use of acceptably conservative analytical methods precludes any reduction in safety margin for systems and components.
Itwasalsoconcluded thatthedosetothepublicfromamanuallyfilleddrumwouldbethesameasfromthesamedrumfilledinaremotemanner.SCN96-012(SE96-022)ThisSCNprovidedforachangetotheWNP-2PhysicalSecurityPlantoallowsecurityofficerswhohavelefttheprotected areatore-entertheprotected areawithoutbeingsubjected toametaldetectorsearch.Inaddition, theplanwasrevisedtoallowfortheremovalofprotected andvitalareakeysfromtheprotected areawhentheyareunderthecontrolandcustodyofon-dutysecurityforcepersonnel.
No changes to hardware were made by this change.The equivalent static method invoked as a replacement for the more rigorous, but less conservative"dynamic method, would not result in a less conservative design.The proposed change invokes static factors that are conservative.
Changingthesecurityplantoallowon-dutyarmedsecurityofficerstore-entertheprotected areawithoutbeingsubjected tometaldetectorsearcheswasendorsedbytheNRCinGenericLetter96-02,"Reconsideration ofNuclearPowerPlantSecurityRequirements Associated withanInternalThreat."Thestaffconsidered thatthischangecouldbemadetothesecurityplansinaccordance withtheprovisions of10CFR50.54(p).
The change to the use of good practice to establish margin for valve.clearance assessment, instead of a nominal 25 percent margin, has no impact on system or component operability.
IWithregardtoremovalofkeysfromtheprotected area,itwasconcluded fromthesafetyevaluation thattheabilitytoprotectvitalequipment targetsetscontinues tobemaintained bypromptresponsetoanyvitalareadooralarmwhenanunauthorized accessattempt'sdetectedbythesecuritysystem.
SCN 96415 (SE 95-089)This.SCN provided for a change to the FSAR to remove the description of the Mechanical Environmental Qualification (Ml~Program for safety-related mechanical and environmental augmented quality equipment.
Thekeycontrolrequirements identified in10CFR73.55(d)(9) arestillbeingmetandhavebeenincorporated intothesecurityplan.Thereareno10CFR73.55(d)(9) stipulations thatthesekeyscannotleavetheprotected areawhenunderthecontrolofasecurityofficer.Itwasalsoconcluded thatthelikelihood ofanattemptatradiological sabotageisnotafunctionofwhetherornotavitalareakeyistakenoff-sitewhileunderthecontrolofanauthorized on-dutysecurityforceofficer.SCN96-014(SE96-013)ThisSCNprovidedforclarification andconsistency pertaining toseismicqualification ofequipment andcomponents.
This change affects only the documentation process for MEQ Program equipment located in a harsh environment.
Themethodforassessing valveclearance wasalsomodified.
It was concluded from the safety evaluation that the suitability of equipment to design requirements, including environmental conditions, will continue to documented as part of engineering processes.
Itwasconcluded fromthesafetyevaluation thattheconsequences ofapreviously analyzedseismicordynamicaccidentwouldnotbeincreased bythesechanges.Consequences canonlyincreaseiftheequipment orcomponents analyzedaredamagedbytheevent.Theproposedchangesonlyinvolveanalytical methodsforseismicanddynamicqualification ofequipment andcomponents.
Elimination of the MEQ Program will not alter the equipment, equipment function, plant configuration or maintenance and surveillance requirements.
Theuseofacceptably conservative analytical methodsprecludes anyreduction insafetymarginforsystemsandcomponents.
I Existing engineering, procurement, maintenance and surveillance processes remain unchanged and will provide assurance that thy equipment continues to meet operability requireinents during normal operations and accident conditions.
Nochangestohardwareweremadebythischange.Theequivalent staticmethodinvokedasareplacement forthemorerigorous, butlessconservative "dynamicmethod,wouldnotresultinalessconservative design.Theproposedchangeinvokesstaticfactorsthatareconservative.
61 SCN 96-017 (SE 96-017)This SCN provided for a change to the FSAR to reflect the elimination of certain response time testing based on NRC endorsement of BWR Owner's Group Licensing Topical Report NEDO-32291,"System Analysis for Elimination of Selected Response Time Requirements," dated December 28, 1994.In addition, the remaining response time test requirements were relocated from the FSAR to the WNP-2 Licensee Controlled Specifications.
Thechangetotheuseofgoodpracticetoestablish marginforvalve.clearance assessment, insteadofanominal25percentmargin,hasnoimpactonsystemorcomponent operability.
It was concluded from the safety evaluation that none of the proposed changes resulted in a physical change or method of operation for any plant components.
SCN96415(SE95-089)This.SCNprovidedforachangetotheFSARtoremovethedescription oftheMechanical Environmental Qualification (Ml~Programforsafety-related mechanical andenvironmental augmented qualityequipment.
Through normal instrument loop calibrations, and other logic and system functional tests required by the.Technical Specifications, safety system actuations required by transient and accident analyses remain unchanged.
Thischangeaffectsonlythedocumentation processforMEQProgramequipment locatedinaharshenvironment.
Each of the selected sensor channels using alternative response time testing were reviewed to ensure that a qualitatively-assessed five second response time was consistent with the necessary actuation times specified within the accident analyses.There were no known failure modes that could be detected by resporise time testing that could also not be detected by other testing required by the Technical Specifications.'he proposed changes would also provide an improvement to plant safety and operation by reducing the time safety systems are unavailable, reducing the potential for safety system actuations, reducing plant shutdown risk, limiting radiation exposure to plant personnel, and eliminating the diversion of key,personnel resources to conduct unnecessary testing.SCN 96-021 (SE 96-020)'I This SCN provided for a change to the FSAR to reflect the use of Option B of 10CFR50, Appendix J, as the basis for the containment leakage testing program.The NRC has approved Option B which allows for implementation of a performance-based containment leakage rate testing program.This FSAR change implements a program which will assure leakage requirements are within current commitments and design basis assumptions.
Itwasconcluded fromthesafetyevaluation thatthesuitability ofequipment todesignrequirements, including environmental conditions, willcontinuetodocumented aspartofengineering processes.
It was concluded from the safety evaluation that this change would not impact normal plant operation, means of accident mitigation, or physically alter the design of the plant.The SCN was written to assure compliance with 10CFR50, Appendix J, as described in the'SER by using the guidelines established, in Regulatory'Guide 1.163.The change does not impact the configuration of any structure, system or component or.its ability to meet the designed safety function.Each valve and penetration will continue-to meet its designed function to isolate and maintain leakage within the specified limits.62  
Elimination oftheMEQProgramwillnotaltertheequipment, equipment
: function, plantconfiguration ormaintenance andsurveillance requirements.
IExistingengineering, procurement, maintenance andsurveillance processes remainunchanged andwillprovideassurance thatthyequipment continues tomeetoperability requireinents duringnormaloperations andaccidentconditions.
61 SCN96-017(SE96-017)ThisSCNprovidedforachangetotheFSARtoreflecttheelimination ofcertainresponsetimetestingbasedonNRCendorsement ofBWROwner'sGroupLicensing TopicalReportNEDO-32291, "SystemAnalysisforElimination ofSelectedResponseTimeRequirements,"
datedDecember28,1994.Inaddition, theremaining responsetimetestrequirements wererelocated fromtheFSARtotheWNP-2LicenseeControlled Specifications.
Itwasconcluded fromthesafetyevaluation thatnoneoftheproposedchangesresultedinaphysicalchangeormethodofoperation foranyplantcomponents.
Throughnormalinstrument loopcalibrations, andotherlogicandsystemfunctional testsrequiredbythe.Technical Specifications, safetysystemactuations requiredbytransient andaccidentanalysesremainunchanged.
Eachoftheselectedsensorchannelsusingalternative responsetimetestingwerereviewedtoensurethataqualitatively-assessed fivesecondresponsetimewasconsistent withthenecessary actuation timesspecified withintheaccidentanalyses.
Therewerenoknownfailuremodesthatcouldbedetectedbyresporise timetestingthatcouldalsonotbedetectedbyothertestingrequiredbytheTechnical Specifications.'he proposedchangeswouldalsoprovideanimprovement toplantsafetyandoperation byreducingthetimesafetysystemsareunavailable, reducingthepotential forsafetysystemactuations, reducingplantshutdownrisk,limitingradiation exposuretoplantpersonnel, andeliminating thediversion ofkey,personnel resources toconductunnecessary testing.SCN96-021(SE96-020)'IThisSCNprovidedforachangetotheFSARtoreflecttheuseofOptionBof10CFR50,AppendixJ,asthebasisforthecontainment leakagetestingprogram.TheNRChasapprovedOptionBwhichallowsforimplementation ofaperformance-based containment leakageratetestingprogram.ThisFSARchangeimplements aprogramwhichwillassureleakagerequirements arewithincurrentcommitments anddesignbasisassumptions.
Itwasconcluded fromthesafetyevaluation thatthischangewouldnotimpactnormalplantoperation, meansofaccidentmitigation, orphysically alterthedesignoftheplant.TheSCNwaswrittentoassurecompliance with10CFR50,AppendixJ,asdescribed inthe'SERbyusingtheguidelines established, inRegulatory'Guide 1.163.Thechangedoesnotimpacttheconfiguration ofanystructure, systemorcomponent or.itsabilitytomeetthedesignedsafetyfunction.
Eachvalveandpenetration willcontinue-tomeetitsdesignedfunctiontoisolateandmaintainleakagewithinthespecified limits.62  


SCN96-022(SE96-026)ThisSCNprovidedforclarification oftheas-builtconfiguration ofthepurgeexhaustportionofthecontrolroomremoteairintakesystem.Theoriginaldesigncomprised twopurgeexhaustsystemsconsisting oftwoelectro-hydraulically-operated (EHO)isolation valvesinseries.Asubsequent modification changedthedesignsuchthat,ineachpurgesystem,onevalveisequippedwithanelectro-hydraulic operatorandisinterlocked withitsassociated remoteairintakevalve.Theother.purgevalveismaintained open.Itwasconcluded fromthesafetyevaluation thatthisactivitydoesnotaffectthefunctionofthesevalves.ThisSCNwaswrittentocorrectthediscrepancy betweentheFSARandactualsystemconfiguration.
SCN 96-022 (SE 96-026)This SCN provided for clarification of the as-built configuration of the purge exhaust portion of the control room remote air intake system.The original design comprised two purge exhaust systems consisting of two electro-hydraulically-operated (EHO)isolation valves in series.A subsequent modification changed the design such that, in each purge system, one valve is equipped with an electro-hydraulic operator and is interlocked with its associated remote air intake valve.The other.purge valve is maintained open.It was concluded from the safety evaluation that this activity does not affect the function of these valves.This SCN was written to correct the discrepancy between the FSAR and actual system configuration.
Thetwodisabledvalvesaremaintained openbymeansofanEHOspringorbyasplitcollarandcapscrews.Thepositionofthevalvesisindicated inthecontrolroomandtheydonotinteractoraffectanyothersystemsorcomponents.
The two disabled valves are maintained open by means of an EHO spring or by a split collar and cap screws.The position of the valves is indicated in the control room and they do not interact or affect any other systems or components.
Thefunctionofthesevalvesistoremainopen.duringallnormalmodesofoperation andalsoduringaccidentandpost-accident conditions.
The function of these valves is to remain open.during all normal modes of operation and also during accident and post-accident conditions.
SCN96423(SE96-043)ThisSCNprovidedforachangetotheFSARtoreflecttheremovalofreference toReactorBuildingElectronics RoomAirConditioner RRA-AC-16.
SCN 96423 (SE 96-043)This SCN provided for a change to the FSAR to reflect the removal of reference to Reactor Building Electronics Room Air Conditioner RRA-AC-16.
Itwasconcluded fromthesafetyevaluation thatremoval,orabandonment inplace,ofthenon-safety related(QualityClassII)airconditioning unitwouldnotaffectanysafety-.relatedprocessequipment orsystems.Removalorabandonment wouldalsonothaveanimpactonanyaccidentanalysis.
It was concluded from the safety evaluation that removal, or abandonment in place, of the non-safety related (Quality Class II)air conditioning unit would not affect any safety-.related process equipment or systems.Removal or abandonment would also not have an impact on any accident analysis.The air conditioning unit is not used for.any safety function.Deactivation of this unit will lessen the heat load internal to the Reactor Building.Deactivation will also reduce electrical loads on the bus from which the unit is powered.~SCN 96-025 (SE 96-025)This SCN provided for a change to the FSAR to reQect''the deletion of reference to the Offgas Charcoal Vault Refrigeration and HVAC System.It was concluded from the safety evaluation that accident scenarios do not credit the Offgas Charcoal Vault Refrigeration and HVAC System with any accident mitigation responsibilities or functions.
Theairconditioning unitisnotusedfor.anysafetyfunction.
Furthermore, gross failure of the refrigeration system has no safety implications since the charcoal adsorbers can be isolated and the plant can be safely shutdown without"the refrigeration system operating.
Deactivation ofthisunitwilllessentheheatloadinternaltotheReactorBuilding.
Deactivation willalsoreduceelectrical loadsonthebusfromwhichtheunitispowered.~SCN96-025(SE96-025)ThisSCNprovidedforachangetotheFSARtoreQect''the deletionofreference totheOffgasCharcoalVaultRefrigeration andHVACSystem.Itwasconcluded fromthesafetyevaluation thataccidentscenarios donotcredittheOffgasCharcoalVaultRefrigeration andHVACSystemwithanyaccidentmitigation responsibilities orfunctions.
Furthermore, grossfailureoftherefrigeration systemhasnosafetyimplications sincethecharcoaladsorbers canbeisolatedandtheplantcanbesafelyshutdownwithout"the refrigeration systemoperating.
63  
63  


ThesystemhMnointeractions withanyequipment orsystemsthatactassafeguards orbarrierstopreventormitigatetheconsequences ofanaccident.
The system hM no interactions with any equipment or systems that act as safeguards or barriers to prevent or mitigate the consequences of an accident.The system was installed to allow for a sightly longer time for select radionuclides in the offgas stream by cooling the charcoal beds.The Technical Specification limiting dose rate of 332 millicuries/second after 30 minutes decay will be met, with significant margin, without the vault refrigeration system in operation.
Thesystemwasinstalled toallowforasightlylongertimeforselectradionuclides intheoffgasstreambycoolingthecharcoalbeds.TheTechnical Specification limitingdoserateof332millicuries/second after30minutesdecaywillbemet,withsignificant margin,withoutthevaultrefrigeration systeminoperation.
~SCN 96426 (SE 96-047)This SCN provided for editorial changes to the FSAR and to reflect existing Plant Service Water (TSW)configuration.
~SCN96426(SE96-047)ThisSCNprovidedforeditorial changestotheFSARandtoreflectexistingPlantServiceWater(TSW)configuration.
It was concluded from the safety evaluation that the changes do not in any way affect the safe operation of the facility.In addition, the intent of the FSAR and basic operation of the TSW System are unaffected by these changes.The TSW System is not required to perform any safety function.Implementation of this SCN does not result in any physical changes to the plant or any change to design temperattires and pressures used in evaluations of TSW System piping.The changes consist of clarification and correction of current information pertaining to the TSW System description.
Itwasconcluded fromthesafetyevaluation thatthechangesdonotinanywayaffectthesafeoperation ofthefacility.
SCN 96-027 (SE 96-019)This SCN provided for a change to the Fire Protection Program and Emergency Plan to reflect revision of the training requirements and relocation of requirements pertaining to fire brigade training program.It was concluded from the SCN that the changes to the fire brigade training program would not lower the ability of safety systems to perform during accident conditions or increase safety system challenges without compensating effects.The changes do not reduce.the level of overall training on the mitigation of radiological releases.The proposed changes do not modify plant equipment and would not result in any new failure modes than those previously evaluated.
Inaddition, theintentoftheFSARandbasicoperation oftheTSWSystemareunaffected bythesechanges.TheTSWSystemisnotrequiredtoperformanysafetyfunction.
The changes to fire brigade training have no impact on the probability of occurrence of fires, or other design basis events, and continue to ensure that any fires are extinguished in a safe manner.  
Implementation ofthisSCNdoesnotresultinanyphysicalchangestotheplantoranychangetodesigntemperattires andpressures usedinevaluations ofTSWSystempiping.Thechangesconsistofclarification andcorrection ofcurrentinformation pertaining totheTSWSystemdescription.
SCN96-027(SE96-019)ThisSCNprovidedforachangetotheFireProtection ProgramandEmergency Plantoreflectrevisionofthetrainingrequirements andrelocation ofrequirements pertaining tofirebrigadetrainingprogram.Itwasconcluded fromtheSCNthatthechangestothefirebrigadetrainingprogramwouldnotlowertheabilityofsafetysystemstoperformduringaccidentconditions orincreasesafetysystemchallenges withoutcompensating effects.Thechangesdonotreduce.thelevelofoveralltrainingonthemitigation ofradiological releases.
Theproposedchangesdonotmodifyplantequipment andwouldnotresultinanynewfailuremodesthanthosepreviously evaluated.
Thechangestofirebrigadetraininghavenoimpactontheprobability ofoccurrence offires,orotherdesignbasisevents,andcontinuetoensurethatanyfiresareextinguished inasafemanner.  
~e  
~e  
~SCN96-028(SE96-057)ThisSCNprovidedforachangetotheFSARtoreflectdeletionofreference tothebackupdieseldrivesforthenon-safety relatedmotor-driven aircompressors intheEmergency DieselGenerator StartingAirSystems(Divisions 1and2).Itwasconcluded fromthesafetyevaluation thatsparingthebackupstartingaircompressor dieseldriveswouldnotaffectairreceiverpressureorthenumber,ofstartsorstartingcapability oftheemergency dieselgenerators.
~SCN 96-028 (SE 96-057)This SCN provided for a change to the FSAR to reflect deletion of reference to the backup diesel drives for the non-safety related motor-driven air compressors in the Emergency Diesel Generator Starting Air Systems (Divisions 1 and 2).It was concluded from the safety evaluation that sparing the backup starting air compressor diesel drives would not affect air receiver pressure or the number, of starts or starting capability of the emergency diesel generators.
Thesafety-related portionsofthestartingairsystemareisolatedfromthenon-safety relatedportionsofthesystembymeansofcheckvalves.Theassumed'malfunction evaluated previously isthe'ailure ofanemergency dieselgenerator tostartandsupplypowertothecriticalelectrical buses.Therefore, theconsequences ofamalfunction ofanyequipment inthedieselstartingairsystemremainsunchanged bysparingthebackupstartingaircompressor dieseldrives.SCN96-029(SE96-042)ThisSCNprovidedforrevisionoftheOffsiteDoseCalculation Manual(ODCM)description oftheReactorBuildingEffluentMonitoring System.Thedescription ofthemainplantventintermediate andhighrangedetectors wasdeleted.~~Itwasconcluded fromthesafetyevaluation thatdetectors PRM-RE-1B andPRM-RE-1C areimportant tosafetyRegulatory Guide1.97monitors.
The safety-related portions of the starting air system are isolated from the non-safety related portions of the system by means of check valves.The assumed'malfunction evaluated previously is the'ailure of an emergency diesel generator to start and supply power to the critical electrical buses.Therefore, the consequences of a malfunction of any equipment in the diesel starting air system remains unchanged by sparing the backup starting air compressor diesel drives.SCN 96-029 (SE 96-042)This SCN provided for revision of the Offsite Dose Calculation Manual (ODCM)description of the Reactor Building Effluent Monitoring System.The description of the main plant vent intermediate and high range detectors was deleted.~~It was concluded from the safety evaluation that detectors PRM-RE-1B and PRM-RE-1C are important to safety Regulatory Guide 1.97 monitors.However, the description of the detectors was not required to be included in the ODCM.'he elimination of these monitors from the ODCM does not alter any design requiremehts or methods of operation for the components.
However,thedescription ofthedetectors wasnotrequiredtobeincludedintheODCM.'heelimination ofthesemonitorsfromtheODCMdoesnotalteranydesignrequiremehts ormethodsofoperation forthecomponents.
P~SCN 96-033 (SE.96-049)This SCN provided for a change to the FSAR to remove unnecessary detailed information pertauiing to theory of operation, provide additional clarification where necessary, and to reflect testing results for the low, intermediate and high range detectors in the Reactor Building Noble Gas Effluent Monitoring System.It was concluded from the safety evaluation that the radiation monitor function is unaffected'by this change.The monitors continue to provide sufficient sensitivity to meet accident monitoring requirements for all calculated maximum accident releases and allow for accurate offsite dose predictions and associated operator'decisions.
P~SCN96-033(SE.96-049)ThisSCNprovidedforachangetotheFSARtoremoveunnecessary detailedinformation pertauiing totheoryofoperation, provideadditional clarification wherenecessary, andtoreflecttestingresultsforthelow,intermediate andhighrangedetectors intheReactorBuildingNobleGasEffluentMonitoring System.Itwasconcluded fromthesafetyevaluation thattheradiation monitorfunctionisunaffected'by thischange.Themonitorscontinuetoprovidesufficient sensitivity tomeetaccidentmonitoring requirements forallcalculated maximumaccidentreleasesandallowforaccurateoffsitedosepredictions andassociated operator'decisions.
65 The tested span for the low range detector is within the range requirements necessary for ODCM monitoring.
65 Thetestedspanforthelowrangedetectoriswithintherangerequirements necessary forODCMmonitoring.
No physical plant equipment changes were made as a result of this FSAR revision.In addition, this change has no impact on any safety-related or'important to safety component function or method of operation.
Nophysicalplantequipment changesweremadeasaresultofthisFSARrevision.
~SCN 96-038 (SE 96-065)This SCN provided for a change to the FSAR to reflect deletion of a reference to Standby Liquid Control (SLC)System minimum area temperature because the SLC tank has safety-related heaters which keep the boron solution above saturation temperature.
Inaddition, thischangehasnoimpactonanysafety-related or'important tosafetycomponent functionormethodofoperation.
Furthermore, the piping from the SL'C storage tank to the pump suction valves is heat traced and insulated.
~SCN96-038(SE96-065)ThisSCNprovidedforachangetotheFSARtoreflectdeletionofareference toStandbyLiquidControl(SLC)Systemminimumareatemperature becausetheSLCtankhassafety-related heaterswhichkeeptheboronsolutionabovesaturation temperature.
It was concluded from the safety evaluation that the sodium pentaborate will be maintained above the saturation temperature.
Furthermore, thepipingfromtheSL'Cstoragetanktothepumpsuctionvalvesisheattracedandinsulated.
The SLC System is a backup reactivity control system to the Control Rod Drive System and this change does not involve any physical.changes to the plant.The'heaters are capable of maintaining the boron solution within design temperature ratings to ensure complete solubility of the solution.SCN 96-042 (SE 96452)This SCN provided for a change to the Fire Protection Program to reflect the establishment of a new fire barrier operability category,"Operable but Nonconforming," which would result in shiftly (once per 12 hours)fire tours.In addition, this SCN allows for changes to the FSAR for not requiring fire tours in the Main Control Room.The bases for fire-rated assemblies was also clarified.
Itwasconcluded fromthesafetyevaluation thatthesodiumpentaborate willbemaintained abovethesaturation temperature.
It was concluded from the safety evaluation that the changes would not lower the ability of safety systems to perform during accident conditions or increase safety system challenges without compensating effects.The changes do not reduce the level of overall training on the mitigation of radiological releases.The proposed changes would not result in any new failure modes than previously evaluated.
TheSLCSystemisabackupreactivity controlsystemtotheControlRodDriveSystemandthischangedoesnotinvolveanyphysical.
The changes have no impact on the probability of occurrence of fires, or other deign basis events, and continue to ensure that any fires are extinguished in a safe manner.Crediting the Main Control Room Operators to perform the function of a fire tour is acceptable.
changestotheplant.The'heaters arecapableofmaintaining theboronsolutionwithindesigntemperature ratingstoensurecompletesolubility ofthesolution.
The control room is continuously occupied and cognizant operators have the capability to detect power generation control complex and control room fires in the incipient stages.  
SCN96-042(SE96452)ThisSCNprovidedforachangetotheFireProtection Programtoreflecttheestablishment ofanewfirebarrieroperability
: category, "Operable butNonconforming,"
whichwouldresultinshiftly(onceper12hours)firetours.Inaddition, thisSCNallowsforchangestotheFSARfornotrequiring firetoursintheMainControlRoom.Thebasesforfire-rated assemblies wasalsoclarified.
Itwasconcluded fromthesafetyevaluation thatthechangeswouldnotlowertheabilityofsafetysystemstoperformduringaccidentconditions orincreasesafetysystemchallenges withoutcompensating effects.Thechangesdonotreducethelevelofoveralltrainingonthemitigation ofradiological releases.
Theproposedchangeswouldnotresultinanynewfailuremodesthanpreviously evaluated.
Thechangeshavenoimpactontheprobability ofoccurrence offires,orotherdeignbasisevents,andcontinuetoensurethatanyfiresareextinguished inasafemanner.Crediting theMainControlRoomOperators toperformthefunctionofafiretourisacceptable.
Thecontrolroomiscontinuously occupiedandcognizant operators havethecapability todetectpowergeneration controlcomplexandcontrolroomfiresintheincipient stages.  


2.7.4ProblemEvaluations
2.7.4 Problem Evaluations
"~~~~~~~Thissectioncontainsinformation pertaining toProblemEvaluation Requests(PERs)andisincludedpursuantto10CFR50.59.
"~~~~~~~This section contains information pertaining to Problem Evaluation Requests (PERs)and is included pursuant to 10CFR50.59.
PER296-0215(SE96-021)ThisPERdocumented asituation'where itwasnotedthataninflatable sealonEquipment HatchMT-DOOR-A2 intheReactorBuildingrailroadcranebayhasneverbeenused.Thisdoorispartofsecondary containment whenReactorBuildingRailroadCraneBayDoorR-106isopen.Theconcernwasthattheinflatable sealmayhavebeenrequiredforsecondary containment integrity.
PER 296-0215 (SE 96-021)This PER documented a situation'where it was noted that an inflatable seal on Equipment Hatch MT-DOOR-A2 in the Reactor Building railroad crane bay has never been used.This door is part of secondary containment when Reactor Building Railroad Crane Bay Door R-106 is open.The concern was that the inflatable seal may have been required for secondary containment integrity.
Thedisposition ofthisproblemwas"permanent accept-as-is."
The disposition of this problem was"permanent accept-as-is."It was concluded from the safety evaluation that the seal is not needed on MT-DOOR-A2.The door is a gasketed, airtight and water resistant component capable of withstanding maximum hydrostatic pressures in the event of a pipe rupture.Secondary containment was tested with Door R-106 open and then closed.Leakage rates were approximately the same for both conditions and were within required limits.The hatch is interlocked with Door R-106 such that both doors can not be open at the same time to preserve secondary containment integrity.
Itwasconcluded fromthesafetyevaluation thatthesealisnotneededonMT-DOOR-A2.Thedoorisagasketed, airtightandwaterresistant component capableofwithstanding maximumhydrostatic pressures intheeventofapiperupture.Secondary containment wastestedwithDoorR-106openandthenclosed.Leakagerateswereapproximately thesameforbothconditions andwerewithinrequiredlimits.Thehatchisinterlocked withDoorR-106suchthatbothdoorscannotbeopenatthesametimetopreservesecondary containment integrity.
The situation as described on this PER has no impact on the interlock function.It was also c'oncluded that the inflatable seal was not required for flooding considerations.
Thesituation asdescribed onthisPERhasnoimpactontheinterlock function.
PER 296-0273 (SE 96-036)This PER documented a situation where cracks were discovered in so'me of the plastic lugs molded into the relay bases and relay terminal bases (relay sockets)of certain"plug-in" type relay assemblies manufactured by ASEA.Some spalling was also noted around the mounting screws.The population consisted of seismic Category I relays used in safety-related applications.
Itwasalsoc'oncluded thattheinflatable sealwasnotrequiredforfloodingconsiderations.
The disposition of this problem was permanent accept-as-is.It was concluded from the safety evaluation that the relays were demonstrated by test and analysis to be capable of performing their intended safety function with the cracks/damage present.The seismic testing exceeded the required acceleration levels by a significant safety factor.The problems identified would not cause the relays to fail during any plant mode or transient.
PER296-0273(SE96-036)ThisPERdocumented asituation wherecrackswerediscovered inso'meoftheplasticlugsmoldedintotherelaybasesandrelayterminalbases(relaysockets)ofcertain"plug-in"typerelayassemblies manufactured byASEA.Somespallingwasalsonotedaroundthemountingscrews.Thepopulation consisted ofseismicCategoryIrelaysusedinsafety-related applications.
Thedisposition ofthisproblemwaspermanent accept-as-is.Itwasconcluded fromthesafetyevaluation thattherelaysweredemonstrated bytestandanalysistobecapableofperforming theirintendedsafetyfunctionwiththecracks/damage present.Theseismictestingexceededtherequiredacceleration levelsbyasignificant safetyfactor.Theproblemsidentified wouldnotcausetherelaystofailduringanyplantmodeortransient.
67 I'
67 I'
Basedonanevaluation ofrelayseismictestreportdata,itwasdetermined thatthefragility levelsusedintheseismictestsboundedtherequiredaccelerations forallthelocations wheretheidentified relaysareinstaHed.
Based on an evaluation of relay seismic test report data, it was determined that the fragility levels used in the seismic tests bounded the required accelerations for all the locations where the identified relays are instaHed.Furthermore, it was concluded that adequate margin exists t'o'conclude that the cracks/damage in the terminal base plastic of the relays was not detrimental to operation during a seismic event.PER 296-0276 (SE 96-045)This PER documented a situation where it was observed during inspection of the jet pumps that set screws on Jet Pump No.18 were not making contact with the inlet mixer'to provide for three-point stabilization.
Furthermore, itwasconcluded thatadequatemarginexistst'o'conclude thatthecracks/damage intheterminalbaseplasticoftherelayswasnotdetrimental tooperation duringaseismicevent.PER296-0276(SE96-045)ThisPERdocumented asituation whereitwasobservedduringinspection ofthejetpumpsthatsetscrewsonJetPumpNo.18werenotmakingcontactwiththeinletmixer'toprovideforthree-point stabilization.
A 10-mil gap was observed between the set screws of the restrainer brackets and the inlet mixer.The jet pump design and installation specifications required that there be no gaps at these points.The disposition of this problem was"permanent accept-as-is." It was concluded from the safety evaluation and a General Electric vibration analysis.that gaps of up 12 mils were acceptable.
A10-milgapwasobservedbetweenthesetscrewsoftherestrainer bracketsandtheinletmixer.Thejetpumpdesignandinstallation specifications requiredthattherebenogapsatthesepoints.Thedisposition ofthisproblemwas"permanent accept-as-is."
This was based on operating experience of other BWR 5 plants and the determination that, as long as in-vessel inspections at succeeding outages show that the set'crew gap is at 12 mils or less, continued operation is acceptable.
Itwasconcluded fromthesafetyevaluation andaGeneralElectricvibration analysis.
The function of the jet pumps would not be adversely affected when the gaps are maintained at this limit.Based on set screw gap vibration analysis and General Electric experience, operation with a gap of 10 mils during one cycle will not affect jet pump structural integrity.
thatgapsofup12milswereacceptable.
Thiswasbasedonoperating experience ofotherBWR5plantsandthedetermination that,aslongasin-vessel inspections atsucceeding outagesshowthattheset'crewgapisat12milsorless,continued operation isacceptable.
Thefunctionofthejetpumpswouldnotbeadversely affectedwhenthegapsaremaintained atthislimit.Basedonsetscrewgapvibration analysisandGeneralElectricexperience, operation withagapof10milsduringonecyclewillnotaffectjetpumpstructural integrity.
Additional
Additional
=operational cyclesmayalsocontinuewiththegapspresentaslongasthewidthislessthan12mils.(SE96-046)ThisPERalsodocumented asituation wheredamagewasobservedonaJetPumpNo.3inlet'mixer wedgeanditsassociated restrainer bracketwearpad.Thisproblemwasdiscovered duringjetpumpinspection efforts.Thedisposition ofthisproblemwas"interimaccept-as-is."
=operational cycles may also continue with the gaps present as long as the width is less than 12 mils.(SE 96-046)This PER also documented a situation where damage was observed on a Jet Pump No.3 inlet'mixer wedge and its associated restrainer bracket wear pad.This problem was discovered during jet pump inspection efforts.The disposition of this problem was"interim accept-as-is." It was concluded from the safety evaluation that the worn inlet'wedge and associated wear pad provide a fixed restraining point for the inlet mixer.It was also concluded that the extent of the damage was not sufficient to cause a failure of either the inlet mixer wedge or restrainer bracket wear pad.*r 68 Installation of the restrainer bracket wedge has restored the three-point restraint required to stabilize the inlet mixer and prevent further damage to the inlet mixer, wedge.Accordingly, it was concluded from evaluation that the current extent of the degradation would allow operation for an additional cycle.PER 296-0278 (SE 96-048)This PER described a situation where broken and'missing anodes on cooling coils were discovered during cleaning of the Standby Service Water (SSW)System, Loop B, room coolers.The anodes were originally supplied to minimize the potential for corrosion, given the water chemistry specified at the time of coil purchase.The disposition of this problem was"re-work." It was-concluded from the safety evaluation that the presence or absence of anodes has no effect on the ability of the SSW System to meet its cooling requirements.
Itwasconcluded fromthesafetyevaluation thattheworninlet'wedgeandassociated wearpadprovideafixedrestraining pointfortheinletmixer.Itwasalsoconcluded thattheextentofthedamagewasnotsufficient tocauseafailureofeithertheinletmixerwedgeorrestrainer bracketwearpad.*r68 Installation oftherestrainer bracketwedgehasrestoredthethree-point restraint requiredtostabilize theinletmixerandpreventfurtherdamagetotheinletmixer,wedge.Accordingly, itwasconcluded fromevaluation thatthecurrentextentofthedegradation wouldallowoperation foranadditional cycle.PER296-0278(SE96-048)ThisPERdescribed asituation wherebrokenand'missing anodesoncoolingcoilswerediscovered duringcleaningoftheStandbyServiceWater(SSW)System,LoopB,roomcoolers.Theanodeswereoriginally suppliedtominimizethepotential forcorrosion, giventhewaterchemistry specified atthetimeofcoilpurchase.
The status of the anodes in the SSW cooling coils does not impact the ability of the system and..associated components to mitigate the effects of design basis accidents or support safe shutdown of the plant.Flow to cooling coil tubes continues around the anode, so no significant flow reduction would be expected to occur if the anode was separated from the cap support.Flow through the cooling coil is adequate for any anode status (installed, removed or damaged).PER 2964360 (SE 95-102-01)
Thedisposition ofthisproblemwas"re-work."
This PER described a situation where a loose jet pump sensing line clamp was noted at location 10C.A 30-mil gap was observed at the top of the clamp and was due to a circumferential weld being at'the location of the clamp.The disposition of this problem was"permanent accept-as-is." It was concluded from the safety evaluation that clamp integrity was proven through the use of crimp and shaker tools.The clamp was confirmed to be tightly installed and no loosening due to vibration would be expected., Based on evaluation, it was concluded that the as-installed configuration of the clamp would not impact the lost parts analysis.It was also determined that there would be no impact on core re-flood analysis capability or emergency core cooling system perforinailce.
Itwas-concluded fromthesafetyevaluation thatthepresenceorabsenceofanodeshasnoeffectontheabilityoftheSSWSystemtomeetitscoolingrequirements.
ThestatusoftheanodesintheSSWcoolingcoilsdoesnotimpacttheabilityofthesystemand..associated components tomitigatetheeffectsofdesignbasisaccidents orsupportsafeshutdownoftheplant.Flowtocoolingcoiltubescontinues aroundtheanode,sonosignificant flowreduction wouldbeexpectedtooccuriftheanodewasseparated fromthecapsupport.Flowthroughthecoolingcoilisadequateforanyanodestatus(installed, removedordamaged).
PER2964360(SE95-102-01)
ThisPERdescribed asituation wherealoosejetpumpsensinglineclampwasnotedatlocation10C.A30-milgapwasobservedatthetopoftheclampandwasduetoacircumferential weldbeingat'thelocationoftheclamp.Thedisposition ofthisproblemwas"permanent accept-as-is."
Itwasconcluded fromthesafetyevaluation thatclampintegrity wasproventhroughtheuseofcrimpandshakertools.Theclampwasconfirmed tobetightlyinstalled andnoloosening duetovibration wouldbeexpected.,
Basedonevaluation, itwasconcluded thattheas-installed configuration oftheclampwouldnotimpactthelostpartsanalysis.
Itwasalsodetermined thattherewouldbenoimpactoncorere-floodanalysiscapability oremergency corecoolingsystemperforinailce.
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~PER296-0436(SE96-051)ThisPERdescribed asituation wheredirectbridgingcircuitseparation discrepancies wereidentified involving annunciator systemfieldcommoncircuitsforcables.ThecablesbridgeddirectlybetweenDivision1andDivision2raceways.
~PER 296-0436 (SE 96-051)This PER described a situation where direct bridging circuit separation discrepancies were identified involving annunciator system field common circuits for cables.The cables bridged directly between Division 1 and Division 2 raceways.The disposition of this problem was"interim accept-as-is." The WNP-2 Electrical Separation Criteria Document (DRD 201)was revised to provide clarification for allowing low energy direct circuit bridges.It was concluded from the safety evaluation that allowing non-class 1E, low energy (instrument and control)cables to bridge directly between redundant raceways would be acceptable when certain acceptable conditions are met.These changes maintain WNP-2 commitments to single failure criteria required by 10CFRSO, Criterion 17, for safety-related electric power systems and will not increase the probability of occurrence or consequences of any previously evaluated transient.
Thedisposition ofthisproblemwas"interimaccept-as-is."
These commitments to electrical'separation criteria ensure that, during accident conditions in conjunction with a postulated localized fire, redundant safety functions cannot be affected.PER 296-0438 (SE 96-58)This PER described a situation where it was noted that it took approximately 15 seconds to withdraw Control Rod Drive (CRD)System Mechanism CRD-DRVE-0627 from position 00 to 02.Normal drive speed is approximately one notch (six inches)every two seconds, with a full stroke in 48 seconds.The drive had to be withdrawn from position 00 using the continuous withdraw command.Beyond position 02, withdrawal speed was within normal limits.Rod insert motion was not affected and was within normal limits.The dispositions of this problem were"interim accept-as-is," and"permanent rework." These classifications were based on continued use of CRD-DRVE-0627 in the degraded condition pending rebuild during the Spring 1997 Maintenance and Refueling Outage.It was concluded from the safety evaluation that the problem was most likely caused by reversal or degradation of the drive piston drive-down seals (bridge and radial).A degraded or reversed drive-down seal assembly can, over time, impact normal.withdrawal movement of the drive.However, this condition would not affect normal insert motion or the safety-related scram function of the drive.There is also no postulated accident scenario that would require event mitigation through withdrawal of a control rod.-0 70
TheWNP-2Electrical Separation CriteriaDocument(DRD201)wasrevisedtoprovideclarification forallowinglowenergydirectcircuitbridges.Itwasconcluded fromthesafetyevaluation thatallowingnon-class 1E,lowenergy(instrument andcontrol)cablestobridgedirectlybetweenredundant racewayswouldbeacceptable whencertainacceptable conditions aremet.ThesechangesmaintainWNP-2commitments tosinglefailurecriteriarequiredby10CFRSO,Criterion 17,forsafety-related electricpowersystemsandwillnotincreasetheprobability ofoccurrence orconsequences ofanypreviously evaluated transient.
Thesecommitments toelectrical'separation criteriaensurethat,duringaccidentconditions inconjunction withapostulated localized fire,redundant safetyfunctions cannotbeaffected.
PER296-0438(SE96-58)ThisPERdescribed asituation whereitwasnotedthatittookapproximately 15secondstowithdrawControlRodDrive(CRD)SystemMechanism CRD-DRVE-0627 fromposition00to02.Normaldrivespeedisapproximately onenotch(sixinches)everytwoseconds,withafullstrokein48seconds.Thedrivehadtobewithdrawn fromposition00usingthecontinuous withdrawcommand.Beyondposition02,withdrawal speedwaswithinnormallimits.Rodinsertmotionwasnotaffectedandwaswithinnormallimits.Thedispositions ofthisproblemwere"interimaccept-as-is,"
and"permanent rework."Theseclassifications werebasedoncontinued useofCRD-DRVE-0627 inthedegradedcondition pendingrebuildduringtheSpring1997Maintenance andRefueling Outage.Itwasconcluded fromthesafetyevaluation thattheproblemwasmostlikelycausedbyreversalordegradation ofthedrivepistondrive-down seals(bridgeandradial).Adegradedorreverseddrive-down sealassemblycan,overtime,impactnormal.withdrawal movementofthedrive.However,thiscondition wouldnotaffectnormalinsertmotionorthesafety-related scramfunctionofthedrive.Thereisalsonopostulated accidentscenariothatwouldrequireeventmitigation throughwithdrawal ofacontrolrod.-070


Thissectioncontainsinformation'pertaining totestsandexperiments notdescribed intheFSARandisincludedpursuantto10CFR50.59.
This section contains information'pertaining to tests and experiments not described in the FSAR and is included pursuant to 10CFR50.59.
~PPM8.9.2(SE96-016)Thisprocedure providesinstructions formonitoring reactorcavityandspentfuelpooltemperatures toverifytheadequacyofnaturalcirculation asanalternate flow'mechanism whileinOperational Mode5(Refueling),
~PPM 8.9.2 (SE 96-016)This procedure provides instructions for monitoring reactor cavity and spent fuel pool temperatures to verify the adequacy of natural circulation as an alternate flow'mechanism while in Operational Mode 5 (Refueling), with the reactor cavity flooded and spent fuel pool gates removed.It was concluded from the safety evaluation that installation and removal of temperature monitoring equipment in the reactor pressure vessel and spent fuel pool would not introduce a new mechanism for initiation of any evaluated accidents.
withthereactorcavityfloodedandspentfuelpoolgatesremoved.Itwasconcluded fromthesafetyevaluation thatinstallation andremovaloftemperature monitoring equipment inthereactorpressurevesselandspentfuelpoolwouldnotintroduce anewmechanism forinitiation ofanyevaluated accidents.
In addition, this activity would not interfere with the normal sequence of events for mitigating such accidents.
Inaddition, thisactivitywouldnotinterfere withthenormalsequenceofeventsformitigating suchaccidents.
The monitoring equipment is non-obtrusive and does not rely on plant support equipment other than electrical power to operate.Should electrical power be lost to the temperature monitoring equipment, power could be restored using other power sources or battery-powered components.
Themonitoring equipment isnon-obtrusive anddoesnotrelyonplantsupportequipment otherthanelectrical powertooperate.Shouldelectrical powerbelosttothetemperature monitoring equipment, powercouldberestoredusingotherpowersourcesorbattery-poweredcomponents.
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PlantProcedure ChangesThesectioncontainsinformation pertaining toPlantProcedure Manual(PPM)changesandisincludedpursuantto10CFR50.59.
Plant Procedure Changes The section contains information pertaining to Plant Procedure Manual (PPM)changes and is included pursuant to 10CFR50.59.
PPM1.3.10C(SE93-093)Thisisanewprocedure whichdescribes theadministrative programforthecontroloftransient combustible materials andprovidesforperiodicinspection fortheaccumulation ofcombustibles.
PPM 1.3.10C (SE 93-093)This is a new procedure which describes the administrative program for the control of transient combustible materials and provides for periodic inspection for the accumulation of combustibles.
Existingprocedural guidanceinthisareawasmovedfromPPM1.3.10tothisnewprocedure.
Existing procedural guidance in this area was moved from PPM 1.3.10 to this new procedure.
Itwasconcluded fromthesafetyevaluation that,althoughsomeaspectsofthetransient
It was concluded from the safety evaluation that, although some aspects of the transient.combustible program are less restrictive than in previous procedural revisions, the controls are still adequate to ensure that combustibles are limited to the extent practical.
.combustible programarelessrestrictive thaninpreviousprocedural revisions, thecontrolsarestilladequatetoensurethatcombustibles arelimitedtotheextentpractical.
'hese changes are not in conflict with previous commitments and do not represent an appreciable reduction in the margin of fire safety.The changes implement a thorough and effective administrative program for control of transient combustibles,, while eliminating a few aspects which were deemed to be an overly conservative burden and marginal to safety.PPM 2.2.1A (SE 96-069)This is a new procedure for controlling Reactor Recirculation (RRC)System flow from the local control and diagnostic panel using the adjustable speed drive channels.This procedure was developed to allow for local control in the event of the loss of control of recirculation pump speed in the Main Control Room.It was concluded from the safety evaluation that this temporary arrangement does not increase the probability of a recirculation pump transient because the trip function of the Adjustable Speed Drive System has not changed.The recirculation flow control failure'is caused by the failure of the master controller.
'hesechangesarenotinconflictwithpreviouscommitments anddonotrepresent anappreciable reduction inthemarginoffiresafety.Thechangesimplement athoroughandeffective administrative programforcontroloftransient combustibles,,
This change is limited to setting the speed limiter to a lower value.The consequences of a flow controller failure would be reduced because the high speed limiter will be set lower that the design value.This change also has no impact on recirculation runback due to the loss of a reactor feedwater pump as long as reactor power is maintained less than the equivalent power that could be established on the 108 percent.rod line (<65 percent core thermal power).This-change does'ot impose any action or modification that is beyond the designed capability of the Adjustable Speed Drive System or associated components such as the RRC pumps...72  
whileeliminating afewaspectswhichweredeemedtobeanoverlyconservative burdenandmarginaltosafety.PPM2.2.1A(SE96-069)Thisisanewprocedure forcontrolling ReactorRecirculation (RRC)Systemflowfromthelocalcontrolanddiagnostic panelusingtheadjustable speeddrivechannels.
Thisprocedure wasdeveloped toallowforlocalcontrolintheeventofthelossofcontrolofrecirculation pumpspeedintheMainControlRoom.Itwasconcluded fromthesafetyevaluation thatthistemporary arrangement doesnotincreasetheprobability ofarecirculation pumptransient becausethetripfunctionoftheAdjustable SpeedDriveSystemhasnotchanged.Therecirculation flowcontrolfailure'iscausedbythefailureofthemastercontroller.
Thischangeislimitedtosettingthespeedlimitertoalowervalue.Theconsequences ofaflowcontroller failurewouldbereducedbecausethehighspeedlimiterwillbesetlowerthatthedesignvalue.Thischangealsohasnoimpactonrecirculation runbackduetothelossofareactorfeedwater pumpaslongasreactorpowerismaintained lessthantheequivalent powerthatcouldbeestablished onthe108percent.rod line(<65percentcorethermalpower).This-changedoes'otimposeanyactionormodification thatisbeyondthedesignedcapability oftheAdjustable SpeedDriveSystemorassociated components suchastheRRCpumps...72  


PPM2.8.1A(SE96-023)Thisisanewprocedure whichprovidesinstructions forOperations personnel tosupportanoutageoftheControlAirSystem(CAS)andServiceAir(SA)Systemformaintenance andinspection purposes.
PPM 2.8.1A (SE 96-023)This is a new procedure which provides instructions for Operations personnel to support an outage of the Control Air System (CAS)and Service Air (SA)System for maintenance and inspection purposes.This procedure can be implemented in Operational Mode 4 (Cold Shutdown), Mode 5 (Refueling) or Mode~(Refueling).
Thisprocedure canbeimplemented inOperational Mode4(ColdShutdown),
It was concluded from the safety evaluation that, during these operational modes, loss of CAS and SA would not result in the loss of any safety-related or important to safety functions.
Mode5(Refueling) orMode~(Refueling).
The CAS and SA systems are not safety-related and provide no safety functions.
Itwasconcluded fromthesafetyevaluation that,duringtheseoperational modes,lossofCASandSAwouldnotresultinthelossofanysafety-related orimportant tosafetyfunctions.
Loss of air to important to safety equipment results in the'equipment reverting to the safe condition (position).
TheCASandSAsystemsarenotsafety-related andprovidenosafetyfunctions.
It has been determined from failure analyses that no transients beyond those previously evaluated can occur from the loss of either (or both)system.In addition, it was~, concluded that complete loss of the systems would not affect the results of previously evaluated transients..
Lossofairtoimportant tosafetyequipment resultsinthe'equipment reverting tothesafecondition (position).
~PPM 2.8.5 (SE 96418)r This procedure provides for operation of the Fuel Pool Cooling (FPC)and Cleanup System during all operational modes.The procedure was revised to include a section on operation of the Residual Heat Removal (RHR)System in the FPC assist mode when RHR, Loop A, is not available for operation.
Ithasbeendetermined fromfailureanalysesthatnotransients beyondthosepreviously evaluated canoccurfromthelossofeither(orboth)system.Inaddition, itwas~,concluded thatcompletelossofthesystemswouldnotaffecttheresultsofpreviously evaluated transients..
A section was also added on operation of RHR, Loop A, in a mode to'assist in maintaining spent fuel pool temperatures if RHR, Loop B, becomes unavailable during or following a full core off-load.It was concluded from the safety evaluation that fuel handling and rod withdrawal accident analyses were unaffected by the decay heat removal operating mode of the RHR.System.Adequate decay heat removal from the reactor pressure vessel and spent fuel pool would be maintained.
~PPM2.8.5(SE96418)rThisprocedure providesforoperation oftheFuelPoolCooling(FPC)andCleanupSystemduringalloperational modes.Theprocedure wasrevisedtoincludeasectiononoperation oftheResidualHeatRemoval(RHR)SystemintheFPCassistmodewhenRHR,LoopA,isnotavailable foroperation.
Adequate level would be maintained in the spent fuel pool in accordance with system design, and temperatures would be within allowable limits.Both the FPC and RHR systems would continued to be operated within'their design limits.PPM 6.5.19 (SE 96-039)This procedure provides for resolution of jet pump set screw gap and wedge problems.The procedure was revised to allow for installation of restrainer bracket wedges,using a General Electric-approved procedure.
Asectionwasalsoaddedonoperation ofRHR,LoopA,inamodeto'assist inmaintaining spentfuelpooltemperatures ifRHR,LoopB,becomesunavailable duringorfollowing afullcoreoff-load.
The.original approach was to install restrainer bracket adjusting screws.-0 73 0
Itwasconcluded fromthesafetyevaluation thatfuelhandlingandrodwithdrawal accidentanalyseswereunaffected bythedecayheatremovaloperating modeoftheRHR.System.Adequatedecayheatremovalfromthereactorpressurevesselandspentfuelpoolwouldbemaintained.
It was concluded from'the safety evaluation that installation of the restrainer bracket wedges will replace the function of the restrainer bracket adjusting screws.The wedges will restore the degree of lateral support required for the original design configuration for the jet pump inlet mixer.The probability of failure of any jet pump component, and subsequent ejections of the jet pump mixer, remains unchanged by installation of the strainer wedges.Because there would.be no change in performance of the jet pump design feature, the functional capability of the jet pumps remains unchanged by installation of restrainer bracket w edges.PPM 8.3.339 (SE 96-106)This procedure provides for testing of the Digital Feedwater Level Control (DFWLC)and Adjustable Speed Drive (ASD)Systems.Included in the procedure was a test to demonstrate the feedwater level control system and recirculation flow run-back feature that would prevent a low vessel water level scram following a single feedwater pump trip during power operation.
Adequatelevelwouldbemaintained inthespentfuelpoolinaccordance withsystemdesign,andtemperatures wouldbewithinallowable limits.BoththeFPCandRHRsystemswouldcontinued tobeoperatedwithin'their designlimits.PPM6.5.19(SE96-039)Thisprocedure providesforresolution ofjetpumpsetscrewgapandwedgeproblems.
The safety evaluation was completed to determine the impact of either deferring or not completing this part of the procedure.
Theprocedure wasrevisedtoallowforinstallation ofrestrainer bracketwedges,using aGeneralElectric-approved procedure.
It was concluded from the safety evaluation that there were no unacceptable consequences in deferring or not performing this part of the procedure.
The.originalapproachwastoinstallrestrainer bracketadjusting screws.-073 0
A comparison of the as-tested ASD run-back rates to previous GE'-NE Control System analyses concluded that ASD run-back rates and DHVLC settings are adequate for avoiding a low level scram due to feedwater pump trip during power operation.
Itwasconcluded from'thesafetyevaluation thatinstallation oftherestrainer bracketwedgeswillreplacethefunctionoftherestrainer bracketadjusting screws.Thewedgeswillrestorethedegreeoflateralsupportrequiredfortheoriginaldesignconfiguration forthejetpumpinletmixer.Theprobability offailureofanyjetpumpcomponent, andsubsequent ejections ofthejetpumpmixer,remainsunchanged byinstallation ofthestrainerwedges.Becausetherewould.benochangeinperformance ofthejetpumpdesignfeature,thefunctional capability ofthejetpumpsremainsunchanged byinstallation ofrestrainer bracketwedges.PPM8.3.339(SE96-106)Thisprocedure providesfortestingoftheDigitalFeedwater LevelControl(DFWLC)andAdjustable SpeedDrive(ASD)Systems.Includedintheprocedure wasatesttodemonstrate thefeedwater levelcontrolsystemandrecirculation flowrun-backfeaturethatwouldpreventalowvesselwaterlevelscramfollowing asinglefeedwater pumptripduringpoweroperation.
The DKVLC and ASD recirculation flow control systems are expected to perform, as described in the FSAR, during a feedwater pump trip transient.
Thesafetyevaluation wascompleted todetermine theimpactofeitherdeferring ornotcompleting thispartoftheprocedure.
Based on system-level test results performed to date, it was determined that an additional integrated test to again'confirm system performance or assumptions used in plant transient analyses was unnecessary.
Itwasconcluded fromthesafetyevaluation thattherewerenounacceptable consequences indeferring ornotperforming thispartoftheprocedure.
PPM 8.3.372 (SE 96-024)This is a new procedure which provides for motor-operated valve in-situ differential pressure operability testing of High Pressure Core Spray (HPCS)System Injection Valve-HPCS-V-4.The procedure was developed to satisfy recommendations contained in the WNP-2 Motor Operated Valve Periodic Verification Plan and NRC Generic Letter 89-13.It may also be used for post-maintenance testing.)The HPCS System provides a mitigating function to maintain reactor inventory or=core spray after a loss of coolant accident..The purpose of performing differential pressure testing of HPCS-V-4 is to verify that this valve will properly operate.when required to perform its open and close safety functions.
Acomparison oftheas-tested ASDrun-backratestopreviousGE'-NEControlSystemanalysesconcluded thatASDrun-backratesandDHVLCsettingsareadequateforavoidingalowlevelscramduetofeedwater pumptripduringpoweroperation.
74 It was concluded from the safety evaluation that the test is conducted during cold shutdown conditions when the HPCS System is not required to be operable and alternate Emergency Core Cooling Systems (ECCS)are available.
TheDKVLCandASDrecirculation flowcontrolsystemsareexpectedtoperform,asdescribed intheFSAR,duringafeedwater pumptriptransient.
During the test, reactor grade water from the condensate storage tanks would be injected into the vessel using normal injection alignment when the vessel is vented'(head vent valves open or head removed).The automatic interlock for closure of HPCS-V-4 at the Level 8 setpoint (+54.5 inches)would be maintained to prevent potential overpressurization or overfill of the vessel.;It was also concluded that the test conditions established by the procedure would not result in exceeding HPCS System or reactor vessel design or operating limits.PPM 9.3.39 (SE 96-050)This procedure provides for installation of the cycle-specific input deck and the CREATE base data into the POWERPLEX Core Monitoring Software System (CMSS).The procedure was revised to incorporate the POWERPLEX input database for Cycle 12.It was concluded from the safety evaluation that the core monitoring system does not interact with plant equipment and will not initiate any previously evaluated accident.The update of the input data base is performed only after completion of detailed engineering calculations.
Basedonsystem-level testresultsperformed todate,itwasdetermined thatanadditional integrated testtoagain'confirmsystemperformance orassumptions usedinplanttransient analyseswasunnecessary.
The POWP26'LEX CMSS is used to verify compliance with specific core operating limits.These operating limits are specifically designed to protect against the most limiting accident types.The proposed update will provide the POWERPLEX monitoring system with the ability to use Cycle 12-approved core operating limits for both ABB and-Siemens fuel.Therefore, the system will maintain the ability to provide core operating limit evaluations.
PPM8.3.372(SE96-024)Thisisanewprocedure whichprovidesformotor-operated valvein-situdifferential pressureoperability testingofHighPressureCoreSpray(HPCS)SystemInjection Valve-HPCS-V-4.
This activity does not change the method by which the'plant is operated in accordance with procedures.
Theprocedure wasdeveloped tosatisfyrecommendations contained intheWNP-2MotorOperatedValvePeriodicVerification PlanandNRCGenericLetter89-13.Itmayalsobeusedforpost-maintenance testing.)TheHPCSSystemprovidesamitigating functiontomaintainreactorinventory or=coresprayafteralossofcoolantaccident..The purposeofperforming differential pressuretestingofHPCS-V-4istoverifythatthisvalvewillproperlyoperate.whenrequiredtoperformitsopenandclosesafetyfunctions.
This procedural revision will allow for core monitoring to be performed using appropriate methodology consistent with the Cycle-12 licensing analyses.~PPM 10.3.2 (SE 95-043)This procedure provides instructions for installation and removal of reactor cavity shield plugs and gates.The procedure was revised to allow for removal of the lower set of reactor pressure vessel shield plugs during Operational Mode 3 (Hot Shutdown).
74 Itwasconcluded fromthesafetyevaluation thatthetestisconducted duringcoldshutdownconditions whentheHPCSSystemisnotrequiredtobeoperableandalternate Emergency CoreCoolingSystems(ECCS)areavailable.
In addition, the lift rating of certain slings was increased to 50 tons.75 It was concluded from the safety evaluation that the fuel handling accident (dropped fuel bundle into the spent fuel pool)would not be affected by removal of the shield plugs.Removal of the plugs would follow a safe load path which does not include travel over the spent fuel pool.Current procedures allow removal of the top-layer reactor cavity shield plugs while.the reactor is critical.Removing the lower set of reactor cavity shield plugs in Operational Mode 3 would not increase the consequences of a previously evaluated accident.A safety factor of 5:1 would still be maintained by increasing the rating of the lifting slings.PPM 10.24.17 (SE 96-067)This procedure provides instructions for performing and documenting control rod friction and settle differential pressure testing.The procedure was revised to incorporate enhanced test equipment connection methodology during plant operation.
Duringthetest,reactorgradewaterfromthecondensate storagetankswouldbeinjectedintothevesselusingnormalinjection alignment whenthevesselisvented'(head ventvalvesopenorheadremoved).
Prior to revision, differential pressure testing equipment was connected to control rod drive insert and withdraw line.high point vent valves.This was changed to allow for connection of the testing equipment to manifold test ports on the associated hydraulic control unit.It was concluded from the safety evaluation that performance of differential pressure testing in accordance with the revised test equipment connection methodology is a controlled evolution specified by the original equipment manufacturer.
Theautomatic interlock forclosureofHPCS-V-4attheLevel8setpoint(+54.5inches)wouldbemaintained topreventpotential overpressurization oroverfillofthevessel.;Itwasalsoconcluded thatthetestconditions established bytheprocedure wouldnotresultinexceeding HPCSSystemorreactorvesseldesignoroperating limits.PPM9.3.39(SE96-050)Thisprocedure providesforinstallation ofthecycle-specific inputdeckandtheCREATEbasedataintothePOWERPLEX CoreMonitoring SoftwareSystem(CMSS).Theprocedure wasrevisedtoincorporate thePOWERPLEX inputdatabaseforCycle12.Itwasconcluded fromthesafetyevaluation thatthecoremonitoring systemdoesnotinteractwithplantequipment andwillnotinitiateanypreviously evaluated accident.
This.change provides a reliable means to isolate the test equipment from the reactor pressure boundary if necessary.
Theupdateoftheinputdatabaseisperformed onlyaftercompletion ofdetailedengineering calculations.
Test connections also restrict the flow path such that any postulated leakage due to breach of the temporary test equipment is bounded by the transient assumed for an instrument line break outside containment.
ThePOWP26'LEX CMSSisusedtoverifycompliance withspecificcoreoperating limits.Theseoperating limitsarespecifically designedtoprotectagainstthemostlimitingaccidenttypes.TheproposedupdatewillprovidethePOWERPLEX monitoring systemwiththeabilitytouseCycle12-approved coreoperating limitsforbothABBand-Siemensfuel.Therefore, thesystemwillmaintaintheabilitytoprovidecoreoperating limitevaluations.
PPM 10.25.1SS (SE 96-082)'his procedure provides for monthly inspections of 10CFR50, Appendix R, emergency'ighting battery units.The procedure was revised to correct and clarify emergency battery light discharge rates such that the values would be in conformance with the safe shutdown calculation and manufacturer information.
Thisactivitydoesnotchangethemethodbywhichthe'plant isoperatedinaccordance withprocedures.
In addition, guidance was added pertaining to the posting of approved portable battery-powered lanterns as compensatory measures during discharge testing..It was concluded from the safety evaluation that there would be no new accident scenarios introduced by these changes.All plant systems and components required to mitigate the consequences of accidents.
Thisprocedural revisionwillallowforcoremonitoring tobeperformed usingappropriate methodology consistent withtheCycle-12licensing analyses.
previously evaluated would be unaffected by the.changes.Rev'ising the procedure to reflect emergency battery light discharge capacity.contained in the shutdown calculation aligns-it with plant design.Adding portable lanterns as compensatory.measures during discharge testing increases the ability of providing lighting in support of post-fire shutdown operator actions'.'76 The sole purpose of the emergency battery lighting is to provide illumination for personnel exiting the plant during a fire or station blackout.~PPM 16.1.1 (SE 96-040)This procedure provides for channel calibration of Reactor Building Effluent Low Range Radiation Monitor PRM-LCRM-1A.
~PPM10.3.2(SE95-043)Thisprocedure providesinstructions forinstallation andremovalofreactorcavityshieldplugsandgates.Theprocedure wasrevisedtoallowforremovalofthelowersetofreactorpressurevesselshieldplugsduringOperational Mode3(HotShutdown).
The procedure was revised to relocate the Offsite Dose Calculation Manual (ODCM)high radiation alarm setpoint from the intermediate range detector to the low range detector.It was concluded from the safety evaluation that the stack monitoring system consists of passive instrumentation and is used to monitor post accident releases from the main plant vent elevated release point.The stack monitoring system does not initiate any'accidents.
Inaddition, theliftratingofcertainslingswasincreased to50tons.75 Itwasconcluded fromthesafetyevaluation thatthefuelhandlingaccident(droppedfuelbundleintothespentfuelpool)wouldnotbeaffectedbyremovaloftheshieldplugs.Removaloftheplugswouldfollowasafeloadpathwhichdoesnotincludetraveloverthespentfuelpool.Currentprocedures allowremovalofthetop-layer reactorcavityshieldplugswhile.thereactoriscritical.
This change moves the ODCM high radiation alarm function from the intermediate range detector to the more sensitive low range detector, tightens tolerances for loop checks, and allows for adjustment of the normalize potentiometer for testing purposes.The accident monitoring function of the stack monitor would be unaffected by these changes.Failure consequences remain unchanged from the alarm/setpoint relocation.
RemovingthelowersetofreactorcavityshieldplugsinOperational Mode3wouldnotincreasetheconsequences ofapreviously evaluated accident.
The consequences of a failure of the low range detector would be identical to that of the original intermediate range detector.77 Miscellaneous
Asafetyfactorof5:1wouldstillbemaintained byincreasing theratingoftheliftingslings.PPM10.24.17(SE96-067)Thisprocedure providesinstructions forperforming anddocumenting controlrodfrictionandsettledifferential pressuretesting.Theprocedure wasrevisedtoincorporate enhancedtestequipment connection methodology duringplantoperation.
'his section contains information pertaining to other plant activities and is included pursuant to 10CFR50.59.
Priortorevision, differential pressuretestingequipment wasconnected tocontrolroddriveinsertandwithdrawline.highpointventvalves.Thiswaschangedtoallowforconnection ofthetestingequipment tomanifoldtestportsontheassociated hydraulic controlunit.Itwasconcluded fromthesafetyevaluation thatperformance ofdifferential pressuretestinginaccordance withtherevisedtestequipment connection methodology isacontrolled evolution specified bytheoriginalequipment manufacturer.
~Clearance Order 93-12-0045 (SE 96-059)This clearance order allowed for deactivation of Process Sampling System (PSR)Booster Pump PSR-P-26.The pump is used to boost sample flow to Sample Point 26.This temporary change was to remain in place until such time that a permanent resolution to correct sample tube blocking problems can be implemented.
This.changeprovidesareliablemeanstoisolatethetestequipment fromthereactorpressureboundaryifnecessary.
It was concluded from the safety evaluation that the liquid sampling system has no safety or direct process control functions.
Testconnections alsorestricttheflowpathsuchthatanypostulated leakageduetobreachofthetemporary testequipment isboundedbythetransient assumedforaninstrument linebreakoutsidecontainment.
Deactivation of the booster pump or isolation of the sample lines would not impact the operation of any equipment important to safety.This activity would not impact any system used to ensure the integrity of the reactor coolant pressure boundary, the capability to shutdown the reactor, or the capability to prevent accidents.
PPM10.25.1SS (SE96-082)'his procedure providesformonthlyinspections of10CFR50,AppendixR,emergency
Chemical analysis of process system liquid will continue through grab sampling at arr alternate point (Sample Rack RCC-SR-44).
'ightingbatteryunits.Theprocedure wasrevisedtocorrectandclarifyemergency batterylightdischarge ratessuchthatthevalueswouldbeinconformance withthesafeshutdowncalculation andmanufacturer information.
~Computer Change Request CCR-TE-95413 (SE 96-001)This change request modified the Siemens Power Corporation POWERPLEX Core Monitoring Sofbvare System (CMSS)to allow the MICROBURN code to use the ABB critical power correlation for monitoring ABB fuel.The POWERPLEX CMSS provides core monitoring capabilities by monitoring power distribution.
Inaddition, guidancewasaddedpertaining tothepostingofapprovedportablebattery-powered lanternsascompensatory measuresduringdischarge testing..
It was concluded from the safety evaluation that the POWERPLEX CMSS is not physically connected to any plant safety systems or any other plant systems important to safety, with the exception that power for the computer is from uninteruptible power source IN-1.The POWERPLEX CMSS does not cause any installed plant safety systems to activate.The computer on which the system is installed is Quality Class G hardware and uses a standard Digital VMS operating system.There are no environmental or technical qualifications for the computer or its operating system.Since the POWERPLEX CMSS is not physically connected to any plant safety systems, it is not and can not be an initiator for any plant transient or accident.Furthermore, changes to the computer program would not change any operational modes, operating procedures, or method of operating plant equipment.
Itwasconcluded fromthesafetyevaluation thattherewouldbenonewaccidentscenarios introduced bythesechanges.Allplantsystemsandcomponents requiredtomitigatetheconsequences ofaccidents.
previously evaluated wouldbeunaffected bythe.changes.
Rev'ising theprocedure toreflectemergency batterylightdischarge capacity.
contained intheshutdowncalculation aligns-itwithplantdesign.Addingportablelanternsascompensatory.measures duringdischarge testingincreases theabilityofproviding lightinginsupportofpost-fire shutdownoperatoractions'.
'76 Thesolepurposeoftheemergency batterylightingistoprovideillumination forpersonnel exitingtheplantduringafireorstationblackout.
~PPM16.1.1(SE96-040)Thisprocedure providesforchannelcalibration ofReactorBuildingEffluentLowRangeRadiation MonitorPRM-LCRM-1A.
Theprocedure wasrevisedtorelocatetheOffsiteDoseCalculation Manual(ODCM)highradiation alarmsetpointfromtheintermediate rangedetectortothelowrangedetector.
Itwasconcluded fromthesafetyevaluation thatthestackmonitoring systemconsistsofpassiveinstrumentation andisusedtomonitorpostaccidentreleasesfromthemainplantventelevatedreleasepoint.Thestackmonitoring systemdoesnotinitiateany'accidents.
ThischangemovestheODCMhighradiation alarmfunctionfromtheintermediate rangedetectortothemoresensitive lowrangedetector, tightenstolerances forloopchecks,andallowsforadjustment ofthenormalize potentiometer fortestingpurposes.
Theaccidentmonitoring functionofthestackmonitorwouldbeunaffected bythesechanges.Failureconsequences remainunchanged fromthealarm/setpoint relocation.
Theconsequences ofafailureofthelowrangedetectorwouldbeidentical tothatoftheoriginalintermediate rangedetector.
77 Miscellaneous
'hissectioncontainsinformation pertaining tootherplantactivities andisincludedpursuantto10CFR50.59.
~Clearance Order93-12-0045 (SE96-059)Thisclearance orderallowedfordeactivation ofProcessSamplingSystem(PSR)BoosterPumpPSR-P-26.
ThepumpisusedtoboostsampleflowtoSamplePoint26.Thistemporary changewastoremaininplaceuntilsuchtimethatapermanent resolution tocorrectsampletubeblockingproblemscanbeimplemented.
Itwasconcluded fromthesafetyevaluation thattheliquidsamplingsystemhasnosafetyordirectprocesscontrolfunctions.
Deactivation oftheboosterpumporisolation ofthesamplelineswouldnotimpacttheoperation ofanyequipment important tosafety.Thisactivitywouldnotimpactanysystemusedtoensuretheintegrity ofthereactorcoolantpressureboundary, thecapability toshutdownthereactor,orthecapability topreventaccidents.
Chemicalanalysisofprocesssystemliquidwillcontinuethroughgrabsamplingatarralternate point(SampleRackRCC-SR-44).
~ComputerChangeRequestCCR-TE-95413 (SE96-001)ThischangerequestmodifiedtheSiemensPowerCorporation POWERPLEX CoreMonitoring SofbvareSystem(CMSS)toallowtheMICROBURN codetousetheABBcriticalpowercorrelation formonitoring ABBfuel.ThePOWERPLEX CMSSprovidescoremonitoring capabilities bymonitoring powerdistribution.
Itwasconcluded fromthesafetyevaluation thatthePOWERPLEX CMSSisnotphysically connected toanyplantsafetysystemsoranyotherplantsystemsimportant tosafety,withtheexception thatpowerforthecomputerisfromuninteruptible powersourceIN-1.ThePOWERPLEX CMSSdoesnotcauseanyinstalled plantsafetysystemstoactivate.
Thecomputeronwhichthesystemisinstalled isQualityClassGhardwareandusesastandardDigitalVMSoperating system.Therearenoenvironmental ortechnical qualifications forthecomputeroritsoperating system.SincethePOWERPLEX CMSSisnotphysically connected toanyplantsafetysystems,itisnotandcannotbeaninitiator foranyplanttransient oraccident.
Furthermore, changestothecomputerprogramwouldnotchangeanyoperational modes,operating procedures, ormethodofoperating plantequipment.
78 I'
78 I'
CoreOperating LimitsReport96-12:Rev 0(SE96-031)Thisrevisionallowedforimplementation oftheWNP-2,Cycle12,CoreOperating LimitsReport(COLR).Theproposedactivityconsisted ofoperation oftheCycle12reloadcorewithcorethermallimitswhichhavebeendeveloped withNRC-approved methodologies.
Core Operating Limits Report 96-12:Rev 0 (SE 96-031)This revision allowed for implementation of the WNP-2, Cycle 12, Core Operating Limits Report (COLR).The proposed activity consisted of operation of the Cycle 12 reload core with core thermal limits which have been developed with NRC-approved methodologies.
Thethermallimitsarespecified intheCOLR.TheCycle-12reloadcoreconsistsoff'uelassemblies oftheSVEA-96design,Siemens9x9-9xdesignandSiemens8x8-2design.TheSVEA-96assemblies arenewtoWNP-2withthisreload.Itwasconcluded fromthesafetyevaluation thatoperation ofCycle12withinthethermalHmitsdefinedinCOLR96-12doesnotincreasetheconsequences oftheanalyzedanticipated operational occurrences oraccidents becausethemechanical, thermal'.
The thermal limits are specified in the COLR.The Cycle-12 reload core consists of f'uel assemblies of the SVEA-96 design, Siemens 9x9-9x design and Siemens 8x8-2 design.The SVEA-96 assemblies are new to WNP-2 with this reload.It was concluded from the safety evaluation that operation of Cycle 12 within the thermal Hmits defined in COLR 96-12 does not increase the consequences of the analyzed anticipated operational occurrences or accidents because the mechanical, thermal'.hydraulic and LOCA design criteria imposed on the fuel to protect it during these events are met.Analyses of the previously-evaluated accidents and bounding anticipated operational occurrences systematically addressed all fuel characteristics, fuel related equipment malfunctions and operator actions.The depth of these analyses precludes the possibility of an accident which has not been previously evaluated, provided that the linear heat generation rate and other thermal limits as established by the COLR are followed.Fire Protection:
hydraulic andLOCAdesigncriteriaimposedonthefueltoprotectitduringtheseeventsaremet.Analysesofthepreviously-evaluated accidents andboundinganticipated operational occurrences systematically addressed allfuelcharacteristics, fuelrelatedequipment malfunctions andoperatoractions.Thedepthoftheseanalysesprecludes thepossibility ofanaccidentwhichhasnotbeenpreviously evaluated, providedthatthelinearheatgeneration rateandotherthermallimitsasestablished bytheCOLRarefollowed.
Penetration Seals (SE 96-053)This.activity consisted of the continuous use of fire tours as adequate ongoing compensatory measures for inoperable fire-rated penetration seals.It was concluded'rom the safety evaluation that fires are neither initiators nor mitigators of any previously analyzed transients.
FireProtection:
These tours can decrease the probability of occurrence of plant fires in that they may discover smoldering pre-fire conditions which could be mitigated prior to outbreak.This activity does not degrade or prevent actions assumed in the accident analysis, adversely affect fission product barriers, alter any assumptions made in evaluating radiological consequences of an accident, or physically modify any plant component or system operation.
Penetration Seals(SE96-053)This.activity consisted ofthecontinuous useoffiretoursasadequateongoingcompensatory measuresforinoperable fire-rated penetration seals.Itwasconcluded'rom thesafetyevaluation thatfiresareneitherinitiators normitigators ofanypreviously analyzedtransients.
~Fire Protection:
Thesetourscandecreasetheprobability ofoccurrence ofplantfiresinthattheymaydiscoversmoldering pre-fireconditions whichcouldbemitigated priortooutbreak.
Vertical Cable Trays (SE 96-054)This activity consisted of the continuous use of fire tours as adequate ongoing compensatory measures for inoperable.
Thisactivitydoesnotdegradeorpreventactionsassumedintheaccidentanalysis, adversely affectfissionproductbarriers, alteranyassumptions madeinevaluating radiological consequences ofanaccident, orphysically modifyanyplantcomponent orsystemoperation.
Thermo-Lag coated vertical cable tray fire breaks.79 It was concluded from the safety evaluation that fires are neither initiators nor mitigators of any previously analyzed transients.
~FireProtection:
Fire tours can decrease the probability of occurrence of plant fires in that they may discover smoldering pre-fire conditions which could be mitigated prior to outbreak.h This activity does not degrade or prevent actions assumed in the accident analysis, adversely affect fission product barriers, alter any assumptions made in evaluating radiological consequences of an accident, or physically modify any plant component or system operation.
VerticalCableTrays(SE96-054)Thisactivityconsisted ofthecontinuous useoffiretoursasadequateongoingcompensatory measuresforinoperable.
~Technical Evaluation Request 96-0009-0 (SE 96-028)This Technical-Evaluation Request provided for the relocation of two Bailey cards and installation of sliding link terminal blocks for Primary Contairiment Sump Flow Monitoring System and Reactor Water Cleanup System isolation instrumentation (LD-~SUM-604 and FDR-SQRT-38).
Thermo-Lag coatedverticalcabletrayfirebreaks.79 Itwasconcluded fromthesafetyevaluation thatfiresareneitherinitiators normitigators ofanypreviously analyzedtransients.
It was concluded from the safety evaluation that the function of the instruments would not be affected by the change in position or the addition of terminal blocks.There are no transients or accidents that'would be affected by this activity.The cards were simply moved to a new location within the same rack and would provide the same functions as the original configuration.
Firetourscandecreasetheprobability ofoccurrence ofplantfiresinthattheymaydiscoversmoldering pre-fireconditions whichcouldbemitigated priortooutbreak.
The installation of the terminal blocks with sliding link disconnects allows for system testing without removing any wiring.System interfaces are not changed and design basis requirements for electrical separation, seismic and instrument loop tolerances,were maintained.
hThisactivitydoesnotdegradeorpreventactionsassumedintheaccidentanalysis, adversely affectfissionproductbarriers, alteranyassumptions madeinevaluating radiological consequences ofanaccident, orphysically modifyanyplantcomponent orsystemoperation.
Technical Evaluation Request 96-0127-0 (SE 96-109)This Technical Evaluation Request'provided for the permanent designation of temporary.valves and spectacle flanges installed in the water box drain lines to allow for on-line tube plugging in the main condenser.
~Technical Evaluation Request96-0009-0 (SE96-028)ThisTechnical
It was concluded from the safety evaluation that implementation of this change would not adversely impact condensate system piping stress evaluations.
-Evaluation Requestprovidedfortherelocation oftwoBaileycardsandinstallation ofslidinglinkterminalblocksforPrimaryContairiment SumpFlowMonitoring SystemandReactorWaterCleanupSystemisolation instrumentation (LD-~SUM-604andFDR-SQRT-38).
The pressure ratings of the current components are within the required tolerances for the system.The-condensate system is a Quality Class II, non-safety related system.The system is,not required to perform any safety function such as maintaining the integrity of the reactor coolant pressure boundary or mitigating the consequences of an accident.80  
Itwasconcluded fromthesafetyevaluation thatthefunctionoftheinstruments wouldnotbeaffectedbythechangeinpositionortheadditionofterminalblocks.Therearenotransients oraccidents that'would beaffectedbythisactivity.
Thecardsweresimplymovedtoanewlocationwithinthesamerackandwouldprovidethesamefunctions astheoriginalconfiguration.
Theinstallation oftheterminalblockswithslidinglinkdisconnects allowsforsystemtestingwithoutremovinganywiring.Systeminterfaces arenotchangedanddesignbasisrequirements forelectrical separation, seismicandinstrument looptolerances,were maintained.
Technical Evaluation Request96-0127-0 (SE96-109)ThisTechnical Evaluation Request'provided forthepermanent designation oftemporary
.valvesandspectacle flangesinstalled inthewaterboxdrainlinestoallowforon-linetubeplugginginthemaincondenser.
Itwasconcluded fromthesafetyevaluation thatimplementation ofthischangewouldnotadversely impactcondensate systempipingstressevaluations.
Thepressureratingsofthecurrentcomponents arewithintherequiredtolerances forthesystem.The-condensate systemisaQualityClassII,non-safety relatedsystem.Thesystemis,notrequiredtoperformanysafetyfunctionsuchasmaintaining theintegrity ofthereactorcoolantpressureboundaryormitigating theconsequences ofanaccident.
80  


Technical Evaluation Request96-0178-0 (SE96-102)ThisTechnical Evaluation Requestprovidedforthereplacement ofseveralglobeandgatepatternvalvesinthePlantServiceWater(TSW)Systemwithballpatternvalves.Thevalveswerereplacedtoallowfordrainwatertoberoutedthroughtheequipment/floor drainsystem.Itwasconcluded fromthesafetyevaluation thatthereplacement ballpatternvalveshaveequalorgreaterpressureratingsthantheexistingvalvesandtheyweighless.TheTSWisaQualityClassII,non-safety relatedsystem.Thesystemisnotrequiredtoperformanysafetyfunctionsuchasmaintaining theintegrity ofthereactorcoolantpressureboundaryormitigating theconsequences ofanaccident.
Technical Evaluation Request 96-0178-0 (SE 96-102)This Technical Evaluation Request provided for the replacement of several globe and gate pattern valves in the Plant Service Water (TSW)System with ball pattern valves.The valves were replaced to allow for drain water to be routed through the equipment/floor drain system.It was concluded from the safety evaluation that the replacement ball pattern valves have equal or greater pressure ratings than the existing valves and they weigh less.The TSW is a Quality Class II, non-safety related system.The system is not required to perform any safety function such as maintaining the integrity of the reactor coolant pressure boundary or mitigating the consequences of an accident.Stress evaluations for small bore piping and valves in these applications would not be adversely impacted by this change.Work Order YS6901 (SE 96-009)This work order provided for repair of Demineralized Water System Valve DW-V-100/57 and isolation of the component from the system by means of a freeze seal in'the horizontal run of piping upstream of the valve.It was concluded from the safety evaluation that the only credible problem area of concern during isolation of the water supply to DW-V-100/57 would be flooding of the Reactor Building 471'levation due to failure of the freeze seal.A decrease in reactor coolant inventory would require freeze seal failure, coincident with a Post Accident Sampling System (PASS)sample being drawn from the jet pumps and failure of PASS Check Valve PSR-V-106 in the Demineralized Water System flush line.However, this event has been previously evaluated and documented in the FSAR.All important to safety equipment affected by a maximum potential flooding event is already identified and included in the plant flooding analysis.Flooding due to failure of the freeze seal would not alter the manner in which equipment is assumed to fail during any flooding event.Work Orders WT5001 and YH1001 (SE 96-037)These work orders provided for installation of a freeze seal in a Control Rod Drive (CRD)System line upstream of CRD Vent Valve CRD-V-101A to allow for inspection
Stressevaluations forsmallborepipingandvalvesintheseapplications wouldnotbeadversely impactedbythischange.WorkOrderYS6901(SE96-009)ThisworkorderprovidedforrepairofDemineralized WaterSystemValveDW-V-100/57andisolation ofthecomponent fromthesystembymeansofafreezesealin'thehorizontal runofpipingupstreamofthevalve.Itwasconcluded fromthesafetyevaluation thattheonlycredibleproblemareaofconcernduringisolation ofthewatersupplytoDW-V-100/57 wouldbefloodingoftheReactorBuilding471'levation duetofailureofthefreezeseal.Adecreaseinreactorcoolantinventory wouldrequirefreezesealfailure,coincident withaPostAccidentSamplingSystem(PASS)samplebeingdrawnfromthejetpumpsandfailureofPASSCheckValvePSR-V-106 intheDemineralized WaterSystemflushline.However,thiseventhasbeenpreviously evaluated anddocumented intheFSAR.Allimportant tosafetyequipment affectedbyamaximumpotential floodingeventisalreadyidentified andincludedintheplantfloodinganalysis.
'f CRD Insert Isolation Valve CRD-V-101/5027.
Floodingduetofailureofthefreezesealwouldnotalterthemannerinwhichequipment isassumedtofailduringanyfloodingevent.WorkOrdersWT5001andYH1001(SE96-037)Theseworkordersprovidedforinstallation ofafreezesealinaControlRodDrive(CRD)SystemlineupstreamofCRDVentValveCRD-V-101A toallowforinspection
The proposed activity would be performed with the reactor.,in cold shutdown,.
'fCRDInsertIsolation ValveCRD-V-101/5027.
depressurized and all control rods.fully inserted.81 f
Theproposedactivitywouldbeperformed withthereactor.,in coldshutdown,.
It was concluded from the safety evaluation that there were no postulated accidents or operational transients associated with a break in the one-inch CRD insert line that could result in an increase in the radiological dose at the site boundary.There were also no postulated accidents or operational transients associated with a break in the line that could result in flooding and impact the functional ability of equipment important to safety.In was also concluded that the piping was capable of accepting the stresses from the freeze seal.If the pressure integrity of the insert line were to fail due to loss of the freeze seal during the rework or replacement of the valve, no control rod withdrawal would occur.~Work Order YT6201 (SE 96-038)This work order provided for installation of a freeze seal in a Control Rod Drive (CRD)System line upstream of CRD Vent Valve CRD-V-102A to allow for inspection of CRD Withdraw Isolation Valve CRD-V-102/2251.
depressurized andallcontrolrods.fullyinserted.
The proposed activity would be performed with the reactor in cold shutdown, depressurized and all control rods fully inserted.It was concluded from the safety evaluation that there were no postulated accidents or operational transients associated with a break in the one-inch CRD insert line that could result in an increase in the'radiological dose at the site boundary.There were also no postulated accidents or operational transients associated with a break in the line that could result in flooding and impact the functional ability of equipment important to safety.-E, In was also concluded that the piping was capable of accepting the stresses from the freeze seal.If the pressure integrity of the insert line were to fail due to loss of the~freeze seal during the rework or replacement of the valve, no control rod withdrawal would occur.h 82 2.8 R1M'ORT OF DIESEL GF22RATOR FAILURES This section contains information pertaining to diesel generator failures, valid and non-valid, and is included pursuant to Technical Specifications 4.8.1.1.3 and 6.9.1.There was one non-valid failure in 1996.There were no valid load demand failures for the three emergency diesel generators.
81 f
The non-valid failure event was documented on Problem Evaluation Request 296-0338 and is.described as follows:~Identity of Diesel Generator and Date of Failure Division One Emergency Diesel Generator (DG-1): May 8, 1996 (2128 hours)~..Number.Designation of Failure in Last 100 Valid Tests This was the first failure of the last 100 tests.However, this test was determined to be a"non-valid" load demand failure.~Cause of Failure 0 During performance of the annual LOOP/LOCA surveillance test for the Division 1 Emergency Diesel Generator, a fuel oil leak developed on the return line to the fuel oil day tank.The leak occurred on a threaded fitting to the flanged connection of the return line.Corrective Measures Taken" The unit was shutdown and the fuel line was replaced and leak tested.Upon completion of successful repair efforts, the diesel generator was re-started and the 24-hour surveillance test was completed without further incident.Length of Time Diesel Generator Unavailable The Diesel Generator was out of service for approximately one hour.Testing activities resumed at 0507 hours on May 9, 1996."Current Surveillance Interval Thirty one days.83 wp 0 REGULATORY CO CHANGES (NEI PROCESS)This section contains information pertaining to Regulatory Commitment Changes (RCCs)and is included pursuant to the NEI Guidelines for Management NRC Commitments.
Itwasconcluded fromthesafetyevaluation thattherewerenopostulated accidents oroperational transients associated withabreakintheone-inchCRDinsertlinethatcouldresultinanincreaseintheradiological doseatthesiteboundary.
~RCC-30985-00 (Vital Area Access Controls)The original commitment desciiption is,"The Security Supervisor responsible for categorizing materials entering the protected area will be present initially to ensure proper vital area access controls are in position anytime (door)R-106 is.opened to allow access." This commitment was made in response to Security Event Report 87-004.This commitment was deleted.The basis for deletion is that a current procedure requires that, prior to allowing personnel access into any vital area, access authorization for the.area is verified by either a review of an access authorization list or through communications with the Central Alarm Station.This alternate method complies with 10CFR73.55(g)(1) and 10CFR73.55(d)(7)(B).
Therewerealsonopostulated accidents oroperational transients associated withabreakinthelinethatcouldresultinfloodingandimpactthefunctional abilityofequipment important tosafety.Inwasalsoconcluded thatthepipingwascapableofaccepting thestressesfromthefreezeseal.Ifthepressureintegrity oftheinsertlineweretofailduetolossofthefreezesealduringthereworkorreplacement ofthevalve,nocontrolrodwithdrawal wouldoccur.~WorkOrderYT6201(SE96-038)Thisworkorderprovidedforinstallation ofafreezesealinaControlRodDrive(CRD)SystemlineupstreamofCRDVentValveCRD-V-102A toallowforinspection ofCRDWithdrawIsolation ValveCRD-V-102/2251.
There is no change to the protection level for personnel to ensure a system, structure or component is capable of performing its function.Access authorization continues to be verified prior to personnel being allowed entry into a vital area.RCC.-106987-00 (Crane Stops)1 The original commitment description is,"Place a physical stop on the monorail supporting MT-HOI-6 to prevent moving RHR-Loop A or Loop B components over the equipment left in service." This commitment was made in response to NUREG-0612 tLetter GO2-83-614, dated July 13, 1983, GC Sorensen (SS)to A Schwencer (NRC),."Response to NUTMEG-0612-Phase II, Control of Heavy Loads;Submittal of"'sic)].
Theproposedactivitywouldbeperformed withthereactorincoldshutdown, depressurized andallcontrolrodsfullyinserted.
This commitment was deleted.The basis for deletion is guidance contained in Generic Letter 85-11,"Completion of Phase II of'Control of Heavy Loads at Nuclear Power Plants'UIREG-0612," dated June 28, 1995., This Generic Letter provided relief to certain previous requirements pertaiiung to heavy loads.This commitment was within, the scope of those requirements that were allowed to be eliminated.
Itwasconcluded fromthesafetyevaluation thattherewerenopostulated accidents oroperational transients associated withabreakintheone-inchCRDinsertlinethatcouldresultinanincreaseinthe'radiological doseatthesiteboundary.
Current procedures are in place to meet the requirements of Phase I and ensure the safe operation of this hoist.84  
Therewerealsonopostulated accidents oroperational transients associated withabreakinthelinethatcouldresultinfloodingandimpactthefunctional abilityofequipment important tosafety.-E,Inwasalsoconcluded thatthepipingwascapableofaccepting thestressesfromthefreezeseal.Ifthepressureintegrity oftheinsertlineweretofailduetolossofthe~freezesealduringthereworkorreplacement ofthevalve,nocontrolrodwithdrawal wouldoccur.h82 2.8R1M'ORTOFDIESELGF22RATOR FAILURESThissectioncontainsinformation pertaining todieselgenerator
~, I'" fV.C,  
: failures, validandnon-valid, andisincludedpursuanttoTechnical Specifications 4.8.1.1.3 and6.9.1.Therewasonenon-valid failurein1996.Therewerenovalidloaddemandfailuresforthethreeemergency dieselgenerators.
~RCC-107116-00 (Positioning of Cranes and Hoists)The original commitment description is,"Certain cranes and hoists will be locked out in a safe position and not placed into use until the equipment they service has been declared inoperable per the Plant Technical Specifications." This commitment was made in response to NUREG-0612
Thenon-valid failureeventwasdocumented onProblemEvaluation Request296-0338andis.described asfollows:~IdentityofDieselGenerator andDateofFailureDivisionOneEmergency DieselGenerator (DG-1):May8,1996(2128hours)~..Number.Designation ofFailureinLast100ValidTestsThiswasthefirstfailureofthelast100tests.However,thistestwasdetermined tobea"non-valid" loaddemandfailure.~CauseofFailure0Duringperformance oftheannualLOOP/LOCA surveillance testfortheDivision1Emergency DieselGenerator, afueloilleakdeveloped onthereturnlinetothefueloildaytank.Theleakoccurredonathreadedfittingtotheflangedconnection ofthereturnline.Corrective MeasuresTaken"Theunitwasshutdownandthefuellinewasreplacedandleaktested.Uponcompletion ofsuccessful repairefforts,thedieselgenerator wasre-started andthe24-hoursurveillance testwascompleted withoutfurtherincident.
[Letter GO2-82-824, dated October 4, 1982, GD Bouchey (SS)to A Schwencer (NRC),"Response to NUREG-0612, Control of Heavy Loads, Revision 1;Submittal of'sic)].This commitment was deleted.The basis for deletion is guidance contained in Generic Letter 85-11,"Completion of Phase II of'Control of Heavy Loads at Nuclear Power Plants'UTMEG-0612," dated June 28, 1995.This Generic Letter provided relief to certain previous requirements pertaining to heavy loads.This commitment was within the scope of those requirements that were allowed to be eliminated.
LengthofTimeDieselGenerator Unavailable TheDieselGenerator wasoutofserviceforapproximately onehour.Testingactivities resumedat0507hoursonMay9,1996."CurrentSurveillance IntervalThirtyonedays.83 wp0 REGULATORY COCHANGES(NEIPROCESS)Thissectioncontainsinformation pertaining toRegulatory Commitment Changes(RCCs)andisincludedpursuanttotheNEIGuidelines forManagement NRCCommitments.
Current procedures are in place to meet the requirements of Phase I and ensure the safe operation of cranes and hoists.~RCC-'107245-00 (Crane Operator Training)0 The original commitment description is, There are no exceptions taken to ANSI B30.2-1976 with respect to operator traiiiing, qualification and conduct.Per plant procedures, this type of tr'aining is documented and records of such training are maintained
~RCC-30985-00 (VitalAreaAccessControls)
'current'y the training staff.Recertifiication is required every three (3)years unless the operator has not operated the crane during" the year and in..that case the operator must be recertified before operating the unit." This commitment was made in response to NUREG-0612
Theoriginalcommitment desciiption is,"TheSecuritySupervisor responsible forcategorizing materials enteringtheprotected areawillbepresentinitially toensurepropervitalareaaccesscontrolsareinpositionanytime(door)R-106is.openedtoallowaccess."Thiscommitment wasmadeinresponsetoSecurityEventReport87-004.Thiscommitment wasdeleted.Thebasisfordeletionisthatacurrentprocedure requiresthat,priortoallowingpersonnel accessintoanyvitalarea,accessauthorization forthe.areaisverifiedbyeitherareviewofanaccessauthorization listorthroughcommunications withtheCentralAlarmStation.Thisalternate methodcomplieswith10CFR73.55(g)(1) and10CFR73.55(d)(7)(B).
[Letter GO2-82-824, dated October 4, 1982, GD Bouchey (SS)to A Schwencer (NRC),"Response to NVREG-0612, Control of Heavy Loads, Revision 1;Submittal of" (sic)).This commitment was revised to,"There are no exceptions taken to ANSI B30.2-1976 with respect to operator training, qualification and conduct.Per plant procedures, this type of training is documented and records of such training are maintained." The basis for revision is that"recertification every three years unless the operator has not operated the crane during the year and in that case the operator must be recertified before operating the unit" is not required by ANSI B30.2-1976.
Thereisnochangetotheprotection levelforpersonnel toensureasystem,structure orcomponent iscapableofperforming itsfunction.
In addition, documentation is retained in a"current" status and is available for review at the Supply System.This approach to document maintenance is consistent with previous guidance issued in this Recertifications are currently evaluated on,a,case-by-case basis and.could'epend'n
Accessauthorization continues tobeverifiedpriortopersonnel beingallowedentryintoavitalarea.RCC.-106987-00 (CraneStops)1Theoriginalcommitment description is,"Placeaphysicalstoponthemonorailsupporting MT-HOI-6topreventmovingRHR-LoopAorLoopBcomponents overtheequipment leftinservice."
'everal factors such as job complexity or past performance of the'crane operator.0 85
Thiscommitment wasmadeinresponsetoNUREG-0612 tLetterGO2-83-614, datedJuly13,1983,GCSorensen(SS)toASchwencer (NRC),."Response toNUTMEG-0612-PhaseII,ControlofHeavyLoads;Submittal of"'sic)].
Thiscommitment wasdeleted.Thebasisfordeletionisguidancecontained inGenericLetter85-11,"Completion ofPhaseIIof'ControlofHeavyLoadsatNuclearPowerPlants'UIREG-0612,"
datedJune28,1995.,ThisGenericLetterprovidedrelieftocertainpreviousrequirements pertaiiung toheavyloads.Thiscommitment waswithin,thescopeofthoserequirements thatwereallowedtobeeliminated.
Currentprocedures areinplacetomeettherequirements ofPhaseIandensurethesafeoperation ofthishoist.84  
~,I'"fV.C,  
~RCC-107116-00 (Positioning ofCranesandHoists)Theoriginalcommitment description is,"Certaincranesandhoistswillbelockedoutinasafepositionandnotplacedintouseuntiltheequipment theyservicehasbeendeclaredinoperable perthePlantTechnical Specifications."
Thiscommitment wasmadeinresponsetoNUREG-0612
[LetterGO2-82-824, datedOctober4,1982,GDBouchey(SS)toASchwencer (NRC),"Response toNUREG-0612, ControlofHeavyLoads,Revision1;Submittal of'sic)].
Thiscommitment wasdeleted.Thebasisfordeletionisguidancecontained inGenericLetter85-11,"Completion ofPhaseIIof'ControlofHeavyLoadsatNuclearPowerPlants'UTMEG-0612,"
datedJune28,1995.ThisGenericLetterprovidedrelieftocertainpreviousrequirements pertaining toheavyloads.Thiscommitment waswithinthescopeofthoserequirements thatwereallowedtobeeliminated.
Currentprocedures areinplacetomeettherequirements ofPhaseIandensurethesafeoperation ofcranesandhoists.~RCC-'107245-00 (CraneOperatorTraining) 0Theoriginalcommitment description is,Therearenoexceptions takentoANSIB30.2-1976withrespecttooperatortraiiiing, qualification andconduct.Perplantprocedures, thistypeoftr'aining isdocumented andrecordsofsuchtrainingaremaintained
'current'y thetrainingstaff.Recertifiication isrequiredeverythree(3)yearsunlesstheoperatorhasnotoperatedthecraneduring"theyearandin..thatcasetheoperatormustberecertified beforeoperating theunit."Thiscommitment wasmadeinresponsetoNUREG-0612
[LetterGO2-82-824, datedOctober4,1982,GDBouchey(SS)toASchwencer (NRC),"Response toNVREG-0612, ControlofHeavyLoads,Revision1;Submittal of"(sic)).Thiscommitment wasrevisedto,"Therearenoexceptions takentoANSIB30.2-1976 withrespecttooperatortraining, qualification andconduct.Perplantprocedures, thistypeoftrainingisdocumented andrecordsofsuchtrainingaremaintained."
Thebasisforrevisionisthat"recertification everythreeyearsunlesstheoperatorhasnotoperatedthecraneduringtheyearandinthatcasetheoperatormustberecertified beforeoperating theunit"isnotrequiredbyANSIB30.2-1976.
Inaddition, documentation isretainedina"current" statusandisavailable forreviewattheSupplySystem.Thisapproachtodocumentmaintenance isconsistent withpreviousguidanceissuedinthisRecertifications arecurrently evaluated on,a,case-by-case basisand.could'epend'n
'everalfactorssuchasjobcomplexity orpastperformance ofthe'crane operator.
085


RCC-131354-00 (ScramTimeTesting)Theoriginalcommitment description is,"Performscramtimetestingonceper60daysonareference sampleofrodshavingVitonSSPVsconsisting of5%butnotlessthan5rods."Thiscommitment wasmadeinresponsetoBWROGSSPVtestingrecommendations (LetterGO2-96-078, datedApril5,1996,JVParrish(SS)toACThadani(NRC),"CRDSSPVswithVitonInternals"
RCC-131354-00 (Scram Time Testing)The original commitment description is,"Perform scram time testing once per 60 days on a reference sample of rods having Viton SSPVs consisting of 5%but not less than 5 rods." This commitment was made in response to BWROG SSPV testing recommendations (Letter GO2-96-078, dated April 5, 1996, JV Parrish (SS)to AC Thadani (NRC),"CRD SSPVs with Viton Internals").This commitment vras revised to,"Perform scram time testing once per 60 days, plus or minus 25%, on a reference sample of rods having Viton SSPVs consisting of 5%but not less than 5 rods." The basis for revision is that the observed rate of change in the performance characteristic of the Viton SSPVs is slow enough to allow adequate response time to an undesirable degraded condition with a 25 percent increase in the testing interval.Furthermore, the 25 percent tolerance is consistent with Technical Specification
).Thiscommitment vrasrevisedto,"Performscramtimetestingonceper60days,plusorminus25%,onareference sampleofrodshavingVitonSSPVsconsisting of5%butnotlessthan5rods."Thebasisforrevisionisthattheobservedrateofchangeintheperformance characteristic oftheVitonSSPVsisslowenoughtoallowadequateresponsetimetoanundesirable degradedcondition witha25percentincreaseinthetestinginterval.
.4.0.2.A tolerance was.not specified in the original commitment and this revision simply clarifies the intended testing interval tolerance.
Furthermore, the25percenttolerance isconsistent withTechnical Specification
RCC-135865-00 (Procedure Review Committee)
.4.0.2.Atolerance was.notspecified intheoriginalcommitment andthisrevisionsimplyclarifies theintendedtestingintervaltolerance.
The original commitment description is;"A POC procedure review committee has been established as part of the procedure change management process to perform additional procedure review prior to general POC member review." This commitment was made in response to NRC Inspection Report 9345 (Letter,GO2-94-026, dated January 28, 1994, JV Parrish (SS)to NRC,"NRC Inspection Report 93-45 Response to Notice of Violation").This commitment was deleted.The basis for deletion is that, as part of a procedure upgrade project, the Supply System transitioned from having department procedure coordinators and procedure reviews performed by selected reviewers, to procedure sponsors and qualified procedure reviewers.
RCC-135865-00 (Procedure ReviewCommittee)
Procedure sponsors are identified as the procedure owner (i.e., most hiowledgeable of the procedure).
Theoriginalcommitment description is;"APOCprocedure reviewcommittee hasbeenestablished aspartoftheprocedure changemanagement processtoperformadditional procedure reviewpriortogeneralPOCmemberreview."Thiscommitment wasmadeinresponsetoNRCInspection Report9345(Letter,GO2-94-026, datedJanuary28,1994,JVParrish(SS)toNRC,"NRCInspection Report93-45ResponsetoNoticeofViolation"
Qualified procedure reviewers are trained and qualified to perform procedure reviews.Procedure review expectations have also been clearly defined.Monitoring of procedure sponsor and qualified procedure reviewer performance for procedure revisions and reviews showed improvement to indicate that procedure review committee reviews were no longer.necessary.
).Thiscommitment wasdeleted.Thebasisfordeletionisthat,aspartofaprocedure upgradeproject,theSupplySystemtransitioned fromhavingdepartment procedure coordinators andprocedure reviewsperformed byselectedreviewers, toprocedure sponsorsandqualified procedure reviewers.
This monitoring was performed by the procedure review subcommittee..
Procedure sponsorsareidentified astheprocedure owner(i.e.,mosthiowledgeable oftheprocedure).
Qualified procedure reviewers aretrainedandqualified toperformprocedure reviews.Procedure reviewexpectations havealsobeenclearlydefined.Monitoring ofprocedure sponsorandqualified procedure reviewerperformance forprocedure revisions andreviewsshowedimprovement toindicatethatprocedure reviewcommittee reviewswerenolonger.necessary.
Thismonitoring wasperformed bytheprocedure reviewsubcommittee..
86}}
86}}

Revision as of 12:15, 6 July 2018

Annual Operating Rept for 1996. W/970228 Ltr
ML17292A721
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 12/31/1996
From: WEBRING R L
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GO2-97-043, GO2-97-43, NUDOCS 9703100241
Download: ML17292A721 (146)


Text

4A.J DOV6.I J REGULRTOINFORMATION DISTRIBUTION NTEM (RIDS))ACCESSION NBR:9703100241 DOC.DATE:~~~NOTARIZED:

NO DOCKET N FACIL:50-397 WPPSS Nuclear'Project, Unit 2, Washington Public Powe ,05000397~~~~~~~~~AUTH.NAME AUTHOR AFFILIATION EBRING,R.L.

Washington Public Power Supply System RECIP.NAME

'ECIPIENT AFFILIATION

SUBJECT:

"Annual Operating Rept for 1996." W/970228 ltr.DISTRIBUTION CODE: IE47D COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.59 Annual, Report of Changes, Tests or Experiments Made NOTES: c Q W out Approv@RECIPIENT ID CODE/NAME PD4-2 PD INTERNAL: ACRS RGN4 FILE 01 EXTERNAL: NOAC COPIES LTTR ENCL 1,~0 1 1 1 1 1 1 RECIPIENT ID CODE/NAME COLBURN,T FILE CENTER NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 0~'C E NOTE TO ALL"RIDSM RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, I ROOM OWFN 5D-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 7 ENCL, 6 0 0 WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~Richland, Washington 99352-0968 February 28, 1997 G02-97-043 Docket No.50-397 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:

Subject:

WNP-2, OPERATING LICENSE NPF-21 ANNUAL OPERATING REPORT 1996

References:

1)Title 10, Code of Federal Regulations, Part 50.59(b)2)WNP-2 Technical Specifications 4.8.1.1.3, 6.9.1.4 and 6.9.1.5 3)Regulatory Guide 1.16, Reporting of Operating Information, Appendix A 4)NEI Guideline for Managing NRC Commitments In accordance with the references, the Supply System hereby submits the annual operating report for calendar year 1996;If you have any questions or desire additional information pertaining to this report, please contact Ms.Lourdes Fernandez at (509)377-4147.Respectfully, R.L.Webring Vice President, Operations Support/PIO Mail Drop JE08 JDA/lm~0003'ttachment cc:-.EW Merschoff, NRC-Region IV KE Perkins, NRC-Region IV, WCFO TG Colburn, NRC-NRR REIRS Project Manager, NRC-NRR 970310024i 961231 PDR'DOCK OS000397 R-PDR NRC Resident Inspector (MD 927N)DL Williams-BPA (MD 399)NS Reynolds-Winston&Strawn!!!!![]!!!lllMII!!!Illljllt!!!

IIIIII!Illl

WASHINGTON NUCLEAR PLANT NO.2 ANNUAL OPERATING REPORT 1996 DOCKET NO.50-397 FACILI'IY OPERATING LICENSE NO.NPF-21 Washington Public Power.Supply System"'P.O.Box 968 Richland, Washington 99352 1 l~~h 0

1.0 INTRODUCTION

TABLE OF CONTEXTS 1.1 1996 Capacity Factors 1.2 1996 Load Profile 2.0 REPORTS 2.1 Annual Personnel Exposure and Monitoring Report 2.2'eactor Coolant Specific Activity Levels 2.3 Main Steam Line Safety/Relief Valve Challenges 2.4 Summary of Plant Operations

2.5 Significant

Corrective Maintenance Performed on Safety-Related Equipment 2.6 Fuel Performance 2.7 10CFR50.59 Changes, Tests and Experiments

.2.7.1 Plant Modifications 2.7.2 Temporary Modifications/Instrument Setpoint Changes 2.7.3 FSAR Changes 2.7.4 Problem Evaluations 2.7.5 Plant Tests and Experiments 2.7.6 Plant Procedure Changes 2.7.7 Miscellaneous 2.8 Diesel Generator Failures 2.9 Regulatory Commitment Changes (NEI Process)=~

td!~

1.0 lXIRODUCTXON

The 1996 Annual Operating Report of Washington Public Power Supply System Plant Number 2 (WNP-2)is submitted pursuant to the requirements of Federal Regulations and Facility Operating License NPF-21.The plant is a 3486 MWt, BWR-5, which began commercial operation on December 13, 1984.On March 2, 1996 WNP-2 had operated continuously for 242 consecutive days when the plant was taken off line at the request of the Bonneville Power Administration, customer for WNP-2 electricity.

The 242 consecutive day run was just 15 short of the plant's record mark of 257 days, set between August.1993 and April 1994.This also represented the first breaker-to-breaker run.The plant was maintained in this reserve shutdown condition for more than one month before the refueling outage scheduled start date due to an abundance of relatively inexpensive power from the Federal Columbia River Power System.On April 13, 1996 the plant officially entered the 1996 Maintenance and Refueling Outage (R-11)as scheduled.

The plant ended the annual outage on June 21, 1996.Following startup, the plant was manually scrammed from 28.5 percent power on June 24, 1996 due to an unexpected plant response during testing of the recently-installed Digital Feedwater Level Control System.The unexpected response was due to a digital feedwater controller error.A change was made to the controller software and plant startup resumed.From June 1996 through August 1996, power production was limited due to problems associated with the recently-installed Reactor Recirculation System Pump Adjustable Speed Drive and Digital Feedwater Level Control Systems.Power production continued to be periodically limited during the remainder of tlie year due to problems with the adjustable speed drives.The Bonneville Power Administration, due to abnormally high run-off conditions on several occasions throughout the remainder of the year, also requested that WNP-2 reduce power levels so that the federal power marketing agency could maximize its generating capability from the region's hydroelectric projects.The eleventh refueling outage was successfully completed during 1996.Significant planned and emergent activities included:~Installation of an Adjustable Speed Drive System for the Reactor Recirculation System pump motors.J~, Installation of a Digital Feedwater'Level Control System: l I~g I' Installation of clamps on each of the jet pump sensing lines.The 80 n'w clamps (four on each line)supplement welded supports and were installed in support of the Adjustable Speed Drive System modification.

~Full core off-load to support the jet pump sensing line modification.

~Core refuel with Asea Brown-Boveri (ABB)assemblies.

This represented ABB's first refuel load for a U.S.commercial nuclear power plant.~Visual inspection of the Reactor Pressure Vessel.~Cleaning of Main Condenser tubes.~Refurbishment of 20 Control Rod Drive Mechanisms.

~Inspection of the Moisture Separator Reheater During December 1996, a new power generation record was set.The gross generation for the month was 882,470 megawatt-hours and net generation equalled 850,855 megawatt-hours.

The.previous record of 868,390 megawatt-hours gross and 837,936 megawatt-hours net occurred in October 1995.

1.1 Capacity Factors-1996 The 1996 capacity factors, based on net electrical energy output are listed below.January Pebruary March>>April>>*97.8 82.1 0 0 June>>>>>>0.8 July 58.6" August September 61.6'6.5 October November'-December 96.2 99.3 103.3 57.1 Entered Economic Dispatch Reserve Shutdown Condition Started Maintenance and Refueling Outage Ended Maintenance and Refueling Outage

Load Profile-1996 0 Generation Q Econ Oisp 1,000 0 FEB MAR APR JUN 1,000 Z'JUL AUG SEP'.OCT NOV DEC 4 2.0 RIM'ORTS The reports in this section are provided pursuant to: 1)the requirements of Technical Specifications 6.9.1.4 and'6.9.1.5,"Annual Reports," 2)the requirements of Technical Specification 4.8.1.1.3,"Reports" (Electrical Power System Surveillance Requirements), 3)the requirements of 10CFR50.59,"Changes, Tests, and Experiments," 4)the guidance contained in Regulatory Guide 1.16,"Reporting of Operating Information," Revision 4-August 1975, and 5)the guidance contained in the NEI Guideline for Managing NRC Commitments, Revision 2, December 1995.Technical Specifications 6.9.1.4 and 6.9.1.5 require that the following reports for the previous calendar year be submitted prior to March 1 of each year:~A tabulation on an annual basis of the number of station, utility, and other personnel (including contractors) receiving exposures greater than 100 mrems/year and their associated man-rem exposure according to work and job functions.

I Documentation of a11 challenges to main steam line safety/relief valves.The results of specific activity analysis in which the primary coolant exceeded the limits of Specification 3.4.5.The limits are, Less than or equal to 0.2 microcuries per gram DOSE EQUIVALENT I-131," and"Less than or equal to 100/E-Bar microcuries per grBII1.Technical Specification 4.8.1.1.3 requires reporting of all diesel generator failures, valid or non-.valid.This report is made pursuant to Specification 6.9.1,"Routine Reports." Regulation 10CFR50.59 requires that licensees submit, as specified in 10CFR50.4, a report containing a brief description of any changes, tests or experiments, including a summary of the safety evaluation of each.The report may be submitted annually or at shorter intervals.

Regulatory Guide 1.16 states that routine operating reports covering the operation of the unit~during the previous calendar year should be submitted prior to March 1 of each year.Each annual operating report should include: 1~A narrative summary of operating experience during the report period relating to the safe operation of the facility, including safety-related maintenance not covered elsewhere.

For each outage or forced reduction in power of over 20 percent of design power level where the reduction extends for-more than four hours: (a)The proximate cause and the system and major component involved (if the outage or forced reduction in power involved equipment malfunction).

v 0 (b)A brief discussion (or reference to reports)of any reportable occurrences pertaining to the outage or reduction.(c)Corrective action taken to reduce the probability of recurrence, if appropriate.

'd)Operating time lost as a result of the outage or power reduction.(e)A description of major safety-related corrective maintenance performed during the outage or power reduction', including system and component involved,and identification of the critical path activity dictating the length of the outage or power reduction.(f)A report of any=single release of radioactivity or single exposure specifically

-associated with the outage which accounts for more than ten percent of the allowable annual values.A tabulation on an annual basis of the number of station, utility and other personnel (including contractors) receiving exposures greater than 100 mrem/year and their associated man-rem exposure according to work and job functions.

~'ndications of failed fuel resulting from irradiated fuel examinations, including eddy current tests, ultrasonic tests, or visual examinations completed during the report period.~~~~~~~~~~~~~The NEI Guideline for Managing NRC Commitments is a commission-endorsed method for licensees to follow for managing or changin'g NRC commitments.

As part of this process and for commitments that satisfy one of the five NEI decision criteria not involving a codified regulatory process, the NEI guidance specifies periodic staff notification, either annually or along'with the FSAR updates as required by 10CFR50.71(e).

The NEI g'uideline further specifies that commitments dispositioned through the NEI process that satisfy none of the NEI decision criteria do not need to be reported in the licensee's periodic report because their regulatory and safety significance is negligible.

10 CFR PART 20 MASHIMCTON PUBLIC POMER SUPPLY SISTEM RADIATION EXPOSURE RECORDS MORN AND JOB tUNCTION REPORT Report for Calendar Yeari 1996'7S'7 Total HAM-RCH!349.890--year to Date Dose-I tation Utility-contractots EsployeesEcployees and Others 17 351 0 595 14 867 15,795 0,381 0+163 3.429 0.093 0.931 1,299 0 087 1+065 806 1 189 6 632 43.856 0.664 121'30 4.080 0.000 0.4 4 9 943 0,285 16'77 3,569 0.046 2 599 2.969 2 392 6.566 0,316 0,000 4,192 0.000 0.000 0.000 0,004 0,000 0,008 0 005 0,000 0,079 0 031 0 149 0 527 ILLAMCE Maintenance Personnel operatinq tersonnel Health thyslcs Personnel supervlsocy Personnel Eagineering Personnel Maintenance Personnel Operatinq Personnel Health Physics Personnel supervisory Personnel Engineering Personnel Maintenance Personnel opecatinq Personnel Health Physics Personnel Supervisory tersonnel Engineering Personnel Nalntenanee Persoanel Opsratinq Personnel Health Physics Personnel Supervisory Personnel Engineering Pecsonnel Naintenance I'ersonnel opecetinq Personnel Health thysies Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel operatinq personnel Health Physics Personnel Supecvlsohcy Personnel Engineering Personnel 0.99 ISSe90 0,00 0 17 0,67 I5~17 0,38 5 44 6.32 17 18 0,00 6o34 0 F 00 0.00 0,00 0,07 0 00 Oo07 0 33 0 72 ROUTINE HAINTENAMCE 55 0 1'3 17 34 2'5 5.82 INSERVICE INSPECTION Oe55 0 00 0 02 0 02 0 10 SPECIAL MAINTENANCE

{Sn attached sheets)0,024 0,000 lo226 0.000 0.000 0,06 0.00 le07 0+00 Oooo 0+482 0.025 0,619 0.000'.135 18 II3 0,837 0 775 1.351 0.241 0 42 0,00 Oooo 0,00 0.07 0 592 0.000 0,000 0 000 0.027 0+71 0,00 0+70 0,00 0.05 HASTE PROCESS ISO 6,415 0,000 3,368 0,003 0 910 11o03 0+00 10.20 0007 3'2 0,008 0,000 0,000 0,228 0~590 REPUELINO 20+07 0.03 0 40 Oooo 1 21 0.00 3'9 0,86;Oo75 2+94~aaorand Totals tv Nalntenance Personnel Operatinq Personnel Health thyeles Personnel Supervisory Personnel Engineering Personnel 159.74 34 14 39 58 16.49 24.31 274.37 i.87 3.'22 I 50 2 29 18o46 353rOS lo00 60 19 9+62 68elo 30o34.491+96 84 49 20o90 15 91 6+22 7029 134 835 1.859 160.022 0 381 0 577 0 378 21 910 0.361 3+746 I 471 21+006 7 450 207e261 tacilitya 02 This report uas produced uith direct reading dosieeter data Nuaber o!persons Receiving over 100 eilllraa is--Nnher ot Individuals

-I tatlon Utility Contraetols Eaployees Eaployees and Others OPERATIONS AMD SURVE 69.49 3e43 91~31 31.86 3+22 O.S3 16.45 0.83 3~68 10.23 ,05 4,04 13.8I 8 38 25'4'el 8 O O cn g'p Bg 9 5', O O c)k~gs~OO g O O 8, PA ID O (g O g FL D~e C6 g~.P O O.o~O' IJ WASHINGTON PUBLIC POWER SUPPLY SYSTEM RADIATION EXPOSURE RECORDS WORK AND JOB FUNCTION REPORT 10 CFR PART 20 Facilitys 02 This report was produced with direct reading dosimeter data Report for Calendar Years 1996 SPECIAL MAINTENANCE

--Number of Individuals

--I I---Year to Date Dose---tation'Utility contractof s Station Utility contracto Employees Employees and Others" Employees Employees and Othe 1.Install Vibration Mitigation Clamp, Jet Pump Sensing Line 2.Reactor Recirculation and Residual Heat Removal Vibration Testing 3..Tube Plugging.Condenser7Neat.

Exchanger 9i C Water Box 4.Adjustable Speed Drive Implementation 5.Source Rance Monitor Drive B Gearbox Replacement 6.Adjust Main Steam Jet Pump Set Screw Oaps 7.Reactor Recirculation Valve 68A, Repair Leak 8.Remove Stellite Control Rod Blade Rollers/Velocity Limiters and Clean Spent Fuel Pool Maintenance Personnel operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervi.sory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel 2'13 0>>00 2>>32 0>>00 0 16 0.00 0>>00 D>>OD 0>>00.0 00 4.60 0.00 0>>'32 0>>00 2'5 0>>00 0.00 0.00 0>>00 0 00 2'8 0>>00 0>>00 0>>00 0>>00 0.00 0.00 0>>40 0.00 0>>00 0>>00 0.00 0>>00 0>>00 0.00 0>>00 0>>00 0>>48 0>>00 Q>>00 0.00 0.00 0.00 0.00 0.00 0>>00 0>>00 0>>00 0>>00 0>>00 0.00 0.00 0.00 0 F 00 0>>42 0>>00 0.00 0,00 0.00 0.00 0>>00 0 00 0.00 0.00 0 00 0>>00 0>>00 0.00 0>>00 0>>QO 0 F 00 Q>>00 0 F 00 0.00 0 00 0.00 0.00 0.00 0>>00 0'.00 12.19 0.00 0.00 0.00 6 40 12 39 0>>00 0.00 0.00 6.52 1.12 0 00 0 00 0 00 1 03 8>>14 0>>00 0>>00 0.00 0>>00 0.67 0>>00 0.00 0.00 0.64 1.54 0>>00 0.00 0>>00 1 06 1 30 0.00 0.00 0.00 0 94 0.75 0.00 0.00 0>>00 0.71 0.634 0 000 0 690 0.000 0.047 0,000 0 000 0.000 0.000 0>>000 1~366 0.000 0.094 0 000 0.876 0,000 0,000 0.000 0 000 Q>>000 0 767 0.000 0.000 0.000 0 000 0.000 0'.000 0.118 0 000 0.000 0,000 0'.000 0 000 0 000 0 000 0.000 0 000 0>>142 0 000 0>>000 0.000 0.000 0.000 0.000 0.000 0.000 0 000 0 000 0.000 0.000 0.000 0.000 0.000 0.000 0 124 0~000 0.000 0 000 0 000 0.000 0.000 0.000 0 000 0.000 0'.000 0.000 0'.000 0 000 0~000 0'.000 0~000 0.000 0.000 0 000 0.000 0.000 0.000 0.000 0.000 0.000 3.623 0.000 0.000 0.000 1.901 3.681 0 000 0>>000 0.000 1 937 0.334 0 000 0.000 0~000 0.305 2.419 0~000 0.000 0.000 0'.000 0.199 0.000 0~000 0~000 0.190 0.457 0.000 0.000 0 000 0'15 0 385 0.000 0.000 0.000 0.279 0.222 0.000 0.000 0~000 0.210

9.hBB Fuel Debris Filter Removal.10.Paint/Label Reactor Building RHR htB>'422 11.'501 Reactor Bide, coating Halls and Doors 12.Rework Penetration Seals, QC 162 14.Miscellaneous Projects 13.Temporary Shieldi.ng for Equipment Drain 8 Residual Heat Removal Pipes Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel r Maintenance Personnel Operating Personnel Health Physics Personnel Bupervisory Personnel Bngineering Personnel Maintenance Personnel, Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Bngineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel Maintenance Personnel Operating Personnel Health Physics Personnel Supervisory Personnel Engineering Personnel 0.00 0,55 0 00 0.00 0.30 1 29 0 00 0.00 0 00 0 00 1.17 0 00 0.00 0 00 0 00 0.00 0.00 0.00 0 00 0 00 0, 61" 0,00 0 00 0 OD 0~00 1 24 0 00 0 35 0 00 0.34 0.00 0.00 Oooo 0~00 0+00 0.00 0.00 0.00 0+00 0+00 0+00 o'.aa 0.00 0,00 Oooo Oroo 0+00 oooo 0+00 0+00 0+00 0+00 oroa 0+00 0.00 o.oa 0 F 00 0,00 0.00 Oooo 0.00 0 F 00 0+00 0.00 0+00 0.00 0 F 00 0.00 0 00 0+00 0.00 a.ao 0.00 0 F 00 0.00 0.73 0.00 0 00 0 00 0+70 2.05 0 00 0 00 0 DD 1 33 3.53 0.00 0 00 Oioa 2~12 0+000 0 164 0.000 0 000 0+090 0 383 0~000 0.000 0.000 0.000 0,348 0~000 Ooaoo 0.000 a'.ooo 0.000 0 000 0+ODD',000 0~000 0.182 0 000 0.000 0,000 0.000~0~368 Ooaoo 0.104 Ooooo 0.101 0.000 0.000 0.000 0 000 0 000 0.000 0.000 0.000 0 000 D.DDD 0.000 0.000 0.000 0.000 0 000 0.000 0 000 0.000 0 000 0.000 0.000 0.000 0.000 0,000 0+000 0.000 0.000 0.000 0.000 0.000 0.000 0~000 0.000 0 000 0.000 0.000 0.000 0.000 0 000 0 ODD 0.000 0.000 0.000 0.000 0.000 0.217 0 000 0 000 0 000 0.208 0.609 0.000 0.000 0.000 0~396 1.048 0.000 0.000 0~000 0 630 I'

2.2 Reactor Coolant Specific Activity Levels This section contains information pertaining to reactor coolant dose-equivalent iodine.The specific activity of the primary coolant was significantly less than 0.2 microcuries per gram'ose-equivalent I-131 and 100/E-Bar microcuries per gram as required by~Technical Specification 3.4.5.This data is provided solely for informational purposes and ease of reference.

Technical Specification 6.9.1.5.c only requires reporting when the results of specific activity analysis of primary coolant exceed the limits of Specification 3.4.5..-~I-h h 10

Main Steam Line Safety/Relief Valve Challenges This section contains information pertaining to main steam line safety/relief valve challenges and is included pursuant to Technical Specification 6.9.1.5(b).

The main steam line safety/relief valve challenges (actuation events)are shown on the following tables.The data includes all in-situ tests.For ease of reference, the foHowing descriptive codes are used for each actuation or failure to'actuate:

Type of Actuation A=Automatic B=Remote Manual C=Spring Cause/Reason for Actuation~.B=C=D=E=Overpressure ADS or other safety Test Inadvertent (Accidental/Spurious)

Manual relief Reactor Operating Condition Prior to Lift A=B=C=D=E=F=G=H=Construction Preoperational, startup or power ascension tests in progress Routine startup Routine shutdown Steady state operations Load changes during routine operation Shutdown (hot or cold), except refueling Refueling~Failures and Reports A=B=:C=D=Failure of electrical or other components not considered part of the valve assembly-No SRVS failure report required-Failure of any part of the valve-SRVS failure report will be filed No failures occurred-No SRVS failure report required LER Submitted-Report LER number in Item 316 NPRDS will be submitted 11

~I NOTE: lneludes all ln-Situ Tests For Each Actuation or Failure'o Actuate: S/R Valve Serial Number Component ID (Location)

MS-RV-1B MS-RV-lc 63790404140 63790404139 63790404049 MS-RV-1A MS-RV-1D MS-RV-2B 63790404134 63790404050 Date of Actuation (Mo/Da/Yr)

Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Ult (Code)Rx Power level Prior to Lift (%Rated nrermal)Time Rcq'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number" Reading and Units Rx Prcssure Prior to Actuation (PSIG)tF AVAILABLE/tF APPLlCABLE Reseat Pressure At Valve Closure (PSIG),Duration of This Actuation (Minutes, Seconds)Failures.Rcporlts (Code)LER Number (5 Digit Number)Comments Regarding This Aetuaiion Auaehcd7 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A 1257 15 NIA Process Computer OPEN 919 NIA 6 SEC.NIA 3/2/96 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A 3/2/96 1257 15 NIA Process Computer OPEN ,919 N/A 4 SEC.N/A 3/2/96 1257 15~NIA Process Computer OPEN 919 NIA 6 SEC.NIA 0

NOTE: Includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404122 63790404054 63790404138 63790404053

.63790404124 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior td LIR (Code)Rx Power Level Prior to LIR (%Rated Thermal)Time Reel'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Prcssure Prior to Aetualton (PSIG)tF AVAILABLB/tF APPL'ICABLB Reseat Pressure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation At taehed7 MS-RV-2C 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A MS-RV-2A 1257 15 NIA'Process Computer OPEN 919 NIA 4 SEC.C, NIA MS-RV-2D 1257 15 NIA Process Computer OPEN 919 NIA 4 SEC.NIA MS-RV-3B 3/2/96 1257 15 NIA Process Computer OPEN 919 N/A 4 SEC.IA MS-RV-3C 1257 15 NIA Process Computer OPEN 919 NIA 6 SEC.N/A 13 0,

NOTE: Includes all In Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404058 63790404126 63790404137 63790404056 63790404135 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated Thermal)Time Rcq'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLE/IF APPLICABLE Reseat Prcssure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation Attached?MS-RV-3A 1257 C D NIA Procea Computer OPEN 919 NIA 6 SEC.N/A MS-RV-3D C NIA.Process Computer OPEN 919 N/A 4 SEC.N/A hIS.RVAB 12S7 15 NIA Process Computer OPEN 919 NIA 4 SEC.N/A MS-ROC 1257 15 NIA Process Computer OPEN 919 N/A 4 SEC.N/A MS.RVAA IS NIA Process Computer OPEN 919 NIA 4 SEC.N/A 14

'

NOTE: Includes all In.Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404060 63790404136 63790404062 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Ac(uation (Code)Rx Operating Condition Prior to LIft (Code)Rx Paver Level Prior to LIII (%Rated Thermal)Time Req'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLBIF AFFUCASLE Reseat Pressure At Valve Closure (PSIG)Duration ol'This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Nuinbcr)Comments Regarding This Actuation At tachcd?MS.RVAD 1257 D.N/A Process Computer OPEN 919 NIA 4 SEC.NIA MS-RV-SB N/A Process Computer OPEN 919 NIA 4 SEC.N/A MS-RV-SC 1257 D IS NIA Process Computer OPEN 919 NIA 6 SEC.

U NOTE: Includes all ln-Situ Tests For Each Actuation or Failure'o Actuate: S/R Valve Serial Number 63790404052 2 63790404126 4 63790404055 637 9040406 l 63790404059 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated Thermal)Time Req'd for Tailpipe Temp to Rctutn to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSlG)IF AVAILABLMF APPLICABLE Reseat Pressure At Valve Closure (PSiG)Duration of fhis Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation At tached?MS-RV-3C 5/28/96 N/A B 0 N/A OPEN 0 NIA NIA MS-RV-3D 5/28/96 NIA B 0 NIA OPEN'0 N/A NIA MS-RV4B 5/28/96 NIA B 0 NIA OPEN 0 NIA NIA'S-RYE 5/28/96 NIA'0 NIA Process Computcr-OPEN 0 N/A NIA MS-RV-5B 5/28/96 NIA B 0 NIA Process Computer OPEN 0 NIA NIA 0

N(yfE: Includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404045 63790404057 637904040S l 63790404048 63790404135 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

'IIme of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated'Ibermal)Time Req'd for Tailpipe Temp to Return m Normal Other Instrumentation Type (Code)Other Instrumentation Number.Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAKABLEIIF APPLICABLE Rcscat Pressure At Valve Closure (PSIG)Duration of'Ibis Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (S Digit Number)Comments Regarding This Actuation At'tacbcd7 MS-RV-1C S/28/96 NIA B NIA" OPEN 0 N/A NIA MS-ROC 5/28/96 NIA B 0 N/A Process Computer OPEN 0 NIA NIA MS-RV-3B 5/28/96'IA B 0 N/A OPEN 0 NIA N/A MS-RV-lA NIA~B 0 NIA Process Computer OPEN N/A NIA MS-RVAA N/A B 0 NIA Process Computer OPEN NIA NIA 17 0

NOTE: Includes all In-Situ Tests For Each Actuation or Failure to Actuatet S/R Valve Serial Number 63790404062 63790404051 63790404045 63790404057 63790404051 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

Time of Day (24 Hour Clock)Type of Actuation (Code)Cause&eaton for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated Thermal)Time Req'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLKIIF APPLICABLE Rcscat Pressure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments Regarding%us Actuation Attachcd7 MS-RV-5C NIA B 0 NIA OPEN 0 NIA N/A MS-RV-3B NIA B C 0 NIA Process Computer OPEN 0 NIA NIA MS-RV-1C 6/8/96 N/A B 0 N/A Process Computer OPEN"0 NIA NIA MS-ROC NIA B 0 NIA OPEN 0 NIA.5 min NIA MS-RV-3B 6/8/96 NIA B 0~N/A Process Computer OPEN 0 NIA NIA 18 NOTE: includes all In.Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Ser J Number 1~<63790404045 63790404048 63790404051 63790404052 63790404126 Component 1D (Location)

Date of Actuation (Mo/Dept/r)

Time of Day (24 Hour Clock)~of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to Litt (Code)Rx Psaver Level Prior to Lilt (%Rated'Ihermal)Time Rcq'd for Tailpipe Temp to Return to Normal Other lnsttumcntation Type (Code)Other lnsttumcntation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IF AVAILABLE/IF APPLICASLE Rcscat Pressure At Val ve Closure (PSIG)Duration of Ihis Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (5 Digit Number)Comments Regarding This Actuation Attached?MS-RV-1C 6/16/96 N/A OPEN N/A NIA MS-RV-1A 6/16/96 0346 C N/A Process Computer OPEN NIA NIA MS-RV-3B 6/16/96 3 N/A OPEN NIA NIA MS-RV-3C 6/16/96 C~8/A OPEN NIA N/A MS-RV-3D 6/16/960352 3 N/A OPEN 919 NIA NIA 19

NIXIE: Includes all In-Situ Tests For Each Actuanon or Failure to Actuate: S/R Valve Seria Number 63790404055 63790404061 63790404059 63790404057 63790404135 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

T1me of Day g4 Hour Clock)'Pype of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to IJft (Cod)Rx Power Level Prior to LiR (%Rated Thermal)Time Req'd for Tailpipe Temp to Renun to Normal Other Instrumentation Type (Code)Other instrumentation Number Reading and Units Rx Prcssure Prior to Actuation (PSIG)IF AYiQLA$1E/IF APPLICABIE Reseat Pressure At Valve Closure (PS1G)Duration of This Actuation (Minutes, Seconds)Failures, Reports (Code)LER Number (5 Digit Number)Conuncnts Regarding This Actuation Attached7 ,MS-RYE 6/16/96 0353 NIA OPEN N/A 4 scc NIA MS-RYE 6/16/96 NIA OPEN NIA C N/A MS-RV-SB 6/16/96 0359 N/A OPEN NIA NIA MS-RYE 6/16/96 0355 N/A OPEN NIA A NIA MS-RYE 6/20/96 B 15 NIA OPEN NIA 1 min, 20 scc NIA 20

NOTE: includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number 63790404055 63790404057 63790404126 63790404059 63790404062 Component ID (Location)

Date of Actuation (Mo/Da/Yr)

Time of Day (24 Hour Clock)Type of Actuation (Code)Cause/R'eaton for Actuation (Code)Rx Operating Condition Prior to Lift (Code)Rx Power Level Prior to Lift (%Rated'Ihermal)Time Req'd for Tailpipe Temp to Return to Normal Other Instrumentation Type (Cab)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)tF AVAKABLMF APPUCAttLE.

Reseat Pressure At Valve Closure (PSIG)Duration of This Actuation (Minutes, Seconds)Failures.Reports (Code)LER Number (5 Digit Number)Comments'Regarding Mis Actuation Attachcd7 MS-RVAB 6/20/96 B 15 NIA OPEN NIA 1 min, 7 scc NIA MS-RYE 6/20/96 B C NIA OPEN NIA 1 min, 16 sec N/A MS-RV-3D 6/20/96 B 15 NIA NIA 1 min, 12 scc NIA MS-RV-SB 6/20/96 12S I B 15 N/A OPEN NIA NIA MS-RV-SC 6/20/96 1253 B 1$NIA Process Computer OPEN NIA 1 min, 5 sec NIA lii, I~i~21~8 i i~~

NOTE: Includes all In-Situ Tests For Each Actuation or Failure to Actuate: S/R Valve Serial Number Component ID (Location)

Date of Actuation (Mo/Da/Yr)

Rime of Day (24 Hour Clock)Type of Actuation (Code)Cause/Reason for Actuation (Code)Rx Operating Condition Prior to LI(t (Code)Rx Pcnver Level Prior to Lilt (%Rated'Ihermal)Time Req'd for Tailpipe Temp to Rctum to Normal Other Instrumentation Type (Code)Other Instrumentation Number Reading and Units Rx Pressure Prior to Actuation (PSIG)IP AVAILABLE/IF APPLICABLE Reseat Pressure At Valve Closure (PSIG)Duration of%his Actuation.(Minutes, Seconds)Failures, Reports (Code)63790404061 MS-RV4D 1622 B N/A OPEN N/A I min.l scc LER Number (5 Digit Number)Comments Regarding'Ihis Actuation Attached?N/A 22 2.4 Summary of Plant Operations This section contains a narrative summary of operating experience and is included pursuant to Regulatory Guide 1.16, Sections C.l.b.(1)and C.l.b.(2).

January 1996 At the begimnng of the month, the plant was operating at full power.From January 12, 1996 through part of January 16, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.

During this time power was reduced to about 60 percent.Following economic dispatch, the plant returned" to full power operation on January 16, 1996.On January 19, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.

During this time power was reduced to about 60 percent.Following economic dispatch, the plant returned to full power operation on January 22, 1996 and operated at or near full power for the remainder of the month.February 1996 At the beginning of the month, the plant was operating at full power.On February 3, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.

During this time power was reduced to about 80 percent.r I On February 4, 1996 the plant was maneuvered into a planned downpower for Main Condenser maintenance.

FoHowing condenser work, the plant returned to full power operation.

II On February 10 and 16, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administration.

During this time power was reduced to about 75 and 55 percent respectively.

Following economic dispatch, the plant was returned to full power and operated at or near full power until February 27, 1996 when it was placed on economic dispatch goad following)

'at the request of the Bonneville Power Administration.

During this time pow'er was reduced to about 80 percent.-The.plant returned to full power operation (100 percent)on February 28, 1996.~p r, F g*-.23

~On February 28, 1996 the plant was placed on economic dispatch goad following) at the request of the Bonneville Power Administratio'n.

During this time power was reduced to about 80 percent.Tlie plant returned to full power operation (100 percent)on February 29, 1996.On February 29, 1996 the plant was placed on economic dispatch.goad following) at the request of the Bonneville Power Administration.

During this time power was reduced to about 60 percent.~At the beginning of the month the plant continued to operate at reduced power due to economic dispatch goad following) at the request of the Bonneville Power Administration.

During this time power generation was about 70 percent.~On March 2, 1996 the Main Turbine Generator was removed from service and the plant.was shutdown for economic dispatch goad following) at the request of the Bonneville Power Administration.

The plant remained in a reserve shutdown condition until the beginning of the annual planned maintenance and refueling outage.April 1996~At the beginning of the month the plant continued to be in a reserve shutdown condition.

On April 13, 1996 the plant entered the annual maintenance and refueling outage.May 1996 The plant was in the annual maintenance and refueling outage for the entire month.June 1996 C The plant ended the annual maintenance and refueling outage on June 21, 1996.Following restart, the plant was manually scrammed on June 24, 1996 due to an unexpected plant response during testing of a recently-installed Digital Feedwater Level Control System.The reason for the unexpected plant response was due to a digital reactor feedwater controller error.A change was made to the controller software and plant startup resumed.At the end of-the month, the plant was operating at 25 percent power and continuing with.startup testing following the maintenance and,refueling outage.-0 24 July 1996 At the beginning of the month the plant was ramped up to 68 percent power.Power was maintained at this level due to problems encountered during testing of the recently-instaHed Reactor Recirculation System Pump Adjustable Speed Drives and the Digital Feedwater Level Control System.~At the end of the month the plant was operating at 68 percent power and continuing with startup testing foHowing the maintenance and refueling outage.August 1996 At the beginning of the month, startup testing following the maintenance and refueling outage was still in progress with the focus on the recently-installed Reactor Recirculation System Pump Adjustable Speed Drives and the Digital Feedwater Level Control System.Power was maintained at 64 percent power.On August 10, 1996 the plant continued to operate as a severe transient coursed through the interconnected electrical transmission grids in the Western United States.l During the evening of August 10, 1996, on-line Reactor Recirculation (RRC)System Pump RRC-P-IB"ran back" from approximately 50 Hi to 15 Hz during testing on part of the Adjustable Speed Drive System for the pump.Reactor power decreased from 64 percent to 48 percent.Reactor power was subsequently restored to'65 percent.On August 11, 1996 an unanticipated increase of approximately two percent power occurred due to an apparent failure of a portion of the control for both reactor recirculation pumps.The part of the computer control involved in the failure was removed from the control circuitry and local reactor recirculation pump control was established.

Testing'and troubleshooting efforts were suspended pending a thorough review of a Reactor Recirculation System Pump Adjustable Speed Drives and Digital Feedwater Level Control System test plan.On August 29, 1996 following development of a revised plan, testing was resumed and the power level was increased to support the effort.At the end of the month the plant was operating at 69 percent power and testing continued.

25 September 1996~The lan p t entered the month at about 69 percent power as testing of the Reactor Recirculation System Pump Adjustable Speed Drives and.the Digital Feedwater Level Control System continued.

On September 5, 1996, following successful testing efforts, reactor power was raised to 100 percent.On September 13, 1996 power was reduced to approximately 52 percent for economic dispatch goad following) at the request of the Bonneville Power Administration.

On September 15, 1996, during routine turbine valve testing, a turbine stop valve Med to open.On September 16, 1996 power was reduced to 25 percent to perform repairs to the Turbine Stop Valve Control System.~Following successful repair efforts, the plant resumed 100 percent power operation on September 17, 1996.~On September 20, 1996 power was reduced to 60 percent power@plug a leaking tube~in the Main Coridenser and to replace some scram solenoid pilot valves.FoHowing repairs, the plant resumed fuH power operation on September 22, 1996 and operated at or near 100 percent power for the remainder of the month.October 1996 The plant entered the month at 100 percent power.On October 9, 1996 power was reduced to approximately 55 percent to repair an Adjustable Speed Drive channel that experienced a Med resistivity meter.On October 10, 1996 the plant resumed 100 percent power On October 11, 1996 power w'as reduced to approximately 75 percent power to perform scram time and turbine valve testing, and then to 60 percent for digital feedwater system testing.Following a firmware change on each of the reactor feedwater pumps and subsequent testing, the plant resumed 100 percent power on October 13, 1996.The plant operated at or near fuH power until October 23, 1996 when power was reduced to repair an Adjustable Speed Drive channel that experienced a failed resistivity meter.During power ascension foHowing,repairs, the same channel tripped on overspeed.

3 At the end of the month'the plant was operating at 92 percent power,26 November 1996~The lan p t entered the month at approximately 92 percent power due to a channel failure in the Adjustable Speed Drive System.On November 1, 1996 power was reduced to approximately 49 percent to perform repairs on Adjustable Speed Drive Channel 1A/2.Following successful repair efforts, plant power was increased to 100 percent on November 3, 1996.On November 9, 1996 a power reduction to 75 percent was commenced to perform monthly turbine valve testing.During this evolution, Main Steam (MS)'System Turbine Intercept Valve MS-V-165C would not re-open during testing.Accordingly, power was reduced to 62 percent as prescribed by the Technical Specifications.

On November 10, power was further reduced to 55 percent to repair the valve.The air solenoid and internal o-rings were replaced.~Following successful repair efforts, plant power was increased to 100 percent on ,.November 13, 1996.~With the exception of a few short downpowers for'outine maintenance, the plant operated at or near 100 percent power during the remainder of the month.December 1996 The plant operated at or near 100 percent power during the month.I 27 2.S Significant Corrective Maintenance Performed on Safety-Related Equipment~~~This section contains a description of major, safety-related corrective maintenance performed during outages or power reductions and is included pursuant to Regulatory Guide 1.16, Section C.l.b(2)(e).

The following descriptions consist of summaries of information provided through the Nuclear Plant Reliability Data System (NPRDS).In addition to safety-related equipment, components considered to be essential for power generation are also included.~APRM-F/U-A During the annual maintenance and refueling outage, an alarm was received on the Average Power Range Monitor (APRM)"A" flow unit: During investigation of the problem, the"C" flow unit was taken to bypass and the"A" unit alarm cleared and did not return until after the"C" flow unit was removed from the bypass mode.The cause of the problem was indeterminate.

The test monitor switch was replaced and tested.No further problems were noted.(Failure Date: 06/18/96)CAC-EHO-FCV/4A 0 During testing of a Containment Atmosphere Control (CAC)System flow control valve, it was discovered that a normally closed limit switch on the electro-hydraulic operator was in the open'position.

The cause of the problem was due to an incorrectly wired connection in.the limit switch.The miswiring apparently occurred during previous maintenance activities.

I The wiring error was corrected and the switch'was adjusted.No further problems were noted.(Failure Date: 02/24/96), CAC-FCV-4B During the performance of a local leak rate test, leakage in excess of allowable limits was discovered on Containment Atmosphere Control (CAC)System Valve CAC-FCV-4B.The cause of the problem was due to line and valve rust which degraded seat.integrity.

The rust was removed and the valve seat was machined and lapped.Following completion of a successful post-maintenance local leak rate test, no further problems were noted.(Failure Date: 05/16/96)28

CAC-V-4 T During the performance of a local leak rate test, a leak rate in excess of allowable limits was discovered on Containment Atmosphere Control (CAC)System Valve CAC-V-4.The cause of the problem was due to line and valve rust which degraded seat integrity.

The rust was removed and the valve seat was machined and lapped.Following completion of a successful post-maintenance local leak rate test, no further problems were noted.(Failure Date: 05/18/96)~COND-DM-1B During power operation, Condensate (COND)System Demineralizer COND-DM-1B failed its resin bleed-through test.There was evidence of resin trachng across the rubber washers at the bayonet fitting on 35 of the septa.New septa (35)were installed in the area immediately adjacent to the draft tube and no further problems were noted.(Failure Date: 08/13/96)COND-DM-1E During routine inspections while at power operation, it was observed that the resin strainer differential pressure on Condensate (COND)System Demineralizer COND-DM-1E had increased from ten psid to 15 psid.Following troubleshooting efforts and additional inspections, it was discovered that the draft tube was loose and not latched.In addition, most of the septa on the inner ring were damaged.The cause of the problem was attributed to fiow-induced vibration or other failure mechanism.

e'elded lochng devices were added to the draft tube and new septa were installed.

No further problems were noted.(Failure Date: 02/27/96).~COND-HX-2A During full power operation', it was noted that the level control valve for Condensate (COND)System Heat Exchanger COND-HX-2A was open further than normal.This was an indication of a tube leak in the heat exchanger.

The cause of the problem was attributed to normal wear.The heat exchanger was drained and nondestructive examinations were performed.

Leaking tubes were plugged and no further problems were noted.(Failuie Date: 03/04/96)

COND-HX-9 During routine sampling-at full power operation, an increase in reactor sulfate levels was observed.The reason for the increase was determined to be a condenser tube leak in Condensate (COND)'System Heat Exchanger COND-HX-9.

The exact cause of the tube leak was indeterminate.

The tube was plugged and no further problems were noted.(Failure Date: 02/02/96)COND-HX-9 During main condenser inspection efforts, damage was noted on spray baskets", welds and a strong back for Condensate (COND)System Heat Exchanger COND-HX-9.

The cause of the problem was attributed to normal usage and stresses.AH damaged components were either repaired or replaced and no further problems were noted.(Failure Date: 05/07/96)COND-HX-9 During power operation, an increase in reactor sulfate levels were observed.The reason for the increase was determined to be a condenser tube leak in Condensate (COND)System Heat Exchanger COND-HX-9.

The exact cause of the tube leak was indeterminate.

The tube was plugged and no further problems were noted.(Failure Date: 09/10/96)COND-P-2A During power operation, inboard and outboard seal leakage was discovered on Condensate (COND)System Pump COND-P-2A.

The cause of the problem was determined to be a casting defect in the bearing assembly that resulted in premature failure of the bearing.A new bearing, bearing body and bearing caps were installed.

Following completion of post-maintenance testing, no further problems were noted.(Failure Date: 08/18/96)COND-P-2B During power operation, mechanical seal leakage was observed on Condensate (COND)System Pump COND-P-2B.

The cause of the problem was determined to be.normal usage and.wear.'0

The inboard and outboard seals'and the outboard shaft sleeve were replaced.No further problems were noted.(Failure Date: 07/31/96)COND-PC V~During the annual maintenance and refueling outage, it was noted that the valve stem was worn on Condensate (COND)System Pressure Control Valve COND-PCV-40.

The cause of the problem was attributed to normal usage and wear.The valve stem, plug, seat ring, gaskets and packing were replaced.Following completion of successful diagnostic testing, no further problems were noted.(Failure Date: 04/23/96)COND-V-141 A During the annual maintenance and refueling outage, Engineering personnel were informed by the vendor for Conderihate (COND)System Valve COND-V-141A that the potential existed for failure of the anti-rotation collar due to key misalignment or lack of a set screw.The cause of the problem was attributed to manu'facturer assembly practices.

A new key was fabricated and installed on the valve.(Failure Date: 05/21/96)During power operation, an increased temperature was observed on a load side fuse clip in Containment Return Air (CRA)Motor ControHer CRA-42-8B6B for a fan in the primary containment cooling system.The cause of the problem was that the fuse clip had separated from the bakelite support, causing a higher resistance which resulted in the" temperature increase.The fuse block was replaced and no"further problems were noted.(Failure Date: 09/24/96)CRA-FN-SB During the annual maintenance and refueling outage, Maintenance personnel observed Containment Return Air (CRA)Fan CRA-FN-SB rotating in the incorrect direction during performance of preventive maintenance.

The cause of the problem was due to reversed phase lead connections.

The lead reversal apparently occurred during previous maintenance activities.

tp 31 0 The leads were re-connected to the correct configuration and no further problems were noted.(Failure Date: 05/16/96)CRD-HCU-2215 During the annual maintenance and refueling outage, Control Rod Drive (CRD)System Hydraulic Control Unit CRD-HCU-2215 level switch failed to actuate during surveillance testing.The cause of the problem was attributed to mechanical binding in the actuating mechanism.

A new level switch was installed and no further problems were noted..(Failure Date: 03/28/96)CRD-HCU-2623 During operation with the plant at 80 percent power, water leakage past the piston was noted on the accumulator for Control Rod Drive (CRD)System Hydraulic Control Unit CRD-HCU-2623.

The cause of the problem was attributed to normal wear or aging of the piston sealing mechanism.

The piston sealing mechanism.was replaced and no further problems were noted.(Failure Date: 02/04/96)~CRD-HCU-3443 During the annual maintenance and refueling outage, hydrogen leakage was noted past the packing and around the stem on a valve associated with Control Rod Drive (CRD)System Hydraulic Control Unit CRD-HCU-3443.

The cause of the problem was attributed to normal wear.The valve was replaced with a new valve and no further problems were noted.(Failure Date: 04/18/96)~CRD-'P-1B During power operation, minor leakage was observed on'he positive seal supply lirie and casing drain plug for Control Rod Drive (CRD)System Pump CDR-P-1B.The cause of the problem was attributed to normal wear.The line was disassembled and a new union joint was installed.

No further problems were noted., (Failure Date: 10/30/96)32

DLO-P-3A2 During full power operation, a broken coupling occurred on Diesel Generator Lube Oil (DLO)Pump DLO-P-3A'2.

The cause was attributed to high vibration due to inadequate pump mounting supp'orts.

The high vibration'resulted in increased stresses which led to crack development.

The coupling was replaced and pumps of similar design were inspected and additional couplings were replaced.A re-design of the support structure was not performed.

This decision was based on a cost benefit analysis.Couplings are to be inspected and replaced when necessary.(Failure Date: 01/05/96)~DLO-P-3B2 During operation with the plant at 60 percent power, a broken coupling occurred on Diesel Generator Lube Oil (DLO)Pump DLO-P-3B2.

The cause was attributed to inadequate design for the effects of resonance, cold spring and differential thermal expansion on coupling alignment.

The coupling was replaced and flex hoses were installed to dampen vibrations.

No further problems were noted.(Failure Date: 02/18/96)8)R-V-3 During the annual maintenance and refueling outage, leakage was observed on'adioactive Floor Drain (FDR)System Valve FDR-V-3.The cause of the problem was.determined to be normal usage,and wear.A contributing cause was line rust which degraded the seat.The..valve was cleaned and a new seat was installed.(Failure Date: 04/26/96)8)R-V-3 During the annual maintenance and refueling.

outage, Radioactive Floor Drain (FDR)System Valve FDR-V-3 failed to close during local leak rate testing.The cause of the problem was determined to be binding in the stem seal area.The stem nut had apparently been over-tightened during previous maintenance work.The stem nut was loosened and no f'urther valve stroking problems related to this event were noted.(Failure Date: 05/19/96)0 33' During power operation, Radioactive Floor Drain (FDR)System Valve FDR-V-3 exceeded the closing time limit during stroke time testing.The cause of the problem was determined to be foreign material and debris that had collected in the seat area.The source was loop seal piping debris that lodged into the seat from increased flow during a drain down of the undervessel drywell FDR sump.The valve was disassembled and cleaned.No further problems were noted with this particular valve.(Failure Date: 07/06/96)FDR-V-4 During power operation, Radioactive Floor Drain (FDR)System Valve FDR-V-4 exceeded the closing time limit during stroke time testing.The cause of the problem was attributed to foreign material and debris that had collected in the seat area.The source , was from loop seal piping debris that lodged into the seat from increased flow during a drain down of the undervessel drywell FDR sump.A contributing cause was loose set screws that allowed the coupling to shift out of alignment.

The valve was disassembled and cleaned.Existing set screws were tightened and an additional set were installed.

No further problems were noted.(Failure Date: 08/01/96)h During power operation, high vibration readings were noted on the bearings for High Pressure Core.Spray (HPCS)System Discharge Piping Fill Pump HPCS-P-3.The cause of the problem was determined to be normal wear leading to bearing degradation.

Th'e pump was disassembled and the shaft, sleeve, bearings, seals and o-rings were replaced.No furtherproblemswerenoted.(FailureDate:

09/11/96)~IRM-EMSQ401F During testing efforts while at power operation, it was noted that positive and negative adjustments could not be made to Intermediate Range Monitor (IRM)15-volt Power supply IRM-EMSQ-601F.

The cause of the problem was attributed to a defective circuit card in the power supply.The power supply was replaced and no further problems were noted.(Failure Date: 08/01/96)34

LPRM-DEJA/57 During power operation, several spurious alarms were observed with Local Power Range Monitor (LPRM)LPRM-DET-40/75.

The cause of the problem was attributed.

to a defective auxiliary circuit card.The auxiliary circuit card was replaced and no further problems were noted.(Failure.Date: 02/04/96)MS-ABC During the annual maintenance and refueling outage, an air leak was observed between the valve and manifold for Main Steam (MS)System Valve Air Operator MS-AO-4C.The cause of the problem was due to failed o-rings due to normal wear and usage.Four o-rings were replaced and no further problems were noted.(Failure Date: 05/28/96)MS-PS-47A During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47A was out of tolerance in the conservative direction.

The cause of the problem was that the piessure switch case had not been vented.The pressure'switch case was vented and no further problems were noted.(Failure Date: 11/26/96)During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47B was out of tolerance in the conservative direction.

The cause of the problem was that the pressure switch case had not been vented.The pressure switch case was vented and no further problems were noted.(Failure Date:~11/26/96)MS-PS-47C During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47C was out of tolerance in=the conservative direction.

The cause of the.problem was that the pressure switch case had not been vented.The pressure switch case was vented and no further problems were noted.:(Failure Date: 11/26/96)

MS-PS-47D During power operation, it was discovered that the setpoint for Main Steam (MS)System Pressure Switch MS-PS-47D was out of tolerance in the conservative direction.

The cause of the problem was that the pressure switch case had not been vented.The pressure switch case was vented and no further problems were noted.(Failure Date: 11/26/96)MS-V-165 C During testing efforts while at power operation, it was noted that Main Steam (MS)System Intercept Valve MS-V-165C would not re-open when a test button was released.The cause of the problem was attributed to poor manufacturing practices resulting in particu1ates in the assembly.The particulates caused binding in the solenoid.The air solenoid valve was replaced.(Failure Date: 09/15/96)MS-V-165 C h During power bperation, it,was again noted that Main Steam (MS)System Intercept Valve MS-V-165C would not re-open during testing.The cause of the problem was attributed to either particulate contamination or problems with the sealing o-rings.The air solenoid and o-rings internal to the valve were replaced.No further problems were noted.(Failure Date: 11/09/96)MS-V-37K During the annual maintenance and refueling outage, it was noted that Main Steam (MS)System Valve MS-V-37K would not properly return to the full-closed position during vacuum breaker operability testing.The cause of the problem was attributed to foreign material buildup (hardened lubricant) at the hinge area which resulted in valve binding.The material buildup was filed down and no further problems were noted.(Failure Date: 05/03/96)MS-V-37V During the annual maintenance and refueling outage, it was noted that Main Steam (MS)System Valve MS-V-37V would not pr'operly, return to the full-closed position during vacuum breaker operability testing.The cause of the problem was attributed to foreign material buildup (hardened lubricant) at the hinge area which resulted.in valve binding.=.36 e

The material buildup was filed down and no further problems were noted (Failure Date: 05/03/96)~RCIC-MO-110 During the annual maintenance and refueling outage, the yoke-to-valve collar for Reactor Core Isolation Cooling (RCIC)System Valve Motor Operator RCIC-MO-110 was found'o be loose and the operator could be rotated by hand.The cause of the problem was attributed to vibration.

The yoke was torqued to 110 ft-lbs and no further problems were noted.(Failure Date: 06/02/96)RCIC-V-66 During local leak rate testing in the annual maintenance and refueling outage, leakage in excess of allowable limits was discovered for Reactor Core Isolation Cooling (RCIC)System Valve RCIC-V-66.

The cause of the problem was attributed to a loose packing follower and an eroded shaft and carbon bushing due to normal aging and abnormal wear during usage.The shaft, bushing and packing set were replaced.No further problems were noted.(Failure Date 04/16/96)RFW-DT-1B During the annual maintenance and refueling outage, it was discovered that the inboard bearing for Reactor Feedwater (RPV)System Turbine RFW-DT-1B prematurely failed.The cause"of the problem was indeterminate.

New bearing pads and housing were installed and no further problems were noted.(Failure Date: 04/27/96)RFW-FR-607 During power operation, it was noted that a pen would stick on Reactor Feedwater (RFW)System Flow Recorder RFW-FR-607 when either increasing or decreasing flow.The cause was isolated problems with the rotor assembly.The pen slide bar was cleaned and the rotor..assembly replaced.No further problems were noted.-(Failure Date: 09/11/96).37 RFW-LS-624B During power operation, a Reactor Pressure Vessel Level-8 trip signal was received from Reactor Feedwater (RFW)System Level Switch RFW-LS-624B.

The signal was received concurrent with a Station Battery Bl-2 ground alarm.The cause of the problem was indeterminate.

The level switch was replaced and no further problems were noted.(Failure Date: 07/08/96)RHR-DPIS-12A During surveillance testing while at power operation, it was noted that Residual Heat Removal (RHR)System Differential Pressure Switch RHR-DPIS-12A could not be properly calibrated.

The cause of the problem was.attributed to normal aging and usage..The pressure switch was replaced and no further problems were noted.(Failure Date: 08/22/96)RHR-P-3 During power operation, Residual Heat Removal (RHR)System Water Leg Pump RHR-P-3 tripped on electrical thermal overload.The cause of the thermal overload trip was due to a failure of the pump thrust bearing.The vibration-induced fatigue failure of the bearing was due to inadequate design and service application.

The pump bearings and shaft were replaced with components of an updated design.No further problems were noted.(Failure Date: 10/16/96)RHR-TRS-601 During power operation, it was observed that the display was gradually failing on Residual Heat Removal (RHR)System Temperature Recorder RHR-TRS-601.

The cause of the problem was attributed to normal aging and usage.A new display was installed and no further problems were noted.(Failure Date: 06/24/96)RPS-EPA-3E During surveillance testing while at Hot Standby, it was noted the Reactor Protection System (RPS)Electrical Protection Assembly RPS-EPA-3E could not be calibrated.

The cause was isolated to a problem with the logic board.38 The logic board was replaced and no further problems were noted.(Failure Date: 03/07/96)~RPS-RLY-K16B During the annual maintenance and refueling outage, it was noted that Reactor Protection System (RPS)Relay RPS-RLY-K16B was in a degraded condition and failing.The cause of the problem was attributed to normal aging and usage.The relay was replaced and no further problems were noted.(Failure Date: 05/14/96)~RRC-PS-18A During testing while at power operation, it was noted that the as-found trip setpoint for Reactor Recirculation (RRC)System Pressure Switch RRC-PS-18A was well below the administrative limit and could not be restored to within the required tolerances.

The cause of the problem was indeterminate.

The pressure switch was replaced and no further problems were noted.(Failure Date: 08/15/96)e~SLC-LT-1 During power operation, it was observed that Standby Liquid Control (SLC)Level Transmitter SLC-LT-1 appeared to be providing erroneous indication of SLC tank level.The cause of the problem was due to a plugged sensing line (bubbler tube)which resulted in air backpressure influencing the output of the level transmitter.

The bubbler tube was rodded out and the transmitter was returned to service.No further problems were noted.(Failure Date: 10/06/96)~SLC-TS-3 During surveillance testing while at 58 percent, power, it was noted that Standby Liquid Control (SLC)System Temperature Switch SLC-TS-3 could not be calibrated.

The cause of the problem was indeterminate.

The temperature switch was-replaced and no further problems were noted.(Failure Date: 02/04/96)I~~39 2.6 Fuel Performance This section contains information relative to fuel integrity.

This input is provided solely for informational purposes and ease of reference.

There were no indications of failed fuel during 1996.Regulatory Guide 1.16, Section C.l.b.(4), only requires reporting where, based on examination, there are indications of failed fuel.Bachground During 1995 the Supply System modified a WNP-2 FSAR commitment pertaining to surveillance of post-irradiated fuel.As part of our routine fuel inspection program that was described in the WNP-2 FSAR, a visual examination was to be performed on five to ten percent of the highest burnup assemblies of the discharged fuel after each refueling.

-The visual examination was for the detection of indications of generic gross cladding defects or anomalies that may have occurred during operation.

This commitment was accepted by the NRC in the WNP-2 Safety Evaluation Report, as adequately addressing the issue of post-irradiation surveillance.

As an alternate approach, the Supply System evaluated post-irradiation fuel inspection activities and determined that it would be acceptable to perform visual inspection only on discharged fuel where there was indication of either actual or suspected gross cladding defects or anomalies.

Examples of such indications include increased Offgas System activity and negative impacts on water chemistry paiameters.

This change to the post-irradiation surveillance program was incorporated, into Amendment 50 (August 1995)to the WNP-2 FSAR.1996 Results Based.on plant operational indicators, there was-no evidence of fuel performance problems'during Cycle 11.Accordingly, a visual inspection of the discharged fuel was determined to be unnecessary.

40 This section contains summaries of the Safety Evaluations (SE)completed for activities implemented during 1996 and is included pursuant to 10CFR50.59.

Federal Regulation 10CFR50.59 and Supply System Operating License NPF-21 allow changes to be made to the facility and procedures as described in the safety analysis report, and tests or experiments to be conducted which are not described in the safety analysis report without prior Nuclear Regulatory Commission approval, unless the proposed change, test or experiment involves a change in the technical specifications incorporated in the license or an unreviewed safety question.A proposed change, test or experiment is deemed to involve an unreviewed safety question if 1)the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased, or 2)a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be created, or 3)the margin of safety as defined in the basis for any technical specification is reduced.Each change summarized in the following sections was evaluated and determined to neither represent an unreviewed safety question nor require a change to the WNP-2 Technical~~~~~~~~~~~~Specifications.

~g In certain instances, a single safety.evaluation was used for several implementing activities.

This is allowed by procedure only where an existing evaluation adequately covers the specific change being considered.

If*the activity extends beyond the plant mode bounds, then a separate evaluation is required.A separate evaluation is also required if out-of-service equipment, equipment lineups, modifications or temporary alterations are in place that invalidate the existing evaluation.

41 2.7.1 Plant Modifications The section contains information pertaining to implemented Plant Modification Records (PMRs)and is included pursuant to 10CFR50.59.

~PNIR 864525-7 (SE 95-084)This PMR provided for snubber optimization of Main Steam System, Loop C, inside the primary containment drywell and containment exhaust purge bypass piping in the reactor building.This modification involved the removal and subsequent replacement of snubbers with rigid struts.It was concluded from the safety evaluation that the affected piping systems, components and supports were reanalyzed and remain qualified to applicable ASME Code and WNP-2 design basis requirements.

Pressure boundary integrity of the piping systems and primary containment are maintained and engineered safety features used in mitigating transients will remain operable.The only possible accidents'are those associated with reactor pressure boundary and containment isolation.

Since the piping and component analyses meet all design requirements and no new pipe breaks are created in main steam piping, then the pressure boundary is maintained.

The containment exhaust purge piping is exempt from postulated pipe rupture due to the ASME exemption criteria of being less than or equal to one-inch in diameter.All equipment will remain functional to maintain containment isolation.

PMR 87-0244-6 (SE 93-200)This PMR provided modification of the Reactor Recirculation (RRC)System by installing Adjustable Speed Drives (ASD)to control recirculation pump speed.This modification also provided direction for ASD interconnections to the Main Control Room.The ASD System is a functional replacement for a hydraulically-controlled flow control valve arrangement.

It was concluded from the safety evaluation that the RRC System has no active safety function.Its primary relation to the design analyses is as an initiator of events.This modification does not alter assumptions pertaining to RRC pump response during transients or accidents.

The coast-down characteristics are similar to all.previous analyses of recirculation system events.A 42 0

'I The design of the ASD interlocks and limiters will prevent operation of the system outside of acceptable operating parameters.

Installation activities would occur during the refueling outage.Any potential failures that could occur during post-modification testing are bounded by previous analyses.~PMR 87-0282-0 (SE 95-098)This PMR provided for the installation of an additional steam tunnel fan/coil air cooling unit to provide for improved peak summer load performance and as backup protection for the existing units.It was concluded from the safety evaluation that the seismically-mounted backup unit provides no safety function.The unit would be installed to meet applicable design requirements preserving the important to safety function of equipment located in the vicinity.All associated mechanical and electrical components:

would also be installed to appropriate standards commensurate with this activity to ensure that no important to safety functions are affected.No previously evaluate'd transients or operator post-accident responses are adversely impacted by the change.r PMR 89-0299-6 (SE 95-100)This.PMR provided for the replacement of flow transmitters in the Containment Atmosphere Control (CAC)System with units of an improved design.It was concluded from the safety evaluation that the five new replacement transmitters would be procured to Quality Class 1 requirements and installed such that the original design function will be maintained.

The new transmitters do not change the function or configuration of the CAC System in response to a design basis accident.All measurement ranges, indications and recording and alarm functions remain the same as prior to the change.PMR 91-0438-0 (SE 94-209)This PMR provided for the replacement of Reactor Feedwater (RFW)analog control system components with a digital control system upgrade.This change was made due to'shortcomings with the.existing system, which had significant impact on plant performance.

The RFW Level Control System controls the discharge of the RFW pumps into the reactor pressure:vessel to maintain.leyel within predetermined limits.~~~~43 It was concluded from the safety evaluation that the modification to the RFW Level Control System and associated Turbine Governor Control System would not increase the probability of a previously evaluated transient or impact the outage safety'plan.

The RFW System is a non-safety related system that is used to control reactor vessel water~level during normal"operation.

The system is.physically isolated when the core is flooded during a refueling outage.The level trips and plausible accidents are bounded by the automatic response of the Reactor Protection System.Implementation of the new level control system reduces operator burden by providing direct and consolidated control of turbine speed.and enabling earlier introduction of the feedwater pumps during startup valve/feedwater pump crossover.

The change does not result in the possibility of increased challenges to important to safety systems.The upset range level indicator or feedwater flow indicators mentioned in Regulatory Guide 1.97 are not changed by this modification.

~PNIR 5Q-0085-0 (SE 96-002)This PMR provided for modification of Containment Atmosphere Control (CAC)System push-button"valve test" switches CAC-RMS-PBA and CAC-RMS-PBB on the hydrogen recombiner control panel.The push-buttons were replaced with maintained-contact control keylock switches.This change prevents the bypassing of the pressure suppression function of the drywell downcomers in the event of single test switch failure or inadvertent depressing of the push-button.

This modification also corrected an operator"work-around" by elimination of the need to install a jumper around the CAC"valve.test" switch during valve testing, rather than depressing the push-button for extended periods.It was concluded from the safety evaluation that the new switches would not introduce~any new failure modes that could increase the consequences of previously evaluated transients.

The keylock feature was added to prevent inadvertent actuation during normal plant operation.

There is no'impact on design basis bypass leakage rates.The addition of two switches in series serves as an additional bariier to single failure of any one switch.The replacement device serves an equivalent function, with improved performance characteristics.

k

~PMR 92-0209 (SE 95-102)This PMR provided for installation of Jet Pump Sensing Line (JPSL)mitigation support assemblies on the sensing lines of each of the 20 existing jet pump diffusers.

Four of the JPSL supports were required on each of the sensing lines.The purpose of this modification was to reduce the resonant vibration responses of the JPSLs by shifting the natural frequencies of the line into a band which will not coincide with the vane passing frequency associated with recirculation pump speed.It was concluded from the safety evaluation that this modification improves the security of the JPSLs and reduces the probability of sensing line failure.The mitigation clamps have been seismically analyzed to ensure they would not fail in a manner that could damage safety-related structures in the event of an earthquake.

Based on the results of stress analysis, loose parts analysis, and material compatibility it was determined that there is no credible failure mode associated with the clamp assembly that could impact previously evaluated accidents.

~PMR 93-0049-0 (SE 95-015)This PMR provided for modification of the control circuitry for High Pressure Core Spray System (HPCS)Valves HPCS-V-10 and HPCS-V-11 by the addition of time-delay on the drop-out timers.This modification will allow trapped rotor flux to decay following movement to a fullwpen position and prevent inadvertent circuit breaker tripping.It was concluded from the safety evaluation that the safety function of these valves would not be impacted by the change.The valves are normally closed, except during testing, and the passive component function (electrical integrity) is maintained with the new: relays.There would be no change in HPCS accident response time or support of secondary containment bypass leak rate.The added time delay simply prevents inadvertent circuit breaker tripping when the valves are immediately taken to the closed position when initially traveling in the open direction.

~PMR 93-0065-0 (SE 96-101)This PMR provided for deletion of the lead-lag function of Radwaste Building Chillers WCH-CR-51A and WCH-.CR-51B and modification of the control circuitry to allow the two chillers to run independently.

" This change will allow the chillers to be controlled independently from their own individual chilled water sensors;rather than from a common sensor.45

It was concluded from'the safety evaluation that the availability of the chillers will not be affected by removal of the lead-lag function from the.control system.The cooling function normally provided by the chillers would be assumed by the Service Water System until such time that the units were returned to service.The affected equipment is non-safety related, does not have an accident mitigation function, does not have an off-site dose reduction function and is not a credited system which supports equipment important to safety.~PMR 93-0157-2 (SE 95-097)This PMR provided for replacement of Reactor Building to Wetwell Vacuum Relief Valves CSP-V-S, CSP-V-6 and CSP-V-9.The valves were replaced with components of an improved design to more reliably meet allowable leakage requirements.

It was concluded from the safety evaluation that the safety function of these CSP valves is to prevent excessive vacuum from developing in primary containment from such cases as inadvertent containment spray actuation.

The new valves were procured and installed to Quality Class 1 and Seismic Category 1 standards.

There was no change in valve opening time, leak-tightness, quality and seismic requirements.

System interfaces were also unchanged.

There were no changes from the original valve function, other than a seal design which will allow for a tighter seal.The ability to seal consistently when in a containment isolation mode would decrease the consequences of an accident.~PNIR 94-0057-0 (SE 94-074)This PMR provided for mechanically blochng Reactor Recirculation (RRC)System Flow Control Valves RRC-V-60A and RRC-V-60B in the full-open position and removal of the associated hydraulic system.This modification was performed in support of the installation of an Adjustable Speed Drive System on the RRC pump motors.It was concluded from the safety evaluation that this change would not have an adverse impact on the reactor coolant pressure boundary.Stress analyses performed on the RCC piping show that piping stresses will not be increased as a result of modifying the flow control valves.The final configuration of the modification would not introduce any new failure modes or operational transients.

Reactor protection trip delay time and pump/motor inertia would also not change.The.Adjustable Speed Drive System was designed to ensure that acceptable fuel thermal margins are maintained in the event of a reactor protection trip.46 PMR 94-0332-1 (SE'95-103)

This PMR provided for the installation of a zinc injection system.The addition of depleted zinc reduces the buildup of Co-60 on primary piping and components.

The modification consisted of the installation of'a vendor-supplied skid for the injection of dissolved zinc oxide into the Reactor Feedwater~V)System.It was concluded from the safety evaluation that zinc levels of less than or equal to 65 ppb would not have an adverse affect on the intergrannular stress corrosion cracking characteristics of primary system components.

Based on information received from the vendor, it was determined that this modification would not impact'RFW pump seals, RFW nozzles or RFW flow measurement instrumentation.

There would also be no"detrimental impact to the fuel assemblies.

Installation and testing of the skid would not interfere with plant operations.

The skid is also isolatable from plant components by the use of double isolation valves.PMR 94-0346-0 (SE 95-066)This PMR provided for the rework and modification of fire-rated penetration seals to support current fire tests and restore the penetrations to an acceptable configuration.

This effort was associated with an ongoing penetration seal upgrade project.The upgrade project was implemented based on the results of an analysis which revealed that not all of the installed configurations are supported by current fire tests or acceptable evaluations.

It was concluded from the safety evaluation that penetration seal design variations have no impact on design basis accidents, only events.The design of the seals is int'ended to mitigate the effects of fires and, in some installations, other design basis events.The changes made by this modification have no impact on the ability of safety systems to perform during accident conditions, nor do they increase challenges to safety systems.The fire barriers and seals within the scope of this modification are currently declared, inoperable and an hourly fire tour has been implemented as a compensatory action.The fire tours will not be removed until the seals and barriers have been declared operable.During the restoration efforts, required safe shutdown systems and components will be maintained in accordance with licensing basis documents.

47

PMR 94-0364-0 (SE 96-006)'This PMR provided for installation of a permanent curtain shielding support structure around a portion of Reactor Recirculation (RRC)System, Loop"A" piping for ALARA considerations.

The permanent structure eliminated the need to assemble tube-lock scaffolding and install shielding during every outage.It was concluded from the safety evaluation that installation of the shielding and the shielding support system would not affect any system, structure or component.

that mitigates the consequences of a design basis accident.The shielding support structure meets Seismic Category 1M requirements to prevent adverse II/I interactions with important to safety systems, structures and components.

3 The shielding and support structure was also designed to withstand all applicable loads, including pipe breaks and missiles.The shielding, which is located in primary containment, does not restrict access to vital areas or otherwise impede actions to.mitigate the consequences of design basis accidents.

PMR 94-0364-1 (SE 96-010)This PMR provided for installation of a permanent curtain shielding support structure around a portion of Reactor Water Cleanup (RWCU)piping for ALARA considerations.

The permanent structure eliminated the need to assemble tube-lock scaffolding and instaH shielding during every outage.It was concluded from the safety evaluation that installation of the shielding and the shielding support system would not affect any system, structure or component that mitigates the consequences of a design basis accident.The shielding support structure meets Seismic Category 1M requirements to prevent adverse II/I interactions with important to safety systems, structures and components.

The shielding and support structure was also designed to withstand all applicable loads, including pipe breaks and missiles.The shielding, which is located in primary containment, does not restrict access to vital areas or otherwise impede actions to mitigate the consequences of design basis accidents.

~PMR 95-0174-0 (SE 95-099)This PMR provided for the installation of an iron injection system.The addition of iron oxalate reduces the buildup" of'Co;.60 on.primary piping and components.

The modification

'consisted of a permanent stainless steel injection point that was welded to the 36-inch condensate booster pump, suction, line.48 0

It was concluded from the safety evaluation that, although iron concentration will be increased in the reactor feedwater, the level would still be well below the design basis value of 5.0 ppb.Increasing the iron concentration from 0.1 ppb to 0.5 ppb would not adversely impact any safety-related structure, system or component.

It was determined that this modification would not impact the performance of reactor feedwater heaters or flow nozzles.The new piping that is installed will be compatible with the existing piping design pressures and temperatures.

The increase in iron concentration will also not affect the integrity of the fuel cladding.The cladding would not become embrittled or experience any wall thinning.PMR 95-0236-0 (SE 95-092)This PMR provided for the replacement of eight top-entry Local Power Range Monitor (LPRM)detector assemblies with bottom-entry models of a better design.This modification was made to provide for improved efficiencies during refueling outages.It was concluded from the safety evaluation that the new LPRM detectors meet or exceed the design requirements of the original detectors.

All of the replacement compone'nts, including cable and connectors, are qualified for the environment in which they would be.installed.

No activities are included which would impact systems arid result in challenges to safety-related equipment.

Following changes to the processing software to compensate for the different sensitivity of the new LPRM detectors, the.function will be identical to the existing system.1 PMR 96-0043-0 (SE 96-015)This PMR provided for the modification to Radwaste Building Release Duct Radiation Monitor Sample Racks WEA-SR-25 and WEA-SR-25A to prevent overheating of the system blower.This change was made to increase the reliability of Sample Rack WEA-SR-25 by reducing flow restrictions to lower exhaust air sample blower operating temperature.

The blower had been operating at a higher than design temperature and required periodic replacement due to premature failure.Loss of the blower would result in the sample racks becoming inoperable.

It was concluded from the safety evaluation that this modification would not alter safety-related system response to an accident condition.

The change will ensure that the radiation monitors perform any required post-accident function for the duration of the transient..

Environmental conditions withinthe rack area are bounded by current radiation and temperature limits.Post modification testing would also verify final operability.

of the sample racks.49

During.the implementation phase, compensatory alternate sampling methods would be implemented and the sample racks not returned to operable status until the modification and associated follow-up testing were completed.

~PMR 96-0057-0 (SE 96-034)This PMR provided for removal of the Demineralized Water (DW)System flush capability for the Residual Heat Removal (RHR)Loops"A" and"B" sample lines.This modification also provided for installation of additional isolation valves in the jet pump sample lines, between the DW System and Post Accident Sampling System (PASS).The reason for the modification was to minimize recurrence of contamination of the DW System through the PASS by means of the demineralized water flushing lines.It was concluded from the safety evaluation that removal of a portion of the DW System flush capability slightly increases the potential for increased dose.However, calculations have shown this slight change in dose would have a negligible effect in total area dose.The potential increase in dose within the secondary containment envelope was reviewed'nd found to be within current design requirements and limits.All credited accident mitigation equipment and systems would remain functional and operable with the implementation of this modification.

The PASS function will not be impacted for post-accident sampling and the ability to obtain data for post-accident evaluation, sheltering or recovery actions would still be maintained.

50

Temporary Modifications and Instrument Setpoint Changes This section contains information pertaining to implemented'Temporary Modification Requests (TMRs)and Instrument Setpoint Change Requests (ISCRs)and is included pursuant to 10CFR50.59.

ISCR 1280 (SE 96-014)This ISCR provided for a change to the setpoints for the isolation signal due to condenser vacuum for Main Steam (MS)System Pressure Switches MS-PS-56A, MS-PS-56B, MS-PS-56C and MS-PS-56D.

The new setpoints were changed by means of a calculation and;will allow less loss of vacuum prior to initiating an MSIV isolation.

It was concluded from the safety evaluation that allowing for less loss of vacuum prior'o initiating an MSIV isolation would result in a reduction in operating margin.The low vacuum function is provided to isolate the main steam system in the event of a loss of main condenser vacuum which would remove the effective capability of the condenser as a heat sink.The reduction in operating margin would not increase the probability of a loss of condenser vacuum event.However, it could slightly increase the probability of an MSIV isolation event.It was determined that any contribution to the increase in the probability of the MSIV isolation event due to the decrease in operating margin caused by the more conservative setpoint ip significantly less than the probability of the MSIV isolation event.In addition, this small increase in the probability of the MSIV isolation event does not contribute to an mcrease in frequency.

ISCR 1284 (SE 96-041)This ISCR provided for revision to the ANALYZE computer program configuration file to turn off the zero stabilizer function for stack monitor intermediate and high range detectors PRM-RE-1B and PRM-RE-1C.

It was determined that the zero stabilizer function could fail at high count rates and result in an incorrect indication of system failure in the main control room.It was concluded from the safety evaluation that this system is a post-accident system with no control functions.

Information from this system is used for decisions pertaining to accident"follow-up actions.However, the information used by Operations personnel in these scenarios will not be affected, by this change.-'=~~51~tl,

The change affects only the zero stabilization function of the multi-channel analyzer system and has no impact on any other part of the system or the plant.The zero stabilizer function of the stack monitor multi-channel analyzer provides automatic correction for small changes in the zero value of the spectrum.Turning off the function.will simply disable the testing of the zero stabilizer range.It will not affect the gain stabilizer function.The gain stabilizer function provides all of the automatic control that is required to maintain the multi-channel analyzer within required tolerances.

This change has no affect on the gross count rate response of the system.Gross count rate indication is the information that is used for accident follow-up decisions.

~TMR 95-105 (SE 95-105)This TMR provided for modification of the suction and discharge lines foi Radwaste.Building HVAC (WOA)Sample Racks WOA-SR-18A, WOA-SR-18B, WOA-SR-19A and WOA-SR-19B to increase fio'w through the system.Increased flow was obtained by.merging.the intake and exhaust lines to the pump suction, and exhausting to the local atmosphere.

The increased flow was necessary to reduce blower operating temperatures to preclude premature failure.It was concluded from the safety evaluation that the modification will ensure that the blowers are operating within vendor recommendations to ensure availability during the required post-accident operating time.The control room remote air intake radiation monitors are not the initiator of any previously evaluated transient.

Based on testing results,.it was concluded that system flow would be increased by approximately.1.5 times the current value, which dropped temperatures within the recommended operating range.With this modification, the blowers could be expected to operate reliably during post-accident conditions.

TMR 96-013 (SE 96-033)This TMR provided for removal of a tab from the indicator shaft for Reactor Core Isolation Cooling (RCIC)System Valve RCIC-V-66 to improve the operating characteristics of the valve.With the tab removed, the indicator shaft will not turn when the hanger arm rotates on the actuator shaft.This would then allow for the ability to sufficiently tighten indicator shaft packing to prevent leakage.It was concluded from the safety evaluation that the hanger arm and disc assembly.of the valve would continue to function a's designed to ensure rapid isolation in the event of an RCIC System line break.'he hanger arm and disc assembly will move more freely, being independent of.the indicator, shaft.52 Removal of the tab from the indicator shaft would not affect the system injection or containment isolation function of the valve.Because the indicator shaft will no longer turn in its packing, there is less probability of packing binding on the shaft or packing degradation due to wear.~TMR 96-023 (SE 96-066)This TMR provided for installation of a filtration system near the Standby Service Water (SSW)spray ponds to remove suspended solids from the spray pond water.The side stream filtration system is designed to remove organic material and silt present in the water, which will assist in maintaining the required heat transfer capability of the SSW System heat exchangers and reduce water treatment costs.It was concluded from the safety evaluation that the change is non-safety related.Potential impacts on important to safety systems and functions were evaluated and it was concluded none of those impacts'would result in the inability of those systems and components to meet their safety function.The impacts evaluated relate to seismic effects, spray pond water inventor requirements, tornado effects and the effects of localized flooding.The SSW system and ultimate heat sink would still be available with full capability to mitigate accidents.

~TMR 96-029 (SE 96-100)This TMR provided for increasing the voltage applied to a Traversing Incore Probe (TIP)indexer.Indexer"B" would not move beyond channel one.This modification would increase the applied torque to the indexer mechanism and restore proper operation.

It was concluded from the safety evaluation that the increase in motor voltage would not impact any of the analyzed transients.

The modification involves increasing the voltage to the indexer motor to a maximum of 200 VAC for no more than five seconds.The voltages and currents to be applied to the non-safety related indexer motor are within the design characteristics of the penetration module.53

0 FSAR Changes This section contains information pertaining to FSAR Licensing Document Change Notices (LDCNS)and FSAR Change Notices (SCNs)and is included pursuant to 10CFR50.59.

LDCN-FSAR-96-063 (SE 96-078)This LDCN provided for a change to the FSAR to allow for the use of optimum flow rate for iodine sampling and substitution of a local alarming continuous air monitor for a mobile monitoring system.'It was concluded from the safety evaluation that dose avoidance during the course of an accident involving radiation releases would be enhanced by the change due to earlier and more reliable indications of iodine in the air.A more reliable continuous air monitor is also being substituted for the currently-installed unit.The use of an optimum flow rate for iodine sampling and implementation of an improved air monitoring system do not increase th'e probability or consequences of an accident previously evaluated.

LOCN-FSAR-96-068 (SE 96-091)This LDCN provided for a change to the FSAR to lower the minimum diesel generator engine bay temperature to 40 degrees fahrenheit.

In addition, the description of the'VAC system for the High Pressure Core Spray (HPCS)System batteries was modified to allow for use of supplemental, heaters or other means to maintain battery temperature greater than or equal to 60 degrees fahrenheit.

It was concluded from the safety evaluation that lowering the diesel engine room temperature from 70 degrees to 40 degrees would not have an adverse affect on the starting capability or reliabiTity of the engines.The diesel engine supplier provided information to the effect that, as long a the coolant and lube oil temperatures are maintained at or above 85 degrees by a"keep warm" system, the engines can achieve a ten-second start in an ambient temperature of 40 degrees.The battery manufacturer supplied information to the effect that the HPCS batteries will provide full-rated capacity as long as the electrolyte temperature is at or above 60 degrees.'ecause lowering'of the.room temperature has no adverse impact and the batteries will.perform as required at 60 degrees, the components will continue to function as required='in support of emergency core cooling system accident.mitigation.

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~LDCN-FSAR-96-077 (SE 96-Q90)This LDCN provided for a change to the PSAR to reflect planned organizational changes within the Plant Support Services Department and the addition of new ALARA review'riteria.

It was concluded from the safety evaluation that, from an organizational perspective, the change only involves realignment of responsibilities.

Current functions such as solid waste processing have not changed.Clear criteria for determiiiing the need for an ALARA review for procedures was also provided.These changes are not in confiict with any licensing basis documentation or commitments.

Although the review of procedures for ALARA considerations is an element of the ALARA Program, the specific review criteria are not part of any regulatory basis for radiological protection requirements.

, LBCN-FSAR-96-079 (SE 96-097)This LDCN provided for a change to the FSAR to refIect updated actions that are to be taken following an earthquake.

It was concluded from the safety evaluation that the changes are consistent or conservative with EPRI guidance and a draft NRC regulatory guide pertaining to earthquake planning and follow-up actions.The recommended actions would ensure that conservative shutdown decisions are made and that the reliability of structures, systems, and components following an earthquake is not reduced.These changes affect only the criteria used to initiate a controlled manual reactor shutdown.No hardware is impacted.'

LDCN-FSAR-96-080 (SE 96-092)" This LDCN provided for several changes to the Fire Protection Program to refiect updated compensatory measures and editorial enhancements.

It was concluded from the safety evaluation that previous fire protection analyses had concluded that compensatory measures could be altered under certain circumstances.

This change allows Control Room Operators to act as a fire tour for inoperable wet-pipe sprinkler system and Halon confinement barriers..The change also allows for'eight hours to establish the operability of video and portable detection systems when sprinkler or-detection systems are inoperable in high radiation or contaminated areas.0-i These changes are consistent with previously-approved safety evaluations and provide reasonable assurance that adequate compensatoiy measures will still be implemented for the observation of fire or fire hazards in the areas of inoperable fire protection equipment.

LDCN-FSAR-96-081 (SE 96-099)This LDCN provided for a change to the FSAR to delete the requirement for Fast Flux Test Facility (FFI'F)personnel on the Hanford Reservation to provide direct WNP-2 Control Room notification of a sodium oxide release.Procedural arrangements are in place between FFTF and Supply System personnel for timely notification of the WNP-2 Control Room in the event of a sodium oxide release.It was concluded from the safety evaluation that changing the method of no'tifying the control room would have no impact on the probability or consequences of a previously-

.evaluated accident.The original assumption of 55 minutes to notify the WNP-2 Control Room is still valid and provides adequate time for personnel to either isolate the control room or put on portable breathing equipment.

e e By continuing to provide ample waniin'g time, Supply System Operators would be able to respond accordingly and place the plant in a normal shutdown condition in the event of an accident.LDCN-FSAR-96-086 (SE 96-096)This LDCN provided for a change to the FSAR to reflect the downgrade of Standby Service Water (SSW)System Pumphouse Air Intake Fan POA-FN-2A from Quality Class-1 to Quality Class-Augmented (QC-A).It was concluded from the safety evaluation that the fan provides no active support for any equipment important to safety.The safety-related cooling function for the standby service water pumphouse HVAC system does not require the operation of POA-FN-2A.

The SSW pump and related equipment are cooled by a safety-related fan-coil unit.The potential loss of the intake fan would not result in pumphouse ambient temperatures.

reaching the maximum normal operating limits for safety-related equipment.

It was determined that a quality classification of QC-A is adequate for this component.

=e~SCN 95-058 (SE 96-035))+This SCN provided for a change to'the FSAR to reflect a revision to the Reactor Core Isolation Cooling (RCIC)System isolation time delay logic.Closure of RCIC System Primary Containment Isolation Valves RCIC-V-8, RCIC-V-63 and RCIC-'V-76 is delayed by logic time delay relays to prevent inadvertent isolation from high flow during system 56

~o initiation when the steam flow to the turbine is momentarily above the high flow setpoint.The calculated time delay relay setpoint in each division was changed from a two-second nominal value to a three-second aHowable value.Process and instrument loop accuracies that were previously not.accounted for were included in the revised calculation.

It was concluded from the safety evaluation that this change would not impact the overall function and accident response of the RCIC System.The safety function of these relays, during design basis event mitigation is to 1)isolate the system to limit mass energy blowdown for an RCIC System high energy line break, and 2)limit long-term secondary containment bypass leakage after'a system trip following a loss of coolant ac'cident.

The allowable value of three seconds is derived from, and bounded by, the upper analytical limit of four seconds used in the event blowdown calculation.

The accident analysis assumes the four second delay (including process and loop inaccuracies) prior to the RCIC valves receiving a closure signal.SCN 95-062 (SE 95-095)This SCN provided for a change to the FSAR to describe changes to the new fuel storage vault.Deck plates were added to the vault racks and only allow fuel to be placed in alternate locations.

These temporary plates constitute a template which limit placements of new fuel to alternate locations in the vault.This change allows for the safe and efficient handling of ABB re-load fuel.It was concluded from the safety evaluation that this activity has the effect of markedly increasing the space between the adjacent fuel assembHes.

The additional spacing renders a criticality accident considerably less than the low probability arrangement previously employed in these racks.The proposed physical changes to the refuel floor to accommodate the change do not impact or increase the consequences of previously evaluated transients.

Items addressed included heavy crane load paths and seismic requirements.

SCN 95-064 (SE 95-091)This SCN provided for a change to the Fire Protection Program to reflect a revision of fire door surveillance requirements.

The primary technical change consists of the performance of weekly position inspections for unlocked, unsupervised fire doors instead of the current inspection by, routine operator tours.It was concluded from the safety evaluation that the less frequent surveillance to nonessential and non-plant block doors will continue:to ensure their operability.

Nonessential fire'doors, by definition, are not credited with ensuring safe fire shutdown..

57 I

The changes in surveillance frequency do not affect the operation of fire protection system equipment beyond that previously evaluated.

Since the change does not alter fire door operation or create new failure modes, extending the period between surveillance testing would not lower the ability of the equip'ment to mitigate or prevent the propagation of fires.'CN 95-070 (SE 96-007)This SCN provided for a change to the FSAR to reflect that the High Pressure Core Spray (HPCS)System diesel generator motor-driven air compressor is powered from Motor Control Center (MCC)MC-6B instead of the HPCS bus.'It was concluded from the safety evaluation that supply power from non-safety related MC-6B to electric motor driven Diesel Starting Air (DSA)System Air Compressor DSA-.M-C/1C would not affect the consequences or probability of a previously evaluated accident.The air compressor is of an augmented quality class due to seismic requirements, but has no specific safety function.0'oss of the air compressor due to loss of MC-6B would not affect operation of the HPCS diesel generator.

Safety-related Diesel Starting Air Receivers DSA-AR-1C and DSA-AR-2C aie capable of maintaining system air pressure and capacity for starting of the diesel generator, regardless of the status of the air compressor.

SCN.,95-072 (SE 95-101)This SCN provided for a change to the FSAR to reflect updated secondary containment

.bypass leakage paths.Some existing bypass paths were eliminated from consideration

'nd others were added based on a technical evaluation.

The overall allowed bypass leak rate of 0;74 scfli was not changed by this SCN.It was concluded from the safety evaluation that revising the FSAR to reflect the potential bypass leakage paths for secondary containment would not impact previously evaluated transients.

The overall allowed leakage was not changed.Since the leak rate was not modified, the offsite and control room dose consequences would not be affected.The primary containment penetrations that were eliminated as secondary containment bypass leak paths were all analyzed to ensure that any leakage would be processed by the Standby Gas Treatment System.The valves eliminated from consideration as potential bypass leakage paths were containment isolation valves.The measured leakage would still be included in the Leak Rate Testing Program (Type B'and Type C).58

~SCN 96-005 (SE 96463)This SCN provided for a change to the FSAR and Emergency Plan to reflect current bases and methods for the controlling and monitoring of contamination.

It was concluded from the safety evaluation that the change would not involve systems, structures or components and does not impact the physical barriers that protect against the uncontrolled release of radioactivity.

Controls have been established to ensure there is no detectable fixed or loose contamination outside of the Radiologically Controlled Area under normal and emergency conditions.

The intent to control licensed material has not been modified.The current mix of isotopes in dry active waste are such that the other detector types will provide greater assurance that licensed radioactive material would be controlled in a manner consistent with ALARA considerations.

SCN 96-008 (SE 95-106)This SCN provided for a change to FSAR drawings to reflect an update of fire area boundaries and fire barriers.In some cases, essential and nonessential fire barriers have been downgraded.

However, the derated barriers are simply corrections or previous errors where no fire rating was actually required.It was concluded from the safety evaluation that the proposed changes do not lower the ability of safety systems to perform during accident conditions.

The changes in fire area boundaries do not affect the operation of, or become hazards to, accident mitigation equipment beyond that previously evaluated.

The proposed barrier changes do not increase radiological releases or exposures to.control room personnel since configuration controls exist to ensure secondary containment and control room ventilation boundary penetration seals are present, independent of the fire rating of the barrier.SCN 96-009 (SE 96-030)This SCN provided for changes to the FSAR and Emergency Plan to allow for removal of on-site Thermoluminescent Dosimeter (TLD)readers and to transfer the processing of exposure information.,to a certified local vendor.59 It was concluded from the safety evaluation that dose avoidance during the course of an accident involving radiation releases would be based on direct readout dosimeters.

The TLDs are processed as a follow-up after any dose has been received and the information is used as comparison to the direct dosimeter information.

The results of TLD measurement of external doses to workers or the public would be available from the vendor within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> upon request of the information.(SE 96-044)This SCN also provided for a change to the FSAR to allow for deletion.of reference to automatic radwaste drum processing (filling, storage and monitoring).

The current method for drum processing consists of a manual operation.

It was'concluded from the safety evaluation that radwaste drum processing is a manual activity that would not increase the probability or consequences of an accident.The processing activity does not affect any safety-related or important to safety plant equipment.

It was also concluded that the dose to the public from a manually filled drum would be the same as from the same drum filled in a remote manner.SCN 96-012 (SE 96-022)This SCN provided for a change to the WNP-2 Physical Security Plan to allow security officers who have left the protected area to re-enter the protected area without being subjected to a metal detector search.In addition, the plan was revised to allow for the removal of protected and vital area keys from the protected area when they are under the control and custody of on-duty security force personnel.

Changing the security plan to allow on-duty armed security officers to re-enter the protected area without being subjected to metal detector searches was endorsed by the NRC in Generic Letter 96-02,"Reconsideration of Nuclear Power Plant Security Requirements Associated with an Internal Threat." The staff considered that this change could be made to the security plans in accordance with the provisions of 10CFR50.54(p).

I With regard to removal of keys from the protected area, it was concluded from the safety evaluation that the ability to protect vital equipment target sets continues to be maintained by prompt response to any vital area door alarm when an unauthorized access attempt's detected by the security system.

The key control requirements identified in 10CFR73.55(d)(9) are still being met and have been incorporated into the security plan.There are no 10CFR73.55(d)(9) stipulations that these keys cannot leave the protected area when under the control of a security officer.It was also concluded that the likelihood of an attempt at radiological sabotage is not a function of whether or not a vital area key is taken off-site while under the control of an authorized on-duty security force officer.SCN 96-014 (SE 96-013)This SCN provided for clarification and consistency pertaining to seismic qualification of equipment and components.

The method for assessing valve clearance was also modified.It was concluded from the safety evaluation that the consequences of a previously analyzed seismic or dynamic accident would not be increased by these changes.Consequences can only increase if the equipment or components analyzed are damaged by the event.The proposed changes only involve analytical methods for seismic and dynamic qualification of equipment and components.

The use of acceptably conservative analytical methods precludes any reduction in safety margin for systems and components.

No changes to hardware were made by this change.The equivalent static method invoked as a replacement for the more rigorous, but less conservative"dynamic method, would not result in a less conservative design.The proposed change invokes static factors that are conservative.

The change to the use of good practice to establish margin for valve.clearance assessment, instead of a nominal 25 percent margin, has no impact on system or component operability.

SCN 96415 (SE 95-089)This.SCN provided for a change to the FSAR to remove the description of the Mechanical Environmental Qualification (Ml~Program for safety-related mechanical and environmental augmented quality equipment.

This change affects only the documentation process for MEQ Program equipment located in a harsh environment.

It was concluded from the safety evaluation that the suitability of equipment to design requirements, including environmental conditions, will continue to documented as part of engineering processes.

Elimination of the MEQ Program will not alter the equipment, equipment function, plant configuration or maintenance and surveillance requirements.

I Existing engineering, procurement, maintenance and surveillance processes remain unchanged and will provide assurance that thy equipment continues to meet operability requireinents during normal operations and accident conditions.

61 SCN 96-017 (SE 96-017)This SCN provided for a change to the FSAR to reflect the elimination of certain response time testing based on NRC endorsement of BWR Owner's Group Licensing Topical Report NEDO-32291,"System Analysis for Elimination of Selected Response Time Requirements," dated December 28, 1994.In addition, the remaining response time test requirements were relocated from the FSAR to the WNP-2 Licensee Controlled Specifications.

It was concluded from the safety evaluation that none of the proposed changes resulted in a physical change or method of operation for any plant components.

Through normal instrument loop calibrations, and other logic and system functional tests required by the.Technical Specifications, safety system actuations required by transient and accident analyses remain unchanged.

Each of the selected sensor channels using alternative response time testing were reviewed to ensure that a qualitatively-assessed five second response time was consistent with the necessary actuation times specified within the accident analyses.There were no known failure modes that could be detected by resporise time testing that could also not be detected by other testing required by the Technical Specifications.'he proposed changes would also provide an improvement to plant safety and operation by reducing the time safety systems are unavailable, reducing the potential for safety system actuations, reducing plant shutdown risk, limiting radiation exposure to plant personnel, and eliminating the diversion of key,personnel resources to conduct unnecessary testing.SCN 96-021 (SE 96-020)'I This SCN provided for a change to the FSAR to reflect the use of Option B of 10CFR50, Appendix J, as the basis for the containment leakage testing program.The NRC has approved Option B which allows for implementation of a performance-based containment leakage rate testing program.This FSAR change implements a program which will assure leakage requirements are within current commitments and design basis assumptions.

It was concluded from the safety evaluation that this change would not impact normal plant operation, means of accident mitigation, or physically alter the design of the plant.The SCN was written to assure compliance with 10CFR50, Appendix J, as described in the'SER by using the guidelines established, in Regulatory'Guide 1.163.The change does not impact the configuration of any structure, system or component or.its ability to meet the designed safety function.Each valve and penetration will continue-to meet its designed function to isolate and maintain leakage within the specified limits.62

SCN 96-022 (SE 96-026)This SCN provided for clarification of the as-built configuration of the purge exhaust portion of the control room remote air intake system.The original design comprised two purge exhaust systems consisting of two electro-hydraulically-operated (EHO)isolation valves in series.A subsequent modification changed the design such that, in each purge system, one valve is equipped with an electro-hydraulic operator and is interlocked with its associated remote air intake valve.The other.purge valve is maintained open.It was concluded from the safety evaluation that this activity does not affect the function of these valves.This SCN was written to correct the discrepancy between the FSAR and actual system configuration.

The two disabled valves are maintained open by means of an EHO spring or by a split collar and cap screws.The position of the valves is indicated in the control room and they do not interact or affect any other systems or components.

The function of these valves is to remain open.during all normal modes of operation and also during accident and post-accident conditions.

SCN 96423 (SE 96-043)This SCN provided for a change to the FSAR to reflect the removal of reference to Reactor Building Electronics Room Air Conditioner RRA-AC-16.

It was concluded from the safety evaluation that removal, or abandonment in place, of the non-safety related (Quality Class II)air conditioning unit would not affect any safety-.related process equipment or systems.Removal or abandonment would also not have an impact on any accident analysis.The air conditioning unit is not used for.any safety function.Deactivation of this unit will lessen the heat load internal to the Reactor Building.Deactivation will also reduce electrical loads on the bus from which the unit is powered.~SCN 96-025 (SE 96-025)This SCN provided for a change to the FSAR to reQectthe deletion of reference to the Offgas Charcoal Vault Refrigeration and HVAC System.It was concluded from the safety evaluation that accident scenarios do not credit the Offgas Charcoal Vault Refrigeration and HVAC System with any accident mitigation responsibilities or functions.

Furthermore, gross failure of the refrigeration system has no safety implications since the charcoal adsorbers can be isolated and the plant can be safely shutdown without"the refrigeration system operating.

63

The system hM no interactions with any equipment or systems that act as safeguards or barriers to prevent or mitigate the consequences of an accident.The system was installed to allow for a sightly longer time for select radionuclides in the offgas stream by cooling the charcoal beds.The Technical Specification limiting dose rate of 332 millicuries/second after 30 minutes decay will be met, with significant margin, without the vault refrigeration system in operation.

~SCN 96426 (SE 96-047)This SCN provided for editorial changes to the FSAR and to reflect existing Plant Service Water (TSW)configuration.

It was concluded from the safety evaluation that the changes do not in any way affect the safe operation of the facility.In addition, the intent of the FSAR and basic operation of the TSW System are unaffected by these changes.The TSW System is not required to perform any safety function.Implementation of this SCN does not result in any physical changes to the plant or any change to design temperattires and pressures used in evaluations of TSW System piping.The changes consist of clarification and correction of current information pertaining to the TSW System description.

SCN 96-027 (SE 96-019)This SCN provided for a change to the Fire Protection Program and Emergency Plan to reflect revision of the training requirements and relocation of requirements pertaining to fire brigade training program.It was concluded from the SCN that the changes to the fire brigade training program would not lower the ability of safety systems to perform during accident conditions or increase safety system challenges without compensating effects.The changes do not reduce.the level of overall training on the mitigation of radiological releases.The proposed changes do not modify plant equipment and would not result in any new failure modes than those previously evaluated.

The changes to fire brigade training have no impact on the probability of occurrence of fires, or other design basis events, and continue to ensure that any fires are extinguished in a safe manner.

~e

~SCN 96-028 (SE 96-057)This SCN provided for a change to the FSAR to reflect deletion of reference to the backup diesel drives for the non-safety related motor-driven air compressors in the Emergency Diesel Generator Starting Air Systems (Divisions 1 and 2).It was concluded from the safety evaluation that sparing the backup starting air compressor diesel drives would not affect air receiver pressure or the number, of starts or starting capability of the emergency diesel generators.

The safety-related portions of the starting air system are isolated from the non-safety related portions of the system by means of check valves.The assumed'malfunction evaluated previously is the'ailure of an emergency diesel generator to start and supply power to the critical electrical buses.Therefore, the consequences of a malfunction of any equipment in the diesel starting air system remains unchanged by sparing the backup starting air compressor diesel drives.SCN 96-029 (SE 96-042)This SCN provided for revision of the Offsite Dose Calculation Manual (ODCM)description of the Reactor Building Effluent Monitoring System.The description of the main plant vent intermediate and high range detectors was deleted.~~It was concluded from the safety evaluation that detectors PRM-RE-1B and PRM-RE-1C are important to safety Regulatory Guide 1.97 monitors.However, the description of the detectors was not required to be included in the ODCM.'he elimination of these monitors from the ODCM does not alter any design requiremehts or methods of operation for the components.

P~SCN 96-033 (SE.96-049)This SCN provided for a change to the FSAR to remove unnecessary detailed information pertauiing to theory of operation, provide additional clarification where necessary, and to reflect testing results for the low, intermediate and high range detectors in the Reactor Building Noble Gas Effluent Monitoring System.It was concluded from the safety evaluation that the radiation monitor function is unaffected'by this change.The monitors continue to provide sufficient sensitivity to meet accident monitoring requirements for all calculated maximum accident releases and allow for accurate offsite dose predictions and associated operator'decisions.

65 The tested span for the low range detector is within the range requirements necessary for ODCM monitoring.

No physical plant equipment changes were made as a result of this FSAR revision.In addition, this change has no impact on any safety-related or'important to safety component function or method of operation.

~SCN 96-038 (SE 96-065)This SCN provided for a change to the FSAR to reflect deletion of a reference to Standby Liquid Control (SLC)System minimum area temperature because the SLC tank has safety-related heaters which keep the boron solution above saturation temperature.

Furthermore, the piping from the SL'C storage tank to the pump suction valves is heat traced and insulated.

It was concluded from the safety evaluation that the sodium pentaborate will be maintained above the saturation temperature.

The SLC System is a backup reactivity control system to the Control Rod Drive System and this change does not involve any physical.changes to the plant.The'heaters are capable of maintaining the boron solution within design temperature ratings to ensure complete solubility of the solution.SCN 96-042 (SE 96452)This SCN provided for a change to the Fire Protection Program to reflect the establishment of a new fire barrier operability category,"Operable but Nonconforming," which would result in shiftly (once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />)fire tours.In addition, this SCN allows for changes to the FSAR for not requiring fire tours in the Main Control Room.The bases for fire-rated assemblies was also clarified.

It was concluded from the safety evaluation that the changes would not lower the ability of safety systems to perform during accident conditions or increase safety system challenges without compensating effects.The changes do not reduce the level of overall training on the mitigation of radiological releases.The proposed changes would not result in any new failure modes than previously evaluated.

The changes have no impact on the probability of occurrence of fires, or other deign basis events, and continue to ensure that any fires are extinguished in a safe manner.Crediting the Main Control Room Operators to perform the function of a fire tour is acceptable.

The control room is continuously occupied and cognizant operators have the capability to detect power generation control complex and control room fires in the incipient stages.

2.7.4 Problem Evaluations

"~~~~~~~This section contains information pertaining to Problem Evaluation Requests (PERs)and is included pursuant to 10CFR50.59.

PER 296-0215 (SE 96-021)This PER documented a situation'where it was noted that an inflatable seal on Equipment Hatch MT-DOOR-A2 in the Reactor Building railroad crane bay has never been used.This door is part of secondary containment when Reactor Building Railroad Crane Bay Door R-106 is open.The concern was that the inflatable seal may have been required for secondary containment integrity.

The disposition of this problem was"permanent accept-as-is."It was concluded from the safety evaluation that the seal is not needed on MT-DOOR-A2.The door is a gasketed, airtight and water resistant component capable of withstanding maximum hydrostatic pressures in the event of a pipe rupture.Secondary containment was tested with Door R-106 open and then closed.Leakage rates were approximately the same for both conditions and were within required limits.The hatch is interlocked with Door R-106 such that both doors can not be open at the same time to preserve secondary containment integrity.

The situation as described on this PER has no impact on the interlock function.It was also c'oncluded that the inflatable seal was not required for flooding considerations.

PER 296-0273 (SE 96-036)This PER documented a situation where cracks were discovered in so'me of the plastic lugs molded into the relay bases and relay terminal bases (relay sockets)of certain"plug-in" type relay assemblies manufactured by ASEA.Some spalling was also noted around the mounting screws.The population consisted of seismic Category I relays used in safety-related applications.

The disposition of this problem was permanent accept-as-is.It was concluded from the safety evaluation that the relays were demonstrated by test and analysis to be capable of performing their intended safety function with the cracks/damage present.The seismic testing exceeded the required acceleration levels by a significant safety factor.The problems identified would not cause the relays to fail during any plant mode or transient.

67 I'

Based on an evaluation of relay seismic test report data, it was determined that the fragility levels used in the seismic tests bounded the required accelerations for all the locations where the identified relays are instaHed.Furthermore, it was concluded that adequate margin exists t'o'conclude that the cracks/damage in the terminal base plastic of the relays was not detrimental to operation during a seismic event.PER 296-0276 (SE 96-045)This PER documented a situation where it was observed during inspection of the jet pumps that set screws on Jet Pump No.18 were not making contact with the inlet mixer'to provide for three-point stabilization.

A 10-mil gap was observed between the set screws of the restrainer brackets and the inlet mixer.The jet pump design and installation specifications required that there be no gaps at these points.The disposition of this problem was"permanent accept-as-is." It was concluded from the safety evaluation and a General Electric vibration analysis.that gaps of up 12 mils were acceptable.

This was based on operating experience of other BWR 5 plants and the determination that, as long as in-vessel inspections at succeeding outages show that the set'crew gap is at 12 mils or less, continued operation is acceptable.

The function of the jet pumps would not be adversely affected when the gaps are maintained at this limit.Based on set screw gap vibration analysis and General Electric experience, operation with a gap of 10 mils during one cycle will not affect jet pump structural integrity.

Additional

=operational cycles may also continue with the gaps present as long as the width is less than 12 mils.(SE 96-046)This PER also documented a situation where damage was observed on a Jet Pump No.3 inlet'mixer wedge and its associated restrainer bracket wear pad.This problem was discovered during jet pump inspection efforts.The disposition of this problem was"interim accept-as-is." It was concluded from the safety evaluation that the worn inlet'wedge and associated wear pad provide a fixed restraining point for the inlet mixer.It was also concluded that the extent of the damage was not sufficient to cause a failure of either the inlet mixer wedge or restrainer bracket wear pad.*r 68 Installation of the restrainer bracket wedge has restored the three-point restraint required to stabilize the inlet mixer and prevent further damage to the inlet mixer, wedge.Accordingly, it was concluded from evaluation that the current extent of the degradation would allow operation for an additional cycle.PER 296-0278 (SE 96-048)This PER described a situation where broken and'missing anodes on cooling coils were discovered during cleaning of the Standby Service Water (SSW)System, Loop B, room coolers.The anodes were originally supplied to minimize the potential for corrosion, given the water chemistry specified at the time of coil purchase.The disposition of this problem was"re-work." It was-concluded from the safety evaluation that the presence or absence of anodes has no effect on the ability of the SSW System to meet its cooling requirements.

The status of the anodes in the SSW cooling coils does not impact the ability of the system and..associated components to mitigate the effects of design basis accidents or support safe shutdown of the plant.Flow to cooling coil tubes continues around the anode, so no significant flow reduction would be expected to occur if the anode was separated from the cap support.Flow through the cooling coil is adequate for any anode status (installed, removed or damaged).PER 2964360 (SE 95-102-01)

This PER described a situation where a loose jet pump sensing line clamp was noted at location 10C.A 30-mil gap was observed at the top of the clamp and was due to a circumferential weld being at'the location of the clamp.The disposition of this problem was"permanent accept-as-is." It was concluded from the safety evaluation that clamp integrity was proven through the use of crimp and shaker tools.The clamp was confirmed to be tightly installed and no loosening due to vibration would be expected., Based on evaluation, it was concluded that the as-installed configuration of the clamp would not impact the lost parts analysis.It was also determined that there would be no impact on core re-flood analysis capability or emergency core cooling system perforinailce.

69

~PER 296-0436 (SE 96-051)This PER described a situation where direct bridging circuit separation discrepancies were identified involving annunciator system field common circuits for cables.The cables bridged directly between Division 1 and Division 2 raceways.The disposition of this problem was"interim accept-as-is." The WNP-2 Electrical Separation Criteria Document (DRD 201)was revised to provide clarification for allowing low energy direct circuit bridges.It was concluded from the safety evaluation that allowing non-class 1E, low energy (instrument and control)cables to bridge directly between redundant raceways would be acceptable when certain acceptable conditions are met.These changes maintain WNP-2 commitments to single failure criteria required by 10CFRSO, Criterion 17, for safety-related electric power systems and will not increase the probability of occurrence or consequences of any previously evaluated transient.

These commitments to electrical'separation criteria ensure that, during accident conditions in conjunction with a postulated localized fire, redundant safety functions cannot be affected.PER 296-0438 (SE 96-58)This PER described a situation where it was noted that it took approximately 15 seconds to withdraw Control Rod Drive (CRD)System Mechanism CRD-DRVE-0627 from position 00 to 02.Normal drive speed is approximately one notch (six inches)every two seconds, with a full stroke in 48 seconds.The drive had to be withdrawn from position 00 using the continuous withdraw command.Beyond position 02, withdrawal speed was within normal limits.Rod insert motion was not affected and was within normal limits.The dispositions of this problem were"interim accept-as-is," and"permanent rework." These classifications were based on continued use of CRD-DRVE-0627 in the degraded condition pending rebuild during the Spring 1997 Maintenance and Refueling Outage.It was concluded from the safety evaluation that the problem was most likely caused by reversal or degradation of the drive piston drive-down seals (bridge and radial).A degraded or reversed drive-down seal assembly can, over time, impact normal.withdrawal movement of the drive.However, this condition would not affect normal insert motion or the safety-related scram function of the drive.There is also no postulated accident scenario that would require event mitigation through withdrawal of a control rod.-0 70

This section contains information'pertaining to tests and experiments not described in the FSAR and is included pursuant to 10CFR50.59.

~PPM 8.9.2 (SE 96-016)This procedure provides instructions for monitoring reactor cavity and spent fuel pool temperatures to verify the adequacy of natural circulation as an alternate flow'mechanism while in Operational Mode 5 (Refueling), with the reactor cavity flooded and spent fuel pool gates removed.It was concluded from the safety evaluation that installation and removal of temperature monitoring equipment in the reactor pressure vessel and spent fuel pool would not introduce a new mechanism for initiation of any evaluated accidents.

In addition, this activity would not interfere with the normal sequence of events for mitigating such accidents.

The monitoring equipment is non-obtrusive and does not rely on plant support equipment other than electrical power to operate.Should electrical power be lost to the temperature monitoring equipment, power could be restored using other power sources or battery-powered components.

71

Plant Procedure Changes The section contains information pertaining to Plant Procedure Manual (PPM)changes and is included pursuant to 10CFR50.59.

PPM 1.3.10C (SE 93-093)This is a new procedure which describes the administrative program for the control of transient combustible materials and provides for periodic inspection for the accumulation of combustibles.

Existing procedural guidance in this area was moved from PPM 1.3.10 to this new procedure.

It was concluded from the safety evaluation that, although some aspects of the transient.combustible program are less restrictive than in previous procedural revisions, the controls are still adequate to ensure that combustibles are limited to the extent practical.

'hese changes are not in conflict with previous commitments and do not represent an appreciable reduction in the margin of fire safety.The changes implement a thorough and effective administrative program for control of transient combustibles,, while eliminating a few aspects which were deemed to be an overly conservative burden and marginal to safety.PPM 2.2.1A (SE 96-069)This is a new procedure for controlling Reactor Recirculation (RRC)System flow from the local control and diagnostic panel using the adjustable speed drive channels.This procedure was developed to allow for local control in the event of the loss of control of recirculation pump speed in the Main Control Room.It was concluded from the safety evaluation that this temporary arrangement does not increase the probability of a recirculation pump transient because the trip function of the Adjustable Speed Drive System has not changed.The recirculation flow control failure'is caused by the failure of the master controller.

This change is limited to setting the speed limiter to a lower value.The consequences of a flow controller failure would be reduced because the high speed limiter will be set lower that the design value.This change also has no impact on recirculation runback due to the loss of a reactor feedwater pump as long as reactor power is maintained less than the equivalent power that could be established on the 108 percent.rod line (<65 percent core thermal power).This-change does'ot impose any action or modification that is beyond the designed capability of the Adjustable Speed Drive System or associated components such as the RRC pumps...72

PPM 2.8.1A (SE 96-023)This is a new procedure which provides instructions for Operations personnel to support an outage of the Control Air System (CAS)and Service Air (SA)System for maintenance and inspection purposes.This procedure can be implemented in Operational Mode 4 (Cold Shutdown), Mode 5 (Refueling) or Mode~(Refueling).

It was concluded from the safety evaluation that, during these operational modes, loss of CAS and SA would not result in the loss of any safety-related or important to safety functions.

The CAS and SA systems are not safety-related and provide no safety functions.

Loss of air to important to safety equipment results in the'equipment reverting to the safe condition (position).

It has been determined from failure analyses that no transients beyond those previously evaluated can occur from the loss of either (or both)system.In addition, it was~, concluded that complete loss of the systems would not affect the results of previously evaluated transients..

~PPM 2.8.5 (SE 96418)r This procedure provides for operation of the Fuel Pool Cooling (FPC)and Cleanup System during all operational modes.The procedure was revised to include a section on operation of the Residual Heat Removal (RHR)System in the FPC assist mode when RHR, Loop A, is not available for operation.

A section was also added on operation of RHR, Loop A, in a mode to'assist in maintaining spent fuel pool temperatures if RHR, Loop B, becomes unavailable during or following a full core off-load.It was concluded from the safety evaluation that fuel handling and rod withdrawal accident analyses were unaffected by the decay heat removal operating mode of the RHR.System.Adequate decay heat removal from the reactor pressure vessel and spent fuel pool would be maintained.

Adequate level would be maintained in the spent fuel pool in accordance with system design, and temperatures would be within allowable limits.Both the FPC and RHR systems would continued to be operated within'their design limits.PPM 6.5.19 (SE 96-039)This procedure provides for resolution of jet pump set screw gap and wedge problems.The procedure was revised to allow for installation of restrainer bracket wedges,using a General Electric-approved procedure.

The.original approach was to install restrainer bracket adjusting screws.-0 73 0

It was concluded from'the safety evaluation that installation of the restrainer bracket wedges will replace the function of the restrainer bracket adjusting screws.The wedges will restore the degree of lateral support required for the original design configuration for the jet pump inlet mixer.The probability of failure of any jet pump component, and subsequent ejections of the jet pump mixer, remains unchanged by installation of the strainer wedges.Because there would.be no change in performance of the jet pump design feature, the functional capability of the jet pumps remains unchanged by installation of restrainer bracket w edges.PPM 8.3.339 (SE 96-106)This procedure provides for testing of the Digital Feedwater Level Control (DFWLC)and Adjustable Speed Drive (ASD)Systems.Included in the procedure was a test to demonstrate the feedwater level control system and recirculation flow run-back feature that would prevent a low vessel water level scram following a single feedwater pump trip during power operation.

The safety evaluation was completed to determine the impact of either deferring or not completing this part of the procedure.

It was concluded from the safety evaluation that there were no unacceptable consequences in deferring or not performing this part of the procedure.

A comparison of the as-tested ASD run-back rates to previous GE'-NE Control System analyses concluded that ASD run-back rates and DHVLC settings are adequate for avoiding a low level scram due to feedwater pump trip during power operation.

The DKVLC and ASD recirculation flow control systems are expected to perform, as described in the FSAR, during a feedwater pump trip transient.

Based on system-level test results performed to date, it was determined that an additional integrated test to again'confirm system performance or assumptions used in plant transient analyses was unnecessary.

PPM 8.3.372 (SE 96-024)This is a new procedure which provides for motor-operated valve in-situ differential pressure operability testing of High Pressure Core Spray (HPCS)System Injection Valve-HPCS-V-4.The procedure was developed to satisfy recommendations contained in the WNP-2 Motor Operated Valve Periodic Verification Plan and NRC Generic Letter 89-13.It may also be used for post-maintenance testing.)The HPCS System provides a mitigating function to maintain reactor inventory or=core spray after a loss of coolant accident..The purpose of performing differential pressure testing of HPCS-V-4 is to verify that this valve will properly operate.when required to perform its open and close safety functions.

74 It was concluded from the safety evaluation that the test is conducted during cold shutdown conditions when the HPCS System is not required to be operable and alternate Emergency Core Cooling Systems (ECCS)are available.

During the test, reactor grade water from the condensate storage tanks would be injected into the vessel using normal injection alignment when the vessel is vented'(head vent valves open or head removed).The automatic interlock for closure of HPCS-V-4 at the Level 8 setpoint (+54.5 inches)would be maintained to prevent potential overpressurization or overfill of the vessel.;It was also concluded that the test conditions established by the procedure would not result in exceeding HPCS System or reactor vessel design or operating limits.PPM 9.3.39 (SE 96-050)This procedure provides for installation of the cycle-specific input deck and the CREATE base data into the POWERPLEX Core Monitoring Software System (CMSS).The procedure was revised to incorporate the POWERPLEX input database for Cycle 12.It was concluded from the safety evaluation that the core monitoring system does not interact with plant equipment and will not initiate any previously evaluated accident.The update of the input data base is performed only after completion of detailed engineering calculations.

The POWP26'LEX CMSS is used to verify compliance with specific core operating limits.These operating limits are specifically designed to protect against the most limiting accident types.The proposed update will provide the POWERPLEX monitoring system with the ability to use Cycle 12-approved core operating limits for both ABB and-Siemens fuel.Therefore, the system will maintain the ability to provide core operating limit evaluations.

This activity does not change the method by which the'plant is operated in accordance with procedures.

This procedural revision will allow for core monitoring to be performed using appropriate methodology consistent with the Cycle-12 licensing analyses.~PPM 10.3.2 (SE 95-043)This procedure provides instructions for installation and removal of reactor cavity shield plugs and gates.The procedure was revised to allow for removal of the lower set of reactor pressure vessel shield plugs during Operational Mode 3 (Hot Shutdown).

In addition, the lift rating of certain slings was increased to 50 tons.75 It was concluded from the safety evaluation that the fuel handling accident (dropped fuel bundle into the spent fuel pool)would not be affected by removal of the shield plugs.Removal of the plugs would follow a safe load path which does not include travel over the spent fuel pool.Current procedures allow removal of the top-layer reactor cavity shield plugs while.the reactor is critical.Removing the lower set of reactor cavity shield plugs in Operational Mode 3 would not increase the consequences of a previously evaluated accident.A safety factor of 5:1 would still be maintained by increasing the rating of the lifting slings.PPM 10.24.17 (SE 96-067)This procedure provides instructions for performing and documenting control rod friction and settle differential pressure testing.The procedure was revised to incorporate enhanced test equipment connection methodology during plant operation.

Prior to revision, differential pressure testing equipment was connected to control rod drive insert and withdraw line.high point vent valves.This was changed to allow for connection of the testing equipment to manifold test ports on the associated hydraulic control unit.It was concluded from the safety evaluation that performance of differential pressure testing in accordance with the revised test equipment connection methodology is a controlled evolution specified by the original equipment manufacturer.

This.change provides a reliable means to isolate the test equipment from the reactor pressure boundary if necessary.

Test connections also restrict the flow path such that any postulated leakage due to breach of the temporary test equipment is bounded by the transient assumed for an instrument line break outside containment.

PPM 10.25.1SS (SE 96-082)'his procedure provides for monthly inspections of 10CFR50, Appendix R, emergency'ighting battery units.The procedure was revised to correct and clarify emergency battery light discharge rates such that the values would be in conformance with the safe shutdown calculation and manufacturer information.

In addition, guidance was added pertaining to the posting of approved portable battery-powered lanterns as compensatory measures during discharge testing..It was concluded from the safety evaluation that there would be no new accident scenarios introduced by these changes.All plant systems and components required to mitigate the consequences of accidents.

previously evaluated would be unaffected by the.changes.Rev'ising the procedure to reflect emergency battery light discharge capacity.contained in the shutdown calculation aligns-it with plant design.Adding portable lanterns as compensatory.measures during discharge testing increases the ability of providing lighting in support of post-fire shutdown operator actions'.'76 The sole purpose of the emergency battery lighting is to provide illumination for personnel exiting the plant during a fire or station blackout.~PPM 16.1.1 (SE 96-040)This procedure provides for channel calibration of Reactor Building Effluent Low Range Radiation Monitor PRM-LCRM-1A.

The procedure was revised to relocate the Offsite Dose Calculation Manual (ODCM)high radiation alarm setpoint from the intermediate range detector to the low range detector.It was concluded from the safety evaluation that the stack monitoring system consists of passive instrumentation and is used to monitor post accident releases from the main plant vent elevated release point.The stack monitoring system does not initiate any'accidents.

This change moves the ODCM high radiation alarm function from the intermediate range detector to the more sensitive low range detector, tightens tolerances for loop checks, and allows for adjustment of the normalize potentiometer for testing purposes.The accident monitoring function of the stack monitor would be unaffected by these changes.Failure consequences remain unchanged from the alarm/setpoint relocation.

The consequences of a failure of the low range detector would be identical to that of the original intermediate range detector.77 Miscellaneous

'his section contains information pertaining to other plant activities and is included pursuant to 10CFR50.59.

~Clearance Order 93-12-0045 (SE 96-059)This clearance order allowed for deactivation of Process Sampling System (PSR)Booster Pump PSR-P-26.The pump is used to boost sample flow to Sample Point 26.This temporary change was to remain in place until such time that a permanent resolution to correct sample tube blocking problems can be implemented.

It was concluded from the safety evaluation that the liquid sampling system has no safety or direct process control functions.

Deactivation of the booster pump or isolation of the sample lines would not impact the operation of any equipment important to safety.This activity would not impact any system used to ensure the integrity of the reactor coolant pressure boundary, the capability to shutdown the reactor, or the capability to prevent accidents.

Chemical analysis of process system liquid will continue through grab sampling at arr alternate point (Sample Rack RCC-SR-44).

~Computer Change Request CCR-TE-95413 (SE 96-001)This change request modified the Siemens Power Corporation POWERPLEX Core Monitoring Sofbvare System (CMSS)to allow the MICROBURN code to use the ABB critical power correlation for monitoring ABB fuel.The POWERPLEX CMSS provides core monitoring capabilities by monitoring power distribution.

It was concluded from the safety evaluation that the POWERPLEX CMSS is not physically connected to any plant safety systems or any other plant systems important to safety, with the exception that power for the computer is from uninteruptible power source IN-1.The POWERPLEX CMSS does not cause any installed plant safety systems to activate.The computer on which the system is installed is Quality Class G hardware and uses a standard Digital VMS operating system.There are no environmental or technical qualifications for the computer or its operating system.Since the POWERPLEX CMSS is not physically connected to any plant safety systems, it is not and can not be an initiator for any plant transient or accident.Furthermore, changes to the computer program would not change any operational modes, operating procedures, or method of operating plant equipment.

78 I'

Core Operating Limits Report 96-12:Rev 0 (SE 96-031)This revision allowed for implementation of the WNP-2, Cycle 12, Core Operating Limits Report (COLR).The proposed activity consisted of operation of the Cycle 12 reload core with core thermal limits which have been developed with NRC-approved methodologies.

The thermal limits are specified in the COLR.The Cycle-12 reload core consists of f'uel assemblies of the SVEA-96 design, Siemens 9x9-9x design and Siemens 8x8-2 design.The SVEA-96 assemblies are new to WNP-2 with this reload.It was concluded from the safety evaluation that operation of Cycle 12 within the thermal Hmits defined in COLR 96-12 does not increase the consequences of the analyzed anticipated operational occurrences or accidents because the mechanical, thermal'.hydraulic and LOCA design criteria imposed on the fuel to protect it during these events are met.Analyses of the previously-evaluated accidents and bounding anticipated operational occurrences systematically addressed all fuel characteristics, fuel related equipment malfunctions and operator actions.The depth of these analyses precludes the possibility of an accident which has not been previously evaluated, provided that the linear heat generation rate and other thermal limits as established by the COLR are followed.Fire Protection:

Penetration Seals (SE 96-053)This.activity consisted of the continuous use of fire tours as adequate ongoing compensatory measures for inoperable fire-rated penetration seals.It was concluded'rom the safety evaluation that fires are neither initiators nor mitigators of any previously analyzed transients.

These tours can decrease the probability of occurrence of plant fires in that they may discover smoldering pre-fire conditions which could be mitigated prior to outbreak.This activity does not degrade or prevent actions assumed in the accident analysis, adversely affect fission product barriers, alter any assumptions made in evaluating radiological consequences of an accident, or physically modify any plant component or system operation.

~Fire Protection:

Vertical Cable Trays (SE 96-054)This activity consisted of the continuous use of fire tours as adequate ongoing compensatory measures for inoperable.

Thermo-Lag coated vertical cable tray fire breaks.79 It was concluded from the safety evaluation that fires are neither initiators nor mitigators of any previously analyzed transients.

Fire tours can decrease the probability of occurrence of plant fires in that they may discover smoldering pre-fire conditions which could be mitigated prior to outbreak.h This activity does not degrade or prevent actions assumed in the accident analysis, adversely affect fission product barriers, alter any assumptions made in evaluating radiological consequences of an accident, or physically modify any plant component or system operation.

~Technical Evaluation Request 96-0009-0 (SE 96-028)This Technical-Evaluation Request provided for the relocation of two Bailey cards and installation of sliding link terminal blocks for Primary Contairiment Sump Flow Monitoring System and Reactor Water Cleanup System isolation instrumentation (LD-~SUM-604 and FDR-SQRT-38).

It was concluded from the safety evaluation that the function of the instruments would not be affected by the change in position or the addition of terminal blocks.There are no transients or accidents that'would be affected by this activity.The cards were simply moved to a new location within the same rack and would provide the same functions as the original configuration.

The installation of the terminal blocks with sliding link disconnects allows for system testing without removing any wiring.System interfaces are not changed and design basis requirements for electrical separation, seismic and instrument loop tolerances,were maintained.

Technical Evaluation Request 96-0127-0 (SE 96-109)This Technical Evaluation Request'provided for the permanent designation of temporary.valves and spectacle flanges installed in the water box drain lines to allow for on-line tube plugging in the main condenser.

It was concluded from the safety evaluation that implementation of this change would not adversely impact condensate system piping stress evaluations.

The pressure ratings of the current components are within the required tolerances for the system.The-condensate system is a Quality Class II, non-safety related system.The system is,not required to perform any safety function such as maintaining the integrity of the reactor coolant pressure boundary or mitigating the consequences of an accident.80

Technical Evaluation Request 96-0178-0 (SE 96-102)This Technical Evaluation Request provided for the replacement of several globe and gate pattern valves in the Plant Service Water (TSW)System with ball pattern valves.The valves were replaced to allow for drain water to be routed through the equipment/floor drain system.It was concluded from the safety evaluation that the replacement ball pattern valves have equal or greater pressure ratings than the existing valves and they weigh less.The TSW is a Quality Class II, non-safety related system.The system is not required to perform any safety function such as maintaining the integrity of the reactor coolant pressure boundary or mitigating the consequences of an accident.Stress evaluations for small bore piping and valves in these applications would not be adversely impacted by this change.Work Order YS6901 (SE 96-009)This work order provided for repair of Demineralized Water System Valve DW-V-100/57 and isolation of the component from the system by means of a freeze seal in'the horizontal run of piping upstream of the valve.It was concluded from the safety evaluation that the only credible problem area of concern during isolation of the water supply to DW-V-100/57 would be flooding of the Reactor Building 471'levation due to failure of the freeze seal.A decrease in reactor coolant inventory would require freeze seal failure, coincident with a Post Accident Sampling System (PASS)sample being drawn from the jet pumps and failure of PASS Check Valve PSR-V-106 in the Demineralized Water System flush line.However, this event has been previously evaluated and documented in the FSAR.All important to safety equipment affected by a maximum potential flooding event is already identified and included in the plant flooding analysis.Flooding due to failure of the freeze seal would not alter the manner in which equipment is assumed to fail during any flooding event.Work Orders WT5001 and YH1001 (SE 96-037)These work orders provided for installation of a freeze seal in a Control Rod Drive (CRD)System line upstream of CRD Vent Valve CRD-V-101A to allow for inspection

'f CRD Insert Isolation Valve CRD-V-101/5027.

The proposed activity would be performed with the reactor.,in cold shutdown,.

depressurized and all control rods.fully inserted.81 f

It was concluded from the safety evaluation that there were no postulated accidents or operational transients associated with a break in the one-inch CRD insert line that could result in an increase in the radiological dose at the site boundary.There were also no postulated accidents or operational transients associated with a break in the line that could result in flooding and impact the functional ability of equipment important to safety.In was also concluded that the piping was capable of accepting the stresses from the freeze seal.If the pressure integrity of the insert line were to fail due to loss of the freeze seal during the rework or replacement of the valve, no control rod withdrawal would occur.~Work Order YT6201 (SE 96-038)This work order provided for installation of a freeze seal in a Control Rod Drive (CRD)System line upstream of CRD Vent Valve CRD-V-102A to allow for inspection of CRD Withdraw Isolation Valve CRD-V-102/2251.

The proposed activity would be performed with the reactor in cold shutdown, depressurized and all control rods fully inserted.It was concluded from the safety evaluation that there were no postulated accidents or operational transients associated with a break in the one-inch CRD insert line that could result in an increase in the'radiological dose at the site boundary.There were also no postulated accidents or operational transients associated with a break in the line that could result in flooding and impact the functional ability of equipment important to safety.-E, In was also concluded that the piping was capable of accepting the stresses from the freeze seal.If the pressure integrity of the insert line were to fail due to loss of the~freeze seal during the rework or replacement of the valve, no control rod withdrawal would occur.h 82 2.8 R1M'ORT OF DIESEL GF22RATOR FAILURES This section contains information pertaining to diesel generator failures, valid and non-valid, and is included pursuant to Technical Specifications 4.8.1.1.3 and 6.9.1.There was one non-valid failure in 1996.There were no valid load demand failures for the three emergency diesel generators.

The non-valid failure event was documented on Problem Evaluation Request 296-0338 and is.described as follows:~Identity of Diesel Generator and Date of Failure Division One Emergency Diesel Generator (DG-1): May 8, 1996 (2128 hours0.0246 days <br />0.591 hours <br />0.00352 weeks <br />8.09704e-4 months <br />)~..Number.Designation of Failure in Last 100 Valid Tests This was the first failure of the last 100 tests.However, this test was determined to be a"non-valid" load demand failure.~Cause of Failure 0 During performance of the annual LOOP/LOCA surveillance test for the Division 1 Emergency Diesel Generator, a fuel oil leak developed on the return line to the fuel oil day tank.The leak occurred on a threaded fitting to the flanged connection of the return line.Corrective Measures Taken" The unit was shutdown and the fuel line was replaced and leak tested.Upon completion of successful repair efforts, the diesel generator was re-started and the 24-hour surveillance test was completed without further incident.Length of Time Diesel Generator Unavailable The Diesel Generator was out of service for approximately one hour.Testing activities resumed at 0507 hours0.00587 days <br />0.141 hours <br />8.382936e-4 weeks <br />1.929135e-4 months <br /> on May 9, 1996."Current Surveillance Interval Thirty one days.83 wp 0 REGULATORY CO CHANGES (NEI PROCESS)This section contains information pertaining to Regulatory Commitment Changes (RCCs)and is included pursuant to the NEI Guidelines for Management NRC Commitments.

~RCC-30985-00 (Vital Area Access Controls)The original commitment desciiption is,"The Security Supervisor responsible for categorizing materials entering the protected area will be present initially to ensure proper vital area access controls are in position anytime (door)R-106 is.opened to allow access." This commitment was made in response to Security Event Report 87-004.This commitment was deleted.The basis for deletion is that a current procedure requires that, prior to allowing personnel access into any vital area, access authorization for the.area is verified by either a review of an access authorization list or through communications with the Central Alarm Station.This alternate method complies with 10CFR73.55(g)(1) and 10CFR73.55(d)(7)(B).

There is no change to the protection level for personnel to ensure a system, structure or component is capable of performing its function.Access authorization continues to be verified prior to personnel being allowed entry into a vital area.RCC.-106987-00 (Crane Stops)1 The original commitment description is,"Place a physical stop on the monorail supporting MT-HOI-6 to prevent moving RHR-Loop A or Loop B components over the equipment left in service." This commitment was made in response to NUREG-0612 tLetter GO2-83-614, dated July 13, 1983, GC Sorensen (SS)to A Schwencer (NRC),."Response to NUTMEG-0612-Phase II, Control of Heavy Loads;Submittal of"'sic)].

This commitment was deleted.The basis for deletion is guidance contained in Generic Letter 85-11,"Completion of Phase II of'Control of Heavy Loads at Nuclear Power Plants'UIREG-0612," dated June 28, 1995., This Generic Letter provided relief to certain previous requirements pertaiiung to heavy loads.This commitment was within, the scope of those requirements that were allowed to be eliminated.

Current procedures are in place to meet the requirements of Phase I and ensure the safe operation of this hoist.84

~, I'" fV.C,

~RCC-107116-00 (Positioning of Cranes and Hoists)The original commitment description is,"Certain cranes and hoists will be locked out in a safe position and not placed into use until the equipment they service has been declared inoperable per the Plant Technical Specifications." This commitment was made in response to NUREG-0612

[Letter GO2-82-824, dated October 4, 1982, GD Bouchey (SS)to A Schwencer (NRC),"Response to NUREG-0612, Control of Heavy Loads, Revision 1;Submittal of'sic)].This commitment was deleted.The basis for deletion is guidance contained in Generic Letter 85-11,"Completion of Phase II of'Control of Heavy Loads at Nuclear Power Plants'UTMEG-0612," dated June 28, 1995.This Generic Letter provided relief to certain previous requirements pertaining to heavy loads.This commitment was within the scope of those requirements that were allowed to be eliminated.

Current procedures are in place to meet the requirements of Phase I and ensure the safe operation of cranes and hoists.~RCC-'107245-00 (Crane Operator Training)0 The original commitment description is, There are no exceptions taken to ANSI B30.2-1976 with respect to operator traiiiing, qualification and conduct.Per plant procedures, this type of tr'aining is documented and records of such training are maintained

'current'y the training staff.Recertifiication is required every three (3)years unless the operator has not operated the crane during" the year and in..that case the operator must be recertified before operating the unit." This commitment was made in response to NUREG-0612

[Letter GO2-82-824, dated October 4, 1982, GD Bouchey (SS)to A Schwencer (NRC),"Response to NVREG-0612, Control of Heavy Loads, Revision 1;Submittal of" (sic)).This commitment was revised to,"There are no exceptions taken to ANSI B30.2-1976 with respect to operator training, qualification and conduct.Per plant procedures, this type of training is documented and records of such training are maintained." The basis for revision is that"recertification every three years unless the operator has not operated the crane during the year and in that case the operator must be recertified before operating the unit" is not required by ANSI B30.2-1976.

In addition, documentation is retained in a"current" status and is available for review at the Supply System.This approach to document maintenance is consistent with previous guidance issued in this Recertifications are currently evaluated on,a,case-by-case basis and.could'epend'n

'everal factors such as job complexity or past performance of the'crane operator.0 85

RCC-131354-00 (Scram Time Testing)The original commitment description is,"Perform scram time testing once per 60 days on a reference sample of rods having Viton SSPVs consisting of 5%but not less than 5 rods." This commitment was made in response to BWROG SSPV testing recommendations (Letter GO2-96-078, dated April 5, 1996, JV Parrish (SS)to AC Thadani (NRC),"CRD SSPVs with Viton Internals").This commitment vras revised to,"Perform scram time testing once per 60 days, plus or minus 25%, on a reference sample of rods having Viton SSPVs consisting of 5%but not less than 5 rods." The basis for revision is that the observed rate of change in the performance characteristic of the Viton SSPVs is slow enough to allow adequate response time to an undesirable degraded condition with a 25 percent increase in the testing interval.Furthermore, the 25 percent tolerance is consistent with Technical Specification

.4.0.2.A tolerance was.not specified in the original commitment and this revision simply clarifies the intended testing interval tolerance.

RCC-135865-00 (Procedure Review Committee)

The original commitment description is;"A POC procedure review committee has been established as part of the procedure change management process to perform additional procedure review prior to general POC member review." This commitment was made in response to NRC Inspection Report 9345 (Letter,GO2-94-026, dated January 28, 1994, JV Parrish (SS)to NRC,"NRC Inspection Report 93-45 Response to Notice of Violation").This commitment was deleted.The basis for deletion is that, as part of a procedure upgrade project, the Supply System transitioned from having department procedure coordinators and procedure reviews performed by selected reviewers, to procedure sponsors and qualified procedure reviewers.

Procedure sponsors are identified as the procedure owner (i.e., most hiowledgeable of the procedure).

Qualified procedure reviewers are trained and qualified to perform procedure reviews.Procedure review expectations have also been clearly defined.Monitoring of procedure sponsor and qualified procedure reviewer performance for procedure revisions and reviews showed improvement to indicate that procedure review committee reviews were no longer.necessary.

This monitoring was performed by the procedure review subcommittee..

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